ML18043A315
| ML18043A315 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 12/04/1978 |
| From: | Bollnow D CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML18043A314 | List: |
| References | |
| NUDOCS 7812110125 | |
| Download: ML18043A315 (4) | |
Text
OPERATING DATA REPORT OPERA TING STATUS.*
- 1. Unit Name:
Palisades Notes
- 2. Reporting Period:
- 3. Licensed Thermal Power (MWt):
- 4. Nameplate Rating (Gross MWe):
781101 - 781130 2530 811. 7
- 5. Design Electrical Rating (Net MWe): _______......::,8.::.0.::.5_
- 6. Maximum Dependable Capacity (GrossMWe):
- 6 7 5
- 7. MaximumDependableCapacity(NetMWe):
- 635 DOCKET NO.
DATE COMPLETED BY TELEPHONE 50-255 12-4-78 DIBollnow 616-764-8913
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
(
- 9. Power Level To Which Restricted, If Any (Net MWe):
. 10. Reasons For Restrictions, If Any:
- 11. Hours In Reporting Period
- 12. Number Of Hours Reacfor Was Critical
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator On-Line
- 15. Unit Reserve Shutdown Hours This Month 720 674.4 674.3
- 16. Gross Thermal Energy Generated (MWH) 1,683,216
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH)
- 19. Unit Service Factor 518,440 491,241 93.7
- 20. Unit Availability Factor 93.7
- 21. Unit Capacity Factor (Using MDC Net).
107
- 4
- 22. Unit Capacity Factor (Using DER Net) 84
- 8
- 23. Unit Forced Outage Rate 6.4
. Yr.-to-Date 8,016 4,322.2 3,957.1 8,593,776 2,544,930 2,379,924 49.4 49.4 46.8 36.9 24.1
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date. and Duration of Each):
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation):
INITIAL CRITICALITY
- INITIAL ELECTRICITY COMMERCIAL; OPERATION.
- - Based on Condenser Backpressure Limitations 78121101R_)
Forecast
...,.. ~--~"'r*,__.,.._...,._'""*-*--'----------------'--
Cumulative 60,927.
33.721.6 31;789.3' 58,615,440 18,131,540 16~993,291 52.2 52.2 43.9
. 34*. 7 38.8 Achieved
('ci/77)
Date 25 781129 F: Forced S: Schcd ulcd I
L (9/77)
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT ~fONTH November 1978
- 11)
- 0.
I-F Reason:
45.7 A
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatury Restriction 1
Licensee Even!
Report :ff None E-Operator Training & License Examination F-Administralive G-Operational Error (Explain)
I I-Other (Explain) 3 Method:
1-Manual t::
'1JV) t::
- 11) 0 "O
- 0. ';)
Eu 8
2-Manual Scram.
3-Automatic Scram.
4-0lher (Explain)
DOCKET NO.
50-255 UNIT NAME DATE COMPLETED BY TELEPHONE DIBollnow 616-764-8913 Cause & Corrective Action to Prevent Recurrence Repair of leaking.CRDM Seals 4
5 Exhibit G
- Instructions for Preparation of Data Entry Sheets fur Licensee Event Report (LER) File (NUREG-0161)
Exhibit I* Sam~ Sour~~
(:~
- ~
e AVERAGE DAILY UNIT POWER LEVEL MONTJi Novemher 1978 DAY' A VERA GE DAILY POWER LEVEL (MWe-Net) 732 2
727 719.
3
- 4.
720 5
658
- 6.
726 741..
7 8*
725 9
725 732 IO 728 11 12 739 13 721 737 14 15 743 16 743 INSTRUCTIONS DAY 17 18 19 20*..
21 22 23 24 25 26 27 28 29 30 31 DOCKET NO.
UNIT DATE COMPLETED BY 50-255 Palisades 12-4-78 DIBollnow TELEPHONE 616-764-8913 AVERAGE DAILY POWER LEVEL (MWe-Net) 717 729 740 748 739 744*
737 745:.
743 748 742 714 27 0
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
- --***---*-**w-*-**--***-*****'-**--*-***-*--**--** * *------
CONSUMERS POWER COMPANY Palisades Nuclear Plant Docket 50-255
SUMMARY
-OF OPERATING EXI>ERIENCE FOR NOVEMBER 1978 During November the; Plant*. ope.rated* nearly continuously at 100% power until required to. s~utciown on.. Novemb~r 2 9 in order t9 repai;t" CRDM seals..
At the end of the month, this outage, which was scheduled to last twelve days, had been in progress for 45.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />.