ML18065A143

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Monthly Operating Rept for Sept 1995 for Palisades Nuclear Plant
ML18065A143
Person / Time
Site: Palisades Entergy icon.png
Issue date: 09/30/1995
From: Berles B, Anthony Williams
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9510110092
Download: ML18065A143 (5)


Text

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I consumers Power POWERING lllllCHIGAN"S PROGRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Coven. Ml 49043 October 4, 1995 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of September, 1995.

If you have any questions or concerns, please feel free to contact me at (616) 764-8913, extension 0113.

Sincerely, A L Wi 11 i ams Reactor Engineer CC:

RAVincent, Palisades Senior Resident Inspector, Palisades DRHahn, Div of Rad Health Services, Lansing, MI BWJorgensen, Michigan Dept of Labor, Lansing, MI JPadgett, Michigan Public Service Commission Records Center, INPO, Atlanta, GA CWMain, Palisades SMMclntyre, Pl3-121 Region III Administrator, USNRC

  • Document Control, 950*22*35*10/L Cycle 12 Reports 9510110092 950930 PDR. 'AD.OCK 05000255 R -" --~

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A CMS' ENERGY COMPANY

OPERAT1NG STATUS:

1.

UNIT NAME

2.
3.

REPORTING PERIOD:*

LICENSED THERMAL.POWER (MWt)

_4.

NAMEPLATE RATING (GROSS MWei 5 *. 6ESIGN ELECTRICAL RATING (NET MWe)

6.

MAXIMUM DEPENDABLE-CAPACITY* (GROSS MWe)

OPERATING DATA REPORT Pal is"ades 950901~950930 2530.0.

811.7 805.0.

. **no

7.

MAXIMUM DEPENDABLE CAPACITY CNET MWe)

    • 730 DOCKET NO.

50-255*

DATE 10~04-95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 NOTES:

8.

IF. CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 THROUGH ?AND 7) SIN.CE LAST REPORT, GIVE REASONS:

9.. POWER LEVEL TO WHICH RESTRICTED, _IF ANY (NET MWe):

10. REASONS FOR RESTRIC~IONS, IF ANY: -

l1. HOURS lN REPORTING PERIOD

12. NUMBER OF HOURS REACTOR WAS CRITICAL
13.
  • REACTOR RESERVE SHUTDOWN HOURS
14. HOURS GENERATOR ON-LINE*

15: UNIT RESERVE SHUTDOWN HOURS

16. GROSS THERMAL ENERGY GENERATED CMWH)
17. GROS_S EL_ECTRICAL ENERGY GENERATED. CMWH).

18: NET ELECTRICAL-~NERGY GENERATED CMWH).

19. UNIT SERVICE. FACTOR
20. UNIT AVAILABILITY.FACTOR
21. "UNIT CAPACITY FACTOR (USIN°G MDC NET)

. 22. UNIT. CAPACITY FACTOR (USING DE_R NET)

23. UNIT-. FORCED *OUTAGE *RATE*

~"'

This Month 720.0 720.0 674.7.

154.4662.3 502789.0.

476223.0 93.7%

93.7%.

.90.6%

. 82.2~

.6.3~

24: SHUTDOW~S SCHEDUl~D{~¥:~}HE~ ~EXT.6.: MONTHS (TYPE,* DATE AND DURATION OF EACH):

_,:r:f ~~*. ]'. ".

25_. IF SHUTDOWN AT.END;,OF_REl?ORT-PERIOO, ESTI.MATED DATE OF STARTUP:

26. UNITS JN TEST *S-TATIJS'°CPRIOR TO COMMERCIAL OPERATION):

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

    • Based on*condenser backpressure
  • Weighted Av.er age (635 MWe used as MDC Net pr for to October 1985)
  • Yr-to-Date Cumulative 6551.0 208478.0 4430.3 11874~.3 4315.6 113977. 7 103487~0.0 248639441.0 3350229.0

. 787'15020. 0

. 3181433. 0

. 742n994.o 65;9%

54. ?"!.

65.9%:

54. ?"!.

66.5%

52.6%*

60.3~.

44.3% - *..

.. 4.5%

29.1%

Forecast Achieved

AVERAGE DAILY UNIT POWER LEVEL MONTH ---~S=EP~T~E~MB~E=R'"----

DAY AVERAGE DAILY POWER LEVEL DAY (MWe Net)

1.

267

17.
2.

159

18.
3.

453

19.
4.

728

20.
5.

758

21.
6.

756

22.
7.

763

23.
8.

777

24.
9.

776

25.
10.

778

26.
11.

726

27.
12.

0

28.
13.

172

29.
14.

592

30.
15.

770

31.
16.

766 INSTRUCTIONS:

DOCKET NO 50-255 UNIT Palisades DATE 10/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 AVERAGE DAILY POWER LEVEL (MWe Net) 769 775 771 768 775 777 778 778 776 772 772 771 769 764 On this format, list the average daily unit power level in MWe-NET for each day in the reporting month.

Compute to the nearest whole megawatt.

J

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SUMMARY

OF OPERATING EXPERIENCE FOR SEPTEMBER 1995 The unit began the month at 49% power.

Power was reduced on 9/01/95 and the unit was taken off-line at 0208 on 9/02/95 (the reactor remained critical) for a forced outage to repair a Motor Operated Disconnect in the switchyard.

The unit was back on-1 ine at 1458 on 9/02/95.

The unit was re.turned to 100% by 0900 on 9/04/95.

On 9/11/95, a broken conductor was discovered between an i sophase bus and the main generator.

A power reduction was initiated from 100% at 1800 and the unit was off-line at 2106 ( the reactor remained criti-cal) for a forced outage to repair the isophase bus.

The unit was placed on-line on 9/13/95 at 0538, and 100% power was reached by 0600 on 9/15/95.

The unit operated at 100% for the remainder of the month.

RE PORT MONTH -----'S"""E'--P T'-=E""'"MB=E=R-'1=9-=-9"'-5 __

No.

Date Type 1 2

8/30/95 F

3 9/11/95 F

l.

F:

Forced S:

Scheduled Duration (Hours)

2.

Reason:

12.8 32.5 Reason2 A

A A-Equipment Failure (Explain) 8-Maintenance or Test C-Refue ling D-Regulatory Restric~ion E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)

UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor3 Report #

4 4

3.

Method:

1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)

4.

System Code4 Component Code 5

Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)

DOCKET NO 50-255 UN IT Pali sades DATE

_____lg/04/95 COMPLETED BY BWBerles TELEPHONE (616)764-8913 Cause & Corrective Action to Prevent Recurrence Power was reduced from 99.6% due to a Motor Operated Disconnect in the switchyard overheating.

The unit was taken off-line at 0208 on 9/2/95 and placed back on-line at 1458 on 9/2.

Power was reduced from 100% on 9/11 at 1800 and the unit was off-line at 2106 to repair a conductor between an isophase bus and the main generator.

The unit was on-line on 9/13 at 0538.

5.

Exhibit I - Same Source I

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