ML18059A862

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Monthly Operating Rept for Feb 1994 for Palisades Nuclear Plant
ML18059A862
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/28/1994
From: Kluskowski P, Van Wagner M
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9403100364
Download: ML18059A862 (5)


Text

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consumers

. Power POW ERi Nii MICHlliAN'S PRDliRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Covert, Ml 49043 March 8, 1994 US Nuclear Regulatory Commission Document Control Desk Washingtqn, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of February, 1994.

If you have a*ny questions or concerns, please feel free to contact me at (616) 764~8913~ extension 0113.

Sincerely;

'pJ Kl uskowski Reactor Engineer*

CC:

DPHoffman, P26-117B JMartin, USNRC JLKuemin, Palisades R.e?ident Inspector, Palisades_

DRHahn, Div of Rad Healt~ Services, Lansing, MI BWJorgensen, Michigan Dept of L~bor, Lansing; MI JPadgett, Michigan Pµblic Service Commission Records Center, INPO, Atlant~, GA RWTaylor, CE, Palis'ades

~

GKatt, Palisades SMMclntyre, Pl3-121

  • Region III Administrator, USNRC Document Control, 950*22*35*10/L Cycle 11 Reports 100'177
  • - J.

1-----:::---:--------_:___.~

9403100364 940228

,:'./

PDR ADOCK 05000255 iJ1 R1 PDR Lll A CMS' ENERGY COMPANY

OPERATING STATUS:

1.

UNIT NAME

2.

REPORTING PERIOD:

3.

LICENSED THERMAL POWER CMWt)

4.

NAMEPLATE RATING (GROSS MWe)

5.

DESIGN ELECTRICAL RATING (NET MWe)

6.

MAXIMUM DEPENDABLE CAPACITY (GROSS MWe)

7.

MAXIMUM DEPENDABLE CAPACITY (NET MWe)

OPERATING DATA REPORT Palisades 940201-940228 2530.0 811. 7 805.0

    • 770
    • 730
8.

IF CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 AND 7) SINCE LAST REPORT GIVE REASONS:

9.

POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):

10. REASONS FOR RESTRICTIONS, IF ANY:

11. HOURS IN REPORTING PERIOD

12. NUMBER OF HOURS REACTOR WAS CRITICAL
13. REACTOR RESERVE SHUTDOWN HOURS
14. HOURS GENERATOR ON-LINE
15. UNIT RESERVE SHUTDOWN HOURS
16. GROSS THERMAL ENERGY GENERATED CMWH)
17. GROSS ELECTRICAL ENERGY GENERATED (MWH)
18. NET ELECTRICAL ENERGY GENERATED CMWH)
19. UNIT SERVICE FACTOR
20. UNIT AVAILABILITY FACTOR
21. UNIT CAPACITY FACTOR (USING MDC NET)
22. UNIT CAPACITY FACTOR (USING DER NET)
23. UNIT FORCED OUTAGE RATE This Month 672.0 406.1 405.3 1004688.0 329910.0 314287.0 60.3%

60.3%

64.1%

58.1%

39. 7"!.
24. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):
25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: March 23, 1994
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

    • Based on condenser backpressure
  • Weighted Average (635 MWe used as MDC Net prior to October 1985)

Yr-to-Date 1416.0 1150. 1 1149.3 2848800.0 937490.0 892790.0 81.2%

81.2%

86.4%

78.3%

18.8%

Forecast DOCKET NO 50-255 DATE 03-04-94 COMPLETED BY MMVanWagner TELEPHONE (616)764-8913 NOTES:

Cumulative 194583.0 109590. 1 104950.9 226511619.0 71555993.0 67475525.0 53.9%

53.9%

51.6%*

43.1%

29.5%

Achieved

AVERAGE DAILY UNIT POWER LEVEL MONTH _ ____,_F-=E=BR=U"'-'A'-'-'RY'--_

DAY AVERAGE DAILY POWER LEVEL (MWe Net)

1.

672

2.

743

3.

789

4.

788

5.

791

6.

788

7.

793

8.

792.

9.

789

10.

787

11.

786

12.

794

13.

789

14.

790

15.

788

16.

791 INSTRUCTIONS:

DAY

17.
18.
19.
20.
21.
22.
23.
24.
25.
26.
27.
28.

DOCKET NO 50-255 UNIT Palisades DATE 03/07/94 COMPLETED BY MMVanWaqner TELEPHONE (616)764-8913 AVERAGE DAILY POWER LEVEL (MWe Net) 707 0

0 0

0 0

0 0

0 0

0 0

On this format, list the average daily unit power level in MWe-NET for each day in the reporting month.

Compute to the nearest whole megawatt.

REPORT MONTH ----'F'"-'E""'B""'R U"'"A""'R_,_Y _,1:..:::9"'-9 4"'---

No.

Date Type 1 01 02/17/94 F

l.
2.

F:

Forced S:

Scheduled Duration Reason2 (Hours) 266.7 A

Reason:

A-Equipment Failure (Explain)

B-Maintenance or Test C-Refue ling D-Regulatory Restriction E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)

UNIT SHUTDOWNS AND POWER REDUCTIONS Method of Licensee Shutting Event Down Reactor3 Report #

3.

Method:

1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)

4.

System Code4 Component Code6 Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)

Cause & Corrective Action to Prevent Recurrence DOCKET NO UNIT DATE COMPLETED BY TELEPHONE Safety Injection System Check Valve Leak and Repair

5.

Exhibit I - Same Source 50-255 Palisades 02/28/94..

MMVanWagner (616)764-8913

\\

'~

' 0

SUMMARY

OF OPERATING EXPERIENCE FOR FEBRUARY 1994 The pl ant began the month operating at 85% power.

Repairs were made to turbine control system and full power was reached at 2030, on February 2.

On February 17, at 1634, power reduction was commenced due to a check valve leak.

The turbine generator went off-line at 2118.

On February 18, at 0120, the reactor was manua 11 y tripped and pl aced in hot shutdown for check valve repairs.