ML18046A264

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IE Insp Rept 50-255/80-18 on 800901-1003.No Noncompliance Noted.Major Areas Inspected:Operational Safety,Maint, Surveillance,Facility Changes & Procedures
ML18046A264
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/31/1980
From: Boyd D, James Heller, Jorgenson B, Peschel J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18046A265 List:
References
50-255-80-18, NUDOCS 8012310433
Download: ML18046A264 (9)


See also: IR 05000255/1980018

Text

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-255/80-18

Docket No. 50-255

Licensee:

Consumers Power Company

212 West Michigan Avenue

Jackosn, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, MI

License No. DPR-20

Inspection Conducted:

September 1-5, 8-12, 15-19, 21-27, 29, 30,

and October 1-3, 1980

Inspectors:

f

Approved By:

B. L.

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Jorgefis~ri(_J CJ~

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D. C. Boyd, C~f,-

Reactor Projects, Section 4

Inspection Summary

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Inspection on September 1-5, 8-12, 15-19, 21-27, 29, 30 and October 1-3,

1980 (Report No. 50-255/80-18)

Areas Inspected:

Routine monthly resident inspection program activities

including; operational safety; maintenance; surveillance; facility changes;

procedures; plant trip; current regulatory items; followup on previously

identified items; and operator strike.

The inspection involved a total of

247 inspector-hours onsite by three NRC inspectors including 24 inspector-

hours onsite during off-shifts.

Results:

No items of noncompliance or deviations were identified in any

of the eight areas inspected.

1.

DETAILS

Persons Contacted

  • R. W. Montross, General Manager
  • J. S. Rang, Operations and Maintenance Superintendent
  • H. J. Palmer, Technical Superintendent

W. S. Skibitsky, Operations Superintendent

  • C. H. Gilmor, Maintenance Superintendent

B. L. Schaner, Operations Supervisor

K. M. Farr, Public Affairs Director

G. H. R. Petitjean, Technical Engineer

F. G. Butler, Senior Engineer

G. D. Gilbody, Quality Assurance Engineer

D. W. Kaupa, Shift Supervisor

W. Hodge, Property Protection Superintendent

Other members of the operations, maintenance and technical staffs

were also contacted briefly,

  • Denotes those present at management* interview October 3, 1980.

2.

Operational Safety Verification

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

month of September 1980.

The inspector verified the operability of

selected emergency systems, reviewed tagout records, and verified

proper return to service of affected components.

Tours of auxiliary

and turbine buildings were conducted to observe plant equipment condi-

tions, including potential fire hazards, fluid leaks, and excessive

vibrations and to verify that maintenance requests had been initiated

for equipment in need of maintenance.

The inspector by observation

and direct interview verified that the physical security plan was being

implemented in accordance with the station security plan.

The insepctor observed plant housekeeping/cleanliness conditions and

verified implementation of radiation protection controls.

During the

month of September 1980, the inspector walked down the accessible

portions of the auxi~iary feedwater and safety injection systems to

verify operability.

Minor housekeeping items were brought to the attention of the duty

Shift Supervisor for his action, as appropriate.

One item, involving the apparent malfunctioning of the closure mech-

anism on a door designated a plant fire barrier, was brought to the

attention of the fire protection specialist.

- 2 -

During walkdown of the auxiliary feedwater system using Feedwater

System Checklist CL 12.1, the Resident Inspector found valve 709 WS

had been changed as a result of a recent facility modification.

The

valve presently serves as an instrument isolation valve for auxiliary

feedwater suction header pressure instrumentation added by the refer-

enced modification.

Previously, the valve had served as a header vent

valve.

Thus, the proper operational condition for the valve is the open

position.

The valve was correctly positioned, and the checklist was

erroneous.

Review of the latest completed CL 12.1, performed in May 1980, shows

the auxiliary operator identified the proper position of the valve as

"open" and made a pen-and-ink change to the checklist; but a temporary

or permanent change was not subsequently made to follow up on the

operator's action.

This was discussed with the Operations Superintendent,

who committed to correct CL 12.1, and who stated problems of this type

had been previously recognized and were the basis for recent revisions

to the plant Administrative Procedures pertaining to checklists.

These

procedures now provide a method for handling checklist vs actual posi-

tion discrepancies which were reviewed by the inspectors and considered

adequate.

Thus, means are developed to correct checklist deficiencies

which may result from a modification to the facility such that a valve,

breaker, or other control acquires a changed service condition.

Means

to prevent such deficiencies by revising checklists and procedures at

the time of facility modification were also reviewed.

This area is not

now clearly controlled; which probably contributed to the inaccuracy

of CL 12.1 above.

This matter was discussed at the management interview.

The inspector also noted during walkdown of CL 12.1 that the auxiliary

feedwater pump suction valve from the condensate storage tank (133 FW),

which is located in a pit in the plant yard adjacent to the tank, was

under water.

This is properly identified on the checklist as a "locked-

open" valve, but the valve position could not be verified.

The licensee,

by letter dated December 11, 1979, in response to an NRC letter dated

October 30, 1979, concerning "Requirements for Auxiliary Feedwater Systems

at Palisades," committed to lock open valves in series with the auxiliary

feedwater pumps' section (which includes valve 133 FW) and to verify

monthly that such valves are in fact locked open.

Discussion with licensee

staff indicated the valve pit may be frequently flooded depending on local

weather, particularly heavy rainfall. It is unclear how the required

monthly valve position verification is made if the valve is submerged.

This was discussed at the management interview.

The inspector also witnessed portions of the radioactive waste system

controls associated with overpack of Urea Formaldehyde solidified waste,

barreling, and radwaste shipments .

- 3 -

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established

under Technical Specifications 10 CFR and administrative procedures.

No items of noncompliance or deviations were identified.

3.

Monthly Maintenance Observation

Station maintenance activities of safety related systems and components

listed below were observed/reviewed to ascertain that they were con-

ducted in accordance with approved procedures, regulatory guides and

industry codes or standards and in conformance with Technical Speci-

cations.

The following items were considered during this review; the limiting

conditions for operation were met while components or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by quali-

fied personnel; parts and materials used were properly certified; radio-

logical controls were implemented; and, fire prevention controls were

implemented.

Work requests were reviewed to determine status of outstanding jobs

and to assure that priority is assigned to safety related equipment

maintenance which may affect system performance.

The following maintenance activities were observed/reviewed:

safety-related snubbers-hydraulic oil addition

emergency diesel-motor preventive maintenance

Following completion of maintenance on the 1-1 emergency diesel-

generator and hyrdaulic snubbers noted above, the inspector verified

that these systems had been returned to service properly.

No items of noncompliance or deviations were identified.

4.

Monthly Surveillance Observation

The inspector observed Technical Specifications required surveillance

testing on the "B" boric acid pump, the low-pressure safety injection

(LPSI) pumps, and on selected snubbers, and verified that testing was

performed in accordance with adequate procedures, that test instru-

mentation was calibrated, that limiting conditions for operation were

met, that removal and restoration of the affected components were

accomplished, that test results conformed with Technical Specifications

and procedure requirements and were reviewed by personnel other than

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L

the individual directing the test, and that any deficiencies identified

during the testing were properly reviewed and resolved by appropriate

management personnel.

Problems were encountered in conduct of surveillance testing on the

LPSI pumps on September 18 and 19 in that the results seemed to

indicate precisely parallel miniflow rate degradation on both pumps.

The common* flow instrument (FI-0404) was not seriously considered

suspect in that it had given expected and consistent results on

testing of the containment spray pumps, showing no degradation.

Inadequate pump isolation, to assure only the miniflow path was

available, was theorized, in that the respective pump discharge

isolation valves were known to leak when closed.

Ultimately, the

test procedure was revised to base operability determination on pump

delta-pressure rather than flowrate via the miniflow path.

Results

from testing by the revised procedure were consistent with baseline

data and showed pump performance not degraded.

Flow data are still

being taken in an attempt to determine why miniflow is decreasing.

No items of noncompliance or deviations were identified.

5.

Facility Change

Selected facility modifications/design changes were reviewed during

this inspection to verify proper review and approval (including

adherence to the requirements of 10 CFR 50.59); to verify installa-

tion in accordance with the approved design; and to verify completion

of appropriate testing and revisions to procedures and drawings.

Identification and use of codes and standards governing modification

work was examined, as were acceptance testing and overall record-

keeping.

The following packages were specifically examined.

FC 468-5 -

FC *379B -

Change of power supply for containment pressure

instrumentation to a Class I-E source

Overhaul and "beefing-up" of MSIV internals

A potential problem relating to procedure and checklist revision as a

result of facility modifications is discussed in Paragraph 2, above.

No items of noncompliance or deviations were identified.

6.

Procedures

Several licensee procedures were examined during this inspection to

determine technical adequacy; consistency to license requirements;

and proper development, review, approval and revision.

The following categories and procedures were specifically reviewed

during this inspection:

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a .

General Plant Operating Procedures (GOP's)

(1)

GOP-2

(2)

GOP-8

Plant Heat Up (cold shutdown to hot

standby)

Plant Shutdown to Hot Standby/shutdown

b.

System Operating Procedures (SOP's)

c.

d.

e.

f.

(1)

SOP-1

Primary Coolant System

(2)

SOP-7

Main Steam System

(3)

SOP-16

Component Cooling Water System

(4)

SOP-15

Service Water System

(5)

SOP-19

Service and Instrument Air System

(6)

SOP-36

Reactor Protective System

Step 6.1.1.1 of SOP-1 references primary coolant system checklist

CL 1.1.

A copy of CLl.l was found in the shift supervisor's

check list file, which is a "controlled" file, lacking an approval

signature or initials on page 5 of 13, as apparently required by

administrative procedure 10-1, Appendix C-4.

This was identified

to the licensee for review and correction.

Off Normal Procedures (ONP's)

(1)

ONP-1

Loss of Load

(2)

ONP-5

Control Rod Drop

(3)

ONP-12

Acts of Nature

(4)

OPN-14

Loss of Condenser Vacuum

(5)

ONP-17

Loss of Shutdown Cooling

(6)

ONP-23

Primary Coolant Leak

Permanent Maintenance Procedures

(1)

Procedure No. PCS-M-1

(2)

Procedure No. CCS-M-1

(3)

Procedure No. MSS-M-1

(4)

Procedure No. SWS-M-1

(5)

Procedure No. RPS-I-2

Emergenc~ 0Eerating Procedures (EOP' s)

(1)

EOP-1

Reactor Trip

(2)

EOP-5

Loss of Instrument Air

(3)

EOP-8.1

Loss of Coolant Accident

(4)

EOP-11

Loss of Containment Integrity

Administrative Procedures

(1)

Operations Administration

(2)

Plant Security

- 6 -

A review was also conducted covering review and approval of procedure

revisions and associated recordkeeping.

Plant Administrative Proce-

dures, Section 3, addresses these matters, providing for review via a

PRC/QA review form (QA-05).

The QA-05 form, supporting documents and

Safety Evaluations are to be maintained in a "QA-5 file".

The licensee's

QA-05 file, however, has not been maintained since 1978.

Rather, the

review records are being kept with the Plant Review Committed (PRC)

meeting minutes.

This was discussed at the management interview.

The licensee's Administrative Procedures, Section 3, and 10 CFR 50.59,

do not differentiate handling of procedure revisions from facility

modifications or from tests and experiments insofar as the review pro-

cess and recordkeeping are concerned.

In practice, the licensee utilizes

a Safety Evaluation form in review of facility modifications and tests/

experiments but not in review of procedure revisions.

This Safety

Evaluation provides details concerning why a review item does or does

not involve an unreviewed safety question as defined in 10 CFR 50.59.

The QA-05 form, which is used in all cases, provides simply for a Y (yes)

or N (no) determination by the reviewer concerning identification of

unreviewed safety questions, without addressing why.

A further requirement

of 10 CFR 50.59 involves maintaining records of selected reviews (including

certain procedure changes), to include a written safety evaluation which

provides the basis for the determination that the change in question does

not involve an unreviewed safety question.

It is not clear that the QA-05

review alone is adequate for this purpose, and licensee compliance to

10 CFR 50.59 for review and recordkeeping relating to selected procedure

changes is considered an Unresolved Item.

This matter will be reviewed

further during a future inspection; and it was discussed at the Management

interview.

No items of noncompliance or deviations were identified.

7.

Plant Trip

Following the plant trip at 0238 hours0.00275 days <br />0.0661 hours <br />3.935185e-4 weeks <br />9.0559e-5 months <br /> on September 28, 1980, the

inspector was contacted by the licensee.

He ascertained the status

of the reactor and safety systems by discussions with plant personnel

and verified proper .communications and immediate licensee actions.

The reactor and turbine were manually tripped from about 82% power

immediately after a DC electrical ground caused an erroneous speed

control signal which led to the sudden closure of all the turbine

intercept valves.

All plant systems responded as designed, and the

plant was returned to operation, later the same day following repair

of the faulty electrical condition.

No items of noncompliance or deviations were identified.

- 7 -

, *

8.

Current Regulatory Matters

Licensee adherence to the stipulations of two Immediate Action Letters,

both involving auxiliary feedwater flowrates as they affect steam

generator level and avoidance of water hammer, was verified during

this inspection.

The first IAL, dated August 26, 1980 also provided

a 55% maximum power level, which was observed by the licensee and

verified by the inspector.

The second IAL, dated September 4, 1980,

superceded the first and provided an 83% maximum power level.

This

was also observed by the licensee as verified by the inspector.

Power level restrictions were removed by an NRC letter effective

September 30, 1980.

Selected procedure changes and operator training

related to removal of power level restrictions were completed as

required and reviewed by the inspector.

The licensee will continue

an evaluation of means to mitigate or eliminate the potential for

water hammer and provide the evaluation results and plans for future

NRC review.

No items of noncompliance or deviations were identified.

9.

Action on Previously Identified Matters

(Closed) Unresolved Item, IE Inspection Report No. 50-255/79-07

Inservice testing acceptance criteria for ESF pumps.

The licensee has requested and received NRC approval for

modification of Technical Specifications to incorporate ASME

Section XI; in part; and certain exemptions/exceptions have

also been approved.

The licensee is not required to use both

flow and delta-pressure measurements in determining operability

of ESF pumps .

10.

Operator Strike

On September 12, 1980, a "wildcat strike" involving plant operations,

maintenance, and construction personnel occurred; lasting slightly

over two hours after the scheduled 0800 hour0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> shift-change.

The

inspector verified proper shift staffing, which was maintained by

holding-over the off-going shift.

Licensee contingency plans for

coping with a potentially longer-duration strike were also reviewed.

No items of noncompliance or deviations were identified.

11.

Unresolved Items

Unresolved items are items for which additional information is required

to make a determination whether the item is a clear item, an item of

noncompliance, or a deviation.

An unresolved item identified during

the course of this inspection is discussed in Paragraph 2 above .

- 8 -

12.

Management Interview

A management interview (attended as indicated in Paragraph 1) was

conducted following completion of the inspection.

The following

items were discussed with licensee responses as indicated.

a.

The inspectors summarized the scope and findings of the inspection.

b.

Proper followup on procedures and checklists, to complete revisions

required as a result of facility modifications, was discussed.

(Paragraph 2)

c.

The inspectors questioned the means by which the position of an

occasionally submerged valve had been and will be verified.

The

licensee agreed to look into the matter.

(Paragraph 2)

d.

The testing evolution and problems experienced in verifying LPSI

pump operability were discussed.

(Paragraph 4)

e.

The inspector identified the apparent inconsistency between

practice and procedure as related to the keeping of a "QA05

file." The licensee agreed to clarify this.

(Paragraph 6)

f.

The inspectors stated the Unresolved Item relating to record-

keeping under 10 CFR 50.59.

The licensee pointed out the QA-05

definition of "unreviewed safety questions" printed thereon, for

use in making reviews involving this determination.

(Paragraph 6)

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