ML18009A748

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Insp Rept 50-400/90-21 on 901020-1116.Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls, Security,Fire Protection,Surveillance Observation,Safety Sys Walkdown & Review of Nonconformance Repts
ML18009A748
Person / Time
Site: Harris 
Issue date: 11/30/1990
From: Carroll B, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A747 List:
References
50-400-90-21, GL-88-05, GL-88-5, NUDOCS 9012170038
Download: ML18009A748 (20)


See also: IR 05000400/1990021

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REG ION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/90-21

m

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

October

20 - November

16,

1990

Inspectors:

J.

e row,

enior

esi

t

spector

M. Sha

non,

esi ent

pect

Approved by:

ar o

,

cting

ection

ie

Divis on of Reactor Projects

License No.:

NPF-63

Da e

igne

Da

e

igne

h

9o

go

Da

gne

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant

operations,

radiological

controls,

security,

fire protection,

surveillance

observation,

maintenance

observation,

safety

system

walkdown,

review of nonconformance

reports, visit to the public document

room, midloop/

reduced inventory activities, review of the spent fuel shipping program,

review

of the boron corrosion program, operator license review,

and licensee

action

on

previous inspection

items.

Numerous facility tours were conducted

and facility

operations

observed.

Some of these

tours

and observations

were conducted

on

backshifts.

Results:

Three violations

were identified:

failure to properly

implement

a radio-

chemistry procedure,

paragraph

2.b.(7);

failure to perform

a written safety

evaluation,

paragraph

9;

and failure to notify the

NRC

upon

employment

termination of a licensed operator,

paragraph

11.

A non-cited

licensee

identified violation concerning

an improper change to

a

surveillance

procedure

was identified, paragraph

6.a.

q012170038

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01 1'30

pop

ADQCK 0

pDp

6

The licensee's

decision to shutdown

the plant

and repair

minor leakage

was

considered

to

be conservative,

paragraph

2.

,Improvements

were

noted in the

licensee's

boron corrosion

program,

paragraph

10.

Mockup training for the

installation

of

steam

generator

nozzle

dams

reduced

personnel

exposure,

paragraph

4.

REPORT

DETAILS

1.

Persons

Contacted

'icensee

Employees

  • J. Collins, Manager,

Operations

  • G. Forehand,

Manager,

gA/gC

C. Gibson, Director, Programs

and Procedures

  • J. Hammond,

Manager,

Onsite Nuclear Safety

C. Hinnant, Plant General

Manager

J. Nevill, Manager,

Technical

Support

  • C. Olexi k, Manager,

Regulatory

Compliance

A. Poland,

Manager,

Environmental

and Radiation Control Support

  • R. Richey,

Vice President,

Harris Nuclear Project

  • J. Sipp,

Manager,

Environmental

and Radiation Control

H. Smith, Manager,

Radwaste

Operation

  • M. Wallace, Sr. Specialist,

Regulatory Compliance

  • E. Willett, Manager,

Outages

and Modifications

  • W. Wilson, Manager,

Spent Nuclear Fuel

Other

licensee

employees

contacted

included

office,

operations,

"

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms

used

throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

The plant

began this inspection

period in power operation

(Mode 1).

On

November

10,

1990,

a plant shutdown

and cooldown was

commenced

to repair

a

small

primary to secondary

steam

generator

leak

and to perform general

reliability related

maintenance.

At 10:55 p.m.,

on November

12, the cold

shutdown

(Mode 5) condition

was

reached.

The plant remained

in the cold

shutdown condition for the duration of this inspection period.

The licensee's

decision

to shutdown

the plant to repair the small leak,

even

though

leakage

was far below regulatory limits, was considered

to be

conservative

and beneficial to safe plant operation.

a.

Shift Logs and Facility Records

The inspector

reviewed

records

and

discussed

various entries

with

operations

personnel

to verify compliance

with the

TSs

and

the

licensee's

administrative

procedures.

The following records

were

reviewed:

Shift Foreman's

Log; Outage Shift Manager's

Log; Control

Operator's

Log; Night Order Book; Equipment Inoperable

Record; Active

Clearance

Log; Jumper

and Wire Removal

Log; Shift Turnover Checklist;

and selected

Radwaste

Logs.

In addition,

the inspector

independently

verified clearance

order tagouts.

No violations or deviations

were identified.

b.

Facility Tours

and Observations

Throughout

the inspection

period, facility tours

were

conducted

to

observe

operations

and

maintenance

activities in progress.

Some

operations

and

maintenance

activity observations

were

conducted

during backshifts.

Also, during this inspection

period,

licensee

meetings

were

attended

by the

inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security

perimeter

fence;

control

room;

emergency

diesel

generator

building; reactor auxiliary building; reactor

containment building;

waste

processing

building; fuel handling building; emergency service

water building; battery

rooms;

and electrical

switchgear

rooms.

During these tours, the following observations

were made:

( I)

Monitoring Instrumentation

-

Equipment operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup,

reactor

operating

parameters,

and auxiliary equipment

operating

parameters

were

observed

to verify that indicated

parameters

were

in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors

verified that operating shift

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner.

In addition, the inspectors

observed shift

turnovers

on various occasions

to verify the continuity of plant

status,

operational

problems,

and

other

pertinent

plant

'nformation during these turnovers.

(3)

Plant

Housekeeping

Conditions. -

Storage

of material

and

components,

and

cleanliness

conditions

of various

areas

throughout

the facility were

observed

to determine

whether

safety and/or fire hazards

existed.

(4)

Radiological

Protection

Program - Radiation protection control

activities

were

observed

routinely to verify that

these

activities

were in conformance

with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also

reviewed

selected

RWPs to verify that the

RWP

was current

and 'that the controls were adequate.

3

(5)

Security Control - In the course of the monthly activities,

the

inspectors

included a,review of the,licensee's

physical security

program.

The

performance

of, various shifts of the security

force

was

observed

in the

conduct

of daily activities

to

include:

protected

and vital area

access

controls; searching

of

personnel,

packages,

and vehicles;

badge

issuance

and retrieval;

escorting

of visitors; patrols;

and

compensatory

posts.

In

addition, the inspector

observed

the operational

status of CCTY

monitors,

the Intrusion Detection

system

in the central

and

secondary

alarm stations,

protected, area lighting, protected

and

vital

area

barrier integrity,

and

the security organization

interface with operations

and maintenance.

On October 28,

1990, the inspector

noted

problems with a control

room security

door failing to properly latch.

On

three

different visits to

the

control

room

the

inspector

noted

problems with the door latching.

Each time

a security guard

was

summoned

to

check

out

the

door for proper operation.

The

inspector

discussed

this matter with licensee

management

on the

following day.

Initial licensee

actions

did not appear

to

be

adequate

for resolving

the

problems.

This

item

has

been

discussed

with regional security personnel

who will review it in

more detail during

a routine security inspection.

(6)

(7)

Fire Protection

- Fire protection activities, staffing,

and

equipment

were observed to verify that fire brigade staffing was

appropriate

and

that fire alarms,

extinguishing

equipment,

actuating

controls,

fire fighting

equipment,

emergency

equipment,

and fire barriers

were operable.

Sampling

Program - Selected

performance

of reactor

coolant

sampling

and boric acid tank sampling

were observed

to verify

that the sample

taken

was representative

of the substance

being

sampled,

appropriate

acceptance

criteria were met, test results

were properly evaluated

and trended,

and sampling

and analysis

procedures

were

utilized

and

properly

implemented.

The

deficiencies

addressed

below were noted.

On October

24,

1990,

the inspector

observed

the sampling of the

"A" steam

generator

to determine activity.

This, sample

was

performed

to calculate

the magnitude

of

a small

primary to

secondary

leak which had developed.

The inspector noticed that

procedures

were not routinely referenced

by the technician

to

draw

or

analyze

the

sample.

Upon

sample

completion,

the

inspector

requested

the

technician

to

walk

through

the

appropriate

procedures.

When

procedure

RCP-660,

Sample

Preparation

for Determination of Radioactivity,

was referenced

by the technician,

the inspector

found that not all of the steps

required

by the procedure

had

been performed.

Specifically step

10.3.1.2.2

required

the addition of 2 ml of nitric acid to the

sample prior to sample'nalysis

for activity.

When questioned

4

about this omission,

the technician stated that

he had forgotten

this step

but that the

omission

should

not have

negated

the

sample results.

On October

26,

1990,

the inspector

observed

a routine reactor

coolant

system

sample

performed

as required

by TS 4.4.7.

Again

procedures

were

not periodically

referenced.

During the

preparation

of thi's

sample for a

gamma

scan, nitric acid

was

also not added.

The inspector

researched

procedure

RCP-660 for

the preparation

of this

sample

and

found that step

10.3. 1. 1.3

specified

the addition of 0.5

ml of nitric acid prior to the

activity analysis.

These

two -observations,

which involved different samples

by two

different technicians,

indicate the inadequate

implementation of

a radiochemistry

procedure

and are considered

to be examples

of

a violation.

Violation (400/90-21-01):

Failure to properly

implement

a radiochemistry

procedure.

One violation was identified.

3.

Surveillance

Observation

(61726)

Surveillance

tests

were observed

to verify that approved

procedures

were

being

used;

qualified personnel

were

conducting

the tests;

tests

were

adequate

to verify equipment

operability;

calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

OST-1004

OST-1020

MST-I0151

RST-201

RST-204

EPT-167

Power Range

Heat Balance Daily Interval

Remote

Shutdown

Monitoring

and

Accident

Monitoring

Instrumentation

Channel

Check Monthly Interval

Steam

Generator

3C Narrow Range

Level (L-0496)

Protection

Set III Operational

Test

Boron Concentration

Surveillance

of the Boric Acid and

Refueling Water Storage

Tanks

Reactor

Coolant

System

Chemistry

and

Radiochemistry

Surveillance

Steam Generator

Secondary

Leak Test

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The inspector

observed/reviewed

maintenance

activities to verify that

correct

equipment

clearances

were

in effect;

work requests

and fire

prevention

work permits,

as

required,

were

issued

and being followed;

quality control

personnel

were available for inspection activities

as

required;

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following

maintenance

(WR/JO) activities:

Calibration of ground fault relays

associated

with feeder

breakers

for

MCC-1A33-SA

and

MCC-1A23-SA in

accordance

with procedure

PIC-E019,

ITE

GRC Ground Fault Relay Calibration.

Repair

leak

on

the

balancing

line for the

"B" charging/safety

injection pump.

Installation of steam

generator

nozzle

dams

and

mockup training in

accordance

with procedure

CM-M0176,

Steam

Generator

Primary Nozzle

Dam Installation, Operation

and Removal.

Replacement

of various valves associated

with "A" essential

chiller.

The

inspectors

observed

licensee

preparations

for installing

steam

generator

nozzle

dams.

A mockup of the steam generator

was utilized and

practice

sessions

held

on installing and removing the nozzle

dams.

This

training

was very realistic,

using full protective clothing dressout

and

formal communications.

As

a result of this training, workers were able to

quickly perform the installation of the nozzle

dams in this high radiation

field and thereby received

less

personnel

exposure.

This type of training

is considered

to

be

a strength

of the

maintenance

and radiological

protection

programs.

No violations or deviations

were identified.

5.

Safety Systems

Walkdown (71710)

The inspectors

conducted

a walkdown of the cold leg accumulator

safety

injection system to verify that the lineup was in accordance

with license

requirements

for system

operability

and that

the

system

drawing

and

procedure correctly reflect "as-built" plant conditions.

Also, accessible

piping inside

containment

was

walked

down for the auxiliary feedwater

system.

No violations or deviations

were identified.

6.

Review of Nonconformance

Reports

(71707)

SOORs

and

NCRs were reviewed to verify the following:

TS were complied

with, corrective actions

as identified in the reports

were accomplished

or

being pursued for completion,

generic

items were identified and reported,

and items were reported

as required

by the TS.

a.

SOOR

90-143

reported

that

procedure

OST-1004

was

revised

using

unqualified or approved

information.

Procedure

OST-1004

was changed

to permit

a heat

balance calculation with continuous

steam generator

blowdown remaining in service.

To account for the heat dispersed

by

the

blowdown system,

an engineering

calculation

was

performed

to

provide the 'method for determining this.

To assist

in the procedure

revision

process,

a draft of this calculation

was

provided

to

procedure writers.

Procedure

OST-1004

was revised

and

approved

on

October 28,

1990, utilizing the draft calculation which had not yet

been adequately

reviewed

and approved

by engineering

personnel.

Upon

discovery of this situation

on October

29,

1990, operating

personnel

performed another heat balance

using the previous

method of isolating

the

blowdown

system.

The draft calculations

were

subsequently

reviewed,

approved,

and

deemed

to be satisfactory.

The licensee

is

presently

performing

an

HPES evaluation to determine

the root cause

for this event.

This licensee

identified violation is not being

cited because criteria specified in Section

V.G. 1 of the

NRC Enforce-

ment Policy were satisfied.

NCV (400/90-21-02):

Failure to use

approved calculations for revising the heat balance

procedure.

b.

SOOR 90-155 reported that

a leak

had developed

on the balancing line

piping of the "B" charging/safety

injection

pump

on November 3,

1990.

The

pump

was

secured

and piping was replaced

to stop the leak.

On

November 12, another

leak developed

in the

same

general

area of the

balancing line.

A review of work history associated

with this

pump

revealed

numerous

leaks

on this piping which included

a cracked

weld

in August 1988,

and

a cracked

pipe in January

1989.

The licensee

is

presently performing

a root cause

evaluation to prevent repetition of

this event.

IFI (400/90-21-03):

Follow the licensee's

activities to

prevent leaks

on the "B" charging/safety

injection pump.

One non-cited violation was identified.

7.

Visit to the Public Document

Room (94600)

The inspector visited the community's public document

room on October 25,

1990.

This facility is located at the

Cameron Village Public Library in

Raleigh,

NC.

The inspector

examined

the type of information available,

the condition of this information,

and the filing system

used for access

to this information.

Selective microfiche and

hardcopy files of various

documents

were reviewed.

The public document

room was found to be orderly

and information accessible.

8.

Nidloop/Reduced

Inventory Activities (71707)

In response

to

a

NRC

Region II memorandum

dated

July 27,

1990,

the

inspectors

reviewed

the licensee's

preparations

for operation of the

RCS

in a reduced

inventory condition.

These actions

were previously discussed

in

NRC Inspection

Report

50-400/90-08.

Generic Letter 88-17,

Loss of

Decay, Heat

Removal,

and

the

current

revisions

to plant

procedures

governing midloop operation

were reviewed.

The inspector also discussed

this matter with licensee

management

and emphasized

that due to the large

number of administrative

controls

in place

governing

operator

actions

while in this

condition,

shrewd

operator

diligence

was

essential.

Licensee

management

stated

they would review their controls

and procedures

with operations

personnel.

No violations or deviations

were identified.

Review of the Spent

Fuel Shipping Program

(71707)

As

a followup to the observations

mentioned

in

NRC Inspection

Reports

50-400/90-17

and 50-400/90-20,

the inspectors

continued to review spent

fuel shipping activities.

The problems

associated

with the

BWR fuel crud

continued to grow with the receipt of two more refueling shipments.

Following the receipt

and

head

removal of cask

IF-303,

the

spent

fuel

water clarity degraded

to the point where fuel transfer

could not take

place.

The operators

were

unable

to see

the fuel

and therefore

fuel

transfer

was delayed for approximately

10 days while the cobalt

and iron

particulate settled

out of solution.

Following the transfer of fuel from the other cask (IF-304), it was noted

that approximately

18 inches of crud had settled

in the bottom of the fuel

cask.

Radiation levels in the bottom of the cask were found to be

as high

as

1260

RAD using underwater

detectors.

By using

a suction

hose

and

pump

the licensee

transferred this crud to vacant spent fuel pool "D".

The inspector

reviewed

previously

performed

surveys

following the last

three fuel shipments

and

noted

a steadily increasing

crud loading in the

shipping

cask.

The

spent

fuel

cask

( IF-304)

surveys

completed

on

August 8,

1990

averaged

370

RADs;

on

September

13,

1990,

averaged

576

RADs;

and

on

November 6,

1990,

averaged

797

RADs.

The

second

cask

( IF-303) revealed similar increases

and following the surveys

completed

on

October 30,

1990, the cask

averaged

483

RADS.

Following the latest

BWR fuel transfer,

the

BWR fuel baskets

were removed

and replaced

with

PWR fuel baskets.

The transfer

was successful

in that

no personnel

or area

contaminations

resulted.

It was noted,

however, that

area radiation levels

approached

100

MR on spent fuel pool monitors during

the

basket

removal

from the

cask.

The .licensee

took the appropriate

precautions

to limit personnel

exposure

during this evolution.

Following the loss of clarity in the spent fuel pools

and transfer canals,

the inspectors

performed

a detailed

review of water chemistry require-

ments.

The

FSAR table

11. 1.7-1 lists the design concentration of specific

activity (uci/gm) for various

nuclides

in the

spent

fuel pools.

The

following table lists, in part,

the nuclide,

design activity, and actual

measured activity for nuclides of interest:

FSAR Table 11.1.7-1

Nuclide

Design Activity Concentration

Sam le on October

12,

1990

measured

Concentration

NN-54

2.6

x 10 -8 uci/gm

1.3 x 10 -4 uci/gm

CO-58

1.0 x 10 -6 uci/gm

1.3

x 10 -4 uci/gm

CO-60

1.3 x 10 -6 uci/gm

2.3

x 10 -3 uci/gm

The

inspector

noticed

that

the

measured

values

exceeded

the

design

concentration

values

by as

much

as

5000 times.

FSAR Section

11. 1. 1 states

that design

basis

source

terms

have

been

used for shielding

and facilities

design

and for calculating the consequences

of postulated

accidents.

FSAR

Section

11.1.7

states

that

the

maximum

spent

fuel

pool fission

and

corrosion

product specific activities are given in Table

11. 1.7-1.

This

section

also states

that the fuel pools will be

used for storage

of

PWR

and

BWR spent fuel from other

CPSL nuclear plants

and that the spent fuel

would not contribute significantly to the fuel pool fission and corrosion

product activities.

10 CFR 50.59 requires

the licensee

to maintain records of changes

in the

facility.

These

records

must include

a written safety evaluation

which

provides

the basis for the determination that the change

does

not involve

an unreviewed

safety question.

The spent

fuel from other

CP&L nuclear.

plants is causing

a significant increase

in the fuel pool activity in that

concentrations

of cobalt

and

manganese

activity have

exceeded

the

FSAR

design activity concentrations.

Although this practice

constitutes

a

change

in the operation of the facility as

described

in the

FSAR, the

licensee

failed to perform

a written safety evaluation

as

required

by

10 CFR 50.59.

This is identified as

a Violation (400/90-21-04):

Failure

to perform

a written safety evaluation.

One violation was identified

10.

Review of Boron Corrosion

Program

(92701).

The licensee's

boron corrosion

program which implements

the requirements

of

NRC Generic Letter

GL 88-05,

Boric Acid Corrosion of Carbon Steel

'eactor

Pressure

Boundary

Components

in

PWR plants,

was

previously

discussed

in

NRC Inspection

Report 50-400/90-10.

During this outage

the

inspector

noted

some

improvements

in the implementation of this program.

A detailed upfront visual inspection of containment

was performed early in

the outage

to identify boric acid leakage

so that appropriate

and timely

corrective action could

be accomplished

within the outage

schedule.

This

inspection identified several

leaks,

but

no corrosion

was found.

Another

area

of improvement

was

a revision to procedure

OST-1081,

Containment

Visual Inspection.

This procedure

now clearly defines

the requirement to

identify boric acid

leakage,

initiate work requests

for repair,

and

notification of the system engineer for corrective action.

This procedure

revision strengthens

the overall

boron corrosion

program.

No violations or deviations

were identified.

11.

Operator License

Review (71707)

During

the

week of October

15,

1990,

a

review of operator

license

applications

from another

nuclear facility was

conducted

in the

NRC

Region II office.

It was

noted that

one

SRO candidate

(docket

number

20019)

had previously

held

an

operator

license

at the

Shearon

Harris

facility and

had terminated

employment in September

1989.

Further review

of the docket revealed that the licensee

had not notified the

NRC of this

fact.

10 CFR 50.74 requires

the licensee

to notify the

NRC within 30 days of

termination of any operator or senior operator.

Failure to notify the

NRC

of employment termination for a senior reactor operator is contrary to

10

-CFR 50.74

and is considered

to be

a violation.

Violation (400/90-21-05):

Failure to notify the

NRC of employment termination of an

SRO.

One violation was identified.

12.

Licensee

Action on Previously Identified Inspection

Findings

(92702

5

92701)

a.

(Closed)

URI 400/90-20-01:

Periodic calibration

check of installed

thermocouples.

The

licensee

provided

the

inspector

with their position

on the

testing of thermocouples.

In an internal corporate

memorandum

dated

August 9,

1984,

the licensee

stated their position that for primary

sensing

elements

which are inherently resistant

to drift, such

as

thermocouples,

a verification of operability of the primary element

and

a calibration of the rest of the instrument string would suffice.

The

inspector

discussed

this

reasoning

with

NRC Headquarters

NRR

personnel

and

Region II personnel.

The licensee's

current practice

of periodically checking

thermocouples

was

deemed to be appropriate.

A review of the, previously questioned

RHR cooler outlet temperature

and

hydrogen

recombiner

temperature

revealed

appropriate operability

verifications with the string calibrations.

b.

(Closed)

Violation 400/89-34-02:

Failure to adhere

to the require-

ments of plant procedures.

This

item

was

previously

discussed

in

NRC

Inspection

Report

50-400/90-06.

The licensee

has

revised

applicable

procedures

to

provide caution

notes

to prevent

the establishment

of inadvertent

flowpaths

between

the

RWST and the

RCS or other systems.

Ih

10

c.

(Closed) Violation 400/90-13-03:

Failure to follow plant procedures

during

the

performance

of nuclear

instrumentation

calibration

procedures.

The inspector

reviewed

and verified implementation of the corrective

actions

as

stated

in

the

licensee's

response

letter

dated

September

6,

1990.

The licensee

has

revised

applicable

procedures

and

counseled

plant

reactor

engineering

personnel

to

prevent

repetition of this event.

13.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1)

at the conclusion of the inspection

on

November

16,

1990.

During this

meeting,

the

inspectors

summarized

the

scope

and

findings of the

inspection

as

they are detailed

in this report, with particular

emphasis

on the Violations,

and the Inspector Follow-up Item addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did not

identify as proprietary

any of the materials

provided to or reviewed

by

the inspectors

during this inspection.

Item Number

Descri tion and Reference

400/90-21-01

400/90-21-02

400/90-21-03

400/90-21-04

400/90-21-05

VIO:

Failure

to

properly

implement

a

radiochemistry

procedure,

paragraph 2.b.(7).

NCV:

Failure to use

approved calculations

for revising

the

heat

balance

procedure,

paragraph

6.a.

IFI:

Follow the licensee's

activities to

prevent

leaks

on the

"B", charging/safety

injection pump, paragraph

6.b.

VIO:

Failure to perform

a written safety

evaluation,

paragraph

9.

VIO:

Failure

to notify the

NRC of

employment termination of an

SRO,

paragraph

11.

14.

Acronyms

and Initialisms

BWR

CCTV

CFR

EPT

FSAR

GL

HPES

Boiling Water

Reactor

Closed Circuit Television

Code of Federal

Regulations

Engineering

Performance

Test

Final Safety Analysis Report

Generic Letter

Human Performance

Evaluation

System

11

IFI

MST

NCR

NCV

NRC

OST

PIC

PWR

QA/QC

RCP

RCS/RC

RHR

RWP

RWST

SOOR

SRO

TS

URI

YIO

WR/JO

Inspector Follow-up Item

Maintenance

Surveillance Test

Non-Conformance

Report

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Surveillance Test

Primary Instrument Control

Pressurized

Water Reactor

Quality Assurance/Quality

Control

Radiochemistry

Procedure

Reactor

Coolant System

Residual

Heat

Removal

Radiation

Work Permit

Refueling Water Storage

Tank

Significant Operational

Occurrence

Report

Senior Reactor Operator

Technical Specification

Unresolved

Item

Violation

Work Request/Job

Order