ML18009A799

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Insp Rept 50-400/90-26 on 901215-910125.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance,Maint,Lers & 10CFR21 Repts,Design Changes & Mods
ML18009A799
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 01/30/1991
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A796 List:
References
50-400-90-26, NUDOCS 9102110055
Download: ML18009A799 (22)


See also: IR 05000400/1990026

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

/

Report No.:

50-400/90-26

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

License No.:

NPF-63

Facility'ame:

Harris

1

Inspection

Conducted:

December

15,

1990 - January

25,

1991

Inspectors:

edrow, Senior Resident

Inspector

. Shannon,

Resident

nspector

Approved by:

H.

C r>stensen,

Section

Chic

Reactor Projects

Branch

1

Division of Reactor Projects-

/ Po/vf

ate Signed

/3o

gl

Date

Soigne

ate Signed

SUMMARY

Scope:

This routine inspection

was

conducted

by two resident

inspectors

in the areas

of plant

operations,

radiological

controls,

security,

fire protection,

surveillance

observation,

maintenance

observation,

licensee

event reports

and

10 CFR Part 21 reports,

design

changes

and modifications, followup of onsite

events,

and licensee

action

on previous

inspection

items.

Numerous facility

tours were conducted

and facility operations

observed.

Some of these tours

and

observations

were conducted

on backshifts.

Results:

Five violations were identified:

failure to maintain administrative control of

a high radiation

area

key, paragraph

2.b.(4); failure to properly implement

a

radiochemistry

procedure,

paragr'aph 2.b.(7);

a non-cited violation for improper

documentation

of. lifted electrical

leads,

paragraph

4;

a non-cited

licensee

identified violation regarding

a failure to test the containment

personnel

air

lock, paragraph 2.c.;

and

a non-cited licensee identified violation regarding

a

failure to make

a four hour report to the

NRC, paragraph

5.e.

The failure to

properly implement radiochemistry

procedures

shows

a continued

lack of attention

to detail

by the licensee's

chemistry department.

9102210055

910130

PDR

ADOCK 05000400

8

PDR

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

  • J. Collins, Manager,

Operations

  • C. Gibson,

Manager,

Programs

and Procedures

  • C. Hinnant, Plant General

Manager

"B. Neyer,

Manager,

Environmental

and Radiation Monitoring

"T. Norton, Manager,

Maintenance

  • C. Olexil;, Manager,

Regulatory

Compliance

"'R. Richey,

Vice President,

Marris Nuclear Project

E. Willett, Manager,

Outages

and Modifications

  • L. Woods,

Manager,

Technical

Support

Other

licensee

employees

contacted

included

office,

operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel..

  • Attended exit interview

,

Acronyms

and Initialisms

used

throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant continued

in power operation

(Mode 1) for the duration of this

inspection

period.

a.

Shift Logs

and Facility Records

The inspector

reviewed

records

and discussed

various entries

with

operations

personnel

to verify compliance

with the

Technical

Specifications

(TS)

and

the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Foreman's

Log; Control

Operator's

Log; Night Order Book; Equipment Inoperable

Record; Active

Clearance

Log; Jumper

and

Wire Removal

Log; Temporary Modification

Log; Chemistry Daily Reports; Shift Turnover Checklist;

and selected

Radwaste

Logs.

.In addition,

the inspector

independently

verified

clearance

order tagouts.

No violations or deviations

were identified.

b.

Facility Tours

and Observations

Throughout

the inspection

period, facility tours

were

conducted

to

observe

operations,

surv'ei llance,

and

maintenance

activities

in

progress.

'Some

of these

observations

were

conducted

during

backshifts.

Also, during this inspection

period,

licensee

meetings

were attended

by the inspectors

to observe

planning

and

management

activities.

The facility tours

and

observations

encompassed

the

following areas:

security perimeter

fence;

control

room;

emergency

diesel

generator

building;

reactor

auxiliary building;

waste

processing

building; 'turbine

building;

fuel

handling

building;

emergency

service

water

building;

battery

rooms;

electrical

switchgear

rooms;

and the technical

support center.

h

During these

tours,

the following observations

were made:

(1)

Monitoring Instrumentation

-

Equipment operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup,

reactor

operating

parameters,

and. auxi li'ary equipment

operating

parameters

were

observed

to verify that indicated

parameters

were

in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors

verified that operating shift,

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner.

In addition,

the inspector

observed shift

turnovers

on various occasions

to verify the continuity of plant

status,

operational

problems,

and

other

pertinent

plant

information during these

turnovers.

(3)

Plant

Ho'usekeeping

Conditions

-

Storage

of material

and

components,

and

cleanliness

conditions

of

various

areas

throughout

the facility were

obser'ved

to determine

whether

safety and/or fire hazards

existed.

(4)

Radiological

Protection

Program - Radiation protection 'control

activities

were

observed

routinely to verify that

these

activities

were in conformance

with the facility policies

and

procedures,

and in compliance with regulatory'equirements.

The

inspectors

also

reviewed

selected

radiation

work permits to

verify that controls were adequate.

On

December

10, at approximately

5:25 p.m.,

licensee

personnel

discovered

that

a high radiation

area

access

key

was missing

during

a routine shift inventory of administratively controlled

keys.

= Technical

Specification

6. 12.2 requires that accessible

areas

with radiation levels greater

than

1000 mR/hr at

18 inches

from a radiation source

be provided with locked doors to prevent

unauthorized

entry with keys

maintained

under administrative

control.

The missing

key

was

subsequently

found in the keyhole for the

door to the

drum storage

area

in the waste

processing

building

at approximately ll:30 p.m.'n

December

10.

Discussion with the

technician

who last

used

the

key determined

that the

key

had

been

in the

door

lock since

approximately

11:00

a.m.

on

December

10.

Based

upon

RWP and dosimetry records,

the licensee

does

not believe

an unauthorized

entry was

made into the locked

area.

Licensee

personnel

removed

the .key from the keyhole

and

initiated

a

SOOR

(SOOR

90-187)

to investigate

this incident.

The inspector

reviewed radiation

surveys

of the

drum storage

area

and discovered that existing radiation levels required that

this area

be locked in accordance

with the TS.

The licensee

has

recently

been

experiencing

problems with the

control of high radiation

areas.

SOOR 90-78 reported that

on

Ilay 25,

1990,

a

locked radiation

area

gate

in the reactor

containment

building was

found not to

be locked with the door

ajar .

SOOR

90-135

reported

that flashing lights,

used to

identify a high radiation area,

were found not to be functioning

on October

5,

1990.

SOOR 90-161 reported that

on November

13,

1990,

the restricted

high radiation

area

key box was improperly

accessed

by an unauthorized

individual.

All of these

problems,

which occurred

in

a relatively short period of time, indicate

the

need for the licensee

to review the controls associated

with

high radiation areas

with appropriate

personnel.

The

missing

key event of December

10 is

a violation of

TS

.6. 12.2.

Although this matter

was identified by the licensee, it

is being cited due to recurrent

problems in this area.

Violation (400/90-26-01):

Failure to maintain administrative

control of a high radiation area

key.

Security Control - In )the course of the monthly activities, the

inspector

included

a review of the licensee's

physical security

program.

The

performance

of various shifts of the security

force

was

observed

in the

conduct of daily activities which

included:

protected

and vital area

access

controls;

searching

of personnel,

packages,

and

vehicles;

badge

issuance

and

retrieval;

escorting

of visitors; patrols;

and

compensatory

posts.

In addition,

the inspector

observed

the operational

status

of

Closed

Circuit Television

(CCTV) monitors,

the

Intrusion Detection

system

in the central

and

secondary

alarm

stations,

protected

area

lighting, protected

and vital area

bar rier integrity,

and the security organization interface with

operations

and maintenance.

Fire Protection

- Fire protection activities,

staffing

and

equipment were observed

to verify that fire brigade staffing was

appropriate

and

that fire alarms,

extinguishing

equipment,

actuating

controls,

fire

fighting

equipment,

emergency

equipment,

and fire barriers

were operable.

'

(7)

Chemistry

Sampling

Program

-- Reactor

coolant

sampling

and

analysis

and boric acid tank analysis

were

observe'd

to verify

that

the

sample

was

representative,

appropriate

acceptance

. criteria

were

met, test results

were properl'y evaluated,

and

sampling

and

analysis

procedures

were utilized

and properly

'mplemented.

On January

8,

1991,

the inspector

observed

the sampling of the

" reactor

coolant

system which was

done for compliance with T.S.

4.4.7.

While the chemistry technician

was purging the

sample

lines,

the inspector

questioned

the length

of, the purge time.

The technician

stated

that

a

one to

two minute. purge

was

required prior to sampling.

Upon returning to the

chemistry'ab,

the inspector

reviewed chemistry procedure

CRC-100,

Reactor

Coolant

System

Chemistry Control,

Rev.

7,

and

noted that the

required

sample

purge

time per

step

10. 1. 1.6 was ten minutes.

The technician

was

again

questioned

about

the .length of the

purge

time

and

responded

that

during

previous

on-the-job

training,

she

had been'nstructed

to purge the

sample line for

one to two minutes.

The failure to purge the

sample line as

required

by procedure

CRC-100 is considered

to be

a violation of

TS 6.8.1.a.

Violation (400/90-26-02):

Failure, to properly

implement

a

radiochemistry

procedure.

This violation and violation 90-21-01,

continues

to show

a lack

of attention

to detail

by

the

licensee

in

implementing

radiochemistry

procedures.

When informed of this finding, the

licensee

implemented additional corrective action consisting of:

counseling

the 'chemistry

technician

and

foremen,

management

discussion

of

procedural

compliance

with supervisors

and

specialists,

initiation of spot checks of procedure

performance,

and corporate

chemistry department initiation of an independent

review of this incident and previous incidents.

c.

Review of Nonconformance

Reports

Significant Operational

Occurrence

Reports

(SOORs)

and Nonconformance

Reports

(NCRs)

were

reviewed

to verify the following:

TS were

complied with, corrective actions

as identified in the reports

were

accomplished

or being

pursued

for completion,

generic

items

were

identified and reported,

and

items

were reported

as required

by the

TS.

SOOR

90-186

reported

that

a

TS required surveillance test

on the

personnel air lock was not performed

as required.

Following multiple

containment entries

on December

6,

1990, the licensee

was testing

the

I

personnel

air lock for overall

leakage

in

accordance

with

TS 4.6. 1.3.b.

This test

was satisfactorily

completed

on December

10.

Upon review of containment

entry logs, licensee

personnel

discovered

that periodic testing of the personnel air lock door seal, leakage

was

not performed

every

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />,

as required

by TS 4.6. 1.3.a.

Although

unofficial door seal

leakage

tests

were performed during the overall

leakage test,

these

tests

were not documented.

'All unofficial test

results

were satisfactory.

The licensee's

corrective

action to

prevent

recurrence

included

adding

a caution

note

to the testing

procedure

which specifies

the additional

requirement

to perform

a

door seal

leakage test.

This matter is considered

to be

a licensee

identified

NCV and

i's not being cited because

the criteria specified

in section

V.G. 1 of the

NRC Enforcement Policy were satisfied.

NC4 (400/90-26-03):

Failure to periodically test

the containment

personnel air lock every

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

3.

Surveillance

Observation

(61726)

Surveillance

tests

were observed

to verify that approved

procedures

were

being

used;

qualified

personnel

were

conducting

the tests;

tests

were

adequate

to verify . equipment

operability;

calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

CRC-100

CRC-524

EST-702

Reactor

Coolant System Chemistry Control

Boron Using the Nettler DL40RC Nemotitrator

Noderator Temperature

Coefficient -

EOL Using The

Boron Nethod

EST-0719

EPT-160T

FNP-101

LP-T-6903B

NST-E0006

NST-E0039

Incore Versus

Excore Axial Flux Difference Comparison

Temporary Procedure for the Boundary Test for the

RAB

Emergency

Exhaust

System.

Incore Thermocouple

and Flux Napping

Loop Calibration Diesel Generator

Room

B Temperature

480

YAC Nolded Case Circuit Breaker Test

Reactor Coolant

Pump

(1C-SN) Undervoltage

Relay

Channel Calibration

6,

NST-E0043

Reactor

Coolant

Pump

(1C-SN) Underfrequency

Relay

(KF) Channel

Calibration

NST-E0044

6.9

KV Emergency. Bus,

1B-SB Under'oltage

Channel

Calibration

NST- I0012

HST- I0088

NST-10122

NST- I0169

OST-1013

OST-1503

OST-1805

PIC-E004

Main Steamline

Pressure,

Loop

2 Channel

Calibration

Reactor

Coolant Loop

1 Hot Leg Temperature

Instrument

Calibration

Pressurizer

Pressure

P-04455 Operational

Test

Nuclear Instrumentation

System

Source

Range

H31

Operational

Test

1A-SA Emergency

Diesel

Generator Operability Test.

Monthly Interval

Pressurizer

PORV Operability quarterly Interval

Pressurizer

PORV Operability 18 Monthly Interval

General

Electric 6.9

KY Overcurrent

Relay Calibration

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The

inspector

observed/reviewed

maintenance

activities to verify that

correct

equipment

clearances

were

in effect;

'work requests

and fire

prevention

work permits,

as

required,

were

issued

and

being followed;

quality control

personnel

were available for -inspection activities

as

required;

and,

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following

maintenance

(WR/JO) activities:

Troubleshoot

slow start of the

"A" emergency

diesel

generator

in

accordance

with procedure

NPT-M0040,

Emergency

Diesel

Generator

On-Engine Starting Air Valve's Periodic Maintenance.

Replacement

of fan belt on the

RAB equipment

room fan AH-16A.

Disassembly

and cleaning of an

emergency

service water screen

wash

pump

and

post

maintenance

testing

in accordance

with procedure

OST-1214,

Emergency

Service

Water

System

Operability,

Train

A,

quarterly Interval.

Troubleshoot

1SI-1

BIT isolation

valve failure to

operate

per

corrective

maintenance

procedure

CM-I-004, Limitorque Calibration

Check

and Stroking,

and

CM-M-0050, Limitorque Valve Actuator Size

SMB-000 Disassembly.

Troubleshoot

the

non vital inverter due to voltage spiking.

Replacement

of S-4 fan

ITE breakers

with Westinghouse

breakers,

per

plant modification

PCR 4687..-

Troubleshoot of the

RCP underfrequency trip circuit failure.

Disassembly

and inspection of 1SI-2 BIT isolation valve

and

1RH-69,

RHR Recirc valve.

On January

2,

1991,

the BIT Inlet Isolation Valve (1S1-1)

was disassembled

for corrective

maintenance

because

the valve would not stroke.

It was

found that

a locking ring which held the torque switch bearing in 'place,

was

missing.

This allowed

the

torque

switch internals

to shift

and

prevented

valve movement.

The licensee

is conducting further inspections

of other torque switches to insure the locking rings are in place.

During disassembly,

the inspector

noted that the technicians

failed to

document lifted electrical

leads

in the valve operator.

The licensee

was

issued

a

similar violation

in

NRC

Inspection

Report

50-400/90-20

(VIO 400/90-20-03)

in which lifted leads

were not properly documented.

Procedure

PLP-702,

Independent

Verification,

was

revised

following

Violation 400/90-20-03

to include

a log sheet

which would individually

document all lifted leads.

This sheet

was not completed

as required

when

the

Limitorque

leads

were lifted.

However,

the licensee

has

not yet

completed

training all personnel

on the .procedure revision.. Therefore,

this matter will not

be cited,

but instead will be

considered

to

be

another

example of violation 400/90-20-03.

5.

Review of Licensee

Event Reports

and

10 CFR Part 21 Reports

(92700)

The following LERs

and

10 CFR Part 21 Reports

were reviewed for potential

generic

impact,

to detect

trends,

and to determine

whether corrective

actions

appeared

appropriate.

Events that were reported

immediately were

reviewed

as

they occur'red

to determine if the

TS were satisfied.

LERs

were reviewed in accordance

with the current

NRC Enforcement Policy.

a ~

(Closed)

LER 90-05:

This

LER reported

an actuation of an engineered

safety

system

due to

a radiation monitor spike caused

by

a loose pin

connection.

This event

was previously discussed

in

NRC Inspection

Report 50-400/90-06.

The licensee

has

revised

the applicable test

procedure

to delete

the

unnecessary

loss of counts

test

thereby

reducing wear

on the coaxial

connector.

(Closed)

LER 90-10:

This

LER reported

inadequate

administrative

control of the

RAB emergency

exhaust

system ventilation boundary.

This matter

was

previously

discussed

in

NRC

Inspection

Report

50-400/90-10.

As

a result of the licensee's

corrective action to

review other ventilation systems for similar problems,

the licensee

discovered

control

room ventilation

damper

and

was

issued

a non-cited

licensee identified violation (NC4 400/90-14-02).

The licensee

submitted

a supplemental

report dated

September

5,

1990,

documenting

results of the review of the other ventilation systems.

The licensee

has

completed

testing of various ventilation 'boundary

doors

and determined

that the

system is not capable

of maintaining

the

required

negative

pressure

with

doors left open.

Plant

procedures

were revised to add administrative controls for specific

ventilation boundary doors.

(Closed)

LER 90-16:

This

LER reported

inadequate

testing of the

FHB

emergency

exhaust

system.

This event

was previously discussed

in NRC

Inspection

Report

50-400/90-13

and

was

the subject

of

a licensee

identified violation

(NC4 400/90-13-02).

The licensee

has revised

the test

procedure for acceptable

flow measurements

and

comparisons

of data collected.

(Closed)

LER 90-22:

This

LER reported that

a surveillance test

was

not

performed

on radiation monitor

REM-3542

due to

a procedural

deficiency.

This matter

was previously discussed

in

NRC Inspection

Report 50-400/90-24

and

was the subject of a licensee identified

NCV

(400/90-24-05).

The licensee

has

counseled

maintenance

procedure

personnel

on this

incident

and

has

tested

the

monitor with

satisfactory results.

(Closed)

LER 90-23:

This

LER reported

the inadvertent start of the

"A" emergency

diesel

generator.

This event occurred

due to personnel

error

on the part of

a licensed

reactor

operator.

The licensee

counseled

the operator

and will review self-verification techniques

with all operators

during their next annual training.

Although this

event

occurred

on

November

24,

1990, it was

not

verbally reported

to the

NRC Operations

Center until

November

26,

1990.

Initially, the shift foreman

and

STA did not consider

the

event to- be immediately reportable.

Further review of the event

by

the licensee's

compliance staff determined that the event should

have

been

reported

within

four

hours,

as

required

by

10 CFR 50.72(b)(2)(ii).

The licensee

reviewed this event with STA's

and

shift foremen

and plan to revise applicable

procedures

to require

independent

reviews for reportabi lity determination.

This matter is

considered

to

be

a licensee

identified

NCV and is not being cited

because

the criteria

specified 'in section

V.G.1 of

the

NRC

Enforcement Policy were satisfied.

NC4(400/90-26-04):-

Failure to make

a four hour report to the

NRC

Operations

Center.

f.

(Closed)

LER 90-24:

This

LER reported that

inadequate

fuses

were

installed in safety related

125

VDC applications.

The licensee

has

replaced

the fuses with fuses properly rated for the application.

g.

(Open)

LER 90-25:

This

LER reported

a required plant shutdown

due to

excessive air leakage

through the containment

personnel air lock.

As

stated

in the

LER,

a plant

shutdown to Mode

5 (cold shutdoWn)

was

performed

on

December

8,

1990, following an unsatisfactory test

on

the personnel

air lock.

Subsequent

repairs

were performed

on the air

lock and testing

was satisfactorily

performed

on December

9,

1990.

The licensee

plans

to implement

a plant modification

(PCR-3877)

to

improve the reliability of the air lock.

The

LER will remain

open

pending completion of this modification.

h.

(Closed)

P2189-12:

This

10 CFR Part 21 Report,

dated

September

29,

1989, discussed

a problem with Limitorque SMB-000 and

SMB-00 CAN-type

torque

switches with fiber spacers.

A plant modification,

PCR-4110,

was

implemented

to,replace

various affected

torque

switches

during

the

1989 outage.

Additional. torque

switches

outside 'of containment

and the

steam

tunnel still contain fiber spacers,

however.

due to the

plant

design

that

bypasses

the

torque

switch

during

an SI,

an

evaluation

has determined

that

no safety hazard existed.

i.

(Closed)

P2189-19:

This

10 CFR Part 21 Report,

dated

November

13,

1989,

discussed

a

problem

with potentially defective

pressure

reducing

sleeves

supplied

as

spare

parts

for Pacific

Pumps

manufactured

by Dresser

Industries.

Two pump sleeves

were found in

the

spare

parts

warehouse,l

one of which

was

returned

to Dresser

Industries.

All sleeves

received

from the manufacturer will be

hardness

tested

as part of receipt inspection in the future.

6.

Design

Changes

and Modifications (37828)

Installation of new or modified systems

were reviewed to verify that the

changes

were reviewed

and

approved

in accordance

with 10 CFR 50.59, that

the

changes

were

performed

in accordance

with technically

adequate

and

approved

procedures,

that

subsequent

testing

and test

results

met

acceptance

criteria or deviations

were resolved in an acceptable

manner,

and that appropriate

drawings

and facility procedures

were revised .as

necessary.

This review included selected

observations

of modifications

and/or testing

in progress.

The following modifications/design

changes

were reviewed:

PCR-5636

PCR-5610

PCR-5605

PCR-5549

Equalizing Valve Penetration

Plugging

CSIP-B Balancing Line Vibration Problem

ASCO Solenoid

Valve FT831654

125/250

YDC Fuse Voltage Rating

No violations or deviations

were identified.

10

7.

Followup of Onsite Events

(93702)

'I

8.

At 1:54

p.m.

on January

24

an

unusual

event

was .declared

due to

a

TS

required

plant

shutdown for excessive

leakage

past

containment

purge

isolation valves.

During the performance of a periodic local leak rate

test

on the

containment

purge

exhaust

penetration,

licensee

personnel

discovered

excessive

seat

leakage.

This leakage

amount

caused

the total

combined

leakage

rate to exceed

the 'limits of TS 3.6.1.2.b

and

a plant

shutdown

was initiated.

At approximately

30 percent

power,

the

purge

isolation

valves

were

repaired

and

a local

leak rate test

completed

satisfactory.

At 4: 15 p.m.

the unusual

event

was terminated

and

a power

increase

back to 100 percent

was initiated.

Licensee

Action

on Previously Identified Inspection

Findings

(92702

5

92701)

a

~

(Clos'ed)

IFI 400/89-13-02:

Instantaneous

trip testing of molded case

circuit breakers.

The licensee

has

purchased

additional

breaker testing

equipment

and

has revised testing

procedures

to incorporate

the pulse trip testing

method versus

the run-up method.

b.

(Closed)-

YIO 400/89-21-01:

Failure

to,adequately

evaluate

the

suitability of

commercial

grade

items

used

in

safety

grade

applications.

The

inspector

reviewed

and verified completion of the corrective

action's listed,in the licensee's

response

letter dated

December

21,

1989.

The subject

breaker

models

were seismically tested

by Wyle

Test

Labs

and evaluated

to be satisfactory for seismic applications.

The critical characteristics

for breakers

already

installed

in

safety-related

applications

were

tested

with satisfactory

results.

Receipt inspection instructions for new breakers

have

been revised to

include appropriate

testing.

Finally, the licensee

reviewed this

incident

with

plant

and

NED

personnel

to

avoid

future

miscommunication

between

these

groups.

c.

(Closed)

IFI 400/89-30-01:

Review the

opening

stroke

time test

results for the pressurizer

power operated relief valves.

The licensee

performed

the test

procedures

for measuring

the

open

stroke time of these

valves with satisfactory results

on December

12,

1989.

d.

(Closed)

URI 400/90-13-04:

Failure to perform

a timely evaluation of

Boric Acid Pump Test data.

A review of this

item

found. that

the boric'cid

pump

remained

operable

and

could

always

perform its

intended

function.

A

thoroughly

documented

evaluation

would have resolved

the boric acid

11

e.

pump

concern

much

sooner.

Technical

support

personnel

have

been

cautioned

to

document their decision

process

and

the

reason

for

coming to the conclusion that was reached.

(Closed)

IFI 400/90-21-03:

Follow the licensee's

activities to

prevent leaks

on the "B" charging/safety

injection pump.

Licensee

personnel

determined

that the failure of the balancing line

pipi ng for this

pump to

be

due to cyclic fatigue.

Vibration was

measured

on this pump's balancing line and compared with the identical

train "A" pump.

The "B" vibration was

an order'f magnitude higher.

The

licensee

installed

a modification

(PCR-5610)

to provide

a

temporary fix to dampen

and reduce

the balancing line vibration.

The

modification significantly

reduced

the vibration

by

an order of

magnitude.

The licensee

is considering

a more permanent fix which

could include

new mechanical

seals for the'pump.

f.

(Closed)

VIO 400/90-20-04:

'Failure to perform compensatory

actions

for an inoperable radiation monitor.

The

- licensee

has

submitted

LER 90-20

on this event.

For record

purposes

the violation will be closed

and further action tracked

by

the

LER.

g.

. (Closed)

IFI 400/89-34-05:

Follow the licensee's

activities to

replace

HVAC system actuators.

The licensee

has replaced/rebuilt

24 of the

37 affected actuators.

Due to extremely

long lead

times involved with the refurbishment of

these

components,

the licensee

expects

to complete

the remaining

13

by mid-1993.

The'icensee

continues

to perform compensatory

measures

and the justification for continued plant operation

remains in effect

until all actuators

are repaired.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1)

at the conclusion of the inspection

on January

25,

1991.

During this

meeting,

the

inspectors

summarized

the

scope

and

findings of the

inspection

as

they are detailed

in this report, with particular

emphasis

on

the

violations

addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this

inspection.

Item Number

400/90-26-01

Descri tion and Reference

VIO:

Failure to 'maintain administrative

control

of

a

high

radiation

area

key,

paragraph 2.b.(4).

12

10.

400/90-26-02

400/90-26-03

400/90-26-04

Acronyms

and Initialisms

VIO:

Failure to properly implement

a

radiochemistry

procedure,

paragraph 2.b.(7).

NC4:

Failure to periodically test the

containment

personnel

air lock every

72

hours',

paragraph

2.c.

NC4:=- Failure to make a'our hour report to

the

NRC Operations

Center,

paragraph

5.e.

BIT

CCTV

CFR

CM

CRC

CSIP

EOL

EPT

EST

.

FHB

FMP

HVAC

IFI

LER

LP

MPT

mR/hr

MST

NCR

NCY

NED

NRC

OST

PCR

PIC

PLP

PORV

RAB

RCP

RHR

RWP

SI

SOOR

STA

TS

Boron Injection Tank

Closed Circuit Television

Code of Federal

Regulations

Corrective Maintenance

Chemistry Radiochemistry

Changing -- Safety Injection

Pump

End of Life

Engineering

Performance

Test

Engineering Surveillance

Test

Fuel Handling Building

Fuel

Management

Procedure

Heating, Ventilation and Air Con

Inspector

Follow-up Item

Licensee

Event Report

Loop Calibration Procedure

Maintenance

Performance

Test

Milliroentgen per hour

Maintenance

Surveillance

Test

Non-Conformance

Report

Non-Cited Violation

Nuclear Engineering

Department

Nuclear Regulatory Commission.

Operations

Surveillance Test

Plant

Change

Request

Primary Instrument Control

Plant Program

Procedure

Power Operated Relief Valve

Reactor Auxiliary Building

Reactor

Coolant

Pump

W

Residual

Heat

Removal

Radiation

Work Permit

Safety Injection

Significant Operational

Occurren

Shift Technical Advisor

Technical Specification

di tioning

ce Report

13

URI

VAC

VDC

VIO

WR/JO

Unresolved

Item

Volts Alternating Current

Voltage Direct Current

Violation

Work Request/Job

Order

E