ML18044A925
| ML18044A925 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 05/12/1980 |
| From: | CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| References | |
| NUDOCS 8005210666 | |
| Download: ML18044A925 (8) | |
Text
5o -JlJ CENTRAL FlLES 5)1~/efJ PALISADES END-OF-YEAR REPORT 1977 A.
Significant Events B.
The plant operated routinely during 1977 with the exception of routine maintenance items and three occurrences caused by loss of offsite power to the plant in September (LER 77-47), November (LER 77-55), and December (LER 77-58) due to a single lockout relay malfunction on the "R" (345 KV) bus supplying the plant from the switchyard.
The apparent safety concerns were forwarded to Headquarters for review.
The plant received authorization to increase power from 2200 MWt to 2530 MWt on November 1, 1977.
The plant performed the required testing and increased power to 2530 MWt on November 6, 1977.
The licensee has commenced the spent fuel pool (safety related) modifications and the addition of*a full flow condensate polishing system (nonsafety related).
Both the major modifications are due to by completed in 1978.
Noncompliance Cited
- 1.
Violations 0
- 2.
Infractions
- a.
Operations 12
- b.
FF&MS 6
- c.
Construction 0
- d.
Security/Safeguards 1
Total 19
- 3.
Deficiencies
- a.
Operations 4
- b.
FF&MS 3
- c.
Construction 0
- d.
Security/Safeguards 7
Total 14
- 4.
Sanction Points 218
--p s 0062106 66
i' Palisades
.5.
- Types of Noncompliance
- a.
- b.
- c.
- d.
- e.
- f.
- g.
Total Failure to follow procedures Inadequate procedures Inadequate maintenance failure to approve procedures Failure to report as required Inadequate management Casual factor - not specific Security/Safeguards (1)
Inadequate plans and procedures (5)
(2)
Failure to follow procedures (2)
(3)
Inadequate maintenance (1) 9 7
1 1
4 3
8 33 C.
Inspector's Evaluation of Licensee Performance The overall performance of the Palisades plant appears to be satisfactory; but with noted areas requiring improvement:
- 1.
Full implementation of training and retraining for all plant personnel during 1978 (excluding licensed personnel training).
- 2.
Continuing pursuit of the many outstanding maintenance items which detract from the overall maintenance program.
(Discussed at the management meeting in October 1977.)
- 3.
Overall management controls appear to need improvement.
- a.
During the period of August 13-16, 1977, the plant continued to be operated even though the containment purge exhaust valve leakage exceeded the allowable (La).
(Discussed at the manage-ment meeting in October 1977.)
- b.
During the repair of the containment exhaust purge valve, the seat was sealed with an unauthorized sealant to reduce the leakage and no *safety evaluation was provided in accordance with 10 CFR 50.59.
(Discussed at the management meeting in October 1977.)
- c.
The essential instrument bus Y-01 was powered from the emergency bus without a safety evaluation as required by 10 CFR 50:59.
Palisades 3 -
- d.
Safety related surveillance procedures were modified in late 1976 and a Technical Specifications requirement was overlooked and not performed until November 1977, subsequent to an NRC audit.
- e.
The safety injection tank level switches were not maintained in the operable status resulting in the loss of water level in one tank for an indeterminate period of time.
- f.
The iodine removal system was placed into service without adequate assurance that the system was fully operational and subsequent to direct questioning by the NRC inspector, the system was discovered in the degraded mode.
- g.
The licensee continues to fail to meet commitments.
The commitment date for completion of corrective actions concerning plant 'Security training and retraining passed without completion.
The item remains open and the item of noncompliance will be closed during 1978.
- h.
The number of significant personnel errors at the plant are a continuing problem, as noted in the next section of this report.
These items specifically detract from the plant performance.
Also, the items of noncompliance concerning personnel errors and inadequate management controls are negative indicators to an operating plant.
D.
Personnel Errors No significant personnel errors occurred resulting in an event which had the potential to significantly affect the health and safety of the public.
The routine inspection requirements revealed no significant personnel errors which resulted in an event which had the potential to significantly affect the public.
Several licensee events reported were attributed to personnel errors.
- 1.
ER 77-08
- 2.
ER 77-23 1/17/77 4/19/77 Following feedwater pump trip, operator attempted to avert reactor trip by manually running in control rods, but did not switch mode selector from auto to manual resulting in one rod being driven in below the group.
Waste gas decay tank overpressured and while isolated, tank loss in violation of TS limits.
Palisades
- 3.
ER 77-25
- 4.
ER 77-31
- 5.
ER 77-35
- 6.
ER 77-40
- 7.
ER 77-51
- 8.
ER 77-52
- 9.
ER 77-63 5/19/77 5/26/77 7 /9/77 8/18/77 9/27 /77 10/26/77 12/22/77 Backup heat tracing circuit for borated lines inadvertently left deenergized for 40 days.
Primary coolant system checks revealed unidentified leakage.
Inadvertent chlorination of service water system instead of "B" cooling tower.
The T-82C SI tank was partially drained on 8/17/77 for instrument maintenance.
Tank not properly refilled.
(See LERs 29, 24 and 36.)
Security door power source shifted to emergency diesel generator without a 50.59 review.
E~ergency diesel generator 1-1 not verified to be operable prior to removing EDG 1-2 from service~
The iodine removal system (hydrazene) was placed into service with the circuit to one of the hydrazene tank outlet valves inoperable.
- 10.
ER 77-64 12/1/77 HPSI pump removed from service without functionally testing the other HPSI pump to verify operability.
E.
Sununary of Unplanned Radioactive Releases Two events occurred during the year resulting in unplanned released.
- 1.
Event Report 50-255/77-23, 4/19/77, was issued as a result of a small release of radioactive gas from a waste gas decay tank due to personnel error.
The release was not detectable on the stack gas monitoring system and the calculated release was approximately 3.6 Curies of gas; primarily Xenon 133.
(IE Inspection Report No. 50-255/77-13)
- 2.
Event Report 50-255/77-56, 11/29/77, was issued as a result of a small release of radioactive gas subsequent to the tripping of the main exhaust fans during a normal release activity.
The release was 5.2 millicuries total; 0.088 microcuries of 1-131.
The procedures have been subsequently revised to assure cessation of a gaseous release when the main exhaust fans trip.
(IE Inspection Report No. 50-255/77-18)
Palisades F.
Number and Character of Reportable Events A total of 53 events were reported by the plant:
(1) no event involved an actual significant event jeopardizing the public; (2) 12 events are considered preventable; (3) 22 additional events are considered of significance; (4) 19 events are considered insignificant and are for reporting/tracking failures; and (5) 19 events were prompt reports.
Preventable Potential degradation of a safety related system Potential for exceeding a~'
safety limit Loss of a portion of a safety related system or engineered safeguard Breakdown in management - controls which could have resulted in a degraded plant safety system TOTAL Others Personnel Error 7
1 1
1
. 10 Deficient Procedures Total 2
9 1
1 1
2 12 External.
Component Failure Design Deficiency Other Total Potential degradation of a safety system Reduction in effectiveness of a safety or safeguards system TOTAL The other nineteen reportable events were minor in nature and were issued to meet reporting requirements, generally.
13 1
3 16 1
5 4
4 18 1
4 5
22 10 19
Palisades G.
Summary of Inspections Rpt No.:
77-01 Onsite Hrs: 98 Inspectors:
4 Type:
FF&MS (Env)
IDfraction Contrary to Sections 3.9.9 and S-1.1 of the Technical Specifications, plant discharge temperature increases greater than 5°F and/or effluent heat rate greater than 0.5 billion Btu/hr were exceeded on 15 occasions.
Infraction - Contrary to TS 3.9.6, chlorine discharge exceeded.02 ppm.
Rpt No.:
77-02 Onsite Hrs:
51 Inspectors: 1 Type:
RIP Deficiency - Contrary to Technical Specification 6.9.2.b.(2), the operation of the fa~ility in excess of the limits of Specification and Table 3.18.1 but for a period less than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> was not reported within 30 days to the NRC.
Rpt No.:
Deviation Deviation 77-03 Onsite Hrs:
87 Inspectors: 1 Type:
- Housekeeping and cleanliness controls (QAPP-2).
- Implementation of corrective system (QAPP-16).
Rpt No.:
77-04 Onsite Hrs:
86 Inspectors: 2 Type:
FF&MS (Rad)
Infraction - Contrary to 10 CFR 20.20l(b), evaluations of whole body Deficiency counts of 4 individuals during 1976 were not adequate to demonstrate compliance with 10 CFR 20.103.
Contrary to 10 CFR 19.ll(d), the documents posted pursuant to 10 CFR 19.ll(b) were not visible to workers engaged in licensed activities.
Rpt No.:
77-05 Onsite Hrs:
36 Inspectors: 1 Type:
FF&MS (Env)
Deficiency - C6ntrary to Technical Specification 6.8.1.d, Sections 2.24.5.3 and 2.24.5.4 of procedure HP 2.24, which require documentation of an inventory~ were not completed.
Deficiency - Contrary to Technical Specification 6.8.1.d, Section 2.6.5.1 of procedure HP 2.6 was not performed.
Rpt No.:
77-06 Onsite Hrs:
51 Inspectors: 2 Type:
FF&MS (Env)
Infraction - Contrary to Section 3.9.6 of Technical Specifications, residual chlorine in water discharged to the.lake was excessive.
Infraction - Contrary to Section 6.9.2.a.(2) of Technical Specifications, a verbal report was not made within the required 24-hour period for an occurrence.
Infraction - Contrary to Sections 3.9.9 and S-1.1 of the Technical Specifications, plant discharge temperature increases greater than 5°F were exceeded on 15 occasions.
Palisades 7 -
Rpt No.:
77-07 Onsite Hrs:
97 Inspectors: 2 Type:
Safeguards Infraction - Contrary to Section F, subparagraph 2.1 of the approved Palisades Nuclear Power Plant Security Plan, the integrity of the 8 foot chain link fence was allowed to deteriorate.
Deficiency - Contrary to 10 CFR 73.55(b)(2), the method of transferring authority from person to person has not been established.
Deficiency - Contrary to 10 CFR 73.55(d)(5), picture badges for individuals not employed by the licensee but who require frequent and extended access to protected and vital areas do not indicate the period for which access has been authorized.
Deficiency - Contrary to 10 CFR 73.55(g)(2), certain intrusion alarms are not tested for performance at the beginning and end of a period for which they are used for security.
Deficiency - Contrary to 10 CFR 73.70(d), a log indicating the reason for entry and the time of exit of all individuals grated access to a normally unoccupied vital area was not being maintained.
Deficiency - Contrary to 10 CFR 73.55(d)(3), a package was not searched for explosives, and/or incendiary devices prior to admittance into the protected area.
Deficiency - Contrary to 10 CFR 73.55(d)(4), the licensee did not exercise positive control over designated vehicles to assure that they were used only by authorized persons and for authorized purposes.
Rpt No.:
77-08 Onsite Hrs:
18 Inspectors: 2 Type:
Safeguards Deficiency - Contrary to 10 CFR 70.Sl(c), the record of fuel assemblies in one of your. SNM Inventory Books appears not to have been maintained on a current basis.
The records did not indicate the correct current core location of several fuel assemblies.
Rpt No.:
77-09 Onsite Hrs:
43 Inspectors: 1 Type:
Operations Infraction - Technical Specification 6.8.3 states, "Temporary changes to procedures of 6.8.1 above may be made provided:
A.
The intent of the original procedure is not altered." Contrary to this, procedure changes were made which changed the intent of the procedures.
Infraction - Contrary to Technical Specification 6.8.1, zero power physics tests were conducted, procedures were not implemented.
Rpt No.:
77-10 Onsite Hrs:
44 Inspectors: 1 Type:
Operations Rpt No.:
77-11 Onsite Hrs:
63 Inspectors: 1 TYPe:
RIP Infraction - Contrary to Technical Specification 3.6.1.a, the facility was operated without containment integrity wh~n leakage through the containment purge exhaust valves exceeded La*
Infraction - Contrary to Technical Specification 6.8.1.a, repairs were being conducted to CV-1805 without a maintenance procedure.
Infraction - Contrary to 10 CFR 50.59, a change was made to the facility without performance of a written safety evaluation.
Infraction - Contrary to Technical Specification 3.9.8, chemicals were.
released to the lake without prior neutralization.
Deficiency - Contrary to Technical Specification 6.9.2.a.(2), exceeding Technical Specifications limits on safety injection tank T82c level was not reported as required.
.~ <
Palisades
- Rpt No.:
77-12 Onsite Hrs:
15 Inspectors: 2 Type:
Operations Rpt No.:
77-13 Onsite Hrs:* 87 Inspectors: 2 Type:
FF&MS (Rad)
Infraction - Contrary to 10 CFR 71.3, Type B quantities of byproduct material were delivered to a carrier for transport on two occasions without authorization by the NRC.
Rpt No.~
77-14 Onsite Hrs:
73 Inspectors: 1 Type:
RIP Infraction - Instrument drift which resulted in operation outside of TS was not promptly reported and followed up with a written report within 14 days.
Deficiency - Three procedures were not fully implemented:
(a) Pipe and tubing in storage not capped; (b) Personnel performing QA receipt inspections reported to organization other than the one identified in QA program policy; and (c) Security training not documented.
Rpt No.:
77-15 Onsite Hrs:
4 Inspectors:
1 Type:
Safeguards Rpt No.:
77-16 Onsite Hrs:
34 Inspectors:
4 Type:. Ops - Mgt Rpt No.:
77-17 Onsite Hrs:
33 *inspectors:
1 Type:
Operations Infraction - SI and containment spray pumps were not alternately started from the control room and locally during surveillance tests.
(TS 4.6.3)
Deficiency - All violations of TS were not reviewed by PRC.
Rpt No.:
77-18 Onsite Hrs:
25 Inspectors:
1 Type:
Operations Infraction - The "B" high pressure SI pump was removed from service without the "A" SI pump being tested for operability.
Infraction - The security door locks were put on emergency power without first conducting a 50.59 review.
Infraction - The 1-2 emergency diesel generator was removed from service without first testing the other diesel generator.
Infraction The plant was operated with the iodine removal system in a degraded mode in excess of the allowed 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
Rpt No.:
77-19 Onsite Hrs:
4 Inspectors:
2 Type:
FF&MS (EP)