ML18025B619

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IE Insp Repts 50-259/81-14,50-260/81-14 & 50-296/81-14 on 810428-0525.Noncompliance Noted:Procedures for Control Room Emergency Pressurization Not Followed & HPCI Sys & Fire Pump Auto Start Inoperable
ML18025B619
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 06/26/1981
From: Cantrell F, Chase J, Paulk G, Sullivan R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18025B609 List:
References
50-259-81-14, 50-260-81-14, 50-296-81-14, NUDOCS 8109010524
Download: ML18025B619 (22)


See also: IR 05000259/1981014

Text

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NUCLEAR REGULATORY COMMISSION

REqION II

101 MARIETTAST., N.W., SUITE 3100

ATLANTA,GEORGIA 30303

Report Nos. 50-259/81-14,

50-260/81-14

and 50-296/81-14

Licensee:

Tennessee

Valley Authority

500A Che'stnut Street Tower II

Chattanooga,

Tennessee

37401

Facility Name:

Browns Ferry Nuclear Plant

Docket Nos. 50-259, 50-260,

and 50-296

License Nos. DPR-33,

DPR-52,

and DPR-68

Inspection at Browns Ferry Site near Athens,

Alabama

I

I

Inspector:

.

T

R.

F. Sullivan

c-.Z

G. L. Paulk

r

-C~

J

W.

hase

Approved by:

F. S. Cantrell, Sectj46

ief, Division of

Resident

and Reactor Project Inspection

Date Signed

Date Signed

z~ ei

Da

e Sig ed

z

P/

Da e

tg

SUMMARY

Inspection

on April 28 through May 25,

1981

Areas Inspected

This routine inspection

involved

246 resident

inspector-hours

in the

areas

of

operational

safety,

reportable'occurrences,

plant physical

protection,

reactor

trips,

surveillance

testing,

main'tenance,

fire protection,

review of star'tup

report, followup of primary leak Unit 3 and TMI action Items.

Results

Of the

10 areas

inspected,

no violations or deviations

were identified in seven

areas.

Three violations were found in three areas;

(Failure to follow procedures

for control

room emergency pressurization

(Units 1,

2 and 3), paragraphs

5 and 8;

Failure

to

have

high

pressure

coolant

injection

system

operable

(Unit 3),

paragraph

8; and,

High pressure fire pumps auto-start

inoperable,

paragraph

12).

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".'".'~"

PDR,ADOCK 05000259

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'

DETAILS

Persons

Contacted

Licensee

Employees

H. L. Abercrombie,

Power Plant Superintendent

J.

R. Bynum, Assistant

Power Plant Superintendent

J.

L. Harness, Assistant

Power Plant Superintendent

R. T. Smith, equality Assurance

Supervisor

R.

G. Metke, Engineering Section Supervisor

D. C. Mims, Engineering

and Test Unit Supervisor

R.

G. Cockrell, Reactor Engineering Unit Superv'isor

J.

B. Studdard,

Operations Section Supervisor

A. L. Burnette, Assistant Operations Supervisor

R. Hunkapillar, Assistant Operations Supervisor

T. L. Chinn, Plant Compliance Supervisor

M. W. Haney, Mechanical Maintenance Section Supervisor

J. A. Teague, Electrical Maintenance

Section Supervisor

J.

K. Pittman, Instrument Maintenance Section Supervisor

J.'. Swindell, Overage Director

, B. Howard, Plant Health Physicians

R.

E. Jackson,

Chief Public Safety

R. Cole,

(}A Site Representative

Office of Power.

Other

licensee

employees

contacted

incl'uded

licensed

senior

reactor

operators,

reactor operators,

auxiliary operators,

craftsman,

technician,.

publ.ic safety officers,

gA personnel

and engineering personnel.

2.

Management Interview

Management

Interviews was conducted

on

May 1, 8,

15 and 22,

1981, with the

Power Plant Superintendent

and/or his assistant

power plant superintendents

and other

members

of his staff.

The inspectors

summarized

the

scope

and

findings of their inspection activities.

The licensee

was informed of the

four apparent

violations identified during the report period.

On June

12,

1981,

a

telephone

conference

was

held

between

Mr. James

P.

O'Rei lly,

Director,

Region II and Mr.

H. J.

Green, Director, Nuclear Operations

TVA.

The topics of discussion

were recent operational

events

and the effects that

plant

modifications

are

having

on

safety-related

systems

and

plant

operations.

The control of work activities at the plant was stressed

during

the discussions.

3.

Licensee Action on Previous Inspection Findings

Not inspected.

Unresolved Items

Unresolved items were not identified during this inspection.

Operati'onal

Safety

The inspectors

kept informed

on

a daily basis of the overall plant status

and

any significant safety

matters

related

to plant operations.

Daily

discussions

were held each morning with plant management

and various members

of the plant'operating staff:

The inspectors

made frequent visits to the control

room such that each

was

visited at least daily when

an inspector

was

on site.

Observation

included

instrument readings,

setpoints

and recordings;

status of operating

systems;

status

and alignments

of emergency

standby

systems;

purpose

of temporary

tags

on equipment controls

and switches;

annunciator

alarms;

adherence

to

procedures;

adherence

to limiting conditions

for operations;

temporary

alterations

in effect; daily journals

and data

sheet

entries;

and control

room

manning.

This inspection

activity also

included

numerous

informal

discussions with operators

and their supervisors.

General

plant tours were conducted

on at least

a weekly basis.

Portions of

the turbine building,

each reactor building and outside

areas

were visited.

Observations

included..-valve

positions

and

system

alignment;

snubber

and

hanger

conditions;

instrument

readings;

housekeeping;

radiation

area

controls; tag controls on equipment; work activities in progress;

vital area

control,s;

personnel.

badging,

personnel

search

and

escort.

Informal

discussions

were held with selected plant personnel

in their functional area

during these'ours.

On May 20,

1980 during

a routine tour of the control building, the inspector

noted that the control

room emergency ventilation

(CREU) unit "B" was not

aligned correctly, in that switch 0-HS-31-152

was in the "on" position vice

"auto" as required

by Operating

Instruction (OI)-31, Air Conditioning

and

Heating .of Reactor Building Control Bay.'he

inspector reported this to the

Assistant

Operation

Supervisor

who in turn directed

the Unit 3 Assistant

Shift Engineer

(ASE) to investigate the problem.

The ASE;; an electrical

engineer

and the inspector,

determined

by review of

drawings, that by having switch 0-HS-31-152 in the

"on" position,

the

"B"

CREY unit

should

have

been

running

and .damper

31-152

should

have

been

opened.

The

"B"

CREY unit was

not running

because

the local start-stop

switch for the

fan

was in the

stop position.

Damper

31-152 was not open

because

lagging

on the ventilation duct

was binding the linkage for the

damper.

The

ASE freed the linkage for damper

31-152 to.allow the damper to operate

and

had the lagging

removed to prevent further binding.

The local control

switch

was

placed

in the start position

and 0-HS-31-152

was placed in the

auto position.

These actions

were performed within 30 minutes of the time

the inspector identified the problem.

The unit was then tested satis-

factorily to ensure operability.

The licensee

has

been

unable to determine

how long the "B" CREV unit was inoperable.

The "A" CREV unit was determined

to be

operable'n

May 22,

1981,

the inspector

identified that not having the "B" CREV unit

operable

was

an apparent

violation to the Assistant

Plant Superintendent.

This event

was described

as

a failure to .follow procedure

(OI-31) which i s

required

by

Technical Specification 6.3.A. l.

The

Assistant

Plant

Superintendent

accepted

the

apparent

violation

without

comment

(259/81-14-01,

260/81-14-01

and 296/81-14-01).

Reactor Trips

The inspectors

reviewed activities associated

with the below listed reactor

trip during this report period.

The review included determination of cause,

safety sign'ificance,

performance

of, personnel

and

systems,

and corrective

action.

The inspectors

examined

instrument recordings,

computer printouts,

operations

journal

entries,

scram

reports

and

had

discussions

with

operations,

maintenance

and engineering

support personnel

as appropriate.

On April 23,

1981, Unit 3 tripped at 5:31 a.m.

from full power due to low

reactor water level. 'uring the transfer of start

busses

a short inter-

ruption of plant preferred

and non-preferred

power resulted in recirculation

pump runback followed by

a rapid increase

back to

90% of full flow.

The

resulting reactor water level collapse

produced

the low water level reactor

trip and

MSIV closure.

HPCI

and

RCIC initiation occurred

but both were

tripped

on high reactor water level before injection into the vessel.

The

main

steam relief valves were manually operated

to control pressure.

Plant

safety systems

responded satisfactorily.

No violations'or deviations were identified within the areas

inspected."

Reportable

Occurrences

The below listed licensee

event repor ts (LERs) were reviewed to determine if

the information provided met

NRC reporting requirements.

The determination

included

adequacy

of event

description

'and corrective

action

taken

or

planned,

existence

of potential

generic

problems

and

the relative safety

significance of each event.

Additional in plant reviews and discussion with

plant personnel

as appropriate

were

conducted

for those

indicated

by

an

asterisk.

LER NO.

259-81011

259-81015

Date

05-15-81

05-20-81

Event

Local fire protection panel

25-331

was deenergized

Continous air monitor for reactor/

turbine

building

ventilation

was

inoperable.'

~260-81014

260-81016

"260-81017

"296"81015

~296"81016

05-11-81

04-07-81

04-27-81

05-05-81

04-08-81

04-08-81

2C Residual

Heat Removal

Heat

Exchanger

had leak on the inner head

gasket.

Mode A of reactor water level

instrumentation

failed

upscale

resulting in turbine trip.

Scram discharge

instrument volume

scram

switch

not

set

within

technical specification limit.

Reactor

zone ventilation system

isolated

during

normal

reactor

operation.

High pressure

coolant injection

turbine

inner

exhaust

disc

ruptured.

With 3C Residual

Heat Removal heat

exchanger

out for maintenance,

the

high

pressure

coolant

injection

pumps

were

determined

to

be

inoperable.

Within the areas

reviewed,

no violations or deviations were identified.

The inspectors

observed

the

performance

of the

below listed surveillance

procedures.

The

inspection

consisted

of

a

review of the

procedure

for

technical

adequ'acy,

conformance to technical specifications,

verification of

test instrument calibration,

observation

on the conduct of the test,

removal

from service

and return to service of the system

and review of test

data'.

SI 4.2.E.2

b.

S I 4.2.B. 27

c.

SI 4.7.A.2

d.

SI 4.9.A.2.C

Air Sampling System Drywell Leak Detection

Suppression

Chamber Level

Primary Containment Integrated leak Rate test

(Isolation Valves Feedwater

System).

Battery Discharge Test

The inspector

had

no

comments

on

the

above

surveillance

test

with the

exception of SI 4.9.A.2.C, Battery Discharge Test which is discussed

below.

On

May

5,

1981,

the

inspector

observed

Surveillance

Instruction

(SI)

.

4:9.A.2.C (Battery Discharge Test) for the Unit 2 battery.

The test started

at 1: 16 p.m.

The inspector

observed

the start of this test from the battery

discharge trailer and then left to observe

other testing areas.

A tour of

the Unit 3 control

room revealed that SI 4.9.A.2.C prerequisite

step 1.5 was

not satisfied.

The prerequisite

requires

that

each

operating

unit high.

pressure

coolant injection (HPCI) valve (73-44)

HPCI, discharge

valve to be

open

and tagged with a caution order when the battery discharge test is in

progress.

Unit

2

and

3 were operating

at full pow'er and Unit

1 was in a

refueling outage during the test.

Unit 2 HPCI discharge

valve was

open

and

tagged

and

the Unit

3

HPCI discharge

valve

was

shut

and not tagged.

The

inspector notified the Assistant Shift Engineer in Unit 2 of the discrepancy

and

he responded

that

he interpreted

the surveillance

procedure

to require

only

opening

the

HPCI

discharge

valve for the unit under test.

The

inspector notified the Assistant Operations Supervisor 'of the discrepancy

at

2:30

p.m.

on

May 5.

He

responded

that prerequisite

step

1.5 was required

for all'operating units and

he immediately called the Shift Engineer to have

the discrepancy corrected.

The inspector

learned later that the Unit 3 operator

opened HPCI'valve 73-44

for unit 3 at 3:00 p.m.

on

May 5 and noted that the

HPCI suction

pressure

gage

pegged

high indicating that the air operated

check valve downstream of

the

HPCI discharge valve'as

leaking past its seat.

The operator

reclosed

HPCI discharge

valve

73-44 to prevent potential

overpressurizing

of the

condensate

system.

Operating Instruction (OI) 57

(II.G) requires that when

a unit battery is out of service

the

HPCI valve

73-44 must

be

opened to

consider

HPCI

system

operable.

Unit

3

HPCI

system

was

not

declared

inoperable

on May 5,

1981,

as required

by OI-57 and Technical Specification

surveillance

requirements

4.5.E.2.

No further action

was

taken

by the

licensee

on this date.

On

May

6

at

9:00

a.m.

the

inspector

informed

the

Assistant

Plant

Superintendent

of the procedural

problems

encountered

the previous

day.

At

1: 15 p.m., the inspector toured the Unit 3 control room and noted

HPCI valve

73-44 was still shut, with the battery discharge test still in progress.

The

inspector

immediately advised

the Shift Engineer that the

HPCI Valve 73-44

was required to be open in accordance

with the test procedures

and if this

valve

could

not

be

opened

the

HPCI

system

was required

to

be declared

inoperable

in

accordance

with Operating

Instruction

57

and

Technical

Specification surveillance

requirement 4.5.E.2.

The Shift Engineer

said

he

would look into the matter.

At 4:00 p.m. the inspector

called the Assistant

Operations

Supervisor

to ask the status

of the Unit

3

HPCI

system.

He

reported

the

HPCI

system fully operational.

The inspector

expressed

his

concerns

over the OI-57 requirement

and the Assistant Operations

Supervisor,

concurred

and declared

HPCI system for Unit 3 inoperable at 4:02 p.m. which

is approximately

27 hours3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br />

from the start of the test,

and

25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />

from the

initial attempt to open

HPCI valve 73-44 for Unit 3.

Procedures

OI-57

and

SI 4.9.A.2.C requires

HPCI

discharge

valves

to

be

opened

in accordance

with the General Electric design analysis criteria step

10

on figures 8.6-4b

and 8.6-4c of the plant's

FSAR.

Several

operators,

assistant

shift engineers,

and shift engineers

were not familiar with the

requirement

of OI-57 or SI 4.9.A.2'.C to

open

HPCI valves

73-44

when

a

battery is out of service.

The failure to adhere

to procedures

is contrary

to Technical Specifications 6.3.A.6

which states

that detailed 'ritten

procedures

shall

be

prepared

and

adhered

to for surveillance

testing

and

requirements.

The

inspector

informed

the

licensee

of this

apparent

violation (260/81-14-01

and 296/81-14-01)

on May 7, 1981,

The failure to declare

high pressure

coolant injection system

inoperable is

contrary to Technical Specification 3.5.ED 1 which states

that

the

high

pressure

coolant

injection

system

shall

be

operable

whenever

there

is

irradiated

fuel in the reactor vessel

and the reactor vessel

pressure

is

gr'eater

than

122 psig.

This matter

and other

events

involving compliance

with Technical

Specification

were discussed

in

a telephone

call

May 11,

1981,

from the Director,

Region II to the Director of Nuclear

Power,

TVA.

This is identified as

a violation (296/81-14-03.)

Plant Physical Protection

During

the

course

of routine inspection activities,

the inspectors

made

observations

of certain

plant

physical

protection

activities.

These

included personnel

badging,

personnel

search

and escort,

vehicle

search

and

escorts,

communications

and vital area access control.

No violations or deviations were identified within the areas

inspected.

10.

Review of Unit 3 Startup Report

The inspector

reviewed

Startup

Report for Unit

3 fuel cyclic four, dated

April 20,

1981.

The review was

conducted

to verify that the information

reported

was technically

adequate

and that the reporting

requirements

of

Technical Specification 6.7. l.a were satisfied.

u.

Within the areas

inspected

no violations or deviations were identified.

Maintenance

The

inspectors

observed

the

below listed

maintenance

activities

for

procedure

adequacy.,

adherence

to procedure

and

observed

the

actual

per-

formance of the work activity.

a.

Mechanical

Maintenance'nstruction

(MMI)-23 Quarterly Inspection

of

High-Pressure

Coolant Injection.

b.

Electrical Maintenance

Instruction (EMI)-78 Torquing of 480

V Shutdown

Board Normal Feeder

Busway Joint Bolts.

No violations or deviations were identified in the areas

inspected.

12.

Fire Protection

~

On May 1,

1981,

the licensee identified to the resident

inspector that the

auto-start capability for all four fire pumps

had

been defeated

by lifting

the auto-start 'circuit electrical

leads

in relay board

52.

Plant staff

concluded

that these electrical

leads

were lifted by

workman installing

circuits for the new 500

KV Cordova line sometime after April 14,

1981.

These electrical

leads

had been identified by the engineer

in charge of the

modifications

as

not to

be lifted'y placing

"masking"'ape

over

the

terminals

and

the electrical

leads prior to the modification beginning.

Other electrical

leads which were identified in,this manner were not

disturbed.

In addition,

no other safety

systems

had

been disabled or worked

on because of this modification.

TVA's evaluation

showed that all four fire pumps

could

have

been started

manually if needed

and at least

one fire pump was running at all times since

April 14 to May 1,

1981 which wo'uld have provided automatic fire protection.

Under the IE new interim enforcement criteria for license identified items,

this item was presented

to the Plant Superintendent

as

an apparent violation

on

May 8,

1981

for

the failure to

have

the

automatic initiation logic

operable

for the

high

pressure

fire protection

system

as

required

by

Technical Specification

3. 11.A. l.b.

The Plant Superintendent

was requested

to

address

the control

of plant modification

work in

response

to the

apparent violation (259/81-14-02,

260/81-14-03

and 296/81-14-04).

Primary Leak Unit 3

On May 21,

1981, at 11:45 p.m. after completing the pumping of nitrogen from

the torus to the drywell to maintain the differential pressure

greater

than

1.3 psig between

torus

and drywell, the operator

noted

a steady

increase

in

drywell

pressure

at approximately

0. 1

psig

per

minute.

The

operator

suspected

a loss of reactor building closed

cooling water

(RBCCW) to the

drywell fans.

He increased

the

RBCCW flow to the drywell..by isolating the

reactor

water cleanup

(RWCU) system.

This action

decreased

the rate at

which the drywell pressure

was increasing

to approximately

0.025

psig per

minute.

To prevent

a primary containment isolation, which occurs at

2 psig

drywell pressure,

the operator

cross

connected

the torus to the drywell via

the

stand-by

gas

treatment

system

to. equalize

pressures.

This

was

done

approximately

5 minutes

into the

event

and, after drywell

pressure

had

reached

1.6 psig.

This action

decreased

the -'drywell pressure

to approx-

imately 1.0 psig.

On

May 22,

1981,

at

1230

a.m.

the drywell equipment

drain

pumps

came

on

indicating

a total

leak rate

in to the drywell of 21.5

gpm.

(This gave

approximately

18

gpm unidentified

leakage

and

Technical Specification 3.6.C. 1 allows less

than

5 gpm'unidentified).

The operator

then

began

a

reactor

shutdown at 12:35 a.m.

and

had the reactor

shutdown at 1:23 a.m.

on

May 22,

1981.

At 12:45 a.m.,

the Senior

Reactor Operator declared

a site

alert and informed the

NRC via the red phone of the situation at 1:00 a.m..

At 2:30 a.m.,

TVA secured

from the site alert and went to an unusal

event

status

because

the

leak rate

was

less

than

25

gpm.

No radioactivity was

released

to the outside environment.

During the cooldown of the reactor,,the

leak rate into the drywell steadly

decreased

until it stabalized

out at approximately

7

gpm at 6:00

a.m.

on

May 22,

1981.

At 12:02 a.m.,

on May 23,

1981,

personnel

entered

the Unit 3

drywell and determined that leakage

was coming from "B" recirculation

pump

discharge

valve

(68-79)

packing.

The

valve

was

then

back

seated

and

repacking

commenced.

During the. repacking of the valve, it was determined

that the majority of the packing

had

been

blown out causing

the leak.

TVA

is currently evaluating the cause

and corrective action.

There was no

t

damage

inside the drywell as

a result of the leakage.

Unit 3 was returned

to service at 0410 on May 26,

1981.

Sequence

of Events

May 21,

1981

11:45 p.m.

11:48 p.m.

11:51 p.m.

Completed pumping nitrogen from torus to drywell, drywell pressure

begins to increase.

Increased

RBCCW system flow

Cross connected drywell to torus via SBGT maxium drywell

pressure

has increased

to 1.6 psig

May 22,

1981

12:30 p.m.

12:35 p.m.

12:45 p.m.

Drywell equipment drain pump started indicating leak of 21.5 gpm.

Commenced reactor shut down

Senior Reactor Operator declares

a site alert

NRC was informed that

a leak rate of 21.45

gpm was occurring into

the drywell.

1:23 a.m.

Reactor is 'shutdown.

Commenced

cooldown leak rate has decreased

to 15.83 gpm.

2:00 a.m.

2:30 a.m.

2:45 a.m.

3:00 a.m.

Con'ditions are stable, no-off site release

Secured

from site alert and went to an unusual. event status

Resident inspector arrived at the site.

Leak rate 16.5 gpm.

4:00 a.m.

4:30 a.m.

6:00 a.m.

May 23,

1981

12:02 a.m.

Leak rate 11.83 gpm.

Radioactivity in the drywell is 2.26

X E-3 uc/cc.

Leak rate is 7 gpm and steady

Entered drywel.l and determined leak to be from packing on

valve 68-79,

B recirc pump discharge

valve

May 25,

1981

3:20 a.m.

Repairs to the

B recirc pump discharge valve are complete.

Commenced startup of the reactor.

May 26,

1981

4:10 a.m.

Reactor

has been returned to power operation

In the above areas

no violations or deviations were identified.

14.

TMI Action Items

The inspectors

conducted

a review 'of the

licensee

response

and action

on

five TMI Action Items which are listed below

a.

I.A.1.3(1)

b.

I.C.5

c.

I.C.6

d.

II.K.3(22a)

e.

II.E.4.2(6)

Shift Manning (Limit Overtime)

Feedback of Operating Experience

Verifying Correct. Performance of Operating

Activities

Final Recommendations

B and 0 Task Force

(Procedures

for RCIC Suction)

Containment Isolation Dependability

Licensee

conformance with the Action Item requirements

was evaluated

against

the criteria established

in NUREGs-0585,

0660

and 0737.

Status of imple-

mentation

was verified through review of procedures,

examination of records

and discussions with various members of the plant staff.

The overall

requirements

were

met or scheduled

to

be

met with some minor

exceptions

on items 14.a,

b,

and c.

On item 14.d, there

are

no plans for

automatic

switchover of RCIC suction

and justification for this conclusion

was

provided

by the licensee.

The procedures

for manual

switchover

were

determined to be adequate.

The licensee

interim action concerning

item 14.e has been to provide admini-.

strative

controls

over

the

containments

purge

valves.

Revisions

to

procedures

have

not permitted

purging into containment

except during cold

shutdown

and also the purge valves are

cautioned

tagged.

TVA has

recently

conducted

an operability analysis

and

has determined that the purge valves

are adequate

for closure against

DBA,

LOCA forces ther'efore modificaiton of

the

purge

valves is not necessary.

Purge

valve closure

times

are

being

reduced

and debris

screens

are being installed during the current refueling

outage

on

Browns Ferry

1.

This information along with TVA's analysis

was

sent to T. A. IppoLito, ORB,

NRR, dated June

2, 1981.

The inspectors

intend to do further fo'llowup of implementation of items 14.a

and

14.b

and will leave

these

open.

Items

14.c,

d and

e are

considered

closed.

N

r

10

e

Within the areas

inspected

no violations or deviations were identified.

15.

Refuel Floor Airborne Radioactivity

1

On May 22,

1981, during work in Unit

1 reactor cavity in connection with the

installation

of

new

feedwater

spargers,

a

routine air

sample

showed

increased

airborne activity which leads to an evacuation of personnel

(about

33)

from the

refuel floor.

Personnel

in the

Reactor cavity were

in

a

plastic enclosure'(tent)

wearing respiratory protection

and were exposed

to

below

MPC of airborn activity.

Air samples

outside

the plastic enclosure

showed. an increase

in level which was the basis for a precautionary

clearing

of all

personnel

from the

refuel floor.

Personnel

not

in respiratory

protection

were exposed

to

a maximum of 14%

MPC for a short period of time.

Surveys of personnel

including nasal

smears

were negative.

The activity was

fairly localized with no increase

evident

on the continuous air monitors,

nor was there any evidence of release

from the refuel floor.

The inspector

discussed

improved work control

measures

with plant manage-

ment.

No violations

or deviations

were

identified within the

areas

inspected.

~,

J