ML18009A872

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Insp Rept 50-400/91-04 on 910223-0322.Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls, Security,Fire Protection,Noncomformance Repts,Maint Observation,Lers,Followup of Onsite Events & Power Sys
ML18009A872
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 04/02/1991
From: Christensen H, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A870 List:
References
50-400-91-04, 50-400-91-4, GL-89-13, IEIN-80-20, IEIN-84-69, IEIN-89-042, IEIN-89-064, IEIN-89-42, IEIN-89-64, NUDOCS 9104230340
Download: ML18009A872 (19)


See also: IR 05000400/1991004

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.'W.

ATLANTA,GEORGIA 30323

E

Report No.:

50-400/91'-04

Licensee:

Carolina

Power and Light Company

=-P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

February

23 - Parch

22,

1991

Lead Inspector:

e row,

endor

e

ent

spector

Other Inspector(s):

N. Shannon,

Resident

Inspector

License No.:

NPF-63

ate

>gne

Approved by:

H. Christensen,

Section Chief

Reactor Projects

Branch

1

Division of Reactor Projects

0 te Signed

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

nonconformance

reports,

surveillance observation,

maintenance

observation,

preparations

for refueling, licensee

event reports,

followup of onsite events,

'review of offsite power system,

and review of plant nuclear safety committee

activities.

Numerous facility tours

wer e conducted

and facility operations

observed.

Some of these tours

and observations

were conducted

on backshifts.

Results:

One violation was identified:

failure to maintain two reactor protection

system reactor coolant

pump underfrequency trip devices operable,

paragraph

6.

Two non-cited licensee identified violations were identified:

failure to

include reactor coolant system vent valves

and

a check valve in the inservice

testing program,

paragraph

2.c;

and failure to perform

a viscosity analysis

on

a diesel

generator

fuel oil shipment,

paragraph

5.

9i04230340

910402

PDR

ADOCK 05000400

G

PDR

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

p.

J.

C.

  • C

D.

B.

T.

J.

C.

A.

R.

H.

'E.

W.

Beane,

Manager, guality Control

Collins, Manager,

Operations

Gibson, Director,

Programs

and Procedures

Hinnant, Plant General

Manager

McCarthy, Manager, Site Engineering

Meyer, Manager,

Environmental

and Radiation Monitoring

Morton, Manager,

Maintenance

Nevill, Manager,

Technical

Support

Olexik, Director, Regulatory

Compliance

Powell, Harris Training Unit Training Manager

Richey, Vice President,

Harris Nuclear Project

Smith, Manager,

Radwaste

Operation

Willett, Manager,

Outages

and Modifications

Wilson, Manager,

Spent Nuclear

Fuel

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

The plant began this inspection

period in power operation

(Mode 1).

On

March 15,

1991,

a plant shutdown

was

commenced to start

a scheduled

refueling outage.

The cold shutdown

(Mode 5) condition was reached

at

10:46 p.m.,

on March 17.

The plant remained in cold shutdown for the

duration of this inspection period.

a..

Shift Logs

and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

and the licensee's

administrative

procedures.

The

following records

were reviewed:

Shift Foreman's

Log; Control

Operator's

Log; Night Order

Book; Equipment Inoperable

Record; Active

Clearance

Log; Jumper

and Wire Removal

Log; Temporary Modification

Log; Chemistry Daily Reports; Shift Turnover Checklist;

and selected

Radwaste

Logs.

In addition, the inspector

independently verified

clearance

order tagouts.

2

b.

Facility Tours

and Observ'ations

Throughout the inspection period, facility tours were conducted to

observe operations,

surveillance,.and

maintenance activities in

progress.

Some of these

observations

were conducted during

.

backshifts.

Also, during 'this inspection period, licensee

meetings

were attended

by the inspectors to observe planning

and management

activities.

The facility tours

and observations

encompassed

the

following areas:

security perimeter fence; control

room; emergency

diesel

generator building; reactor auxiliary building; waste

processing

building; turbine building; fuel handling building;

emergency

service water building; battery rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

the following observations

were made:

( 1)

Monitoring Instrumentation - Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup, reactor operating

parameters,

and auxiliary equipment

operating

parameters

were observed to verify that indicated

parameters

were in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors verified that operating shift

staffing was in accordance

with TS'requirements

and that

control

room operations

were being conducted in an orderly and

professional

manner.

In addition, the inspector

observed shift

turnovers

on various occasions

to verify the continuity of

plant status,

operational

problems,

and other pertinent plant

information during these turnovers.

(3)

Plant Housekeeping

Conditions - Storage of material

and

components,

and cleanliness

conditions of various areas

throughout the facility were observed to determine whether

safety and/or fire hazards

existed.

1

(4)

Radiological Protection

Program - Radiation protection control

activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The inspectors

also reviewed selected

radiation work-permits to

verify that controls were adequate.

(5)

Security Control - In the course of the monthly activities, the

inspector included

a review of the licensee's

physical security

program.

The performance of various shifts of the security

force was observed

in the conduct of daily activities which

included:

protected

and vital area

access

controls; searching

of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of Closed Circuit Television monitors, the Intrusion

Detection

system in the. central

and secondary

alarm stations,

protected

area l'ighting, 'protected

and vital area barrier

integrity, and the security organization interface with

operations

and maintenance.

(6)

Fire Protection - Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing

was appropriate

and that fire alarms, extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

c.

Review of Nonconformance

Reports

Adverse Condition Reports

and Nonconformance

Reports

were reviewed to

verify the following:

TS were complied with, corrective actions

as

identified in the reports

were accomplished

or being pursued for

completion, generic

items were identified and reported,

and items

were reported

as required

by the TS;

ACR 91-060 reported that

RCS vent valves

(1RC-900,

1RC-901,

1RC-'02,

1RC-903,

1RC-904,

1RC-905)

and

an

RCS vent check valve (1RC-993)

were not required to be open stroke tested

and .forward flow tested

respectively,

by the licensee's

IST program procedure

ISI-203,

ASYiE

Section

XI Pump

and Valve Program Plan.

This matter

was identified

during the licensee's

corrective action regarding

LER 91-01 which

reported'hat

a control

room

HVAC check valve was not tested.

The

licensee's

corrective action included

a review of all other IST

system

check valves for similar problems.

Although the licensee's

approved

IST program stroke tested

the vent valves in the closed

direction, the open safety function of these

valves

was overlooked.

'imilarly, the check valve safety function to permit forward flow was

also overlooked during program development.

Since these

valves are

routinely operated,

and flow verified, during

RCS fill and vent

evolutions,

the licensee

believes

the valves are operable.

Appro-

priate testing will be performed during-the upcoming refueling

outage.

This matter is considered

to be

a licensee identified

NCV

and is not being cited because

the crit'eria specified in section

V.G. 1 of the

NRC Enforcement Policy were satisfied.

NCV (400/91-04-01):

Failure to include

RCS vent valves

and

a check

valve in the

IST program.

One non-cited violation was identified.

3.

Surveillance Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

MST-I004?

Calibration of Nuclear Instrumentation

Power

Range

N44

MST-I0050

MST-I0159

MST-I0635

OST-1042

OST-1119.

OST-1808

Calibration of Nuclear Instrumentation

Source

Range

N31

Reactor

Coolant Loop 3 Flow Instrument Protection

Set II Operational

Test

Self Heating Test of Installed Resistance

Thermometers

Seismic Monitoring Operability Monthly Interval

Containment

Spray Operability quarterly Interval

Main Steam Isolation:

ESF Response

Time 18 Month

Interval

OST-1823

1A-SA Emergency Diesel

Generator

18 Month Operability

Test

EST-202

Main Steam Safety Valve Test

EST-212

Type

C Local Leak Rate Tests

EPT-171

EPT-177

EPT-311

C

CCW Pump Corrosion Inhibitor Addition

Auxiliary Feedwater

Flow Balancing

1MS-T AFW Pump

1X-SAB Trip and Throttle Valve

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment

clearances

were in effect; work requests

and fire

prevention

work permits,

as required,

were issued

and being followed;

quality control

personnel

were available for inspection activities

as

required;

and

TS requirements

were being followed.

i

0

Maintenance

was observed

and work packages

were reviewed for the

following maintenance

(WR/JO) activities:

WR91ADIB1 and 91ADICl Installation of Instrumentation

on the

CCW/SW

Heat Exchanger to perform monitoring required

by GL 89-13

WR91ACEY1'Dam'per rebuild and solenoid replacement

on AY-D14-1, an

RAB penetration

area

damper.

Review of installation of monitoring equipment for VOTES testing of

valve 1AF-143, Auxiliary Feed to "B" SG.

Review of field installation for

PORV safety upgrade,

PCR 5044.

No violations or deviations

were identified.

5.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential generic impact, to detect

trends,

and to determine whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with the current

NRC Enforcement Policy.

(Open)

LER 91-03:

This

LER reported that following receipt of a fuel oil

shipment

on January

21,

1991, the licensee failed to determine

the

kinematic viscosity.

The condition was discovered

during

a documentation

review by the chemistry foreman.

The licensee attributed this event to

personnel .error caused

by a lack of familiarity to an infrequent evolution,

performed approximately

once every two years.

A satisfactory analysis for

kinematic viscosity was conducted

on the remaining oil sample

on

February

21,

1991.

Additional corrective action planned

by the licensee

will include additional training for chemi,stry personnel

and'

procedure

revision to require

a documented

comparison of the supplier's viscosity

and the viscosity determined

by the

HNP laboratory.

This matter is

considered

to be

a licensee identified

NCV and is not being cited because

the criteria specified'n section V.G.l of the

NRC Enforcement Policy were

satisfied.

NCV (400/91-04-02):

Failure to perform

a viscosity analysis

on a diesel

generator fuel oil shipment.

One non-cited violation was identified.

6.

Followup of Onsite Events

(93702)

At 2: 12 a.m.,

on March 5,

1991, the licensee

declared

an unusual

event

due

to the failure of two channels

of the reactor protection system's

RCP

underfrequency trip circuit and resultant

TS required plant shutdown.

0

During the performance of surveillance testing,

the "8" train

underfrequency trip circuit associated

with the "A" RCP was found to be

inoperable at 12:45 a.m.

This inoperable

channel,

along with a previously

inoperable

"8" train underfrequency

channel

associated

with the "C" RCP,

required the licensee to implement

a plant shutdown in accordance

with

TS 3.0.3.

Plans to reduce

power were formulated

and actual

power

reduction

commenced at 2: 12 a.m.

Upon reaching approximately

45 percent

power, troubleshooting activities in the

RCP breaker cubicles discovered

disconnected

umbilical cords for the "A" and "C" RCPs.

These

cords

complete the circuit between

the

RCP breakers

and the reactor protection

system for the "8" train underfrequency trip.

The cords were reconnected

and applicable surveillance testing

was completed satisfactorily at

5:03 a.m.

The plant shutdown

was stopped

and the unusual

event terminated.

The reactor protection

system

RCP underfrequency trip circuit is comprised

. of two underfrequency trip devices for each

RCP;

one supplies

a signal to

the reactor protection system train "A" and the other to train "8"

The

"A" train circuits utilize internal breaker switches

which touch side

panel

contacts

of the breaker cubicle for electrical continuity.

To

provide electrical

separation

between trains, the "8" train uses umbilical

cords which plug into the breaker.

These connections

allow breaker

removal

from the cubicles.

The licensee's

investigation into this event revealed that the

RCP

breakers

had last been

racked out of their cubicles during the November

1990 outage,

when mid-loop

RCS operations

were required to perform steam

generator

tube repairs.

Since the umbilical cords were unplugged for

this operation,

the licensee

believes that .the cords were not properly

reconnected

upon racking the breakers

back in during plant restart.

Plant procedures

did. not contain appropriate

steps for reconnecting

of

the umbilical cords.

Also,

a review of surveillance-testing

records

revealed

the following.

Surveillance testing

on these circuits is

performed every

92 days

on

a staggered

test basis.

The "8" RCP

underfrequency trip circuit had

been tested satisfactorily

on December

11,

1990.

During surveillance testing

on January

8, 1991, the "8" train

underfrequency

channel

associated

with the "C" RCP was found to be

inoperable.

This channel

was placed in the tripped condition and power

operation continued.

The performance of troubleshooting for this failure

was limited because

licensee

management

was sensitive to a previous

reactor trip which had occurred

when

a

RCP breaker cubicle was accidentally

bumped.

Although the source of this problem was determined to be at the

breaker cubicle,

no inspection

was performed inside the cubicle.

Following

the similar problem which occurred

on March 5, and with reactor

power less

that

50 percent,

troubleshooting

was allowed inside the breaker cubicle

where the disconnected

umbilical cords were found.

The failure to have

two reactor protection system

RCP underfrequency trip

devices

operable

from the plant startup

on November 27, 1990, until

March 5,

1991 (approximately

98 days), is contrary to the requirements

of

TS 3.3. 1 and is considered

to be

a violation.

Violation (400/91-04-03):

Failure to "maintain two reactor protection

system

RCP underfrequency trip devices

operable.

The inspectors

considered

troublesh'ooting activities to also

be

deficient.

No .troubleshooting

was performed inside the breaker cubicles

during appropriate

windows which became available

on January

24 and

February

25 when reactor

power was reduced to less

than

30 percent for

other reasons.

This contributed'o the excessive

time for which the

problem existed,

and is considered

to be

a weakness.

One violation was identified.

7.'eview of Offsite Power System

(71707)

The inspectors

reviewed the licensee's

offsite power distribution system

and administrative controls for familiarization.

A tour of. the

" switchyard

was conducted,

administrative

procedures

reviewed,

and

licensee

personnel

interviewed.

In conjunction with this effort, the

licensee's

actions with respect to related industry events

were also

reviewed.

The offsite distributi'on system consists

of a 230

KV switchyard which

has'even

feeder lines from five different substations.

Two independent

startup transformers

receive

power from this switchyard through

underground

cables.

When the plant is online, the main generator

output

is transmitted to the switchyard through overhead lines.

Two auxiliary

transformers

also receive

power from the main generator

and supply power

to the onsite distribution system.

The .switchyard is divided into two

busses

which can supply power to either startup transformer.

Plant

operations

personnel

have direct control

os the six critical switchyard

breakers

which supply power to the startup transformers with the

dispatcher

having control of the remaining eleven breakers.

Switchyard

protection utilizes

a breaker

and

a half scheme to isolate faults with a

double breaker protection

scheme for the generating unit.

Breakers

have

redundant trip circuits powered

from two separate

batteries.

The

switchyard is physically protected

by a fence

and locked gate.

'Only

authorized

personnel

are allowed access.

Significant maintenance activities are reviewed

by an onsite

plant-transmission

activities coordinator.

This person

reviews major

modifications/system

outages for potential conflicts with plant

activities.

Minor routine activities are scheduled

through the shift

foreman.

Maintenance is usually planned at least

a week in advance.

Transmission

department

personnel

are required to notify the shift

foreman prior to comnencing

work and to inform the dispatcher prior to

breaker operation.

These

communications

have

been formalized with

required repeat

backs.

0

The licensee

has

an interdepartmental

procedure

(FG

8 PTG-TD-004) which

relates

the general

division of responsibilities with respect to

maintenance

of the switchyard, relays,

and associated

control equipment.

This procedure

was written for all the licensee's

plants

and provides

a

general

description of components for which the plants

are responsible

and those

under the cognizance 'of. the transmission

departments.

,Provisions

were also

made for technical

guidance

and administrative

advice.

The licensee is presently'pgrading

this procedure

through

a

customer/supplier

agreement

which will be site specific and clarify the

specific responsibility,of each group.

Due to numerous

industry events,

the licensee

has

formed

a project quality

team to recommend

improvements

to- enhance offsite power reliability.

Approximately 96 industry events

involving loss of offsite power were

reviewed

by thi.s team, including those discussed

in NUREG 1410, Loss of

Vital AC Power

and the Residual

Heat

Removal

System During Mid-Loop

Operations

at Vogtle Unit

1 on March 20,

1990;

IN 80-20,

Loss of Decay

Heat Removal Capability at Davis-Besse

Unit 1 While in a Refueling Mode;

IN 89-42,

Equipment Availability for Conditions During Outages

not Covered

by Technical Specifications;

IN 84-69, Operation of Emergency Diesel

Generators;

IN 89-.64, Electrical

Bus Bar Failures;

and two events which

happened

at the licensee's

plants involving a loss of offsite power at

plant Brunswick on June

17,

1989,

and the generator/transformer fire at

plant Harris

on October 9, 1989.

Recommendations

from this team included

the completion of the customer/supplier

agreement,

closeout inspections

following maintenance

of electrical

equipment,

expansion of the

thermography

program to include major electrical

transmission

components,

and distribution of operating experience

feedback

information to the

transmission

department.

The switchyard is toured weekly by Operations

personnel

during a check of.

the offsite power system performed in accordance

with TS 4.8.1.1.3,.a

and

procedure

OST-1023, Offsite Power Availability Verification,

The check

includes

a physical verification that switchyard breakers

are in the

proper position.

In conclusion,

the inspector considered

the offsite power system to be

a

very reliable source of power.

Licensee efforts to improve this

reliability were considered

to be pro-active.

No violations or deviations

were identified.

Review of Plant Nuclear Safety

Committee Activities (40500)

The inspectors

attended

PNSC meetings

which discussed

outage activities

to be performed during mid-loop operations of the

RCS.

A detailed review

of all maintenance activities scheduled

during mid-loop operations

was

performed.

All activities that could affect mid-loop operation

and

associated

systems

were identified as hold work items.

The individual

work crews were also notified that specific work request

could not be

worked during mid-loop.

The detailed review performed

by the licensee

should prevent

any problems related to mid-loop operations.

Meeting

minutes

were also reviewed to verify accurate

documentation.

No violations of deviations

were identified.

9.,

Licensee

Action on Previously Identified Inspection

Findings

(92702,

92701)

(Closed)

IFI 400/89-16-02:

Fuel 8asket

Removal

on August 9, 1989.

Followup of this item was performed

and documented

in Inspection Report

50-400/89-23,

paragraph

4.a, and was the subject of a violation

(400/89-23-03).

Subsequent

procedural

controls for fuel handling were

reviewed

hy the resident staff and found to be satisfactory.

Following

approximately

20 additional

shipments

no similar problems

have

been

encountered.

10.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1)

at the conclusion of the inspection

on March 22,

1991.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violation and the Non-cited Violations addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did

not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Item Number

400/91-04-01

400/91-04-02

400/91-04-03

11.

Acronyms

and

AC

ACR

AFh'LARA

ASME

Descri tion and Reference

NCV:

Failure to include

RCS vent valves

and check

vhlve in the

IST program,

paragraph

2.c.

NCV:

Failure to perform a viscosity analysis

on

a

diesel

generator fuel oil shipment,

paragraph

5.

VIO:

Failure to maintain two reactor protection

system

RCP underfrequency trip devices

operable,

paragraph

6.

Initialisms

Alternating Current

Adverse Condition Report

Auxiliary Feedwater

As Low As Reasonably

Achievable

American Society of Mechanical

Engineers

10

CCTV

CCW.

CFR

EPT

ESF

EST

GL

GP

HVAC

IFI

IN

ISI

IST

KV

LER

MST

NCR

NCV

NRC

OST

PCR

PNSC

PORV

QA/QC

'AB

RCP

RCS/RC

SG

TS

YIO

WR/JO

Closed Circuit Television

Component

Cooling Water

Code of Federal

Regulations

'Engineering

Performance

Test

Engineering Safety Features

Engineering Surveillance

Test

Generic Letter

General

Procedure

Heating, Ventilation and Air Conditioning

Inspector

Follow-up Item

Information Notice

Inservice Inspection

Inservice Testing

'ilovolt

Licensee

Event Report

Naintenance

Surveillance Test

Non-Conformance

Report

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Surveillance Test

Plant

Change

Request

Plant Nuclear Safety Committee

Power Operated Relief Valve

Quality Assurance/Quality

Control

Reactor Auxiliary.Building

Reactor Coolant

Pump

Reactor

Coolant System

Steam .Generator

Technical Specification

Violation

Work Request/Job

Order