ML18009A535
| ML18009A535 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 05/04/1990 |
| From: | Dance H, Shannon M, Tedrow J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18009A533 | List: |
| References | |
| 50-400-90-06, 50-400-90-6, NUDOCS 9005160059 | |
| Download: ML18009A535 (21) | |
See also: IR 05000400/1990006
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report No.:
50-400/90-06
Licensee:
Carolina
Power and Light Company
P. 0.
Box 1551
Raleigh,
NC 27602
Docket No.:
50-400
Facility Name:
Harris
1
Inspection
Conducted:
March
17 - April 20,
1990
Inspectors:
C IG&~2-
J.
Tedrow, Senior Residen
Inspector
8-c
M.
S annon,
esi ent
nspector
License
NoeI
g +9/
Da e Signed
a
e
igne
Approved by:
ance,
ection
se
Reactor Projects
Branch
1
Division of Reactor Projects
ate
>gne
SUMMARY
Scope:
This routine inspection
was conducted
by two resident
inspectors
in the areas
of plant
operations,
radiological
controls,
security,
fire protection,
surveillance
observation,
maintenance
observation,
licensee
event
reports,
review of non-conformance
reports,
followup of onsite events, verification of
diesel
fuel quality assurance,
and
licensee
action
on previous
inspection
items.
Numerous facility tours
were
conducted
and facility operations
observed.
Some of these
tours
and observations
were conducted
on backshifts.
Results:
Two violations were identified:
Failure to complete
post maintenance
testing
prior to returning
equipment
to service,
paragraphs
6.b
and 6.c;
Fail'ure to verify valve leakage following operation of an
RCS pressure
isolation
valve, paragraph
7.a.
A weakness
is identified in paragraph
6.b regarding operators'nowledge
of
priority/emergency
work requirements.
9005160059
900504
ADOCK 05000400
The
computerized ~ta
base
and
administrative
controls
established
for
~
~
scheduling
surveillance
testing
is
considered
to
be
a
program
strength,
paragraph
3.a.
Licensee identified violations are discussed
in paragraphs
6.a
and 6.d.
REPORT
DETAILS
1.
Persons
Contacted
Licensee
Employees
- R. Biggerstaff, Unit Manager Site Engineering
- J. Collins, Manager,
Operations
- G. Forehand,
Director,
QA/QC
C. Gibson, Director,
Programs
and Procedures
- P. Hadel,
Manager,
Maintenance
- C. Hinnant, Plant General
Manager
- D. McCarthy,
NED Site Principle Engineer
- S. McCoy, Procedure
Coordinator
C. Olexik, Manager, Shift Operations
- R. Richey,
Manager,
Harris Nuclear Project Department
J. Sipp, Manager,
Environmental
and Radiation Monitoring
H. Smith, Supervisor,
Radwaste
Operation
- D. Tibbits, Director, Regulatory Compliance
- M. Wallace, Senior Specialist,
Regulatory
Compliance
E. Willett, Manager,
Outages
and Modifications
- L. Woods,
Manager, Technical
Support
Other
licensee
employees
contacted
included
office,
operations,
engineering,
maintenance,
chemistry/radiation
and corporate
personnel.
- Attended exit interview
and initialisms
used
throughout this report
are listed in the
last paragraph.
2.
Review of Plant Operations
(71707)
The plant continued in power operation
(Mode 1) for the duration of this
inspection period.
Shift Logs and Facility Records
The inspector
reviewed
records
and discussed
various entries
with
operations
personnel
to verify compliance
with the
Technical
Specifications
(TS) and the licensee's
administrative procedures.
The following records
were reviewed:
Shift Foreman's
Log; Control
Operator's
Log; Auxiliary Operator's
Log;
Night
Order
Book;
Equipment
Record; Active Clearance
Log; Jumper
and Wire
Removal
Log;
Shift
Turnover
Checklist;
and
selected
Chemistry/Radiation
Protection
and
Radwaste
Logs.
In addition,
the
inspector
independently verified clearance
order tagouts.
No violations or deviations
were identified.
b.
Faci 1 it~ours
and Obser vati ons
Throughout
the inspection
period, facility tours
were conducted
to
observe
operations
and
maintenance
activities in progress.
Some
operations
and
maintenance
activity observations
were
conducted
during backshifts.
Also, during this inspection
period,
licensee
meetings
were
attended
by the inspectors
to observe
planning
and
management
activities.
The facility tours
and
observations
encompassed
the following areas:
security perimeter
fence; control
room;
emergency
diesel
generator
building;
reactor
auxiliary
building;
waste
processing
building;
fuel
handling
building;
emergency
service
water building; battery
rooms;
and electrical
switchgear
rooms.
During these tours,
the following observations
were made:
(I)
Monitoring Instrumentation
- Equipment operating
status,
area
atmospheric
and liquid radiation monitors, electrical
system
lineup,
reactor
operating
parameters,
and auxiliary equipment
operating
parameters
were
observed
to verify that indicated
parameters
were
in accordance
with the
TS for the current
operational
mode.
(2)
Shift Staffing - The inspectors
verified that operating shift
staffing
was
in
accordance
with
TS
requirements
and that
control
room operations
were being conducted
in an orderly and
professional
manner.
In addition,
the inspector
observed shift
turnovers
on various
occasions
to verify the continuity of
plant status,
operations
problems,
and other pertinent plant
information during these turnovers.
(3)
Plant
Housekeeping
Conditions
-
Storage
of material
and
components,
and
cleanliness
conditions
of various
areas
throughout
the facility were
observed
to determine
whether
. safety and/or fire hazards
existed.
(4)
Radiological
Protection
Program - Radiation protection control
activities
were
observed
routinely to verify that
these
activities
were in conformance
with the facility policies
and
procedures,
and
in compliance
with regulatory
requirements.
The inspectors
also
reviewed selected
RWPs to verify that the
RWP was current
and that the controls were adequate.
(5)
Security Control - In the course of the monthly activities, the
inspector
included
a review of the licensee's
physical security
program.
The
performance
of various shifts of the security
force
was
observed
in the
conduct
of daily activities to
include:
protected
and vital area
access
controls;
searching
of personnel,
packages,
and
vehicles;
badge
issuance
and
retrieval;
escorting
of visitors; patrols;
and
compensatory
posts.
In addition,
the inspectors
observed
the operational
stIKs of CCTV monitors,
the Intrusion Detection
system in the
central
and
secondary
alarm stations,
protected
area lighting,
protected
and vital
area barrier integrity,
and the security
organization interface with operations
and maintenance.
(6)
Fire Protection
- Fire protection activities,
staffing
and
equipment
were
observed
to verify that fire brigade staffing
was appropriate
and that fire alarms,
extinguishing
equipment,
actuating
controls,
fire
fighting
equipment,
emergency
equipment,
and fire barriers
were operable.
No violations or deviations
were identified.
3.
Surveillance
Observation
(61726)
Surveillance
tests
were observed
to verify that approved
procedures
were
being
used;
qualified personnel
were
conducting
the tests;
tests
were
adequate
to verify equipment
operability;
calibrated
equipment
was
utilized; and
TS requirements
were followed.
The following tests
were observed
and/or data reviewed:
OST-1026
OST-1038
OST-1044
OST-1506
Leakage
Sampling,
Chemical Addition, and Main Steam Drain Systems
ISI Valve Test
ESFAS Train "A" Slave Relay Test
Reactor Coolant System Isolation Valve Leak Test
The inspectors
reviewed
the licensee's
program established
for scheduling
surveillance
testing
(procedure
PLP-103,
Surveillance
and Periodic Test
Program)
and discussed
program
requirements
with licensee
personnel.
A
computer ized
system is
employed
to schedule
surveillance testing.
This
system
is utilized to
generate
a weekly test
summary
of scheduled
surveillance tests for the next four-week period which is distributed to
area
managers
each
week.
Also,
a Daily Batch Report is generated
which
identifies all
surveillance
tests
which
are
past
due,
overdue,
or
completed
with exceptions.
The
system
computes
the
due date for any
surveillance
test
based
on
the
previous
completion
date
or
date
scheduled,
whichever
is earlier,
followed
by
an
overdue
date
which
includes
any extensions
authorized
by the
TS.
Any tests
not completed
within three 'days
of the
overdue
date
receive
additional
management
attention in the morning management
meeting
and are published in a Daily
Immediate
Attention List.
The
computer
data
base
is maintained
by
compliance
personnel
to reflect
changes
in procedures,
TS,
and plant
modifications.
An audit of the data
base
is performed annually.
The
computerized
data
base
and
established
administrative
controls
are
considered
to be
a program strength.
The
computerized
system
discussed
above
only applies
to surveillance
tests
with a longer frequency
than three
days.
More frequent tests
and
event related
tests
are
scheduled
independently
by area
managers.
The
inspectors
rCVTewed the 'operations
department
method for scheduling daily
surveillances
and discussed
this method with operations
personnel.
Oaily
surveillances
are
scheduled
at
specific
times
during
the
day for
accomplishment.
A list of the required tests
is maintained
by the shift
foremen
and this list is annotated
for test completions.
Event related
tests
are
scheduled
within separate
procedures
response
procedures
or operating
procedures)
that pertain to'he specific event.
4.
Maintenance
Observation
(62703)
The inspectors
observed/reviewed
maintenance
activities to verify that
correct
equipment
clearances
were
in effect;
work requests
and fire
prevention
work permits,
as
required,
were
issued
and
being followed;
quality control
personnel
were available for inspection activities
as
required;
and,
TS requirements
were being followed.
Maintenance
was
observed
and
work
packages
were
reviewed
for the
following maintenance
(WR/JO) activities:
Replace
motor bearings
and realign the
"A" main feedwater
pump in
accordance
with procedure
CMM-0133, Main Feed
Pump Motor.
Replace
thermal
overload
devices for the
"B" emergency
screen
wash
pump.
Replace
reed switch indication for valve
in accordance
with
procedure
MPT-I0019, Target
Rock Valve Inspection
and Refurbishment.
Adjustment of packing for valve 1SI-l.
Repair rotating element for the "8" emergency
screen
wash
pump.
No violations or deviations
were identified.
5.
Review of Licensee
Event Reports
(92700)
The following LERs were reviewed for potential
generic
impact, to detect
trends,
and to determine
whether corrective actions
appeared
appropriate.
Events that were reported
immediately were reviewed
as they occurred
to
determine if the
TS were satisfied.
LERs were reviewed in accordance
with the current
a.
(Closed)
LER 90-02:
This
LER reported
that
the
gPTR
was
not
verified within limits while the monitoring alarm
was
This
event
was
previously
discussed
in
NRC
Inspection
Report
50-400/90-02
and
was
the subject
of
a violation (400/90-02-02).
Further action
on this matter will be tracked
by the violation.
b.
(Open)
LER 90-03:
This
LER reported
that
a train of essential
services
chilled water
was inoperable
due to air intrusion into the
co
system.
This
LER will remain
open
pending
completion of the
corrective
actions
as stated
in the
LER.
(Closed)
LER 90-04:
This
LER reported
a missed
leak rate evaluation
which
was
caused
by
a
procedure
deficiency.
This event
occurred
February
27,
1990,
when the plant computer,
which provides
an alarm
upon excessive
leakage,
failed.
Without the computer,
the licensee's
procedures
require hourly manual
logging of indicated
sump level
and
evaluation
of
level, leakrate.
Plant
operators
failed to
evaluate
the
leakage within the
one
hour time
span for two hourly
intervals.
On
March
28,
the plant
computer failed again
and plant operators
failed to comply with requirements
for evaluation of sump leakrate.
The
licensee's
corrective
action for these
two events
included
revising the applicable
response
procedure
APP-ALB-001,
Main Control
Board, to incorporate
the r'equirements
and appropriate
cautions
for performing
the
manual
logging of
leakage
and
training operations
personnel
on the procedure
change.
Although this
action
was in progress
after the first event occurred, it was not
completed in time to prevent the second
event
on March 28.
d.
(Open)
LER 90-05:
This
LER reported
an engineered
safety
system
actuation
due to
a radiation monitor spike
caused
by
a loose
pin
connection.
The
licensee
plans
to
revise
surveillance
test
procedure
Containment
Atmosphere
- Reactor
Coolant
Leak
Detection
Monitor Operational
Test,
to delete
requirements
for
disconnection
of the coaxial
cable
where
the
loose
connection
was
found.
This
LER will remain
open pending completion of this action.
e.
(Open)
LER 90-06:
This
LER reported
the operation of the plant in
an unanalyzed
condition with waste
gas
decay
tanks
cross
connected.
This
matter
was
previously
discussed
in
NRC
Inspection
Report
50-400/90-04
and
was
the subject of an IFI (90-04-04).
This
LER
will remain
open
pending
completion of the corrective actions
as
stated
in the
LER.
6.
Review of Nonconformance
Reports
(71707)
Significant
Operational
Occurrence
Reports
(SOORs)
and
Nonconformance
Reports
(NCRs)
were reviewed to verify the following:
TS were complied
with, corrective actions
as identified in the reports
were accomplished
or
being
pursued
for completion,
generic
items
were identified
and
reported,
and items were reported
as required
by the TS.
a.
SOOR
90-44
reported
that
a
120 volt
AC electrical
conductor
protective
device
was
inadequate.
As
discussed
in the
FSAR,
section
8.3. 1. 1.2. 15,
these circuits are
typically provided with two protective devices;
either
two circuit
breakers
in series,
or
a circuit breaker
in series
with
a fuse.
Lfcense~ngineering
personnel
discovered this discrepancy
during
a
comparison of surveillance test
procedures
with engineering calcula-
tions.
During the
comparison,
engineering
personnel
noticed that
penetration circuit PP-1B311
(SB)
had
a
30
amp breaker installed
as
the secondary
overcurrent protective device in series with a six amp
fuse installed
as the primary overcurrent protective device.
It was
determined
that the existing
30
amp breaker did not provide sufficient
protection
against
instantaneous
short circuit current to prevent
damage
to the penetration.
The configuration presented
in the
FSAR,
section 8.3. 1. 1.2.15
and figure 8.3. 1-10, includes
a bounding case of
a
15
amp breaker
in series
with
a
20
amp
fuse for
120 volt AC
electrical
The licensee's initial investigation into
this event determined that the
30
amp breaker
had
been installed in
the circuit during initial plant construction.
Upon notification of this condition,
operations
personnel
declared
the
electrical
and
implemented
the
requirements
of the
TS.
Plant modification
PCR-5157,
Secondary
Protection
to
ARP-19
Circuits,
was
implemented
to
install
20
amp
fuses
in series
with the six
amp fuses.
This
modification
was
completed
on
March
19
and
the
was
subsequently
declared
This matter is considered
to be
a
licensee
identified
and is not being cited
because
criteria
specified
in section
V.G. 1 of the
NRC
Enforcement
Policy were
satisfied.
(90-06-01):
Failure
to maintain
an
conductor protective
device.
SOOR
90-45 reported that the post maintenance
testing
performed
on
spent fuel pool containment isolation valve 1SP-916
was not adequate.
During the
performance
of
a surveillance test
on March
15,
1990,
valve
1SP-916 failed to provide full closed indication.
The valve
was
declared
and
priority/emergency
maintenance
was
authorized
by the shift foreman to repair the valve.
The licensee's
procedures
allow this type of maintenance
to be performed without the
usual
preplanning
and documentation,
provided that the documentation
is followed up and reviewed afterwards.
At 3:05 a.m.,
on March
16,
the valve limit switch was replaced
to
correct the valve indication problem.
A cycling test
and verification
of isolation time was
performed
as post maintenance
testing
and the
valve was declared
Later on March 16, the work request
was
generated
and
reviewed
to determine
appropriate
post
maintenance
testing.
This
review determined
that
performance
of
a
Type
C
containment
leak rate test
was also required prior to considering
the
valve operable.
Subsequent
reviews of the generated
work request for
completion signatures
by maintenance
and operations
personnel
failed
to detect
the required additional
post maintenance
test.
On March
22, licensee
i nservice testing
personnel
reviewed the completed work
request
and noticed that all post maintenance
testing
had not been
performed.
The lienee's
administrative
controls
established
for inoperable
equipment
(procedure
OMM-3, Equipment
Record)
specifies
that prior to declaring
equipment
the required
post maintenance
testing
must
be completed.
Failure to complete the
Type
C containment
leakrate test prior to declaring
valve
is contrary to the requirements'f
procedure
OMM-3 and is
considered
to be
a violation.
Violation (400/90-06-02):
Failure
to
complete
post
maintenance
testing prior to returning inoperable
equipment to service.
The licensee
has
recently
experienced
problems with performance
of
priority/emergency
work.
In
NRC Inspection
Report 50-400/89-34
the
licensee
was
issued
a violation for failing to generate
a work
request
(89-34-02,
example 2).
The licensee attributed the cause for
this nonconformance
to be due to a lack of familiarity on the part of
plant operators
with priority/emergency
work requirements.
Apparently
the licensee's
corrective action for that violation was not completely
effective
and this area is still considered
weak.
SOOR
90-57
reported
that following work
on valve
injection
tank inlet isolation valve,
required
post
maintenance
testing
was not performed.
On March 22,
1990,
packing
was adjusted
on
valve
to
stop
leakage.
The
work request
for this
maintenance
stipulated
that
a
stroke
timing test
be
performed
following maintenance.
However,
the valve
was
declared
without completing the required
post maintenance
testing.
Following
additional
reviews of the completed
work request,
licensee
personnel
identified the missed testing
on April 9,
and the appropriate test
was
subsequently
performed.
This matter is considered
to be another
example of the violation discussed
in paragraph
6.b of this report.
SOOR 90-54 reported that
an individual's
exposure
was not reported
as
required.
On
Oecember
15,
1989, following the termination of
employment
of
a contracted
security officer,
no report of this
individual's exposure
was
made to the
NRC or to the individual within
30 days
as required
by
and
Licensee
personnel
discovered this during routine issuance
of the individual's
dosimetry
on April 3,
1990.
The licensee's
corrective action will
consist of revising administrative controls for terminating contract
employees
to include
contracted
security
personnel.
This is
a
licensee
identified
and is not being cited
because
criteria
specified
in section
V.G. 1 of the
NRC
Enforcement
Policy were
satisfied.
(90-06-03):
Failure
to report
an individual's radiation
exposure
upon termination.
7.
Follow=up of~site
Events
(93702)
a ~
b.
On April 5,
1990,
the licensee
indicated that valve 1SI-359,
hot leg recirculation valve to the
RCS,
was operated
on February
13,
1990 without the subsequent
performance of a leakage verification as
required
by
TS 4.4.6.2.2.d for isolation valves
associated
with the
RCS.
The licensee
declared
the untested
valve inoperable at 1:00 p.m.
and
complied with the action requirements
of
TS 3.4.6.2.c.
Valve
leakage
was
subsequently
verified within limits by 4:30
p.m.
on
April 5.
This matter
was identified by the licensee
during
a review of the
IST program.
The inspectors
discussed
this matter with licensee
personnel
and discovered that the valve was routinely operated
once
a
quarter in accordance
with the licensee's
IST program,
since
March
1987, yet
no
leakage
verifications
were
performed following these
valve operations.
The inspectors
counted
approximately
13 valve
operations after which no leakage verification had
been performed.
Although this matter
was identified
by the licensee, it is being
cited
due
to the failure of licensee
personnel
to identify the
problem for approximately
three years
even
though there
was
ample
opportunity to do so.
Violation (90-06-04):
Failure to verify valve
leakage
following
operation of valve 1SI-359.
During the performance of procedure
OST-1124
on April 15,
1990,
the
supply
breaker
to the 6.9
KV emergency
bus
inadvertantly
opened
deenergizing
the
bus.
This condition resulted
in the automatic
actuation
of the
emergency
diesel
generator
on
a
bus
condition.
The emergency
diesel
generator
operated
as
designed
and
reenergized
the bus loads.
Upon loss of bus
power,
containment isolation valves associated
with
radiation monitor
REM-3502 A, Containment
Leak Detector, lost power
and closed.
This action resulted in a loss of process
flow into the
monitor
and
caused
the monitor to alarm
which resulted
in the
automatic isolation of the containment
purge system.
Similar events
were reported
by the licensee
in LERs 88-13 and 88-35
and are discussed
in
NRC Inspection Report 50-400/88-40.
The licensee
is presently investigating
why this event reoccurred.
IFI (90-06-05):
Review the licensee's
investigation into the cause
for repeated
loss of power to the "A" emergency
bus while performing
undervoltage testing.
,
Verification~ Quality .Assurance
Regarding
Diesel
Fuel
(71707)
(Closed)
TI 2515/93:
The inspector verified that the licensee
included
the
emergency
DG fuel oil in its Quality Assurance
Program.
A review of
the
licensee's
fuel oil purchasing
specification
sheet
and
fuel oil
analysis
sheet,
was performed.
The results of this inspection acceptable
and this item is considered
closed.
9.
Licensee
Action
on Previously Identified Inspection
Findings
(92702
&
92701)
(Closed) Violation 89-34-01,
Failure to perform surveillance testing
for an inoperable
emergency
diesel
generator.
The inspector
reviewed
and verified implementation of the corrective
actions
as stated in the licensee's
response letter dated
February
26,
1990.
b.
c ~
(Open) Violation 89-34-02,
Failure to adhere
to the requirements
of
plant procedures.
The inspector
reviewed
and verified implementation of the corrective
actions
as
stated
in the licensee's
response
letter
dated
March 2,
1990.
Action remaining to
be accomplished
on this matter includes
the revision of procedure
OST-1804,
RHR Remote Position Indication
and
Timing,
and other
procedures
to include appropriate
cautions
when
RWST suction
valves
are
cycled.
This action is
due to
be
completed
December
31,
1990.
(Closed)
Violation 88-33-01,
Failure
to follow approved fire,
protection procedures.
The inspector
reviewed
and verified implementation of the corrective
actions
as stated in the licensee's
response letter dated
November 29,
1988.
d.
e.
(Closed)
IFI 88-33-02,
Concern
with licensee
using
compensatory
measures
to meet the fire protection program.
The licensee
has
reduced
the
number of circumstances
requiring the
use of compensating
fire watches
by
a factor of approximatesly
two-thirds.
A 100 percent
inspection of fire bar rier penetrations
was also completed
and discrepancies
corrected.
(Closed)
IFI 90-04-04,
Review the licensee's
corrective action to
prevent cross connection of waste
gas
decay tanks.
The licensee
has
issued
LER 90-06
on this event documenting corrective
actions
taken to prevent
recurrence.
For record
purposes,
the IFI
will be closed
and future action tracked
by the LER.
10
Exit Intervi@F (30703)
The inspectors
met with licensee
representatives
(denoted in paragraph
1)
at the conclusion of the inspection
on April 20,
1990.
During this
meeting,
the
inspectors
summarized
the
scope
and
findings of the
inspection
as they are detailed in this report, with particular emphasis
on the Violations
and
Inspector
Follow-up item addressed
below.
The
licensee
representatives
acknowledged
the inspector's
comments
and did
not identify as proprietary
any of the materials
provided to or reviewed
by the inspectors
during this inspection.
Item Number
Descri tion and Reference
90-06-01
90-06-02
90-06-03
90-06-04
90-06-05
NCV:
Failure to maintain
an
conductor protective device,
paragraph
6.a.
VIO:
Failure to complete
post
maintenance
testing
prior to returning
equipment
to service,
paragraphs
6.b and 6.c.
NCV:
Failure to report
an individual's radiation
exposure
upon termination,
paragraph
6.d.
VIO:
Failure
to verify valve
leakage
following
operation of valve 1SI-359,
paragraph
7.a.
IFI:
Review the licensee's
investigation
into the
cause for repeated
loss of power to the "A" emergency
bus while performing undervoltage
testing,
paragraph
7.b.
and Initialisms
ALB
APP
CFR
CMM
IFI
KV
LER
MPT
Alternating Current
Alarm Response
Procedure
Annunciator Panel
Procedure
Auxiliary Relay Panel
Closed Circuit Television
Code of Federal
Regulations
Corrective Maintenance
Manual
Engineered
Safety Feature
Accuation System
Final Safety Analysis Report
Inspector Follow-up Item
Inservice Inspection
Inservice Testing
Kilovolt
Licensee
Event Report
Maintenance
Performance
Test
Maintenance
Surveillance Test
Nonconformance
Report
Non-cited Violation
11
NED
NRC
OMM
OST
PLP
SOOR
TI
TS
WR/JO
Nuclear Engineering
Department
Nuclear Regulatory
Commission
Operations
Maintenance
Manual
Operations
Surveillance Test
Plant
Change
Request
Plant Program
Quality Assurance
Quality Control
Quadrant
Power Tilt Ratio
Residual
Heat Removal
Radiation
Work Permit
Refueling Water Storage
Tank
Significant Operational
Occurrence
Report
Temporary Instruction
Technical Specification
Violation
Work Request/Job
Order
r