ML18010B010

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Insp Rept 50-400/92-30 on 921219-930122.Violation Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance Observation, Maint Observation & Followup on Onsite Events
ML18010B010
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 01/29/1993
From: Christensen H, Darrell Roberts, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010B008 List:
References
50-400-92-30, NUDOCS 9302160128
Download: ML18010B010 (14)


See also: IR 05000400/1992030

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET,'N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/92-30

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Licensee

No.:

NPF-63

Facility Name:

Harris

1

Inspection'onducted:

December

19,

1992 - January

22,

1993

Inspectors:

J.

T

row,

enior Resid

I

pector

ate Signed

H. Shannon,

den

I

pect

D te

igned

D. Robert

,

esident

specto

Accompanying

Pers nnel:

. Watkins, Intern Resident

Inspector

App

d tl':

A

~.

C r'ensen,

Section Chief

Division of Reactor Projects

D te

igned

j ze

93

Date Si

ed

SUNMARY

Scope:

This routine inspection

was conducted

by the resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

surveillance observation,

maintenance

observation,

followup of onsite events,

licensee

event reports

and licensee

action

on previous inspection

items.

Numerous facility tours were conducted

and facility operations

observed.

Some

of these tours

and observations

were conducted

on backshifts.

Results:

One violation was identified:

Failure to properly tag out fan AH-26A prior to

working on electrical circuits, paragraph

4.a.

The licensee's

proactive measures

to identify and repair boric acid leakage

from the reactor coolant

system were considered

to be conservative,

paragraph

5.a.

A weakness

was identified concerning

operator performance

which resulted

in an

automatic turbine runback,

paragraph

5.b.

930216012B

930129

PDR

ADOCK 05000400

8

PDR

Use of a steam generator

"mockup" facility enhanced

reactor coolant system

leak repair efforts

and

was successful

in minimizing the radiation exposure

received

by plant personnel,

paragraph

2.b.(4).

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees

  • J. Collins, Manager,

Operations

J. Cribb, Manager, guality Control

  • C. Gibson,

Manager,

Programs

and Procedures

C. Hinnant,

General

Manager,

Harris Plant

D. Knepper,

Project Engineer,

Nuclear Engineering

Dept.

  • B. Heyer,

Manager,

Environmental

and Radiation Monitoring

T. Horton, Manager,

Maintenance

J. Moyer, Manager,

Project Assessment

  • J. Nevill, Manager,

Technical

Support

A. Powell,

Manager,

Harris Training Unit

  • W. Seyler,

Manager,

Outages

and Modifications

  • H. Smith,

Manager,

Radwaste

Oper ation

  • G. Vaughn,

Yice President,

Harris Nuclear Project

W. Wilson, Hanager,

Spent Nuclear

Fuel

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

"Attended exit interview

2.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Review of Plant Operations

{71707)

The plant continued in power operation

{Mode 1) for the duration of this

inspection period.

a ~

Shift Logs and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

{TS) and the licensee's

administrative procedures,

The following records

were reviewed:

Shift Supervisor's

Log;

Control Operator's

Log; Night Order Book; Equipment Inoperable

Record; Active Clearance

Log; Grounding Device Log; Temporary

Modification Log; Chemistry Daily Reports; Shift Turnover

Checklist;

and selected

Radwaste

Logs.

In addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well organized,

and

provided sufficient information on plant status

and events.

With

the exception of the example noted in paragraph

4.a of this

report,

clearance

tagouts

were found to be properly implemented.

Facility Tours

and Observations

Throughout the inspection period, facility tours were conducted

to

observe operations,

surveillance,

and maintenance activities in

progress.

5ome of these

observations

were conducted during

backshifts.

Also, during this inspection period, licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence;

control

room;

emergency diesel

generator building; reactor

auxiliary building; waste processing

building; turbine building;

fuel handling building; emergency

service water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support

center.

During these tours,

the following observations

were made:

(I)

Monitoring Instrumentation

- Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters

were observed

to verify that

indicated

parameters

were in accordance

with the

TS for the

current operational

mode.

(2)

Shift Staffing - The inspectors verified that operating

shift stafFing

was in accordance

with TS requirements

and

that control

room operations

were being conducted

in an

orderly and professional

manner.

In addition, the inspector

observed shift turnovers

on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these

turnovers.

(3)

Plant Housekeeping

Conditions

- Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout the facility were observed to determine whether

safety and/or fire hazards

existed.

(4)

Radiological. Protection

Program - Radiation protection

control activities were observed routinely to verify that

these activities were in conformance with the facility

policies

and procedures,

and in compliance with regulatory

requirements.

The inspectors

a'iso reviewed selected

radiation work permits to verify that controls were

adequate.

The inspectors

reviewed the licensee's

planning for the

containment entry on January

7, to stop the

RCS leak

observed

on the "A" steam generator drain piping.

The job

planning, radiation work permit, post job critiques,

and

survey data sheets

were reviewed.

A power reduction to ten

percent

was performed to lower general

area radiation

dose

rates

from approximately eight rem per hour to less than two

rem per hour.

Training on

a mockup facility of the area

was

conducted

including full protective clothing dressout of the

participants.

These efforts were effective in limiting the

radiation exposure

received

by plant personnel

to 750 mrem

to repair the leak.

This exposure

was

much less

than that

expected

to be received

from a routine plant shutdown

an'cl

startup activity.

(5)

Security Control

- The performance of various shifts of the

security force was observed

in the conduct of daily

activities which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors;

patrols;

and compensatory posts.'n

addition, the inspector

observed

the operational

status of closed circuit television

monitors, the intrusion detection

system in the central

and

secondary

alarm stations,

protected

area lighting, protected

and vital area barrier integrity,

and the security

organization interface with operations

and maintenance.

(6)

Fire Protection

- Fire protection staffing and equipment

were observed

to verify that fire brigade staffing was

appropriate

and that fire alarms,

actuating controls, fire

fighting equipment,

and fire barriers

were operable.

During a tour of the reactor auxiliary building on

January

8, the inspector noticed several

drums were present

on the 305 foot elevation of the auxiliary building.

The

drums contained

charcoal

which had

been

removed

from several

plant

HVAC units nearby.

This matter

was discussed

with

licensee

personnel

to ascertain

the combustible loading in

this fire zone.

The plant

FSAR, section

9.5A contains the

fire protection hazards

analysis

and allows

a transient

combustible charcoal fire load of 14,088 pounds in this

area.

Since the drums contained only approximately

12,600

pounds of charcoal, this temporary condition was considered

to be acceptable.

Licensee

management

subsequently

planned

to remove the drums.

The inspectors

found plant housekeeping

and material condition of

safety related

components

to be good.

The licensee's

adherence

to

radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

Review of Nonconformance

Reports

Adverse Condition Reports

(ACRs) were reviewed to verify the

following:

TS were complied with, corrective actions

and generic

items were identified,

and items were reported

as required

by

10 CFR 50.73.

Surveillance

Obser vation (61726)

Surveillance tests

were observed to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

OST-1026

Reactor Coolant System

Leakage

Evaluation

OST-1081

HST- I0190

Containment Visual Inspection Prior to Establishing

Containment Integrity and After Each Containment

Entry

When Containment Integrity is Established.

Reactor Coolant System

Wide Range

Pressure

P-0402

Operational

Test of Train A CVCS Hiniflow Circuit

MST-I0237

Containment

Pressure

(P-0951) Operational

Test

HST-I0238

Containment

Pressure

(P-0952) Operational

Test

HST-I0255

Reactor

Coolant

Loop Hot Leg Temperature

Instrument

Operational

Test

EPT-150

EST-221

ESW Flow Balance

Type

C LLRT of Containment

Purge Hake-up Penetration

(H-57)

The performance of these

procedures

was found to be satisfactory with

proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

a ~

b.

Procedure

OST-1081

documented

the containment

closeout

inspection

which was performed following the containment entry on January

7,

to isolate the identified

RCS leakage

which is discussed

further

in paragraph

5.a of this report.

Some boric acid crystallization

was found in the area

around the "A" steam generator drain line

which had leaked onto

a nonsafety-related

air handling unit, the

"A" steam generator

seismic monitoring device,

and

on

a sample

valve.

The inspector

reviewed

a videotape

which was

made of the

area.

Licensee

personnel

evaluated

the equipment which was

exposed to the boric acid

and determined that it was acceptable

to

remain in this condition until the unit was shutdown for an

outage.

During a tour of the reactor auxiliary building, the inspector

noticed that several

service water valves

had two or three notches

scratched

on their valve positioner to mark the required throttled

position for the valve.

The inspector discussed

this observation

with licensee

personnel

who stated that the valves

had

been

throttled to the latest position during the performance of a

system flow balance test.

The inspector reviewed the latest valve

lineup sheet for the valves which specified that the valve

position

be established

while performing procedure

EPT-150.

The

latest procedure

EPT-I50 was also reviewed.

The test procedur'e

established

the, required flows through the various heat exchangers

and specified that the throttled position for the valves

be marked

with a paint stick.

This marking was intended to be

a rough

throttled position mark for subsequent

usage

by plant operators.

The inspector questioned

whether the correct throttled position

could be re-established

following valve repositioning with two or

three marks present

on the operators.

Licensee

personnel

agreed

to review their method of controlling the throttled positions for

these

valves.

No violations or deviations

were identified.

Haintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were in effect; work requests

and fire

prevention

work permits,

as required,

were issued

and being followed;

quality control personnel

were available for inspection activities

as

required;

and

TS requirements

were being followed.

Haintenance

was observed

and work packages

were reviewed for the

following maintenance activities:

~

Replacement

of the motor for air handler

AH-26A.

~

Troubleshoot

loud noise

from the S-IV Inverter and replacement

of

the inverter's transformer in accordance

with procedure

CH-E0020,

Replace Oil Filled and Electrolytic Capacitors

and/or Ferro-

Resonant

Transformer Assembly in Mestinghouse

7.5

KVA Static

Inverters.

~

Repair leakage

on the "A" and "B" spent fuel

pump casings

in

accordance

with procedures

CH-H0010,

Goulds

Pump 3405 Disassembly

and Haintenance,

and HPT-H0062,

Gould 3405

Pump Nonmetallic

'omponent

Replacement.

~

Replace defective

manual

override plate for valve lAF-19.

Determinate/reterminate

operator

as necessary

for replacement

and

perform post maintenance

testing

as per PIC-I058.

The performance of work was generally satisfactory with proper

documentation of removed

components

and independent verification of the

reinstallation.

The repairs

made to the spent fuel cooling pumps

improved the equipment

condition considerably

by stopping boric acid leakage

around the

pump

casing.

An exact replacement for the AH-26A motor could not

be located

so the

licensee

purchased

a similar motor from the equipment

vendor.

An

engineering

evaluation for the replacement

motor was performed

(PCR-6734,

AH-26-lA Replacement

Motor), which concluded that the

new

motor was acceptable

and more efficient.

The inspector

reviewed this

evaluation

and concluded that the licensee's

action

was appropriate.

a 0

On January

8,

1993, during the replacement of the motor for fan

AH-26, the inspector

observed

the post maintenance

testing

conducted.

Upon initial fan startup,

the fan/motor was observed

to rotate in the wrong direction.

While this situation

was being

discussed

among licensee

personnel,

an electrician proceeded'to

swap motor leads in the power supply junction box.

The

electrician did not utilize any electrical safety devices while

doing this work.

Operating personnel

noticed the electrician

and

stopped this activity; however,

the motor leads

had already

been

swapped

and reterminated.

The inspector questioned

licensee

personnel

whether

an equipment clearance

had

been established

for

changing the direction of fan rotation

and was informed that one

had not been obtained.

The fan had

been

secured

by turning off

the control switch.

The inspector considered

work on this 480

volt electrical

system without an equipment clearance

or use of

appropriate electrical protection devices to be dangerous,

considering

the fact that the fan could have received

an automatic

start signal which would have energized

the circuit.

The licensee's

administrative

procedures

AP-020, Clearance

Procedure,

and AP-003,

General

Plant Personnel

Safety

and

Housekeeping,

require plant personnel

to obtain

an equipment

clearance

to deenergize

electrical

equipment prior to work. If

the work is to be performed

on energized

equipment,

then the

procedures

require special

permission

and use of rubber gloves,

rubber mats,

insulated tools

and face shields for 480 volt

circuits.

Failure to properly tag out the power supply for AH-26A

prior to working on the circuit or to utilize appropriate

electrical safety devices to work on potentially energized

components

is contrary to procedures

AP-020 and AP-003,

and is

considered

to be

a violation of TS 6.8.l.a.

Violation (400/92-30-01):

Failure to properly tag out fan AH-26A

prior to working on electrical circuits.

Although licensee

management

was present during this maintenance

activity, the poor electrical safety practices

were not initially

noticed until the work had

been completed.

The subsequent

fan

start for post maintenance

testing

was performed with increased

management

personnel

present

and utilization of appropriate

electrical safety devices.

b.

On January

12,

1993,

the S-IV vital instrument

bus transformer

was

replaced after plant personnel

identified

a higher than usual

humming sound

coming from it.

The

same transformer

had just been

installed

as

a replacement

during refueling outage

number

4 in

October

1992.

During the last three years,

the transformers

associated

with the inverters for all four vital instrument

bu'sses

have

been replaced

due to failure or degradation.

The inspectors

noted that this failure rate

was excessive

and that to date

no

root cause determination

had

been

made.

Inspector

Followup Item (400/92-30-02):

Follow the licensee's

actions to determine the root cause of recurrent transformer

failures in the uninterruptible

AC power system.

Followup of Onsite

Events

(93702)

a ~

b.

On January

6, licensee

personnel

made

a containment entry to

identify the source of increased

RCS unidentified leakage.

The

licensee

had performed

leakage calculations

which showed that

unidentified leakage

was approximately 0.5 gpm.

This was of

concern, yet well below the

TS limit of

1 gpm.

Leakage

was

observed

coming from the drain line for the "A" steam generator.

Two drain valves

(1RC-35

and

1RC-36) were leaking past their seats

and

a pipe plug to seal

the drain line was not in place.

On

January

7, licensee

management

conservatively

decided to reduce

power and attempt to stop the

RCS leakage.

Plant power was

reduced to

10 percent,

thereby lowering general

radiation levels

to facilitate access.

Operators

were able to access

the drain

valves, fully close them,

and stop the leakage.

In addition,

a

pipe plug was installed in the drain line.

Leakage calculations

performed following this activity indicated that the licensee's

efforts were successful

in reducing unidentified leakage to less

than 0. 1 gpm.

The licensee

plans to perform

a root cause

investigation to determine

why the drain line was leaking.

The

inspectors will follow the licensee's

activities during subsequent

routine inspections.

During the subsequent

power increase

on January

8,

a turbine

runback

was received at approximately

87 percent

power (turbine

first stage

pressure

of 535 psig).

Being in the control

room at

the time the runback occurred,

the inspector noted that the

runback condition lasted for a short time and lowered turbine load

by approximately

20

NW.

Operators

immediately suspended

the power

increase

and determined

the cause of the runback to be the failure

to have either heater drain

pump running.

The heater drain

pumps

were subsequently

started

and the plant power increase

resumed.

The inspector reviewed the power escalation

procedure,

GP-005,

Power Operation,

which was being used to control

the power

increase,

and noted that the procedure directed that both heater

drain

pumps

be started at approximately

50 percent

power.

The

heater drain

pumps were not started at this time due to problems

with pump seal

water flow.

The procedure

allowed continued

power

6.

escalation

while the problem with the heater drain

pumps

was being

fixed.

The licensee's

investigation into this event revealed that

the turbine runback setpoint

was actually lower than that

specified in setpoint

documents (i.e.,

90 percent

power or a

turbine first stage

pressure

of 555 psig).

The inspector discussed

this matter with licensee

personnel

and

discovered that the instrumentation

associated

with the runback

circuitry was not safety-related,

but did receive

a periodic

calibration

on

an

18 month frequency

as part of the preventive

maintenance

program.

The tolerance

allowed for the calibration

was

15 psig.

A review of the equipment

maintenance

history showed

that the instrumentation

had drifted from setpoint

on several

prior occasions.

Licensee

personnel

stated that they would review

this instrumentation for determination of an appropriate

calibration frequency.

Although the turbine runback signal

was received

a little

prematurely,

the inspector considered

that sufficient time and

margin existed for operators

to start

a heater drain

pump prior to

approaching

the runback signal setpoint.

The failure of operators

to start

a heater drain

pump prior to receiving

a turbine runback

is considered

to be

a weakness.

Licensee Action on Previously Identified Inspection

Findings

(92702

5

92701)

a 0

b.

(Closed) Violation 400/89-35-01:

Failure to perform inservice

testing

on check valves.

The inspector

reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated

February

9,

1990.

Appropriate changes

have

been

made to the inservice testing

program

and testing procedures.

This item was discussed

with

Region II inservice testing specialists

who agreed that the

licensee's

actions

were appropriate.

(Closed)

IFI 400/91-13-02:

Follow the licensee's

activities

regarding the narrow margin for minimum flow from the turbine

driven

AFW pump.

The licensee

has reanalyzed

the design requirements

associated

with the turbine driven

AFW pump

and

has concluded that the

pump

must

be capable of supplying flow to all three

steam generators.

An adequate

decay heat

removal flowrate of 430 gpm to only two

steam generators

is guaranteed

by the turbine driven

AFW pump in

conjunction with a motor driven

AFW pump or by two motor driven

AFW pumps,

assuming

a single failure of one of the pumps.

Therefore,

the setpoint of the turbine driven

AFW pump

differential pressure

controller does not severely restrict the

AFW flowrate near the minimum design.

Also the licensee

has re-

evaluated

the steam generator overfill analysis

and has

C.

established

a

new maximum flow limit of 550

gpm based

on

additional

main steam

PORV capacity.

The licensee

plans to revise

the sections

in the

FSAR which describe

using only one

AFW pump to

supply feedwater to the steam generators.

(Closed)

IFI 400/92-13-03:

Follow the licensee's

evaluation

o'

inaccurate

estimated critical positions.

The licensee

contacted

the nuclear

steam supply system vendor for

assistance

on the discrepancy

observed

between calculated

estimated critical positions

and the actual

rod positions

where

criticality was observed.

The vendor verified that the computer

program utilized by the licensee

was appropriate

and

recommended

new calculated

values for assumed

control rod worth.

The computer

core models tend to become less

accurate if a long continuous at-

power run is accomplished

and fuel burnup factors are introdOced.

Subsequent

plant startups with the

new revisions to the computer

program

have produced

estimated critical positions very close to

actual critical control rod position.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generi'c impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as

they occurred to determine if the

TS were satisfied.

LERs were reviewed

in accordance

with the current

NRC Enforcement Policy.

(Closed)

LER 92-14:

Pipe wall thinning in auxiliary feedwater

and main

feedwater

systems

caused

by flow erosion.

This event

was previously discussed

in

NRC Inspection

Report 50-400/92-

27.

The licensee

issued

a supplement

to the

LER dated

January

15,

1993.

An analysis of the piping was performed

by the license's metallurgical

services unit who determined that the cause of the pipe wall thinning

was due to erosion corrosion.

The effectiveness

of the computerized

pipe wall thinning program was evaluated

by the Electrical

Power

Research

Institute (EPRI).

The program was

deemed to be accurate within

the assumptions

made from input data.

Input data

assumed

nominal wall

thicknesses

for piping at the time of installation.

Industry experience

shows that manufacturing tolerances

can create

instances

where initial

pipe wall thickness

are considerably less

than nominal.

Exit Interview {30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

I) at the conclusion of the inspection

on January

22,

1993.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violation and Inspector Follow-up Item addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did

not identify as proprietary

any of the materials

provided to or reviewed

10

by the inspectors

during this inspection.

No dissenting

comments

from

the licensee

were received.

Item Number

400/92-30-OI

400/92-30-02

Descri tion and Reference

VIO:

Failure to properly tag out fan

AH-26A'rior

to working on electrical circuits,

paragraph

4.a.

IFI:

Follow the licensee's

actions to determine

the root cause of recent transformer failures in

the uninterruptible

AC power system,

paragraph

4.b.

Acronyms

and Initialisms

AC

ACR

AFW

  • CFR

CVCS

EPT

ESW

FSAR

GPH

HVAC

IFI

KVA

LER

LLRT

HPT

NREM

HW

NRC

OST

PCR

PORV

PSIG

RCS

TS

VIO

Alternating Current

Adverse Condition Report

Auxiliary Feedwater

Code of Federal

Regulations

Chemical

Volume Control

System

Engineering

Performance

Test

Emergency Service Water

Final Safety Analysis Report

Gallons

Per Minute

Heating, Ventilation and Air Conditioning

Inspector Follow-up Item

Kilovolt-ampere

Licensee

Event Report

Local

Leak Rate Test

Maintenance

Performance

Test

Hillirem

Megawatt

Nuclear Regulatory

Commission

Operations Surveillance

Test

Plant

Change

Request

Power Operated Relief Valve

Pounds

Per Square

Inch Gage

Reactor

Coolant System

Technical Specification

Violation