ML18033B399

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SALP Repts 50-259/90-07,50-260/90-07 & 50-296/90-07 for Browns Ferry Nuclear Plant for 890103-900331
ML18033B399
Person / Time
Site: Browns Ferry  
Issue date: 06/14/1990
From:
Office of Nuclear Reactor Regulation
To:
Shared Package
ML18033B398 List:
References
50-259-90-07, 50-259-90-7, 50-260-90-07, 50-260-90-7, 50-296-90-07, 50-296-90-7, NUDOCS 9006210558
Download: ML18033B399 (53)


See also: IR 05000259/1990007

Text

ENCLOSURE

INITIALSALP

REPORT

U. S.

NUCLEAR REGULATORY C001ISSION

OFFICE

OF NUCLEAR REACTOR REGULATION

SYSTEhNTIC ASSESSMENT

OF LICENSEE

PERFORhiANCE

INSPECTION

REPORT

NUMBER

50-259/50-260/50-296

90-07

TENNESSEE

YALLEY AUTHORITY

BROMNS

FERRY NUCLEAR PLANT

JANUARY 3,

1989 - l4ARCH 31,

1990

TABLE OF CONTENTS

Page

I.

INTRODUCTION .....................................................

1

II.

SUMMARY OF RESULTS ..............................................

2

I

. 'ITERIA .............".""""....".".""'".""....."... 3

III

'CR

IV.

PERFORMANCE ANALYSIS ................,...'.."...............

~....

4

A.

Shutdown Operations .......................

B.

Radiological Controls .....................

C.

Maintenance/Surveillance .........,........

D.

Emergency

Preparedness ....................

E

Security ...........,......................

f.

Engineering/Technical

Support .......;...,.

G.

Safety Assessment/guality

Verification ....

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4

~ ~ ~

9

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11

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17

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19

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~ ~ ~

21J

V.

SUPPORTING

DATA AHG SUMMARIES

~ -" ~ ~ . ~ ~.... ~ .. ~""~" ~ ~ ~ "~~....

31

A.

8.

-C.

D.

Licensee Activities .............;.........

Direct Inspection

and Review Activities ...

Enforcement Activity.......................

Review of Licensee

Event Reports ..........

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~

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INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is

ar,

integrated

Nuclear

Regulatory

Commission

(NRC) staff effort to collect

available

observations

and

data

on

a periodic basis

and to evaluate

licensee

performance

on the basis of this information.

The program is

supplemental

to normal regulatory processes

used to ensure

compliance with

YRC rules

and regulations.

It is intended to be sufficiently diagnostic

to provide

a rational basis for allocation of NRC resources

and to provide

meaningful

feedback

to the

licensee's

management

regarding

the

NRC's

assessment

of their facility's performance

in each functional area.

, An

NRC

SALP Board,

composed of the staff members

listed below, met

on

May 15,

and

June

12,

1990,

to review the observations

and

data

on

perforttiance,

and

to assess

licensee

performance

in accordance

with the

guidance

in

NRC

Manual

Chapter

NRC-0516,

"Systematic

Assessment

of

Licenset:

Performance."

The

guidance

and

evaluation

criteria

are

suomarized

in Section III of this report.

The Board's

findings

and

recommendations

were

forwarded

to the Director, Division of Reactor

Projects III, IV,

V and

Special

Projects, Office of Nuclear

Reactor

Regulat)on

(NRR), for approval

and issuance.

This report is the

NRC's assessment

of the licensee's

safety

performance

at the Tennessee

Valley Authority's

(TVA) Browns Ferry facility for the

period

January

3,

1989

through

March 31, 1990.

The facility has

been

shutdown for

a

period of five years,

and

the

SALP process

has

been

suspended.

Because

the last full SALP would not be an accurate

basis

upon

which to

base

performance

trends,

the first six months of this period

were used

as the basis period.

The

SALP Board was

composed of:

B. D. Liaw, Deputy Director, Division of Reactor Inspection ard Safeguards

(SALP Board Chairman)

S.

C. Black, Deputy Director, Project Directorate I1-4, Division of Reactor

.Projects I/II, NRR

D. R. Carpenter,

NPC Site Manager,

TVA Projects,

Region II

D. M. Collins, Chief, Emergency

Preparedness

and Radiological Protection

Branch,

Region II

G. E. Gears',

Senior Project Manager,

License

Renewal Project Directorate,

NRR

G. T. Hubbard, Section Chief, Plant Systems

Branch, Division of System

Technology,

NRR

PE.

E. Merschoff, Acting Director, Division of Reactor Safety,

Region II

B. A. Milson, Chief, TVA Projects,

Region II

1

Attendees at SALP Board Meeting:

PR. H. Bernhard, Project Engineer,

TVAPD, NRR

8M. M. Branch, Senior Resident Inspector,

Matts Bar

8J. J. Blake, Chief, Materials Processes

Section

(MPS), Region II

~

II .

0

    • D. M. Crutchfie'id, Director, Division of Reactor Projects - III,'V

and

V and Special Projects,

NRR

$ E. H. Girard, Reactor Inspector,

MPS, Region II

W. S. Little, Chief,

TVA Section

B, TVAPD,

NRR

O'.

R. Marston, Radiation Specialist,

Region II.

8E. J. McAlpine, Chief, Radiation Safety Projects,

Region II

8C. A. Patterson,

Restart Coordinator,

Browns Ferry,

TVAPD, Region II

PC.

D. Perny, Acting Chief, Security Section,

Region II

kR. C. Pierson, Assistant Director for Technical

Programs,

TVAPD, NRR

8W. H. Rankin, Chief; Emergency

Preparedness

Section,

Region II

fT. M. Ross, Project Manager,

TVAPD, NRR

8*T. S. Rotella, Reactor

Systems

Engineer,

TVAPD, NRR

W. E. Scott, Senior Operations

Engineer,

Performance

and guality

Evaluation Branch,

NRR

PR. B. Shortridge,

Radiation Specialist,

Region II

fE. 0. Testa,

Senior Radiation Specialist,

Region II

"* Not Present

May 15,

1990

  • Attended via Telecon

May 15,

1990

PHot present

June 11, 1990

SUMMARY OF RESULTS

Cyc> 8 of the

Browns Ferry

SALP started

January 3,

1989

and

ended

March 31,

1990.

The period was divided into two parts for the purposes

of

this SALP:

a Base Period from January 3, 1989 until June 30, 1989,

arid an

Assessment

Period from July 1,

1989 through March 31,

1990.

Due to the

length of time the

SALP process

was

suspended

for Browns Ferry, this

divisicn allowed the facility to be rated against

a more recent perfor-

mance period.

The Base Period

was not rated.

The functional

area

of shutdown

operations

showed

improvement

over the

performance

in the

Base Period.

Unsatisfactory

performance

during opera-

tor requalification

exams early in the Assessment

Period

was corrected

by

increased

attention

tc

training.

Simulator

performance

during

inspections,

exercises,

and the requalificaticn

exams

given later in the

period

were satisfactory.

Weaknesses

were noted

in the

response

to

coni.rol

room

instrumentation

during

normal

shift

operations

and

compensatory fire protection measures.

Radiological

Controls

showed

strengths

in the training

program,

the

acquisition of

new

equipment,

and

the effectiveness

of programs for

conducting

day-to-day operations

at the plant.

Browns Ferry decided to

install

the

permanent

Post Accident

Sample

System

in advance of their

coamitment

dat<<.

Performance

measures

in this assessment

area

were

a

continuing strength.

Maintenance

performance

improvved during the Assessment

Period.

A Main-

tenance

Team Inspection

found the

program to be satisfactory,

and noted

many strengths.

During both periods,

modifications

was found tc be

an

0

e

area of weakness.

A lack of procedural

compliance

and poor work practices

were found,

and

problems

were noted in the area of surveillance activi-

ties.

An assessment. of the effectiveness

of the corrective actions taken

in response

to escalated

enforcement in this area

has not yet been

made.

Browns

Ferry's

performance

during

a full scale

emergency

exercise

demonstrated

strengths

in the

area

of Emergency

Preparedness.

TVA

continues to show improvements

in this area.

Major security upgrades

continue at the facility.

Long term compensatory

measures

remain

in place until upgrades

are

completed.

Problems

were

identified

in the

control

of Special

Nuclear Material

inventories.

Strengths

were

noted

in the

use of quality audits,

in the trending of

events

and their corrective action implementation,

and in the quality of

NRC submittals.

The quality of programs

in the Engineering

and Technical

Support areas

has

improved.

Inspections

found adequate

control of the engineering

process

ard gled enqineer ing reviews.

Timeliness of followup on identifiea issues

coula be improved.

The System Engineering

Program was

a strength.

- The Safety

Assessment

and guality Verification area

had

weaknesses

in

timeliness

and thoroughness

of submittals

and responses.

The quality of

the products

improved during the assessment

period.

Management's

use of

internal audits

and reviews for, feedback

on the quality of plant programs

is

a strength.

The

SALP Board Ratings in each functional area are:

Functional Area

Patino This Period

7 I 89.-.3 31/90

Shutdown Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technica'l

Support

Safety Assessment/guality

Verification

III. CRITERIA

2

1

3, Improving

2, Improving

2

2

3, Improving

Licensee

performance

is assessed

in the functional

areas

shown

above.

Functional

areas

normally represent

areas

significant to nuclear safety

and the environment.

Special

areas

may be added to highlight significant

observations.

The evaluation crit~ria which were used,

as applicable,

to assess

each

functional

area

are described

in detail in

NRC Manual Chapter

NRC-0516.

This chapter

is in the Public

Document

Poom files.

Therefore,

these

criteria are

not repeated

here,

but will be presented

in detail at the

public meeting to be held with licensee

manage>rene

to discuss

the

SALP

results.

, However,

the

NRC is not limited to these criteria

and others

may

have

been

used,

where appropriate.

On the basis

of the

NRC assessment,

each functional

area

evaluated

is

rated according to three performance

categories.

The definitions of these

performance

categories

are

shown below:

Category 1.

Licensee

management

attention

and

involvement

are

readily evident and place emphasis

on superior performance of nuclear

safety

or

safeguards

activities, with the resulting

performance

substantially

exceeding

regulatory requirements.

Licensee

resources

are

ample

and effectively used

so that

a high level of plant

and

personnel

performance

is being achieved.

Reduced

NRC attention

may

be appropriate.

B.

Category 2.

Licensee

manaoement

attention to and involvement in the

performance of nuclear safety or safeguards

activities are good.

The

licensee

has attained

a level of performance

above that

needed

to

meet regulatory

requirements.

Licensee

resources

are

adequate

and

reasonably

allocated

so that

good plant and personnel

performance

is

being achieved.

NRC attention

may be maintained at normal levels.

C.

Category 3.

Licensee

management

aatention

to and involvement in the

performance

of nuclear

safety

or safeguards

activities

are

not

sufficient.

The licensee's

performance

does not significantly exceed

that

needed

to

meet

minimal regulatory

requirements.

Licensee

resources

appear

to

be

strained

cr not effectively used.

NRC

attention

should be increased

above normal levels.

The

SALP Board

may also include

an appraisal

of the performance

trend of a

functional

area.

This rating modifier will only be

used

when both

a

definite trend of performance

throughout the rating period is present,

and

4he Board believes that continuation of the trend

may result in the

change

of the performance level.

The trend modifier, if used, is defined as:

Irproving:

Licensee

performance

was

determined

to

be

improving

during the assessment

period.

Declining:

Licensee

performance

was

determined

to be declining

during

the

assessment

period

and

the

licensee

had

not taken

meaningful steps to address

this pattern.

IV.

PERFORMANCE

ANALYSIS

A.

Shutdown Operations

1.

Base Period Analysis:

This functional

area

addresses

the

control

and

performance

of

operations

activities related to units in an extended

outage,

and

0

fire protection.

The assessment

was based

on routine inspections,

a

special

reactive

core monitoring inspection,

and

an instrumentation

team inspection.

The

SALP period

began with Unit 2 fuel loading.

This was the first

major operations activity since

the 'unit was

shutdown in September

1984.

Significant weaknesses

were

noted

during the fuel loading

operatfor s with

10

CFR Part 50.59 reviews,

review and approval of

procedures,

and technical specifications

(TSs).

A special

reactive

inspection

was conducted to determine

the conditions that led to the

loading of

74 fuel

bundles

without adequate

indication of core

neutron flux levels.

The inspection

indicated that the licensee

accepted

without question

those

provisions

of TSs which did not

preclude

unmonitored

core

alterations.

Mhen

the

problem

was

initially identified,

the licensee's

assessment

and actions

were

nonconservative,

and incomplete.

Once the full significance of the

issues

of'nmonitored

core loading were acknowledged,

the corrective

actiors

taken

by the

1i.censee

were

conservative

and acceptable.

Corrective actions

included

a review of TSs and the

TS interpretation

documents'o

ensure

they were not in conflict with the plant design

basis.

kith the exception of fuel load, few'perational activities occurred.

The plant

was

shutdown,

with the operators

in

a monitoring

mode.

Operational activities that did occur were the placing of systems

in

- arid out of service to support

system modifications.

In'general,

control

room day-to-day operations

were satisfactory.

Ho

specific problems

were identified with the shift logs, night order

bcoks,

clearance

hold order books, configuration logs,

and Temporary

Alteration Change

Form

(TACF) files.

Proper control

room staffing

was maintained

and shift turnover meetings

were formally conducted.

Control

room drawings

were found to be clear

and legible, although

a

significant backlog of drawings requiring updating existed.

Several

events

occurred

which indicate irconsistencies

in Operations

response.

In one event, Operations

demonstrated

a lack of aggressive

response

to control

room indications of plant status.

An incident

occurred

on February

10,

1989 that resulted

in 200,000

gallons of

potentially contaminated

water being lost from a condensate

storage

tank.

Operators

failed to respond to a decrease

in the tank level

indication until the next shift.

V

Several

instances

occurred

where the compensatory

measures

taken for.

fire protection did not meet TS.

The corrective action taken

was to

train Fire Protection personnel

on the TS requirements,

but personnel

in the Shift Operations

Sup~rvisor

(SOS) position did not receive

this additional training.

In each

of these

events,

the

SOS

had

reviewed

and approved. the incorrect compensatory

measures.

This lack

of recognition of the SOS'ole

in these

events

was considered

a-

0

weakness

in root

cause

determination,

and

SOS

training

and

performance.

The licensee initiated

a

number of steps

to upgrade the control room

. and operator

work stations.

These included

an elevated

work station

for the Shift Operations

Supervisor,

quiet floor coverings,

labeling

of annunciators,

and improved operator aids.

In the

area

of fire protection,

an experienced

professional fire

brigade

was maintained on-site.

This exceeded

'NRC requirements

and

was

a strength of the fire protection program.

Operator training in

regard to the post-fire safe

shutdown instructions

was only fair.

Some operators

did not understand

the procedural

requirements.

TYA's

Fire

School

is

accredited

by

the

National

Fire

Protection

Association's

Professional

gualffications Board.

Two violations were identified in the base period;

Assessment

Period Analysis:

The

assessment

period analysis

was

based

on routine inspection,

operator

examinations,

and

a

special fire protection

inspection.

Operational

activities

consisted

of placing

systems

in and out of

service for Divisional Outages

(until the

core

was unloaded),

and

defueling the reactor;

During

the

weeks

of July 10-21,

1989,

the

NRC

conducted

requalification examinations for 24 operators

licensed to operate

the

Browns Ferry Nuclear Plant (BFNP).

Of the 12 reactor operators

(ROs)

and

12 senior

reactor

operators

(SROs) tested,

eight

ROs

and

seven

SRGs

passed

the examination for an overall

pass

rate of 63%.

In

accordance

with

the criteria

outlined

in

Section

ES-601

of

NUREG 1021,

Examiner

Standards,

the

NRC's

programmatic

evaluation

determined

the

BFN Requalification

Program

was unsatisfactory

.

Positive

management

attention

was

noted in solving training needs.

The active role

by management

in upgrading training provided

an

enhanced

program to support

safe plant operations.

The adequacy

of

these efforts

was

demonstrated

by the

100% pass

rate for all those

taking

the requalification

and initial examinations

the

weeks

of

January

22 and February 6, 1990.

Successful

usage

of the

emergency

operating

instructions

was

demonstrated

during

operator

examinations,

a

training

program

inspection,

and the annual

emergency

preparedness

exercise.

Control

of licensed

operator

status

was

found to

be

good

and

personnel

qualifications were reviewed at shift turnover.

The Unit 2 core

was defueled

during the

assessment

period.

This

operation

was performed in a methodical

and conservative

manner.

The

licensee

used

dunking

chambers

to monitor the

neutron

count rate

during defueling.

Only

one

minor problem occurred

resu1ting

in

slightly bending

the refueling

boom.

This occurred while moving the

empty boom back to the'vessel.

Management

immediately took action to

evaluate

and determine

the root cause,

and to take prompt corrective

action.

Overall the defueling

was well done.

Changes

were

made to strengthen

the Operations

organization.

An

Operations

t<anager

position over the Operations

Superintendent

was

created.

The Operations

Nanager

and three assistants

were hired to

bring in new management

perspectives.

These assistants

were assigned

to

upgrade

operator

training,

upgrade

procedures,

and

improve

nor -licensed

operator

performance.

To reduce

the administrative

burden

on the Shift Operations

Supervisor,

a Shift Support Supervisor

was created.

This

change

resulted

in increased

involvement of the

SOS

in operational activities.

Staffing could support operation of

one unit with a six crew rotation.

The ability of the

new operations

organization to function

as

a

team at an operating plant has not yet

been demonstrated.

The

Operations

organization

continues

to

have

problems

with

performing timely and

adequate

actions

in response

to control

room

alarms

associated

with off-normal conditions.

A second violation in

less

than

a year

associated

with loss of large quantities

of

potent>ally

contaminated

reactor

grade

water

occurred.

This

violation involved the overflow of water from the spent fuel storage

pool into the ventilation

system

and

onto

areas

of the reactor

building.

If the initial control

room alarm

had

been

adequately

. pursued

in accordance

with the Alarm Response

Procedure,

the event

would have been avoided.

An unplanned

engineered

safety feature

actuation

occurred

during

a

routine

power supply transfer

because

the operator

did not follow

procedures

to verify an alternate

power supply available prior to the

transfer.

A circuit breaker

was found out of position but this was

noi indicated

by the

configuration

control

records.

Previous

corrective actions for sim'ilar events

were ineffective.

The licensee's

program to provide incident investigations

when

an

error or plant event

occurs

has

been

strengthened.

These

reviews

included identification of the root cause

and corrective actions.

The investigation

reports

were self-critical with good corrective

actions.

The corrective actions

were found to be formally tracked

and

completed.

These rigorous self evaluations

and

good corrective

actions

are

a strength

of the

licensee

programs.

The licensee

initiated

a

scram reduction

program which included

a review of all

past

scrams

between

1978

and the

shutdowns

in 1985.

One

hundred

twenty-two scram reouction

recommendations

were made in the,.review.

Although plant

housekeeping

is generally

gocd,

housekeeping

and

identification of material deficiencies

in less frequently traveled

areas

of the plant

was poor.

Examples

which were corrected after.

being .identified by inspectors

were the Residual

Heat

Removal Service

.Water

(RHRSW) cable tray tunnel

and

Standby

Gas

Treatment

System

rooms.

Control room improvements

completed included extensive relabeling

and

work station upgrades

to enhance

control

room operations.

Relabeling

was especially

noteworthy.

The annunciator

windows are clear

and

easy to read.

New operator aids are in place.

Red and green colored

carpeting

has

been

placed

throughout the control

rooms to designate

restricted

access

areas.

During the assessment

period

a procedures

review and upgrade

program

was initiated to correct problems in operating

and abnormal operating

instructions.

A number of changes

were

made to clarify TS in

ar.

effort to avoid misinterpretation or liberal interpretation of TS.

A

violation was identified for not correctly updating controlled copies

of TS used

in plant operations.

Continuing

problems

were

noted with compensatory fire protection

measures.

A

TS violation was identified involving two fire door's

found open wiihout compensatory

measure's

being taken.

This item was

significant in that the two doors were on

a frequently traveled

path

to the

control

room

arid plant

personnel

did not question

this

conaition.

Another

TS violation occurred

when fire hose

stations

were

removed

from service

and

compensatory

fire hoses

were not

connected

as required.

In addition, the fire hose stations

in all

three reactor buildings

had

been

removed

from service,

placing the

plant outside of TS requirements.

Although procedures

were in place

that

established

a

system

to

control

compensatory

measures,

management

control

of the

system

was

ineffective.

Operations

personnel

were not knowledgeable

of the fire protection

compensatory

, measures

in place.

As

a result of these

events,

the responsibility

for fire protection

was integrated

into Operations

arid the on-duty

fire brigade

now reports directly to the SOS.

An inspection of the licensee's fire protectior program was performed

late .in the

assessment

period.

The inspection

did not note

any

weaknesses

in the areas

of fire protection control

and surveillance

procedures,

surveillance

inspection

and test results, fire brigade

tra'ining

and staffing, guality Assurance

(gA) audits, fire fighting

equipment,

arid fire, protection systems.

In addition, the performance

of the fire brigade

was

observed

during

an

unannounced drill ard

found to be acceptable.

Five violations were identified during the assessment

period.

Assessment

Period Performance

Rating.

Category:

2

Recommendations:

The

Board

recommends

that the

high level of management

attention

continue to,ensure

a safe

and essentially trouble free startup,

power

ascension

and operation of Unit 2.

A more aggressive

involvement and

sense

of ownership

by the operations staff could have prevented

some

of the problems in other areas

such

as post-maintenance/modification

'esting.

The effort to minimize personnel

error must continue to

receive increased

management

attention.

Radiological Controls

Base Period'Analysis

No inspections

were performed

fn the

base

period iri tie area of the

radiation

protection

program.

One

chemistry

and

radiological

effluent inspection

was conducted.

The

inspection

noted

an

aggressive

program

was

in place for

maintenance

of water quality.

An audit

had

been

conducted

in

effluert monitoring

by the

corporate

gA organization.

Plant

gA

conducted

quality surveillances

in the chemistry

and radiological

effluent areas.

Staffing was

51 persons of an allocation of 52.

New

equipment

had

been

installed

in

the

chemistry, laboratory

arid

additional

upgrades

were planned.

Mater chemistry

was maintained

under close control

and reviewed

by

management.

Administrative limits and action levels

were

changed

procedurally to bring the plant levels in line with the

new Electric

Power

Research

Institute

(EPRI) guidelines.

The Chemistry Notice

System

was

implemented to assure

an appropriate

level of management

would

be notified whenever

chemistry

samples

exhibited

deviant

trends,

equipment

was

out of service,

and

samples

indicated

unsatisfactory results.

I

During the

base

period,

plans

were to startup

the plant with an

Interim Post Accident Sample

System

(PASS) in=place.

There were no

violations or deviations in this area in the base period.

Assessment

Period Analysis

One

radiation

protection

inspection

was

performed

during

the

appraisal

period.

Key management

changes

were implemented

by the licensee during'his

assessment

period.

The health

physics

technical

supervisor

was

promoted

to Radiation

Protection

t':anager

when

the position

was

vacated.

The Radiation Protection

(RP)

group

was reorganized

into

four functionial groups with managers

over each

group.

The

RP group

0

10

had

been

downsized

from approximately

225 to 180 people.

During the

downsizing

and reorganization,

the level of RP program effectiveness

was

maintained.

All health

physics

(HP) contractor

support

was

terminated

early in the

assessment

period.

Improvements

in

RP

program

support

were

evidenced

by the active

involvement of the

Senior Vice President

of Nuclear

Power.

Senior management's

direct

review and

comment

on key elements

of the

RP program have also

had

a

positive effect

on morale.

The solid

radwaste

group,

which

had

previously been

a part of Operations,

was

moved under the

RP group to

better

enhance

radiological controls.

Overall, radiation protection

management

consisted of a staff with strong technical

backgrounds

and

good power plant experience.

Collective annual site person-rem

was

1181 for 1987,

1155 for 1988,

and

656 for 1989, resulting in

a three year

average

of 997.

The

three year person-rem

average

was

good because

the licensee

was in

extended

outage with extensive modification throughout the assessment

period.

The reduction in collective dose

between

1988

and

1989 was

attributed to effective use of shielding

packages

and to the shift of

environmental qualification work from high cose

areas

in the plant to

lower dose

areas.,Through

the

end of March 1990, collective dose

was

216 p~rson-rem,

indicating

a downward trend.

Personnel

contamination

events

(PCEs), were

241 for 1987,

468 for

1988,

and

147 for 1989.

The large rise in 1988

was attributed to

contaminations

on

shoes

in the clean

areas

of the Radiation Control

Area (RCA).

The significant reduction of PCEs

nosed in 1989

was

a

result

of increased

mopping

of

RCA clean

areas,

placing solid

barriers

around

contaminated

areas,

and the overall reduction of

plant

contaminated

area.

Radiological

controls

utilized during

unexpected

events, for example spills of contaminated

liquids, were

effective in minimizing contaminated

area

and in maintaining the

low

level of PCEs.

Through March 1990 only 10

PCEs

have

been reported,

indicating

a significant improvement and'ontinuing

downward trend.

Reductions

in contaminated

area

also

showed

an improving trend.

In

1988 approximately

12.2 percent

of the total

RCA (910,485 ft~) was

considered

contaminated.

In 1989 this was reduced to 10.5 percent

followed by a further reduction to 7.4 percent

in March of 1990.

Other licensee initiatives observed

during this appraisal

period were

as follows:

(1) the addition of

12

automated

personnel

friskers

located

throughout the

RCA for better personnel

contamination ident-

ification and control, (2) utilization of recirculation pipe, reactor

vessel

drain line,

and control rod drive seismic support

mockups for

job t,raining and dose reduction,

and (3) the addition of 3 As-Low-As-

Reasonably-Achievable

(ALARA) program engineers

ard the requiring of

an

ALARA review for jobs that

could result

in

a

one

person-rem

exposure.

Continuing training for

HP technicians

was increased

from 20 to 90

hours

annually.

Also,

a

new

5 part

course

was

added for general

0

0

11

employees

in ALARA awareness.

The last

segment of the course

was

a

practical

factors

demonstration

of the students'erformance

on

a

'functioning plant systems

mockup.

The mockup

was representative

of

in-plant valves, filters,

and

a demineralizer.

The licensee's

training

program 'was

considered

effective

fn preparing

licensee

personnel

for in-plant radiological operations.

Continued

management

support for the

chemistry

ard radiological

effluents

programs

was demonstrated

by adequate staff levels for the

chemistry

department

and

by the

upgrade

of laboratory,

count room,

and effluent monitoring equipment.

Support

was also demonstrated

by

the decision to install the

permanent

PASS

system prior to Unit 2

startup,

instead of the interim unit originally planned.

Liquid and gaseous

effluents

and corresponding

dcses

showed

a slight

decline

from previous, periods.

The

Radiological

Envfronmental

tlonito> fng Program

was

conducted

by an offsite agency

of TYA.

No

unusual results

were noted.

Annual Technical Specification audits

were conducted

by'

corporate

qroup.

More detailed surveillance audits were conducted

by an onsite

Ouality Surveillance

organization.

Audit findings appeared

to be

minor fn nature

and were corrected

fn a timely manner.

The licensee's

beta isotope

program was evaluated

through comparative

-analysfs

of

NRC provided

samples.

All analyses

were

fn- agreement

wfth

NRC r esults.

3.

No violations or deviations

were identified fn the Radiological

Controls area.

Assessment

Period Performance

Rating

Category:

1

C.

tiaintenance

ard Surveillance

Base Period Analysis:

The

conduct

of

plant

maintenance

and

the

installation

of

modifications

were

reviewed

on

a routine

basis

during the

base

period.

In additior, special

inspections

were conducted

fn the areas

of quality verification, desfgn control, arid Appendix R.

Inspection findings and reported

events

indicated

numerous

weaknesses

fn the

Browns

Ferry maintenance

program

and the installation of

modifications

during the

base

period.

The

weaknesses

included

problems

with fdentffjfng conditions

which adversely

affect the

plant,

work planning

and

scheduling,

material availability, work

impact

evaluations,

procedure

adequacy,

procedur al

adherence,

implementation

of work activities,

operability

requirements

for

12

,safety-related

equipment,

and preventive maintenance activities.

The

lack cf coordination

among responsible

groups

complicated

the work.

Licensee

corrective

actions

taken

during

the 'base

period

were

ineffective,

indicated

a

lack of

management

involvement

and

attention,

and reflected

a reactive approach to problem solving.

Problems

were identified in the

areas

of post-maintenance

and

post-modification testing

(PNT).

Numerous operational

related

events

occurred

due to

PNT deficiencies,

some of these

included engineered

safety features

(ESF) actuations,

TS violations',

and inoperable

and

damaged

equipment.

Oeficiencies

in the

PNT program were attributed

to

a lack of planning, failure to follow instructions

by maintenance

arid modifications

personnel,

and

confusing

and

inadequate

PHT

instructions. 'everal

instances

of improper

cable

terminations

occurred

during the period.

These

improper electrical

connections

were indicative of

a

weakness

in electrical. maintenance

performed

during plant mooiiications.

Proper

PNT would have identified the

improper connections.

Hanagement

was ineffective in identifying the

cause of the events

and preventing

subsequent

similar occurrences;

Licensee

investigations'or

maintenance

and modification related

events

were ri utinely superficial

and were routinely completed after

the

component

or

system

was -returned

to service.

Programmatic

conitrols for dispositioning

PHT deficiencies

dsd not require either

root cause

analysis

os

management

involvement tu resolve

possible

-safety significant issues.

S

TVA conducted

a

maintenance

self-assessr.;ent

in

Viay 1989,

which

concluded that program implementation

problems existed,

A weakness

was

noted in the control of backlogged

maintenance

requests;

There

was

a backlog of approximately

7500 maintenance

requests

of which

4500

items were startup

items.

A backlog of approximately

860 late

p~ eventive maintenance

(PH) requests

existed.

The overall

PH program

was determined to be weak.

The licensee

made

numerous

changes

in the conduct of. maintenance

and

the maintenance

organizaticn during the base period.

The Maintenance

Superintendent

was

replaced

twice

and

Maintenance

Managers

were

reassfgned

to different

areas

of responsibility.

To

complete

maintenance

and modifications in an organized

manner,

the licensee

divided the plant

systems

>nto three divisions to be worked in

divisional

outages.

Each

division

included

associated

instrumentation,

electrical

and mechanical

equipment.

The licensee

conducted

two routine

outage

meetings

daily coinciding with shift.

changes.

The first line supervisors

from the various plant groups

met

to

discuss

the

real-time

progress

of ongoing activities,

schedules

for planned activities,

and overall

schedules

for the

divisional

outages.

These

discussions

provided

a

forum for

interaction

between

the

different

groups

and

enhanced

the

prioritization and

coordination

of work activities

by the various

groups'

13

The .licensee

experienced

numerous

delays

in the

completion

of

scheduled

milestones

during

most

of the

period.

After the

maintenance

changes,

the maintenance

department

exceeded

MR work off

rates

and

by the

end of the period decreased

the overall backlog.

The installation of modifications

remained well behind

schedule

and

with lower than

expected

productivity rates

throughout

the

base

period.

The licensee

encountered

numerous

problems with the procurement

of

materials

and

components for maintenance

and modifications.

These

problems

contributed to the failure to meet schedules

and were the

result of inadequate

assessments

of wor k requirements,

poor planning,

and untimely requests for materials

and components.

The licensee

experienced

several liquid spills during the performance

of maintenance

activities.

These

were attributed

to inadequate

scoping of work and inadequate

equipment clearances.

A

number

of

CAgRs

were, written

on the

lack of 'timeliness

in

conducting

Measurement

and Test

Equipment

(MATE) out-of-tolerance

investigations.

These

CAgRs were to determine if previous

use of

out-of-tolerance

MSTE

was

acceptable

and

evaluate

the potential

impact upon op~rability cf systems

or equipment.

Investigations

were

routinely performed

beyond the TVA's required time period.

The lack

of licensee

management

action

on these

CA(Rs indicated

an inadequate

- sensitivity to potential plant safety problems.

The area

of TS surveillance testing

was reviewed- and observed

on

a

routine

basis

during the

base

period.

In addition,

a

special

inspection

was

conducted

on instrument

adequacy

in January - March,

1989,

which included

reviews of surveillance

testing

in progress.

The findings included

numerous

examples

of inadequate

Surveillance

Instructions (SIs)

and calibration procedures,

failure to follow SIs,

failure to perform SIs within the

TS required frequency,

and failure

to perform SIs

implemented

as

TS compensatory

measures.

Management

failure to resolve

SI problems,

and failure to utilize the procedure

change

process

when procedure

deficiencies

were identified were also

problems.

NRC inspectors

identified that the

licensee failed to

implement fully a

commitment in the Nuclear Performance

Plan

(NPP),

Volume 3,

to review

and

upgrade

SIs.

Insufficient management

attention

had

been directed

toward full implementation of the

NPP

cooziitments with regard

to the

SI upgrade

program

and toward the

adeouacy of the review, walkdown, validation and verification of SIs.

This was evidenced

by the numerous deficiencies identified during

NRC

inspections

in the base period.

The

licensee

implemented

significant actions

to address

the

Sl

problerrs

and provided

more detailed

procedures

for SI verification

and validation.

These

actions,

as

evidenced

by the continuing

events,

did not result. in

a decrease

in the SI deficiencies

by the

end of the base period.

0

St

14

Seven violations

and

one deviation

were identified during. the base

period.

Assessment

Period Analysis

The

conduct of plant maintenance

was

reviewed

on

a routine basis

during the, assessment

period.

In addition,

a Naintenance

Team

Inspection

(NTI) was

conducted

fn Oecevber

1989,

through

January

1990.

The HTI findings indicated that both the maintenance

program

and its

implementation

were satisfactory.

The satisfactory rating indicated

adequate

development

and implementation

of the important elements

of

a maintenance

program, with the areas

of weakness

being approximately

offset by strengths

iti other areas.

This was

a qualified rating,

as

Browns Ferry

has not operated

in over five years

and the capability

of maintenarice

to support

plant operation

could not

be directly

assessed.

Because

of the nuoh~r of key areas

not assessed

the NTI

recommended

a

followup maintenance

inspection

after restart

of

Unst 2.

The

new

maintenance

management

personnel

appeared

to work well

together

ard

address

prob1ems

fn a timely manner.

Nanagement

was

very receptive to

NRC findings and focused

increased

attentior. to the

work off rates

and proper

performance

of maintenance.

Hanagement

emphasized

compliance

with procedures

arid completion of assigned

work.

The

m .intenance

organization

made significant progress

in

reducing

the

number of open

Haintenance

Requests

(HR)

and

CAgRs

during

the

assessment

period.

The

decrease

in emergent

work

occurring

on

a aay-to-day basis,

the increased

management

attention

to improving work off rates,

and the

increased

emphasis

placed

on

eliminating late preventive

It'.aintenance

items all contributed to the

. reduction.

A number of management initiatives were

implemented tu increase

the

quality of maintenance.

These

included participation

in Owner's

Groups,

and the

use of performance

indicators

and trending in the

maintenance

process.

Engineering

support for maintenance

was strong

as evidenced

by the

technical

support that

management

provided for maintenance

through

System

Engineering.

The System

Engineering

Program

was noted

as

a

significant strength

during the NTI.

The

NRC staff observed

that

systems

engineers

were fully involved in decisions

associated

with

maintenance,

modification, ard design of their designated

systems.

The maintenance

backlog

appeared

to be excessive.

Ouring the HTI,

there

were

2300

open

NRs

on Unit 2,

and

a total of 4500 open

HRs on

all three units.

The

cause

of the large

number of open

NRs

was

attributed to inadequate

coordination of the work control process,

0

outlays

caused

by

the unavailability of

spare

parts,

drawing

discrepancies,

and plant modifications which had not been

completed.

The

maintenance

facilities

were

rated

as

more

than

adequate.

Maintenance

shops

were well organized

and contained

good equipment.

The control of issuance

of calibrated

tools

was

good.

The

N&TE

controls for .-calibrated

tools

were

very

accurate

and

the

lab

facilities for tool calibration were found to be good.

Inspection

findings

and

events

reports

indicated

that

problems

occurred early in the assessment

period which were the result of poor

work practices,

inattention to detail during the performance of work,

and failure to follow procedures.

Increased

management

attention

was

given to these

problems

and corrective

actions

were

implemented,

including personnel

disciplinary actions,

and increased

attention to

maintenance

by the general

foremen.

Many of the maintenance

problems

were

resolved

as

evidenced

by the

lack of reported

events

aria

work-related violations throughout

the

remainder of the

assessment-

period.

Maintenance

personne1

errors

decreased

sigrificantly from

the base period

and the early part of the assessment

period.

The

MTI identified that the maintenance

data

base

had insufficient

trending capability aria limited equipment operating history.

The NTI

noted unattended,

partly disassembled

.equipment

which

had not been

tagged

to identify in-process

work.

Tagging

practices

weri:

identified as

a weakness'during

the NTI.

Staffirg levels in the maintenance

organization

were above average at

the time of the inspection,

but were

reduceo after the NTI.

The

effect of the reduced staffing has not been

assessed.

A weakness

was

identified with the communication

between

upper management

and lower

levels of maintenance

management

and craft personnel

in that the

existing

communication

did not appear

to be effective in improving

the conduct of maintenance.

There also

appeared

to be

inadequate

coordination of maintenance

work between

the individual maintenance

craft

groups,

and

other

organizations

such

as

Operations,

Modifications, and Planning

and Scheduling.

The guality Control (gC)

.

staff

was satisfactorily organized,

staffed,

and trained to support

the plant's maintenance activities.

The maintenance

training program

was found to be generally strong.

The

licensee

has

implemented

a

good

technical

training

and

qualification program for craft personnel.

Training is provided

on a

rotating shift basis

and

most of the craft personnel

had

completed

upgraded training.

The majority of the craft had more than ten years

of work experience;

The

NTI noted,

however,

that electrical

maintenance

personnel

required to perform SIs

had not received training in SI performance,

Instrumentation

and

Controls

( ISC) maintenance

perso>nel

received

0

0

16

little or no refresher training,

and that few onsfte

mockups for 15G

training existed.

The

implementation of modifications

was

reviewed

by the resfdert

inspection

staff

on

a

routine

basis,

by

inspections

on

the

installation of modificatiors related to Inspection

and Enforcement

Bulletins

(IEB) 79-02

and 79-14,

and

by

a Safety

System gualfty

Evaluation

(SSQE)

team inspectiorI.

. Inspection

findfngs

and

operational

events

indicated

that

the

licensee's

performance

in modifications

was

poor near the end of the

assessment

period.

Violatfons were

issued for several

examples of

the'ailure to follow the procedures

and devfatfori from the drawings

during pipe support

and other hardware installations.

The violations

were attributed to inattention to detail,'oor work practices,

and

the failure of personnel

to follow instructions.

The

SS(E

identiffed

cases

of failure to follow the

General

Construction

Specifications,

drawings

and

instructions

fn

the

installation of modifications.

Browns Ferry identified cases

of work

performed

not ir, accordance

with procedures

and of violating

gC

holdpoints

in

two

non-cited

violations.

These

are

further

indications of poor work practices.

The licensee

has consistently failed to meet scheduled

milestones for

- the

completion

of. modifications.

Vodfffcatfons work rates

in the

plant increased

by the

end of the assessment

period due to increased

management

attention

and to review of work in the field.

The area of TS surveillance testing

was reviewed

and observea

through

inspections

ard during

a special

inspection

conducted

fn September

through

October

1989.

Inspection

findings

and

reported

events

sndicated

problems. with inadequate

test procedures,

failure to meet

surveillance

test

intervals,

failure to

implement

and

mafntafn

compensatory

measures

required

by TS,

and the failure to follow

procedures.

The problems also included lack of communication

between

operations,

surveillance,

maintenance,

and engineering

staffs.

In

addition,

the violations identified were similar to violations that

occurred

over the past

two years.

The deficiencies

indicated that

sufficient management

attention

was lacking and dfd not correct the

identified problems or adequately

implement the improved surveillance

test

program that has

been

developed

since

1986.

Escalated

enforcement

action

was

taken

fn this area.

A severity

level III violation was

issued for a programmatic

breakdown of the

surveillance

testing program.'he

escalated

enforcement

included

violations occurring in August and September

1989, which were similar

to violations issued

fn the two prior years.

Since

the. enforcement

conference

was

held

on

the

escalated

enforcement

action,

licensee

management

has

taken

steps

to improve

17

3.

personnel

accountability

arid adherence

te the surveillance

testing

program

requirements.

This

increased

managem'ant

attention

and

enhanced

personnel

performance

have resulted

in the absence

of new

events.

The

removal of fuel from the

core in January

1990,

the

subsequent

relaxation of TS requirements,

and the less restrictive

TS

amenidments

issued

for

secondary

containment

ard

the

Standby

Gas

Treatment

System,

have

reduced

the plant activity fn this area to a

minimum.

Because

of these

factors,

an

adequate

analysis

of the

improvement of the surveillance

program could not be made at the end

of the assessment

period.

Seven violations

were

issued

in the maintenance/surveillance

area

during the assessment

period.

Assessment

Period Performance

Rating:

Category:

3

Trend:

Improving

Recomendatiuns:

D.

The

Board

recommends

continued

management

attention

in the

area of

surveillance testing, to assure

that the corrective actions

taken

as

a

result

of the

escalated

enforcement

action

are

effective.

Implementation

of modifications is

a

weakness

in this functional

area,

and

emphasis

on

problem resolution

fn this

area

should

continue.

The

maintenance

area

generally

showed

significant

improvement but management

attention

should continue particularly in

those

areas

not assessed

by the

NRC Maintenance

Team Inispection.

Emergency

Preparedness

Base Period Analysis

This functional area

includes evaluation of activities related to the

implementation

of the

Emergency

Plan'and

procedures;

support

and

training of onsite

and offsite emergency

response

organizations,

and

licensee

performance

during

emergency

exercises

arid actual

events.

Performance

is also evaluated

in the areas

of event notifications,

recovery actions, protective actions,

and interactions

between

onsste

and offsite

emergency

response

organizations

during exercise

and

actual events.

During the base period one routine inspection

and one

remedial exercise evaluation were performed.

The

licensee's

emergency

preparedness

(EP)

program

continued

to

improve during the

base

period despite

the loss of two engineering

aiae positions

on the

EP staff.

The licensee's

Prompt Notification

System

was

enhanced

by the addition of 45 sirens to provide fixed-

siren

coverage

in the 5-to-10

>pile radius

formerly covered

via

mobile-siren routes.

18

, The

emergency

preparedness

program received

management

support to

upgrade

the basic

emergency

elements

needed

to identify promptly,

correctly classify,

adequately

staff,

and to

implement

the

key

elements

of the Radiological

Emergency

Plan

(REP)

and respective

procedures

in response

to emergency

events.

The corporate

EP staff

has continued to show strong support

by providing necessary

resources

in the areas

of scenario

development for exercises

and revisions to

the Emergency

Plan and Implementing Procedures.

'mergency

response facilities,

equipment

and supplies

were properly

maintained

and

the training of emergency

response

personnel

was

effective.

However,

the

large

number of make-up

sessions

for

emergency

response

training

had the potential of reducing

EP staff

time available for undertaking

program initiatives.

Two

REP

and

Emergency

Plan

Implementing

Procedures

(EPIPs)

changes

were approved

by licensee

management

and transmitted to the

NRC in a

timely

manner.

The

1 icen see '

yearly

internal

audit

was

comprehensive

ard included

an evaluation of the offsite interfaces.

There were five emergency

declarations

during the base period, all of

which were Notification of Unusual

Events.

Four of the five were

weather

related

(tornado

warning).

The other

involved loss of

qualified offsite

power.

All were

determined

to

be correctly

classified in a timely manner with appropriate offsite notifications

completed.

The l,icensee's

performance

during

a remedial exercise,

conducted

on

Hay 31,

1989,

was considered fully successful

and demonstrated

that

the licensee

could effec4ively implement the Raaiological

Emergency

Plan

and

procedures.

In general,

the

licensee

demonstrated

the

ability to identify off-normal conditions,

classify

events

in the

appropriate

emergency

category,

notify

appropriate

offsite

authorities,

ard

make appropriate

protective action recommendations.

The scenario

development

team did not have

a clear understanding

of

the Site

Area

Emergency

Action Level event

used

in the exercise;

'however,

the Site

Emergency

Director,

based

on his

judgement,

overcame

the

scenario difficulty and

made

a correct

and

prompt

classification.

The exercise

critique was effective

and detailed.

There were no exercise

weaknesses

identified.

2.

Assessment

Period Analysis

No inspections

were

conducted

in this area

during the

assessment

period.

However",

a full-scale exercise

was observed.

The licensee's

performance

during the exercise,

conducted

on November I and 2, 1989,

was

considered fully successful

and

demonstrated

that the licensee

coula effectively

implement

the

Emergency

Plan

and

implemer ting

procedures.

The exercise

included'n evaluation of the licensee's

ability to perform

assessments

cf plant status

and radiological

hazarCs,

and

make proper notifications to offsite authorities.

The

Emergency

Response

Facilities

were staffed in

a timely manner

and

were

adequate

to support

the response.

No equipment

or facility

related deficiencies

were found.

The

NRC participated

in the exercise,

including

a

Headquarters

Executive

Team,

and the Region II Base

and Site Teams.

The licensee

provided

support to the State for the ingestion

exposure

pathway

portion of the exercise

on the second

day.

The scenario

was adequate

to exercise fully the licensee

organization

as" well as the State,

Local, and the

NRC organizations.

Site accountability

was timely and

classification

and

notifications

were

prompt'nd

well within

,acceptable

time limit criteria.

The .critique reflected

an in-depth

analysis

of exercise

observations

and

management

commitments to,

improve the program.

TVA's response

to Bulletin 79-18, Audibility Problems

Encountered

on

Evacuation of Personnel

From High - Noise Areas,

has not been

com-

pleted,

but is still scheduled

for completion during the Unit 2

cycle

6 outage.

Overall,

during

the

assessment

period,

the

licensee

demonstrated

improvement in the capability to implement the

REP during simulated

and actual events.

No violations were reported

in the assessment

period.

S.

Assessment

Period Performance

Rating

Category:

2

Trend:

Improving

Security

Base Period Analysis

This functional area

addresses

the licensee's

program for controlling

personnel

access

to the safety related vital equipment.

During the

base

period there were

two inspections

of the licensee's

safeguards

program.

The licensee

continued to make

improvements

in the operation of its

alarms stations

and its training of the security officers.

Progress

was noted in completing the Unit 2 start-up

items.

This is largely

attributable

to

aggressive

and

knowledgeable

'site

security

management.

Package

search

capability at the

warehouse

improved

during this p~riod because

of the enhancement

of the N-ray equipment

and better trained operators.

There were five examples of failure to control safeguards

information

in a licensee identified viclation and

one instance cf the licensee

0

20

exceeding

the

one hour notification requirement

by three

hours for a

non-cited violation.

2.

Assessment

Period Analysis

There

were

two Security

inspections

and

one Material Control

and

Accountability inspection during the assessment

period.

Two severity

level

IV violations were identified for failure to control safeguards

information and failure to control protected

area

access.

Inadequate

physical

inventories

in 1987

and

1988 resulted in the identification

of 26 discrepancies

in 1989 involving nuclear material

control

and

accountability

which were not detected

in the earlier inventories.

One severity

level

IV violation

and

a civil penalty for repeat

violations were issued for failure to perform adequate

inventories.

The licensee

continued

tc experience

problems, with its safeguards

information program.

However, extensive

corrective actions

appeared

to be effective towards the end of the

SALP rating period.

Norale of

-the security officers was also

noted to be improving.

Inspectors

noted

the, quality assurance

audits

by three

auditing groups

were

thorough,

complete,

and effective.

The licensee

trended

and assured

that effective corrective

measures

were taken in response

to Safe-

guards

Events.

At the

Corporate

level the

licensee

continued to

experience

change

of key personnel.

.Responses

to Generic Letters

(GL)

have

been

thorough

and reflect" technical

ana

procedural

forethought.

Staffing was adequate

and procedures

have improved.

Physical Security,

Contingency,

Security Training,

and gualification

Plan revisions

were well coordinated, within and

by the licensee's

security organization prior to submittal to the

HRC.

Plan submittals

were clearly written and required little or no additional discussion

with the licensee.

Support of the site security program is still evidenced

by the strong

fiscal

commitments to upgrading

or replacing out-dated

equipment

and

hardware.

Physical

barriers

inside

the control

room

have

been

completed,

relocation

of part of the protected

area

perimeter is

finished,

and detection

and

assessment

capabilities

are

improved.

Interim upgrade

items

have

been

completed;

however,

slippage

of

scheduled

completion dates

has occurred

and resulted in the continued

use of long term compensatory

measures.

The licensee

plans

a major

security system

upgrade to be implemented in 1992.

Progress

was

made

toward this implementation durirg this assessment

period.

The

new

system would reduce the number of compensatory

posts

now in effect.

There were three violations reported in the assessment

period.

Assessment

Period Performance

Rating

Category:

2

21

Recorder dati ons

The Board

recommends

special

attention be'laced

on maintenance

of

the existing

equipment until the major security

system

upgrade,

scheduled for 1992, is fully implemented.

Engineering

and Technical Support

Base Period Analysis

The Engineering/Technical

Support

functional

area

addresses

the

adequacy

of the technical

and

engine~ring

support for all plant

activities.

It includes

licensee activities associated

with design

baseline.

evaluation

ard resultant

modifications,

engineering

and

technical

support

provided for the restart effort and to support

operations,

maintenance,

surveillance,

tr aining,

procurement,

and

configuration

management.

The

bases

for this assessment

were the

licensee's

technical

submittals,

and inspections

conducted

in this

area

including Seismic,

Appendix

R, Bulletin Closeout,

and

the

Monthly Resident

Reports.

Early

in the

base

period,

the

licensee's

engineering/technical

support staff continued to struggle with the

scope of work required

to resolve

the

many technical

and design 'issues

identified in Browns

Ferry's

Nuclear

Performance

Plan.

In addition,

the support staff

continued

to be

hampered

by its inabil'ity to assist effectively in

the

completion

of the

large

backlog

of modifications

already

identified.

The

combination

of the

large

BFNP

work backlog,

ineffective TVA engineering

and aodification efforts,

and unrealistic

restart

dates

contributed significantly to the

problems

TVA had in

reaching the timely resolution of significant restart

issues.

Unable

to correct its ineffective engineering/modification

structure

and the

attendart

constra>nts;

TYA often relied

on

pursuing

additional

analytical

methods

to further limit major restart mr,difications and

used

a pre-restart/post-restart

approach

to defer the correction of

noted deficiencies..

For example,

during the base period,

TVA had

made little progress

in

correcting past deficiencies that had been identified with piping and

supports at

BFNP.

In addition,

TVA has

shown an inability to adhere

to design criteria, past

commitments, or, incorporate the results

from

other independent

review efforts in the civil engineering discipline.

t'.anagement

.involvement

and

control

were

lacking in the

areas

of

nzsonry walls in that information on certain modifications of several

walls was not accurate.

The

NRC identified errors in the nuclear

steam

supply system

(NSSS)

seismic calculation of the reactor

pressure

vessel

during the

base

period.

The analytical

model

was found to have

assumed

that the

control rod drive

(CRD) housings

were seismically-restrained

when, in

fact,

no seismic

restraints

were installed

at

the

Browns Ferry

0,

22

2 ~

facility.'his resulted

in

a violation issued during the assessment

period.

During

the

base

per iod,

the

licensee

reorganized

the

onsite

engineering

and modification groups.

The new organization resulted

in

improving

the

site's

focus

on

accountability,

and

the

responsiveness

and

effectiveness

of

these

groups.

The

new

organization

put the engineering

and modification groups

under

one

site administrative

and functional authority who reports directly to

the Site Director.

As

a result,

Design

Nuclear Engineering

(DNE)

management

oversight

and involvement

was evident during the morning

turnover

and

outage

planning

meetings.

The reorganization

also

resulted in the iritiation of a duty DNE manager for weekend

and back

shift engineering

support for Operations,

and provided for direct

management

involvement'n

the

organization

'and

allocation

of

resources for the Restart

Test Program.

The base

period ended with the new organizational

structure

beginning

to establish

control

and accountability within the engineering

and

modifications

groups.

This

was

clearly

demonstrated

by site

management

placing

a temporary

hold on all engineering

work because

ot unsatisfactory

engineering quality.

measures

were developed

and

implemented to improve the quality and timeliness of engineering

work

packages.

- During the base

period,

no routine training inspections

or operator

licensing

examirations

were

conducted.

No

requalification

examinations

were administered,

however,

BFNP was in the final stages

of preparation for a requalification

exam to be conducted

during the

assessment

period.

The

NRC spent the week of June 26,

1989 reviewing

the 'xamination

material

for

inclusion

in

the

upcoming

requalification

exams.

Several

weaknesses

were identified

ard

comunicated to the

BFNP training staff.

Four violations and

one deviation were issued.

Assessment

Period Analysis

In the

assessment

period,

TVA senior

management

increased

their

involvement and control.

With the reorganization of the engineering

and modifications

group,

stea'dy

improvements

were

noted

in TVA's

disposition of the many restart technical

issues.

Management

involvement

and control were evident in the Seismic Class

I small

bore piping program.

A specific instance

was management's

effect on the size of the rigorous analysis

sample for the small bore

piping

program.

TVA

had

originally

committed

to

analyze

approximately

ten percent of the program scope.

However, additional

piping .within the

program

scope

was identified during implementation

of the Design Baseline

and Verification Program.-

This resulted

in

the analysis

sample

being

less

than

ten

percent.

Although it

23

involved

a

considerable

investment

in resources,

TVA agreed

to

increase

the sample size to meet the original ten percent

commitment.

Some

instances

in which management

control

was

less

than

adequate

included lack of timely followup on identified items in the areas of

emergency lighting, proper tagging of valves,

safe

shutdown lists and

instructions,

and component lists.

Increased

TVA management

attentior

has started

to affect issues

of

timeliness

and quality of the

products

from the

DNE groups.

In

addition,

TVA management

initiated the development of specific tools

to track the progress of these

groups in producing quality and timely

products.

This is

a major strength

shown during this period.

The approaches

taken

by the engineering staff to resolve technical

issues

from

a

safety

standpoint

showed

considerable

improvement

during

the

assessment

period.

TYA's resolutions

of the t~chnical

issues

associated

with Appendix R, post-fire

safe

shutdown,

cable

irstallation

practices,

Regulatory

Guide 1.97

( in

terms

of

alternative

instrumentation),

the

TS

submittals

for continuous

neutron

monst~ring

during refueling,

and

provisions

for

thermal

hydraulic stability were all clear

and complete.

Inspections

performed

of the engineering

effort to resolve

the

electrical

issues

at

Browns

Ferry founa

adequate

control of the

engineering

process

and

good

engineering

reviews of the

issues.

-Problems

were found, but with the large

amount of work examined,

the

problems did not represent

a significant percent of the output.

During the assessment

period,

the ongoing

BFNP Seismic Design

Program

implementation

was found to be satisfactory.

The licensee's

response

to the

CRD housing violation was to install seismic restraints

on the

Unit 2

CRD

housings.

The modification

was

accomplished

in

a

comprehensive,

well

planned

manner.

Further,

the

licensee

constructed

a

new full-scale model of the

CRD housings

and restraints

in order to rehearse

physical installation of the modification to

minimize radiation exposure

and time during actual installation.

The

installation

of

CRD

housing

seismic

restraints

is

a positive

indication of the licensee's

commitment to enhance

the safety of the

plant.

A detailed

review by an inspection

team of the

BFN Core Spray System

indicated that there appeared-to

be adequate

program implementation

fn the following areas to support Unit 2 startup:

Design Baseline

and

Verification Program,

TVA As-Constructed

Malkdowns, Drawing Control

Program,

ASllE Code Section XI, Restart

Test

Program (Prestartup),

Design

Changes,

Instrument

Line

Slope,

Melding,

g-List

Implementation,

ard Contractor

Recommendations.

The Calculations

and

Ycdification Controls

areas

were identified as requiring additional

TVA attention

and

NRC followup.

The staff evaluation

indicates

significant improvement in TVA's resolution of technica'1

issues

when

compared to the base period.

24

The

reported

events

pertaining

to Engineering/Technical

Support

involved seismic criteria, single failure issues

and

unplanned

ESF

actuations.

The

ESF

events

were traceable

to the nine circuit

protectors

installed in each unit.

The licensee's

engineering

and

technical

support

personnel

are

pursuing.

a

hardware fix for this

problem in a deliberate,

controlled,

and professional

manner.

The licensee

has

implemented

programs to address

-concerns identified

with design criteria,

thermal

stresses

and as-built details

of

piping/pipe supports,

and to address

concerns

identified with TVA's

past

implementation of

NRC Bulletins 79-02 (Pipe Support

Base Plate

Designs

Using Concrete

Expansion

Anchor Bolts)

and

79-14

(Seismic

Analyses for As-Built Safety-Related

Piping Systems).

These

programs

involved reinspection

and re-evaluation

of all piping systems

and

implementation of required restart modifications.

An inspection

was

performed

to verify that the pipe support

design modifications

had

been

completed

iri accordance

with design

documents.

The procedures

and

pipe

support

calculations

were

determined

to

be acceptable.

However,

a violation was identified for failure to follow procedures

in the construction

of. pipe

supports

arid in the guality Control

inspection of the completed supports.

The Maintenance

Team Inspection

noted the System Engineering

Program

as

a strength

in the Technical Staff.

.

The number of drawing deviations

increased

from 1500 during the base

p~riod to over

2000 during the

assessment

period.

Inconsistencies

existed

between

procedural

time limits for revision/correction

of

primary drawings significant to plant operational

safety.

Previous

corrective

action

was insufficient.

Using

updated

drawings with.

large

numbers of deviations is cumbersome

and increases

the potential

for errors.

During

the latter part of this

assessment

period,

Region II

ir.spectors

conducted

an, inspection

of the licensee's

control

room

operator

aria licensed

operator requalification accredited

trairiing

programs.

Improvements

in the area reflected

increased

management

attention.

The results of the inspection indicated that the program

appeared

to be adequate

to support safe plant operation,

however, the

simulator

had

numerous fidelity problems.

The licensee

proposes

to

correct

these

problems with the simulator upgrade

program scheduled

to

be

completed

by

December

1991.

The

Emergency

Operating

Instructions

(EOIs) were evaluated

as not being user friendly, but

are

adequate

for Unit 2 restart.

The upgrade to Revision

4 of the

'wner's guidelines will be performed after start-up of Unit 2.

Two violations

and three non-cited violations were identified during

the assessment

period.

Performance

Rating:

Category:

2

25

G.

Safety Assessment

and gualfty Verification

Base Period Analysis

During the base

period there

were frequent

changes

fn both sfte ana

corporate

management.

This contributed to programatfc instability

during the

base

period

and resulted

in minimal completion of work

activities

and the failure to meet scheduled

milestones.

During the

earlier

part of the

base

period,

corporate

management

was

riot

effectively involved fn site actfvities.

However, there

was

a steady

increase

in corporate

management

participation

and effectiveness

toward the

end of the

base

period.

The licensee

also performed

a

corporate audit on operatiorial readiness

during the base period.

A reorganization of the Plant Reporting Section which was responsible

for review,

investigation,

and reporting plant events,

occurred

during the

base

period.

NRC concerns

about failures to report

and

inadequate

root

cause

analysis

associated

with plant events

were

addressed

by TVA management.

Root cause

determination training was

provided to members of the management

and technical

organiizatfons

and

corrective

actions

and

Licensee

Event

Report

(LER) quality

was

improved.

While the licensee's

reportabflity threshold

and root

cause

determinations

improved

throughout

the

base

period,

the

licensee

on occasfoni

took the

approach

of fully analyzing

an event

prior to submitting

a

LER, resultfrig'n late submittals.

This

~

occurred

even with indication of

a problem existing when the event

was discovered.

Two examples of failure to submit

a

LER within 30

says

of the

discovery

of the

event

per

10

CFR Part 50.73

were

identified during the base

period.

An additional

example of failure

to

make

a four hour report

fn accordance

with

10

CFR Part

50.72

involved

an

unianalyzed

condition

dealing

wfth non-seismically

qualified clay pipe.

Significant

TVA and

NRC staff resources

were

concentrated

on the

resolution of technical

issues

during the

base

period, especially

concerning

Seismic

and Electrical Design

issues.

Licensee positions

ard submfttals

on these

issues

were often not timely, not sound,

ana

.

not well thcught out.

In the Seismic Design area,

many meetings

had

to

be

held

to

resolve

long-standing

issues

involving design

acceptance

criteria for restart.

There

were

instances

during the

base

period

when

the

licensee

provided

data

(e.g.,

electrical

separatiori)

that

had not receivea

adequate

I'evfew, resultfng fn the

need for further licensee

re-evaluation.

In the licensee's

response

to

Generic Letter 88-01,

NRC Position

on

Intergranular

Stress

Corrosion

Crackfng in

BNR Austenftfc Stainless

Steel

Piping,

the

licensee

had failed to include approximately

5GO welds in the three

units requiring examinatfcn

under the

GL 88-Cl fntergrar.ular stress

corrvsfon cracking program.

26

During the

base

period the

licensee

was constantly

in

a reactive

problem solving mode.

TVA made little progress

in correcting design

deficiencies

in the plant during the

base

period.

TVA identified

many of these

design deficiencies

as early as 1984.

In addition,

TVA

continued to change

many of its technical

positions during the base

period.

Thus, resolution of significant technical

issues

was often

protracted.

Even in those technical

areas

where the corporate staff had developed

considerable

experience

at Sequoyah,

a pro-active approach

to similar

Browns

Ferry

problems

was

not evident,

Corporate's

role often

appeared

to result

in less

conservative

positions.

The position

taken

on ampacity

was divergent

from the

one approved for Sequoyah

without a clear rationale.

During the base period,

the staff's review of the

TS change

requests

showed

an unclear

trend of the licensee's

technical

and licensing

capabilities.

Variability in the quality of

TS submittals

was

observed.

With

a

change

in Site Licensing

management,

there

was

a

discernible

improvement in the quality of submittals during the latter

portion of this base period.

The

NRC staff

conducted

an

inspection

in the

area

of quality

verification.

This

inspection

was'performed

to

assess

the

effectiveress

of the

licensee's

organization

for achieving

and

self-verifyino quality

in their functions.

Although

several

weaknesses

were

identified

during this

inspection,

the final

assessment

cannot'e

made until completion of the planned guality

Assurance

Programmatic

Team Inspection to be conducted

in the future.

The licensee's

10

CFR Part 50.59 program was reviewed during

a Design

Change

Program Inspection,

and in most

cases

found to comply with

minimum regulatory requirements,

however significant weaknesses

were

.

identified.

In addition,

two special

reactive

inspections

were

conducted

duritig the

base

period

to

determine

the

conditions

associated

with separate

problems

involving

inadequate

10

CFR

Part 50.59

reviews.

The results of the inspections

are

discussed

below.

The first inspection

dealt with the initiation of Unit

2

core

reloading without adequate

monitoring of the core neutron flux.

The

second

inspection

dealt with the failure by

TVA to identify and

correct

a condition where three

separate

EECW discharge

flow paths

associated

with safety

related

components

were

not seismically

qualified

due

to

the

presence

of vitrified clay piping.

The

condition did net

meet the

earthquake

design

requirements

of the

Final Safety Analysis Report, Section 10.10.2,

and

had existed since

original plant construction.

The condition went undetected

by the

licensee

in spite of numerous

opportunities

to discover it.

When

finally identified by contractor

personnel

working for

- the licensee

engineering

organization, it took 23 days for the information to be

0

27

reported to licensee

operations

personnel.

This delay resulted

in the

s fte proceeding

with Unit 2 core reload

unaware that

a 1 1 Emergency

Core

Cooling

Systems.

required

by Technical

Specifications

were

potentially inoperable.

This problem also raised

the concern that

the

licensee'may

not

have effectively

implemented

commitments

in

response

to

NRC Order

EA 85-49.

Mhen the problem was identified to

plant operations,

their response

was conservative,

complete,

and

'adequate.

In addition,

corporate

management

conducted

a thorough

review of the event which led to an aggressive

correction plan.

Three violations were identified during the base period.

2.

Assessment

Period Analysis:

t

Safety

assessment

and quality verification activities were. monitored

by Resident

Inspector activities,

team inspections

and through review

of technical submittals

made during the period.

The most significant improvement in this functional area

has

been in

the

implementation

of the

licensee's

corrective action

programs.

'This

was evident

by the progrweatic

upgrades

in the handling of

identified safety significant issues,

improvements

in the tracking

and assurance

of timeliness of addressing

identified problems,

and

an

increased

level of attention

by management

in the review of Condition

Adverse to guality (CA/) documents.

The latter is accomplished

by daily

- Management

Review Coomittee

meetings

to discuss

the disposition of

all

CA( reports.

These

meetings

include the Site Director, Plant

Manager,

Site

gA Yanager,

and Site Engineering

Manager.

Additional

improvements

were

notea

in better comunications

between

managers,

supervisors,

and

the staff, ard

increased

attention

by senior

TVA

, management

toward improvement of the CA( programs.

Management

feedback

was also obtained

through the semi-arnual

audits

of the Correction of Deficiencies

Program.

The remaining

concern in

this

area

is the large

number of items that must

be escalated

to

managemert prior to corrective action being taken.

During the December

1989 through

February

1990 time period,

the

HRC

conducted

an in-depth

team inspection of the

BFHP Maintenance

Program

and its

implementation.

The inspection

included

reviews of the

licensee's

auality assurance

program.

The quality, control, storage,

and

retrievability of

records

for mater ials,

equipment,

and

construction

was satisfactory.

management

demonstrated

a continuing

interest in work planning

and the orderly control, of records.

Generally, the work done

by TVA on licensing issues

showed

evidence

of prior planning

by management.

TN established

target

dates for

submittals

and generally

met those

dates.

Yet there

were several

instances,

most notably the evaluation of offsite hazardous

materials

and

an

amendment

request

on Standby

Gas Treatment

System operability

requirements

that were either delayed or not timely.

0

28

Ouring the

assessment

period,

TVA submfttals

generally

improved.

TVA's approach

to many technical

issues

exhibited

conservatism

and

were

generally

thorough

and

sound.

This

was especially

true

concerning

Fire

Protection,

the

Mafntenance

Program,

and

t~iicrobiologfcally Induced Corrosion

Program.

The staff noted fn an

October

1989 site visit that

TVA lacked aggressiveness

fn addressirg

the staff's

comments

on

BFN Emergency

Operating

Procedures

detailed

fn Inspect.fon

Report

88-200.

Inconsistencies

fn the quality and

in-depth

analyses

of TVA's submittals

were

evident

during

the

assessment

period;

however,

a definite trend toward

improvement in

quality and timeliness

was noted.

TVA exhibited strong

management

attention in identifying weaknesses

curing the

assessment

period.

Reliance

on the

gA Team inspection,

the Operational

Readiness

Pevfew

Team,

and the Nuclear Experience

Review Group providea continuing evidence

of TVA management

concern

for the status

of the restart effort.

The System Plant Acceptance

Evaluation

(SPAE)

process

was

implemented

to review the

system

documentation

to ensure

completion of the work scope prior to return

to service.

Still, this auait-type

feedback

only confirmed TVA's

problems with the successful

implementation of many of the corrective

action programs.

In those

cases

where

TVA management

implemented

continuous

feedback,

progress

was

being

made

toward

developing

consistent

quality

- engineering

work.

For

example,

the licensee's

measurement

of the

number of Field Change

Notices requfred for each

Engineering

Change

Notice appeared

to provide

a direct measurement

of the progress

being

made

toward providing quality engineering

work to the field.

Audits

corducted in the security, chemistry,

and radiological controls areas

by the

licensee

continued

to provide

feedback

to

management

on

achieved quality of the programs.

A broad spectra

of safety

issues

were identified by TVA employees

in

the

Employee

Concern

Task

Group

(ECTG)

program that reflected

a

previous

.lack of management

involvam~nt with quzlfty.

The

NRC

staff's

review of the

Browns Ferry -ECTG investigations,

correctfve

actions,

and

planned

programmatic

improver~nts

resu1ted

fn the

conclusion that the evaluations

were adequate

ard well documented.

Routine

NRC inspectiors

found that the safety analyses

of TACFs were

of good quality,

LERs were

adequately

closed,

and

10

CFR Part

21

reviews were well. done.

Conservatism

fn the licensee's

technical

approach

to problems

was

generally exhibited

and decision

making

was usually

on

a level that

ensured

adequate

management

review.

Yet

technical

reviews

occasiorally

lacked details

and

adequate

technical

bases.

Several

examples

were identified of the failure to take

prompt effective

action to correct identified deficiencies

related to problems with

engineering

calculations

and

welding

record

retrfevablity.

0

29

Additionally, the

licensee

failed to identify many

hardware defi-

ciencies during

a walkdown on the Core Spray System performed shortly

before

the scheduled

NRC vertical slice inspection.

The licensee's

presentations

during

meetings

continued

to

show

improvements

suggesting

better

communication

among licensee organizations.

During the

assessment

period, the licensee'generally

responded

well

to

NRC initiatives.

Host noteworthy

was the licensee's

revised

commitment to expedite

the necessary

modification work to complete

the

remaining

NUREG-0737

issues.

The licensee

also

committed to

install

hardened

wetwell vents

(Generic Letter 89-16)

on Unit 2

before the requested

completion date.

A followup inspection

performed

on

GL 88-01 issues

found Browns Ferry

responsive

to correcting

the deficiencies

identified in the

base

perioo.

The corrective actions

were determined to be thorough.

However,

there

have

been

some

instances

where

TVA has

not

been

responsive

in

a timely manner.

The schedule for correction of the

instrument

sense line was delayed at least twice ano correction for a

long

krown

design

deficiency

in

the

control

room

emergency

ventilation

system still is not complete.

TVA's recent

Operational

Readiness

Review indicated that the

BFNP response

to

NRC

IEB 88-04,

Potential

Safety-Related

Pump Loss,

may reflect

a lack of technical

and critical review.

The site licensing organization

improved the timeliness

of TVA's

responses

to the

NRC; however,

weaknesses still exist in both the

timeliness

arid quality of Notice of Violation responses.

A number of

the

licensee's

written responses

received

during the 'assessment

period were not timely and frequent extensions

were requested

to the

time requirements

of 10

CFR Part 2.201.

One deviation

was issued for

the failure to submit

a special

report in accordanice

wiKh a prior

commitment to the

NRC.

The staffing of the site licensing organization generally

supported

improvements in the timeliness of responses

to the

NRC, even with the

apparent

downsizing of the staff.

But continuing

changes

in line

personnel

in site licensing resulted in some problems with delivering

consistent,

high-quality submittals to the

NRC.

Consultants

have

been effectively used

by the licensing staff to support

the

heavy

work loaa supportirg restart.

There is

a defined

program of training established

at the site.

management,

provided identification of emerging training 'needs

and the

formulation of records.

Training was maintained

as

a high priority

relative to work scheduling.

The training 'facilities, curriculum,

and

instructors

appeared

to reflect

quality

and

indicated

responsiveness

to industry initiatives ard guid~lina.s.

30

-Procedural

compliance

continued tc be

a problem and was

a result of

fnacequate

training and line'organfzatfcral

interfaces.

There still

are quality problems with some

procedures.

A staff review of the

Browns Ferry

Emergency

Operating

Instructions

indicated

a

need to

revise the

EOI Writer's Guide to reflect the specific

human factors

concerns

pointed

out previously

in Inspection

Report 88-200.

In

addition,

TVA's

Phase

II Operational

Readiness

Review

Report

(triarch 9, 1990)

indicated similar deficiencies

fn

a wfde variety of

procedures

and associated writer's guides.

Three

violations

and

two deviations

were identified during

the

assessm~et

period:

3.

Performance

Rating:

Category:

3

Trend:

Improving

31

SUPPORTING

DATA AND SUMMARIES

Licensee Activities

The start of the

base

perivd corresponded

to the

commencement

of fuel

loading.

This occurred

at 9:50 a.m.

(CST)

on January

3, 1989.

The core

reload

was

complete at 11:Ol a.m., on January

30,

1989.

The reload

was

delayed while in progress

by refueling bridge

and

source

range

neutron

monitoring problems.

Maintenance

and mod'ificatic n work continued after reload.

Work was

performed with the

major plant

equipment

divided into

one of three

divisions

to minimize

Technical .Specifications

impact

on

the

work

schedule.

New

emerging

work items

made

the existing

schedule

impractical if

divisional outages

were to continue.

TYA decided to offload the core to

expedite

work completion,

to

complete

a

Special

Nuclear

Materials

inventory,

and to resolve

some Environmental gualifications issues.

The

Unit

2 core offload began

at 2:00

a.m.

on January

6,

1990,

and

was

complete

at 4:33 p.m.

on January

23, l990.

The offload enabled

Browns

Ferry, with Tech

Spec relief, to begin working in

a Bulk Work fashion,

with minimal restrictions

caused

by equipment restrictions.

All-three units at

Browns Ferry are offloaded.

Unit 2 is currently

scheduled for critically in September

1990.

Direct Inspection

and Review Activities

In adaition to the routine

inspections

performed at the

Browns Ferry

facility by the

NRC staff,

a

number of special

team inspections

were

conoucted.

These

were conducted

in fire protection, quality verification,

design

control,

Appendix

R, maintenance,.

and

seismic.

The inspection

results

are discussed

in the applicable functional area.

Review activities were all associated

with licensing activities based,

in

part,

upon licensing actions successfully

completed during this appraisal

period.

These

activities

included

the following:

one waiver of

compliance

issued,

three requests

for relief granted,

one exemption,

one

emergency

or exioent

license

amendment

issued,

two Hulti-Plant Action

items resolved,

and eleven significant plant specific issues

resolved.

To

support licensing activities, meetings

were also held with TYA to address

licensing

and other technical

issues.

32

C.

Enforcement Activity

FUNCTIONAL

AREA

3 ut own

pera

sons

Radiological Controls

Maintenance/Surveillanc~

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/guality

Verification

TFQ

4

1

5

1

3

2

1

2

2

1

2

SEVERITY LEVEL

BASE PERIOD

ASSESSMENT

PERIOD

Dev.

V

IV

III .

Dev.

V

IV III

~

~

~

0

33

D.-

Review of Licensee

Event Reports

(LERs)

During the

SALP period

71

LERs .were analyzed,

35 of which were in the

assessment

period.

Most

LERs were well written and issued in a timely

manner.

The distribution of these

events

by cause

as determined

by the

NRC was as follows:

Ease Period

Cause

Personnel

Error

Design, Manufacturing, Construction/Installation

External

Causes

Defective Procedure

t:,anagement/guality

Assurance Deficiency

Other

% + W W&&&W W W&W W W &W&W&&& A&W WA&WW&W W W WWW W W WWW 0

Total

Unit

1

2

3

4

9

2

6

3

1

1

3

1

2

4

A&W&&WW&&W&WWW&WW&W

14

19

3

- Assessment

Period

Cause

WW

W&&&WW && W&&&WAW&&&&&W&&&

Personnel

Error

Design, hhnufacturing, Construction/Installation

External

Causes

Defective Procedure

Management/guality

Assurance

Deficiency

Other

W&%&WW&&&W

~

Total

Unit

1

2

3

3

5

2

5

1

1

5

1

4

6

2

18

12

5

0