ML18036A500

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Insp Repts 50-259/91-41,50-260/91-41 & 50-296/91-41 on 911116-1215.Violation & Deviation Noted.Major Areas Inspected:Surveillance Observation,Maint Observation, Operational Safety Verification & ROs
ML18036A500
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/09/1992
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036A497 List:
References
50-259-91-41, 50-260-91-41, 50-296-91-41, NUDOCS 9201270181
Download: ML18036A500 (34)


See also: IR 05000259/1991041

Text

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UNITEO STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns

Fe. ry Site near Decatur,

Alabama

Inspection

Conducted:

November

16 - December

15,

1991

Inspector:

C. A.

P

Inspector

Accompanied

by:

E. Christnot, Resident

Inspector

W. Bearden,

Resident

Inspector

R.

Ber hard, Project Engineer

Report Nos.:

50-259/91-41;

50-260/91-41,

and 50-296/91-41

(

z

Dat

S gned

Approved by:

Paul J.

ogg;

>e

Rea tor

'

ion 4A

Division of Re ctor Projects

Da

e S'gned

SUMMARY

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety verification,

power

ascension

test

report

review, corrective

action

program,

Unit

3

restart

activities,

contractor

control,

reportable

occurrences,

action

on previous

inspection

findings,

and nuclear safety

review

board.

Results:

A violation and deviation, were identified concerning

the control of

contractor

work activities.

The violation was for failure to have

adequate

design

control- of a site telecommunications

subcontractor,

paragraph

eight.

A site

procedure

to control

these activities

was

not utilized.

Significant quantities

of missing

doc'umentation

for

work performed

to implement

a design

change

was identified

by the

site quality organization.

A stop work order was issued.

(y 10f 70j8i 92010~

pDR

@DOCK

8

The deviation

was from a reply to

a previous violation concerning

the

removal of fire wrap,

paragraph

seven.

To better control contractor

activities,

walkdowns

were to

be

resumed

using

a

phased

approach.

The construction contractor

performed safety re1ated

work but was not

authorized

to perform

the

work.

The contractor

had

only

been

authorized

to perform

non safety related

work such

as scaffolding.

This

was

identified

by

the site quality organization.

Work

activities were stopped

to correct the problem.

All remaining operational

readiness

assessment

team

open items,

the

power

ascension

test

report,

one

licensee

event

report,

one

unresolved

item,

one

inspector

followup item,

and five violations

were closed.

REPORT

DETAILS

Persons

Contacted

Licensee

Employees:

0. Zeringue,

Vice President,

Browns Ferry Operations

  • H. McCluskey, Vice President,

Browns Ferry Restart

  • J. Scalice,

Plant Manager

  • J. Swindell, Restart

Manager

N. Herrell, Operations

Manager

  • J. Rupert, Project Engineer
  • N. Bajestani,

Technical

Support Manager

R. Jones,

Operations

Superintendent

A. Sorrell, Maintenance

Manager

'~G. Turner, Site (}uality Assurance

Manager

R. Baron, Site Licensing Manager

"J. McCarthy, Unit 3 Licensing

  • P. Salas,

Compliance Supervisor

  • J. Corey, Site Radiological Control Manager

A. Brittain, Site Security Manager

Other

licensee

employees

or contractors

contacted

included

licensed

reactor

operators,

auxiliary operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • E. Christnot,

Resident

Inspector

  • M. Bearden,

Resident

Inspector

R.,Bernhard,

Project Engineer

"Attended exit interview

Acronyms

and initialisms

used

throughout this report

are listed in the

last paragraph.

Surveillance Observation

(61726)

The inspectors

observed

and reviewed the performance of required SIs.

The

inspections

included

reviews

of the

SIs for technical

adequacy

and

conformance

to

TS,

verification

of test

instrument

calibration,

observations

of the conduct of testing,

confirmation of proper

removal

from service

and return to service of systems,

and reviews of test data.

The inspectors

also verified that

LCOs were met, testing

was accomplished

by qualified personnel,

and

the SIs

were

completed within the required

frequency.

A review of the

TS surveillance

requirements

and the plant's

progr'am for

ensuring

implementation

of the

requirements

was

performed.

SSP-8.2,

Surveillance

Program,

Revision 0,

dated

September

13,

1991

and 2-SI-1,

Surveillance

Program,

Revision 7, dated

August 23,

1991 were

compared

to

the

requirements

of the Unit

2

TS with an effective

page list dated

November

5,

1991.

Over 700 requirements

were

compared to 2-SI-1 to insure

the

TS

were

implemented

in the

program.

From the review,

over

30

questions

were generated

for further inspection.

The

30 questions

were

discussed

with individuals in work control

who implement the program

and

the

engineer

responsible

for maintaining

2-SI-1.

The questions

were

resolved or action initiated to address

them.

From the review the following observations

were made.

~The

high on-time completion

rate of SIs at

BFNP

seems

to be the

result of manpower

loading of SIs before other work items,

the high

visibility the Sls

have at the

Plan of the

Day meetings,

and

the

planning of SI work activities;

2-SI-l, which lists the'SI requirements,

is 'updated

every six months.

Changes

to the SI are

made through submission of a Form SSP-158,

SI-1

Surveillance

Program

Change

Form.

The

system

engineer

uses

the

normal procedure for plant procedure

changes

to implement the SSP-158

changes

at the SI-1 update interval.

It was

noted that

a tracking

system

to insure

SSP-'158

incorporation

does

not exist.

SI-1 is

current only when all outstanding

SSP'-158s

are also considered.

It

is not currently possible

to determine

SI-1 status

due to lack of

tracking of SSP-158s.

The current revision of SI-1 reflects

the

former practice of using

PMI-35 forms from the superseded

PMI-17.12.

SSP-8.2

indicates

SSP-158s

are

gA records

with lifetime retention,

but does

not indicate

how to track them.

In addi tion, SSP-2.3,

Administration of Site Procedures,

Form SSP-23,

Procedure

Verification Review Checklist,

Step

33 is not specific

enough to ensure

SI changes

that impact frequency,

scope

changes

or

name

changes

generate

an SSP-158.

The

TS have

requirements

to verify initiating logic or control logic

in Table 4.2.8.

Many of the logic functions are recognized

in TS as

being functionally verified as part of a channel

check or some other

TS required test.

SI-1 does

address

these functions in its listings,

however the SIs that are

performed to meet the logic function do not

indicate that their function is also to confirm the

system logic.

The inspector

reviewed several

SIs

and did not find marked acceptance

criteria indicating system logic function was verified.

In addition,

these

SIs did not indicate

which other SIs, if multiple SIs are

needed

to verify system logic, are'eouired

to complete

the test

requirement.

Some

typographical

errors

were

noted

in SI-1.

In addition, four

entries

in Attachment

2 indicated

"Instrument

Channel"

when the

TS

did not.

The system engineer

was notified of the discrepancies

and

will correct

them on the next procedure revision.

Attachment

2 of 2-SI-I indicated

a frequency of "12 M" for 4.2.F'-2.

A TS

change

made

the frequency

"6 M".

No SSP-158

was found.

No

changes

to the SIs were required

as they were already

performed at

6

month intervals.

TS changes

may result in the

need for SSP-158s

to

be generated if SI-I is impacted,

but no other

SI change is required

that would generate

one via the SSP-23

review.

l

Interviews with gA indicated

a periodic comprehensive

audit comparing

the

TS to SI-I is not performed.

The current

program divides the SI

audits

by responsible

organizations

and

checks that each

groups

SIs

at the time of the organization's

audit=.

While verifying, SI-4.7.A.3.b met the

TS requirements,

the inspector

discovered

the

SI manually

cycled

the

vacuum

breakers

prior to

verifying their setpoint.

The

vacuum

breakers

setpoint

should

be

determined

"as found" to give

an indication if they would operate

properly if required.

The system engineer

is processing

a procedure

change to correct this.

No violations

or

deviations

were

identified

in

the

Surveillance

Observation

area.

3.

Yiaintenance

Observation

(62703)

Plant

maintenance

activities

were

observed

and

reviewed for selected

safety-related

systems

and

components

to

ascertain

that

they

were

conducted

in accordance

with requirements.

The following items

were

considered

during

these

reviews:

LCOs maintained,

use .of approved

procedures,

functional testing and/or calibrations

were performed prior to

returning

components

or

systems

to service,

gC

records

maintained,

activities accomplished

by qualified personnel,

use of properly certified

parts

and

materials,

proper

use

of

clearance

procedures,

'and

implementation of radiological controls

as required.

Work documentation

(NR,

WR,

and

WO) were reviewed to determine

the status

of outstanding

jobs

and

to

assure

that priority was

assigned

to

safety-related

equipment maintenance

which might affect plant safety.

The

inspectors

observed

the following maintenance

activities

during this

reporting period:

a.

Teflon Tape

The inspector

continued

to review the licensee's

program for control

of usage

of teflon tape.

Teflon tape

is

a potential

problem in

applications with stainless

steel

due to breakdown of the teflon into

fluorine with excessive

temperatures

and radiation

exposure.

The

inspector

determined

that at

BFNP teflon tape is controlled

as

a

special-issue

chemical

in accordance

with Site Standard

Practice

SSP

13.2,

Chemical Traffic Control

Program.

SSP - 13.2 recently

replaced

SDSP

-

24.2

which

provided

previous

guidance

and

requirements.

SSP - 13.2,

paragraph

3.5. 11 requires

the site

C

8

E

Superintendent

or designee

to sign all requisition form 575Ns for all

special

issue

chemicals

such

as teflon tape.

SSP - 13.2 further

requires

the

C

IW

E

Superintendent

or

designee

to routinely

investigate

usage

of special

issue

chemicals

and provides

special

requirements

for use of chemicals

by contractors

working onsite.

The inspector

requested

the licensee

provide

a listing of all recent

issuance

of teflon

tape

to. craft personnel.

From this

computer

listing (power stores

transaction

history) the inspector

determined

that teflon tape

had

been

issued

on four separate

occasions

during

1991.

Those

issuances

involved

a total of 22 spool's of tape.

The

inspector

then

reviewed

the four Form

575Ns

associated

with these

transactions

and

noted

that

each

had

been

cosigned

by

a

representative

of the chemistry section

and that issuance

of teflon

tape

appeared

appropriate

for these

specific work activities.

The

work performed

under the four referenced

work orders

were performed

on sewage

treatment,

hypochlorite injection or other systems

that did

not connect to the

RPV.

The inspector

concurred with the licensee's

determination

that

these

examples

of teflon tape

issuance

were

authorized

usage.

b.

Unit I/2 A Diesel

Generator

Outage

, The

inspectors

followed licensee

activities

associated

with the

scheduled

outage

on the Unit 1/2

A D/G.

This outage

was planned to

start

on December 8,

1991,

and involved the performance of the annual

and six year

inspection of the diesel

engine

and generator.

The

inspector

noted

that

the

licensee

entered

LCO 2-91-312-3.9.B.3

at

5:35

a.m.

on

December

8,

1991,

which required

that the

D/G

be

.returned

to operable

status within

7 days.

The D/G was

removed from

service

under

Hold Order 0-91-0840.

However the licensee

was unable

to perform any of the planned activities

due to an unplanned

scram

which occurred

on December

9,

1991.

The

D/G was returned to service

and tested

at 3:00 a.m. to demonstrate

operability to support Unit 2

restart following that unplanned trip.

The licensee

rescheduled

the

D/G inspections

to occur shortly after the unit is restarted.

The

inspector

did not identify any problems

associated

with the planned

D/G outage.

No violations or deviations

were identified in the Maintenance

Observation

area.

4.

Operational

Safety Verification (71707,

93702)

The

NRC inspectors

followed the overall plant status

and

any significant

safety matters

related to plant operations.

Daily discussions

were held

with plant

management

and various

members

of the plant operating staff.

The inspectors

made

routine visits,to

the control

rooms.

Inspection

observations

included

instrument

readings,

setpoints

and

recordings,

status

of oper'ating

systems,

status

and alignments of emergency

standby

systems,

verification of. onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of temporary

tags

on

equipment

controls

and

switches,

annunciator

alarm

status,

adherence

to

procedures,

adherence

to

LCOs,

nuclear

instruments

operability, temporary'lterations

in effect, daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This inspection

activity also

included

numerous

informal, discussions

with operators

and

supervisors.

General

plant tours- were conducted.

Portions of the turbine buildings,

each reactor building, and general

plant areas

were visited.

Observations

included

valve

position

and

system

alignment,

snubber

and

hanger

conditions,

containment

isolation

alignments,

instrument

readings,

housekeeping,

power

supply

and

breaker

alignments,

radiation

and

contaminated

area controls,

tag- controls

on equipment,

work activities in

progress,

and radiological protection controls.

Informal discussions

were

held with selected

plant personnel

in their functional

areas

during these-

tours.

a.

Plant Status

Unit 2 tripped from 80/ power

on

December

8, 1991, ending

48 days nf

continuous

operation.

A 30 'ampere fuse blew in the secondary

side of

.a potential

transformer.

This resulted

in actuation

of the main

generator

protective circuit and

a generator

load reject.

A turbine

trip and reactor trip followed.

The licensee

conducted

an incident

investigation of the event

and restarted

the unit on

December

10,

1991.

No reason

other than

a fatigue failure of the fuse could

be

identified.

There

was

no work in progress

nor were there

any power

system

transients

noted

at

the

time of the

event.

Long

term

corrective

actions

are

continuing

including

a modification to the

protective circuit.

These

actions

wi 11

be followed by the inspector

with the closure of the trip report.

b.

Leak in Unit 2 Reactor Building Nain Steam Tunnel

The inspector

reviewed

the

circumstances

associated

with an event

which occurred

on the midnight shift on November

26, 1991,'here

a

minor steam

leak

was identified by licensee

personnel

on

a four inch

RWCU line located in the Unit 2 reactor

bui,lding main

steam tunnel.

The g')and packing nut had

become

loose

on 2-FCV-69-580 located

on the

RWCU return line to the feedwater

system.

Licensee

personnel

entered

the

steam

tunnel after

sensors

indicated

increasing

temperatures.

Upon entering

the

steam

tunnel

the

SRO

was

able to identify the

location of the leak

and estimate

the size of the leak

as

.25

gpm.

'6

Due to the licensee's

ability to evaluate

the problem quickly, the

leak

was isolated

and repaired prior to conditions

degrading.

The

inspector

determined that operations

personnel

responded

well to this

abnormal

condition and identified and corrected

a problem which could

have led to an automatic

shutdown if allowed to continue.

No violations or deviations

were identified in the Operational

Safety

Verification area.

5.

Power Ascension Test Report

Review (72301,

72532)

The inspectors

reviewed

the licensee's

PATP Start-up Report "dated October

29,

1991.

The

PATP

had

commenced

on

February

20,

1991, with the

commencement

of core

reloading

and

completed

on August 6,

1991.

The

licensee's- Unit 2 Cycle

6 report

was submitted

to the

NRC as required

by

TS 6.9.1.1.

The

PATP was performed in three

phases

and consisted of 21 different power

ascension, tests.

A total of 59 separate. test deficiencies

were identified

during the

PATP.

Phase I, Open

Vessel

Testing,

was completed

on May 21,

1991,

with the

completion of 2-TI-149',

Water

Level

Measurements,

and

initial thermal

expansion

walkdowns.

Phase II, Heat-up

to

55% Power,

commenced

on

May 23,

1991, with plant startup,

and

was complete

on July

16,

1991,

when authorization

was

received

to continue with the

power

ascension

above

55'A power.

Phase III was complete

on August 6,

1991, with

the completion of Turbine Generator

Torsional Testing.

The insp'ectors

had previously reviewed the

PATP as

documented

in IR 91-26.

In this report specific

concerns

had

been

raised

concer'ning

testing

results

associated

with TI-131,

TI-174,

and

TI-189.

The

inspector

reviewed

the test results

associated

with these

three

tests

with the

licensee

and determined

that the original concerns

as described

in the

above

stated

inspection

report

have

been satisfied.

Additionally the

inspector

reviewed

the listing of test deficiencies

and determined

that

the licensee

had dispositioned all but two of the

59 deficiencies.

In

each

case

the deficiencies

had

b'een dispositioned

by reperforming portions

of the test,

adjustments

and/or special

testing

under

a work request,

engineering

evaluation,

or contact with vendor for clarification.

The

inspector

did not disagree

with any of the licensee's

basis

used for

closing these test deficiencies.

Two test deficiencies

associated

with 2-TI-190, System Thermal

Expansion,

remain

open

pending

further action

by the

licensee.

The

inspector

discussed

these

test deficiencies

with

a region

based

inspector.

The

regional

inspector

reviewed

the

licensee's

evaluations

and corrective

actions

completed

to date associated

with these

two test deficiencies

and

determined that the licensee's

actions

were acceptable.

No violations or deviations

were identified in the

Power Ascension

Test

Report Review area.

6.

Corrective Action Program

(30702)

The

inspector

reviewed

recently

issued

licensee

procedures

and

held

meetings

with site

gA organization

personnel

for

the

purpose

of

determining

the status of recent

changes

to the corrective action program

at Browns Ferry.

Based

on this review the inspector

determined

tha't the

new program

does

not represent

a significant change

in the way that the

licensee

does

business

in this area.

The

new program replaces

the use of

a single form used for CAgRs

and

PRDs with two separate

forms for use

as

SCARs, Significant Corrective Action Reports,

and P"Rs,

Problem Evaluation

Reports.

However the 'actual criteria

used

to classify

a significant

condition adverse

to quality has not changed.

Timeliness

requirements

and

requirements

concerning

escalation

of delinquent

action

has

not chang'ed

significantly.

An additional

change is the creation of a third form for

use with FIRs, Finding Identification Reports,

which may only be used

by

NgA organization

personnel

for non-significant

prob')ems identified during

performance of a

gA audit or monitoring activity.

Under the

new program

existing

ACPs, Administrative Control

Programs,

such

as

WOs, IIRs,

COTS,

LERs, etc. will continue to be used similar to as under the old program.

The responsibility for tracking

and trending of items will be transferred

'rom the site

gA organization

to site licensing.

The inspector

reviewed

Site Standard

Practice

SSP-2.3,

Finding Identification Reports,

SSP-3.6,

Problem Evaluation Reports,

and SSP-3.4,

Corrective Action. These

licensee

procedures

superseded

SDSP-3.7

and

SDSP-3.13,

which

covered

the

old

program. Additionally, the inspector monitored training conducted

by the

Browns Ferry Corrective Action Coordinator

on

November

25,

1991.

This

training

was

one of a series

of classes

required of all managers

and

supervisors

prior to implementation

of the

new program.

The

new program

was

implemented

by the

licensee

on

December

2,

1991.

The inspector

determined that the

new program is the

same

as the program that is already

in place at the licensee's

other nuclear facilities.

Implementation of

the

new program at those facilities had already occurred earlier this year

and

had

been

intentionally

delayed

at

Browns

Ferry

as

a

conscious

decision

not to change

the existing

program during the Unit 2 restart.

The inspector

was

informed by licensee

personnel

there

had

been

problems

at the other facilities with the implementation of the

new program which

resulted

in delinquent

action

backlogs.

The

inspector

was further

informed that

those

problems

which

have

been

corrected

at

the other

~ facilities were due to reduced

emphasis

on management

review under the

new

program, i.e.

lack of a

MRC.

Browns Ferry intends

to implement the

new

program using

the

MRC somewhat similar to its'tilization under the old

program.

Part

of the training

was

reading

of

a

VP

BFN Operations

Memorandum

dated

October

31,

1991,

which outlined expectations

in this

area.

Specifically

mentioned

in this

memorandum

was

an

expected

timeliness

rate of 98/ with de1inquent

action

backlogs

considered

as

unacceptable

performance.

The inspector

also

reviewed

the most recently

issued

Site guality Trend

Report

dated

November

5,

1991, to determine

the level of timeliness

for

corrective actiors.

That report covered trending of Conditions Adverse to

guality,

quality

assurance

findings,

external

findings,

Inc'ident

Investigation Reports,

and Corrected

on the Spot

items for Unit 2 during

September

1991.

At the

end of the

month there

were ll open significant

CAgRs

one of which had delinquent corrective action.

There also existed

33 non-significant

CAgRs

and

15

PRDs at the

end of the

month.

The

inspector

noted that the overall timeliness

rate

had continued to improve.

The percentage

of delinquent

items for this period

was 8.6l (the rate

has

continued to decrease

from approximately

20% in November 1990).

Many site

organizations

have

not

had

any recent delinquent

items.

However during

the past six months the onsite Nuclear Engineering organization

has

had

an

overall

40%

delinquency

rate.

This

problem

was identified

by the

licensee's

gA organization

as

an adverse

trend

and

documented

under

CARR

BFA910216112.

No other apparent

adverse

trends

were identified in the

licensee

report.

The inspectors will continue to monitor 'the licensee's

implementation of the

new program

and report

on performance

in this area

after adequate

time

has

elapsed

to allow an assessment

of adequacy

and

timeliness of corrective actions

under the

new program at this site.

No violations

or deviations

were identified in the Corrective

Action

Program

Review area.

Unit 3 Restart Activities (30702)

The inspector

reviewed

and

observed

the licensee's

activities

involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation

of pre-job field wo'rk,

in-progress field work,

and

gA/gC activities; attendance

at restart craft

level

progress

meetings,

restart

program

meetings,

and

management

meetings;

periodic

discussions

with both

TVA and contractor

personnel,

skilled craftsmen,

supervisors,

m'anagers,

and executives.

'a ~

Contractor'ctivities

The inspector

observed

and

reviewed

the activities of two of TYA's

Unit 3 main contractors,

GE and

SWEC.

The inspector

also

observed

activities

performed

by additional

contractors

such

as Digital and

PCC.

The activities included the following:

1)

Training

The inspector

reviewed

and observed

training given to

SWEC and

GE

technical

personnel.

The specific

items

consisted

of

procedure

MMM No. 2.5,

Maintenance

Training, which establishes

and 'efines

the

requirements

and

responsibilities

for

implementation

of

maintenance

and

modifications

services

training

at

BFNP;

SWTP

004,

Introduction

to

Regulatory

Requirement

- TVA's Nuclear guality Assurance;

SWTP 003, Print

Reading

-

Use

of

TYA Drawings;

informal

training

for'amiliarization

with procedure

MAI-4.3, HVAC Duct Systems,

which

establishes

the

requirements

for fabrication,

installation,

modification, verification,

and

documentation

of

HVAC duct

systems;

and

SWTP-004, Plant Reference

Material

and Control-Work

Control

Process.

The training

was

conducted

in

a classroom

environment,

attendance

sheets

were filled out

and for the

SWTP's

an

examination

was

given

to the participants.

The

inspector

concluded

from these

reviews

and

observations

that

SWEC

was

conducting

training for personnel

and

using

TVA's

methods.

Reactor

Vessel

Internals

The inspector

continued to monitor the activities performed

by

GE associated

with the reactor

vessel

internals.

The IVVI was

completed

and

involved

an

inspection

of the

Steam

Dryer.

Several

indications

were observed

and actions

were being taken

to address

them.

This

was identified as

an IFI in IR'1-38.

The jet

pump

beam replacement

was completed.

This replacement

included

removal of the eld

beams,

replacement

with new

beams

and tack welding of the

new beams.

Other activities included

placement of the separator

and dryer in the vessel,

drain

down

of the vessel,

removal

of the

steam

plugs,

placement

of the

drywell head,

and installation of shield plugs.

Work Release

The inspector

continued

to monitor the licensee's

and

SWEC's

activities

involved with contractor

work authorization.

The

specific

items

reviewed

were

par t of the pilot program for work

documentation

preparation

and involved

12

WOs.

These

WOs were

prepared

by

SWEC personnel,

reviewed

by

SWEC and

TVA gA and Unit

3 work control.

The inspector

observed

these activities

as the

process

developed.

No significant deficiencies

were identified.

The licensee

approved

SWEC activities for preparation

of work

documents

Boot Incident

On

November

14,

1991,

a licensee

gA person

questioned if work

previously

performed

by

SWEC

was within the

scope

of the

contractor

work release

program.

It was determined

that

the

work was outside

the scope.

A stop work order was issued.

An

incident investigation

was initiated on the problem.

It was

determined

that

on

November 4,, 1991,

SWEC

personnel

performed

work order 91-422447-00.

This work involved partial

removal of a boot seal at

a secondary

containment penetration

to

allow data verification of

a

pipe

support.

The

work

was

authorized

by Plant Operations

and conducted

in accordance

with

the procedure.

However,

SWEC personnel

were only authorized to

do scaffolding

work at

the

time

under

the contractor

work

release

program.

The contractor

work release

program

was

outlined in IR 91-4Q,

10

The

licensee

determined

that

the

CWL

program

was

not

communicated

downward to the craft level.

There

was

general

confusion about implementation

and understanding

of the program.

The

licensee

initiated

several

corrective. action

steps

to

correct the problem.

These

included withdrawing all work orders

from construction

until

they

could

be

reviewed

for

scope

definition.

Only scaffolding

WOs were released.

All

SWEC

supervisors

and

engineers

were to

be retrained

in the

CWL

program.

The

inspecto'r

reviewed

the

licensee

reply to

NOV 91-26-02

concerning

removal of fire wrap from operable

equipment.

In

this reply it was

stated

that actions

taken

to

improve

the

'control of inspection requests

of contractor walkdown activities

would be resumption of these activities using

a phased

approach.

This

was

not

done for the construction contractors.

SWfC was

not scheduled

to

be released

to perform safety related

work

activities until December

9,

1991.

This is

a deviation from the

NOV reply to

91-26-02.

This

item is identified

as

DEV

296/91-41-01,

Control

of

Construction

Contractor

Work

Activities.

5)

On

December

9,

1991,

the licensee initiated

a plan of the

day

meeting for Unit 3 restart activities.

The inspector

attended

several

of the meetings.

The meetings

are attended

by senior

licensee

and contractor personnel.

b.

Operations Activities

The inspector

reviewed

and observed

the Unit 3 operations activities

involved with the reactor

vessel

drain

down.

This activity was

performed

in accordance

to procedure

3-SOI-31A, Drain

Down of U-3

Reactor

Vessel

and

Cavity to

Condensate

Storage

System.

The

operations

group

and

various

support

groups

held

several

pre-job

.planning

meetings

and briefings.

The

inspector

noted

that

a

scheduling fragnet

was developed

to indicate to personnel

the various

times at which certain activities

were to occur.

These activities

included

system line

ups

to drain

the water to 85 storage

tank,

placement of the

steam

separator

and dryer into the reactor vessel,

and

removal of the

main steam line plugs.

The inspector

concluded

that

these activities

were controlled

by approved

procedures

and

performed

by qualified individuals.

One deviation

was identified in the Unit 3 Restart Activities.

8.

Contractor

Control

(37702)

The inspector

continued

to review the activities of the sub-contractor,

Key Communications,

and

the resulting incident investigation.

The review

involved field work

and

design

change activities

associated

with

DCHs

W9276A,

W9277A,

and

W9279A.

The review indicated that

DCN

W9276A was

issued to replace existing

phone switch and

make associated

changes

in the

Plant

Communications

Room,

located

on the

1C level of the Contro'l

Bay.

DCN W9277A was

issued

to delete wires and cables

in order to allow switch

replacement

and

DCN

W9279A was

issued

to install cables,

splices,

and

terminations

in the yard area

outside

the

power block and in the turbine

building.

The fol lowup indicated that

'a

WP for DCN W9276A was required to

be written to implement the

DCN and

none

was written although

the

new

switch was

made operable.

WP-0087-91

was written to implement

DCN W9277A

and

the

WP

was

never

signed

into

work status

although it was

a

prerequisite for DCN 9276A.

WP-2045-91

was written to implement

DCN 9279A

and

was

signed into work and never utilized.

This resulted

in the work

associated

with

WP

2045-91

being

near

to completion

and

with

no

documentation.

10 CFR 50,

Appendix

B, Criterion III, Des.ign Control,

requires

that

measures

shall

be established

for the identification and control of design

interfaces

and for coordination

among participating design organizations.

The

licensee

uses

SDSP

16. 17 to control contractor activities.

These

requirements

were not met or followed for the subcontractor.

Work plans

were

not utilized

and

on October

13,

1991, electrical

cables

were cut

servicing the

PREAS.

In Inspection

Report 91-40, this item was identified

as

a

URI.

This

item is

changed

to

a

VIO 259,

260,

296/91-41-02,

. Inadequate

Design Controls for Sub-Contractor.

One violation was identified in the area of Contractor Control;

Reportable

Occurrences

(92700)

The

LERs listed

below

were

reviewed

to determine if the

information

provided

met

NRC

requirements.

The

determinations

included

the

verification of compliance

with

TS

and

regulatory

requirements,

and

addressed

the

adequacy

of the event description,

the corrective actions

taken,

the

existence

of potential

generic

problems,

compliance

with

reporting

requirements,

and

the relative

safety

significance of each

event.

=Additional in-plant reviews

and discussions

with plant personnel,

as appropriate,

were conducted.

(CLOSED)

LER 260/91-13,

T.S.

Violation Following

Loss

of Primary

Containment

Caused

by Personnel

Error.

This

LER had

been

submitted

by the licensee

due to the

same

breach of

primary containment

event

described

in VIO 91-23-01

closed

in this

IR.

The inspector

reviewed

the licensee's

corrective actions

associated

with

this

LER as part of the followup review of corrective actions

associated

with the violations issued for this event.

0

12

10.

Action on Previous

Inspection

Findings

(92701,

92702)

a

~

b.

C.

d.

(CLOSED) IFI 259, 260, 296/91-38-04,

Procurement

Stop Work

This

item. was originally identified when the inspector

was

informed

gA had issued

SWOs concerning

BNA activities.

The inspector

reviewed

two

SWOs identified

as

BFSW-001

and

BFSW-002.

The inspector

noted

that

both

SWOs clearly indicated

the activities that

were to

be

stopped,

the

reasons

for the

SWOs

and the corrective actions

needed

to lift the

SWOs.

The inspector

concluded

from this review that gA

reviewed

BNAs activities

and

had taken appr'opriate

action

as

needed.

(CLOSED)

URI 259,

260,

296/91-40-02,

Adequacy of Design

Controls

During Sub-Contractor Activities.

The

item

was originally identified

when

on

October

13,

1991,

information

was

received

that

indicated

a

sub-contractor,

Keys

Communication,

was

disconnecting

PREAS

readers.

These

PREAS

terminals

are

used

as part of the personnel

accountability

system

during

a radiological

event.

As

a result of review and followup,

this item was

changed

into

a VIO 259,

260, 296/91-41-02,

Inadequate

Design Controls for Sub-Contractor.

(CLOSED) VIO 259, 260, 296/91-10-03,

Inadequate

Test Controls

This

VIO was

issued for two examples

of failure to implement test

control

measures

for returning

components

to service.

The first

example

was identified when

on March 18,

1991, during integrated

leak

rate test,

the reactor

building torus

vacuum breakers'opened

when the

torus pressure

was greater

than the reactor building pressure.

The

second

example

was identified when

on October 4,

1990,

during the

performance of a SI, the

A3

RHRSW pump did not start.

The inspector

reviewed the licensee's

response

to the VIO, dated

June

21,

1991.

The licensee

indicated that for the first example

an

adequate

review was not performed for a

FCR

.

The

design for the

pressure differential switches for the vacuum breakers

was controlled

by

ECN P3051

and the installation of the switches

was controlled

by

WP 2036-84.

During the installation

a

FCR was not reviewed for PNT.

The licensee

indicated that for the

second

example

personnel

failed

to

adhere

to

PNI

17.1,

Conduct of Testing,

which requires

that

equipment

awaiting

PNT

be

adequately

tagged.

Had the

PMT been

performed

the failure of A3

RMRSW to start would have

been detected.

The inspector

reviewed .the licensee's

corrective which included the

requirement

in

SDSP

12.4 that

FCRs,

now referred

to as

FDChs,

be

reviewed for

PNT

and that all licensed

and non-licensed

operator

review incident investigation

number

II-B-91-074.

The

inspector

determined that the corrective action

had

been completed.

(CLOSED)

VIO 259,

260,

296/91-24-02,

Failure

to Follow Clearance

Procedures.

13

This

VIO had

been

issued

due to the 'licensee's

failure to follow

applicable

procedures

which resulted

in an event where the

1D D/G was

motorized.

On July 9,

1991, while releasing

Hold Notice 0-91-0501

following maintenance

on the

1D D/G the

.25

amp position indication

fuse

was incorrectly installed in the control

power circuit.

The

actual

control

power fuses

are

required

to

be

15

amp fuses..

The

individual that reinstalled

the

fuses

had transposed

the position

indication fuses

and control

power fuses..

The individual then racked

in the breaker

but failed to trip check the breaker.

Had that step

been

performed

the

.25

amp fuses

would have

blown at that point.

Independent

verification

was

later

performed

on

the

fuse

reinstallation

which failed to identify'he error.

Later following

two hours of operation

performed

as

PNT, the

D/G the generator

output

breaker

could not

be tripped from the control

panel

in the control

room.

The breaker

remained

closed for approximately

seven

minutes

before it was tripped locally.

Following to the event the licensee

removed

the

D/G from service to

perform engine

and

generator

tests

to determine if any equipment

damage

had

occurred.

No

damage

was identi'fied, and

the

D/G was

returned to operable status

on July 10,

1991.

The

inspector

reviewed

the licensee's

response

to the

VIO dated

September

5,

1991.

In that

response

the licensee

attributed

the

failure to personnel

error

by the individual that reinstalled

the

fuses

and

the

second

individual required

to perform

independent

verification of the activity.

As corrective actions

the licensee

took personnel

action against

the individuals involved and committed

to conduct additional, training

on procedural

requirements

associated

with racking

in breakers

and

independent

verification for all

operations

personnel.

The inspector

reviewed Final

Event Report,

II-B-91-135, which documented

the licensee's

investigation of this

event.

Additionally, the

inspector

examined

training

attendance

records

related to this event for operations

personnel.

The training

sessions

included

specific

training

on

Final

Event

Report,

II-B-91-135,

SDSP

3.15,

Independent

Verification,

and

breaker

operations'ased

on this review the inspector

determined

that the

completed

corrective

actions

should

be

adequate

to

prevent

reoccurrence.

(CLOSED)

VIO 259,

260,

296/91-23-01,

Breach of Primary Containment

when Reactor

was Critical

(CLOSED)

VIO 259,

260, 296/91-23-02,

Failure to Follow Work Control

Procedures

(CLOSED)

VIO 259,

260, 296/91-23-03,

Inadequate

Procedures

to Control

Drywell Entry when Containment Integrity is Required.

These

three

VIOs were categorized

in the

aggregate

as

a Severity

Level III problem

and

involved escalated

enforcement

with

a civil

0

penalty for licensee

actions

which led to an event that occurred

on

June

5,

1991,

when primary containment

was .not maintained

during

a

time while the reactor

was critical

and at

150 psig

and

365 degrees

F.

This event

occurred

as

the result of both drywell personnel

access

doors

being

open while licensee

personnel

were in the Unit 2-

drywell

performing

thermal

expansion

walkdowns

duri'ng

the

PATP.

Interlocks for both drywell doors

were defeated at 2:45 a.m.

on June

5,

1991,

to facilitate frequent entry by personnel

performing the

walkdowns.

This occurred without the approval

and notification of

the

SOS.

The failure

was

identified

by appropriate

'licensee

personnel

at 6:30'.m.

and primary containment integrity immediately

restored.

Licensee

management

decided

to place

the plant in cold

shutdown

at 10:00

a.m.

The unit was

not re'started

until June

10

after the

licensee

had

conducted

a detailed investigation into the

event

and initiated

a planned

corrective action

program associated

with the event.

The

inspector

reviewed

the licensee's

response

to the violations

dated

September

6,

1991.

In that response

the licensee

attributes

the failure to

an unauthorized

action

by a'echanical

maintenance

craftsman.

Contributing

factors

in this failure were

lack of

attention

by those

personnel

in the direct area

during the event,

inadequate

procedures

which failed to control containment

entry and

the method

used

to defeat

the door interlocks which resulted

in an

erroneous

door position indication in the control

room.

The response

also provided

the details

of the licensee's

corrective action plan

which included the following:

Those

personnel

directly involved in de'feating

the drywell door

interlocks

received disciplinary action.

Personnel

that were

shown

to

have

observed

the

drywell

doors

open

but did not

question

the condition were counseled.

Employee

training

sessions

were

conducted

to outline

a

new

improved

operating

plant

philosophy.

The training sessions

included

a

description

of

the

event,

plant

personnel

responsibilities,

and

SOS

authority

and

responsibility.

Additional training

was

provided

to

maintenance

craft

and

supervisory

personnel

on expected

performance

and documentation

of assigned

work.

Existing plant procedures

that were considered

inadequate

were

revised

to more clearly describe

requirements

for drywell entry

when primary containment integrity is required.

TYA has

developed

various

programs

intended

to

enhance

job

performance

of maintenance

craftsman

and ,supervision.

These

include

a

screening

and

evaluation

program

to

assess

job

performance of maintenance

foreman.

This program is intended to

include

screening

and evaluation

of both current

foreman

and

future

candidates

to ensure

they

possess

adequate

skills to

perform their supervisory

duties.

Additionally the licensee's

15

general

employee training program will be enhanced

to emphasize

the importance of the plant's safety barriers

and responsibility

to follow procedures.

The inspector verified current revisions of licensee

procedures

to

verify that corrective

actions

had

been

completed

in this area.

2-0I-64,

Primary

Containment

System

. Operating

Instruction,

was

revised to require that all door manipulations will be performed

by

operations

personnel

and that at least

one of the

two airlock doors

be closed

always

when primary containment

is required.

SDSP

14.15,

Entry and

Work in'he Primary Containment,

was revised

to require

that drywell entries

be performed in accordance

with 2-0I-64 while

-primary containment

is required

and that entries

be

performed

in

accordance

'with MNI-129, Opening

and Closing of Drywell Personnel

'Airlock Doors, while primary containment

is not required.

MMI-129

was

revised

to

change

the

method of defeating

the interlocks

so

control

room indication of door position

was not affected,

to allow

defeating

interlocks only when primary containment

is not required

and to require

SOS notification prior to defeating

interlocks.'ased

on conversations

held with selected

licensee

personnel

the

inspector

determined

that personnel

were

knowledgeable

of the event

and

that

adequate

training

on sensitivity

to operating

plant

requirements

had

occurred.

The inspector

also

noted that special

training

on drywell

door operation,

primary containment

TS,

and

correct

method of defeating

interlocks

had

been

conducted

during the

period 'directly prior to the decision to restart

the unit on June

10,

1991.

Two sessions

of this training had

been monitored. by

NRC shift

inspectors

as

part of the 'continuous

shift coverage

that

was

occurring

during that

time period.

Additionally the

inspector

determined

that the licensee's

new program for craft supervision

had

been

implemented.

The first class

of maintenance

foreman

which

includes

elements

of the proposed

screening

and evaluation

process

is

currently ongoing

and

scheduled

for completion prior to the

end of

this reporting period.

ORAT Open

Item Closure

An

ORAT inspection

was

conducted

prior to restart

of Unit 2.

Thirteen

open

items

were identified in IR 50-260/91-201.

A followup

was performed

and

documented

in IR 50-260/91-202.

In IR 91-202

open

items

1,

2,

4,

6,

7, 8,

and

11

wer e cl osed.

One

new itern

was

identified in

IR 91-202

which

was

closed

in IR 91-26.

The

team

verified that all corrective actions

to address

the restart

concerns

had

been

implemented

except

review

of

the

final

incident

investigation report concerning

the fuel handling event.

Closure of

the remaining items follows:

16

1.)

(CLOSED)

Open

Item 260/91-201-03,

Fuel

Handling

Event

Final

Incident Investigation Report.

The

inspector

reviewed

the

licensee's

final

incident

investigation report.

The report was revised to include

a

human

performance

evaluation

system.

This evaluation

provided

more

comprehensive

recurrence

controls

and identified problem areas

related to the event.

a.)

Inadequate

verbal

communication

-

adequate

information

transfer

did not occur

between

personnel

involved in the

event.

b.)

Inadequate

written communication - procedural

guidance

was

not provided

on signal

spikes related to noise.

c.)

Poor

work practices

-

incomplete

troubleshooting

was

performed to resolve

the case of the unusual

spikes.

d.)

Poor

managerial

methods

- high standards

for resolving

problems

before

continuing activities

not effectively

communicated.

The results

of the incident investigation report were discussed

in

a

TVA/NRC management

meeting

held at the site

on

Nay 13,

1991.

Several

incident

investigation

improvements

were

discussed

in

the

meeting

including 'n

overall

program

effectiveness

review.

The inspector

concluded that

a thorough

self-critical

review of the

event

was

conducted.

This

was

essential

for effective

problem resolution after

the plant

restart.

2.)

(CLOSED)

Open

Item

260/91-201-05,

Correction

of Procedure

Deficiencies

Including Procedure

Style

Guide

Terminology

and

Definitions

The

inspector

reviewed

the

licensee's

response

and

closure

package

for this

item.

Site

Standard

Practice

2.2, Writing

Procedures

was

issued

on

October

8,

1991.

The

procedure

combines

the style

guide for writing instructions

and site

writers guides into one

document.

Guidance

is provided in the

SSP

on

logic

terms,

referencing

and

branching,

emphasis

techniques,

and definition of terms..

Procedural

discrepancies

were identified in 2-0I-71, O-OI-57D,

and

2-01-74.

Procedure

changes

were

made

or

addressed

to

correct

the discrepancies.

Additionally,

a

memorandum

was

issued

by Operations

management

to remind personnel

of their

responsibilities

and

the

importance

of taking

time

when

verifying procedure

revisions.

The

inspector

reviewed

the

licensee

response

procedure

revisions

and operations

memorandum.

This item was. resolved

by these actions.

0

17

(CLOSED) Open Item 260/91-201-09,

Locked Valve Program Training

The

inspector

reviewed

the

licensee's

response

and

closure

package.

Live-time training

was

conducted

for the operating

crews.

The lessons

plans

and attendance

sheets

were reviewed.

Items

addressed

were

the

locked-valve

program,

independent

verification, versus

second party verification, and surveillance

and procedural

adherence.

These actions

resolved

the concern.

(CLOSED)

Open

Item

260/91-201-10,

Independent

Verification

Training

The

inspector

reviewed

the licensee's

response

and

closure

package for this item.

Several

weaknesses

were noted during

a

walkdown of 1-SI-4.5.8.11,

RHR

Unit

1 X-tie for Unit

2

Operation.

The weaknesses

were addressed

or

a SI revision made.

Training was

conducted with item 260/91-201-09.

These

actions

resolve the concerns.

(CLOSED) 260/91-201-12,

Weaknesses

in Training Program

The inspector

reviewed

the licensee's

closure

package

and reply

for this item.

.The

ORAT identified that adverse

trend control

limits for several

indicators

were

too high.

When

no audits

were

performed

during

a period

a reject

rate of zero

was'ntered.

Some trend data

was not being forward to site

gA as

required.

The licensee

eliminated

the control limits.

Each

item trended is

now analyzed

on its

own significance, merit, or

impact.

Nore discussion

and analyses

of the item was required

from line organizations

for the trend report.

When

no audit is

performed

the trend indicates

no data instead of zero.

Site

gA

contacted

the various line organizations

.to insure all required

data

is forwarded to site gA.

The inspector

reviewed

some

gA

trend reports

and the reports

provide detailed

explanations

of

the indicators.

Where

no audit

was

performed

no

data

is

indicated.

These actions

resolve

the concern.

(CLOSED) 260/91-201-13,

Improvements

in Incident Investigation

Reports

The

inspector

reviewed

the

licensee's

closure

package

and

response

for this item.

Changes

were

made to the final event

report

package

to identify team

members

trained in root cause

analysis.

Other specific

items

were addressed

in the

response

of closure

package.

In

a TVA/NRC management

meeting

on May 13,

1991, the improvements to incident investigations

were outlined.

These

are

as follows:

training - basic root cause

analysis

techniques

human performance

enhancement

system methodology

increase

number of'ualified investigators

18

plant manager

approval of team composition for category

1

events

category

1 events

reviewed

by multidiscipline management

committee

freezing of event

scene

and immediate conduct of interviews

improved trending system

overall program effectiveness

review

A new Site Standard

Practice

12.9,

Incident Investigation

and

Root Cause Analysis,

was

issued

on September

4, 1991.

This was

a

new procedure

to implement Corporate

Standard

12.9.

In general

since

the

plant restart

on

Nay

24,

1991,

the

inspector

has

noted

a general

improvement in the effectiveness

of incident reports.

They have

been

thorough

and self-critical.

These actions

resolve

the concern.

In summary all

ORAT open items are closed.

Item

260/91-201-01

260/91-201-02

260/91-201-03

260/91-201-04

260/91-201-05

260/91-201-06

260/91-201-07

260/91-201-08

260/91-201-09

260/91-201-10

260/91-201-11

260/91-201-12

260/91-201-13

Inspection

Report Closed

91-202

91-202

91-41

91-202

91-41

91-202

91-202

91-202

91-41

91-41

91-202

91-41

91-41

260/91-202-01

91-16

ll.

Nuclear Safety Review Board

The inspector

attended

selected. activities of the

NSRB conducted

December

12,

1991.

Plant

management

discussed

NSRB

items of interest.

Areas

covered

included

both Unit

2

and Unit 3 activities.

Haj or

items of

interest

were

foreign

material

exclusion,

the

management

review

committee's

function with resp'ect to the

CARR process,

Unit 3 progress

and

0

19

schedule,

incorporation of Unit 2 lessons

learned into the Unit 3 program

and

a report

on Unit 3 fuel inspection results.

The

NSRB

members

were interactive

with the

management

on the

issues

discussed.

Several

items for plant ac'tion were identified.

Results of

NSRB directed audits

were discussed.

For those activities reviewed

by the

inspector,

the

NSRB's activities were consistent with the requirements

of

the TS.

Exit Interview {30703)

The inspection

scope

and findings were

summarized

on

December

16, .1991

with those

persons

indicated

in paragraph

1

above.

The

inspectors

described,

the

areas

inspected

and

discussed

in detail

the

inspection

findings listed below.

The licensee

did not identify as proprietary any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item Number

296/91-41-01

259, 260, 296/91-41-02

Description

and Reference

DEV, Control of Construction Contractor

Work Activities, paragraph

7.

VIO, Inadequate

Design Controls for Sub-

Contractor,

paragraph

8.

Licensee

management

was

informed that

6

ORAT items,

1

LER,

1 IFI,

1 URI,

and

5 VIOs were closed.

Acronyms and

ACP

BFNP

BNA

CAQR

CSE

CFR

COTS

CWL

DCN

DEV

D/G

ECN

FCR

FDCN

GE

GPH

HVAC

IFI

IIR

Initia 1 i sms

Adminstrative Control

Program

Browns Ferry Nuclear Plant

Bechtel

North America

Condition Adverse to Quality Report

Chemistry

8 Environmental

Code of Federal

Regulation

Corrected

on the spot

Contractor

Work Release

Desi,gn

Change Notice

Deviation

Diesel

Generator

Engineering

Change

Notice

Field'Change

Request

Field Design

Change Notice

General Electric

Gallons

Per Minute

Heating, Ventilation,

5 Air Conditioning

Inspector

Followup Item

Incident Investigation

Report

20

IR

IVVI

LCO

MAI

MR

MRC

NOV

NQA

NRC

NSRB

OI

ORAT

PATP

PCC

PER

PMI

PMT

PRD

PREAS

QA

QC

RHR

RHRSW

RPV

RWCU

SDSP

SI

SOI

SRO

SSP

SWEC

SWO

SWTP

TS

TVA

URI

VIO

WO

WP

WR

Inspection

Report

In Vessel

Visual Inspection

Limiting Condition for Operation

Modification Alteration Instruction

~ Maintenance

Management

Manual

'aintenance

Request

Management

Review Committee

Notice of Violation

Nuclear Quality Assurance

Nuclear Regulatory

Commission

Nuclear'Safety

Review Board

Operating Instruction

Operational

Readiness

Assessment

Team

Power Ascension Test Program

Project Cost and Control

Problem Evaluation Report

Plant Manager Instruction

Post Maintenance/Modification

Test

. Problem Reporting

Document

Personnel

Radiological Accountability System

Quality Assurance

Quality Control

Residual

Heat Removal

Residual

Heat Removal

Service

Water

Reactor

Pressure

Vessel

Reactor

Water Cleanup

Site Director Standard

Practice

Surveillance

Instruction

Special

Operating Instruction

Senior Reactor Operator

Site Standard

Practice

Stone Webster Engineering

Company

Stop

Work Order

Stone

Webster Training Program

Technical Specification

Tennessee

Valley Authority

Unresolved

Item

Violation

Work Order

Work Plan

Work Request

D'