ML18059A862
| ML18059A862 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 02/28/1994 |
| From: | Kluskowski P, Van Wagner M CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9403100364 | |
| Download: ML18059A862 (5) | |
Text
. i*
consumers
. Power POW ERi Nii MICHlliAN'S PRDliRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Covert, Ml 49043 March 8, 1994 US Nuclear Regulatory Commission Document Control Desk Washingtqn, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of February, 1994.
If you have a*ny questions or concerns, please feel free to contact me at (616) 764~8913~ extension 0113.
Sincerely;
'pJ Kl uskowski Reactor Engineer*
CC:
DPHoffman, P26-117B JMartin, USNRC JLKuemin, Palisades R.e?ident Inspector, Palisades_
DRHahn, Div of Rad Healt~ Services, Lansing, MI BWJorgensen, Michigan Dept of L~bor, Lansing; MI JPadgett, Michigan Pµblic Service Commission Records Center, INPO, Atlant~, GA RWTaylor, CE, Palis'ades
~
GKatt, Palisades SMMclntyre, Pl3-121
- Region III Administrator, USNRC Document Control, 950*22*35*10/L Cycle 11 Reports 100'177
- - J.
1-----:::---:--------_:___.~
9403100364 940228
,:'./
PDR ADOCK 05000255 iJ1 R1 PDR Lll A CMS' ENERGY COMPANY
OPERATING STATUS:
- 1.
UNIT NAME
- 2.
REPORTING PERIOD:
- 3.
LICENSED THERMAL POWER CMWt)
- 4.
NAMEPLATE RATING (GROSS MWe)
- 5.
DESIGN ELECTRICAL RATING (NET MWe)
- 6.
MAXIMUM DEPENDABLE CAPACITY (GROSS MWe)
- 7.
MAXIMUM DEPENDABLE CAPACITY (NET MWe)
OPERATING DATA REPORT Palisades 940201-940228 2530.0 811. 7 805.0
- 770
- 730
- 8.
IF CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 AND 7) SINCE LAST REPORT GIVE REASONS:
- 9.
POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):
- 10. REASONS FOR RESTRICTIONS, IF ANY:
11. HOURS IN REPORTING PERIOD
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL
- 13. REACTOR RESERVE SHUTDOWN HOURS
- 14. HOURS GENERATOR ON-LINE
- 15. UNIT RESERVE SHUTDOWN HOURS
- 16. GROSS THERMAL ENERGY GENERATED CMWH)
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH)
- 18. NET ELECTRICAL ENERGY GENERATED CMWH)
- 19. UNIT SERVICE FACTOR
- 20. UNIT AVAILABILITY FACTOR
- 21. UNIT CAPACITY FACTOR (USING MDC NET)
- 22. UNIT CAPACITY FACTOR (USING DER NET)
- 23. UNIT FORCED OUTAGE RATE This Month 672.0 406.1 405.3 1004688.0 329910.0 314287.0 60.3%
60.3%
64.1%
58.1%
- 39. 7"!.
- 24. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):
- 25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: March 23, 1994
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
- Based on condenser backpressure
- Weighted Average (635 MWe used as MDC Net prior to October 1985)
Yr-to-Date 1416.0 1150. 1 1149.3 2848800.0 937490.0 892790.0 81.2%
81.2%
86.4%
78.3%
18.8%
Forecast DOCKET NO 50-255 DATE 03-04-94 COMPLETED BY MMVanWagner TELEPHONE (616)764-8913 NOTES:
Cumulative 194583.0 109590. 1 104950.9 226511619.0 71555993.0 67475525.0 53.9%
53.9%
51.6%*
43.1%
29.5%
Achieved
AVERAGE DAILY UNIT POWER LEVEL MONTH _ ____,_F-=E=BR=U"'-'A'-'-'RY'--_
DAY AVERAGE DAILY POWER LEVEL (MWe Net)
- 1.
672
- 2.
743
- 3.
789
- 4.
788
- 5.
791
- 6.
788
- 7.
793
- 8.
792.
- 9.
789
- 10.
787
- 11.
786
- 12.
794
- 13.
789
- 14.
790
- 15.
788
- 16.
791 INSTRUCTIONS:
DAY
- 17.
- 18.
- 19.
- 20.
- 21.
- 22.
- 23.
- 24.
- 25.
- 26.
- 27.
- 28.
DOCKET NO 50-255 UNIT Palisades DATE 03/07/94 COMPLETED BY MMVanWaqner TELEPHONE (616)764-8913 AVERAGE DAILY POWER LEVEL (MWe Net) 707 0
0 0
0 0
0 0
0 0
0 0
On this format, list the average daily unit power level in MWe-NET for each day in the reporting month.
Compute to the nearest whole megawatt.
REPORT MONTH ----'F'"-'E""'B""'R U"'"A""'R_,_Y _,1:..:::9"'-9 4"'---
No.
Date Type 1 01 02/17/94 F
- l.
- 2.
F:
Forced S:
Scheduled Duration Reason2 (Hours) 266.7 A
Reason:
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refue ling D-Regulatory Restriction E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain)
UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor3 Report #
- 3.
Method:
1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)
- 4.
System Code4 Component Code6 Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
Cause & Corrective Action to Prevent Recurrence DOCKET NO UNIT DATE COMPLETED BY TELEPHONE Safety Injection System Check Valve Leak and Repair
- 5.
Exhibit I - Same Source 50-255 Palisades 02/28/94..
MMVanWagner (616)764-8913
\\
'~
' 0
SUMMARY
OF OPERATING EXPERIENCE FOR FEBRUARY 1994 The pl ant began the month operating at 85% power.
Repairs were made to turbine control system and full power was reached at 2030, on February 2.
On February 17, at 1634, power reduction was commenced due to a check valve leak.
The turbine generator went off-line at 2118.
On February 18, at 0120, the reactor was manua 11 y tripped and pl aced in hot shutdown for check valve repairs.