ML18009A401

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Insp Rept 50-400/90-02 on 900216.Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls,Fire Protection,Security,Surveillance Observation,Lers,Review of NRC Bulletin,Maint Observation & Cold Weather Preparations
ML18009A401
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 02/27/1990
From: Dance H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A397 List:
References
50-400-90-02, 50-400-90-2, NUDOCS 9003210065
Download: ML18009A401 (25)


See also: IR 05000400/1990002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/90-02

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conduc

d

Inspectors:

J.

Te row, Senior Resident

Inspector

C

a non.

si ent

nspector

~

~

Approved by:

a ce,

ection

)e

Division of Reactor

Projects

License No.:

NPF-63

27

Q

Da e

igne

~/~v

ate

)gne

/

a e

gned

SUMMARY

Scope:

This routine inspection

was conducted

by two resident inspectors

in the areas

. of plant operations,

radiological controls, security, fire protection,

surveillance observation,

maintenance

observation,

licensee

event reports,

review of an

NRC Bulletin, cold weather preparations,

and licensee action

on

previous inspection

items.

Numerous facility tours were conducted

and facility

operations

observed.

Some of these tours

and observations

were conducted

on

backshifts.

Results:

Two violations were identified:

Failure to properly implement procedure

OST-1039 resulting in inadequate

gPTR data calculation,

paragraph 2.b.(1);

Failure to calculate

the

gPTR as required

by TS 4.2.4.1,

paragraph 2.b.(l).

A weakness

is identified in paragraph 2.b.(1) concerning

the technical

support

staff's failure to properly implement plant procedures.

90032l0065

900227

PDR

ADOCK 05000400

Q

PDC

Licensee strengths

were identified relating to the administrative controls

established

for equipment clearances,

paragraph

2.a,

and plant housekeeping,

paragraph 2.b.(3).

Licensee identified violations are discussed

in paragraphs

5.f, 5.h, 5.m,

and 5.q.

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

D. Braund, Supervisor,

Security

J. Collins, Manager, Operations

  • G. Forehand,

Director,

QA/QC

  • C. Gibson, Director, Programs

and Procedures

  • P. Hadel. Manager.

Maintenance

  • C. Hinnant, Plant General

Manager

C. Olexik, Supervisor, Shift Operations

  • R. Richey. Manager, Harris Nuclear Project Department
  • J. Sipp, Manager,

Environmental

and Radiation Monitoring

  • H. Smith, Supervisor,

Radwaste

Operation

  • D. Tibbits, Director, Regulatory Compliance
  • B. Van Metre, Manager,

Technical

Support

E. Willett, Manager

Outages

and Modifications

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

The plant resumed

100 percent

power operation after an inoperable

main

steam safety valve was returned to service

on January

6 and continued in

power operation

(Mode 1) for the duration of this inspection period.

Shift Logs and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS) and the licensee

s administrative procedures.

The following records

were reviewed:

Shift Foreman's

Log; Control

Operator's

Log; Auxiliary Operator's

Log; Night Order

Book; Equipment

Inoperable

Record; Active Clearance

Log; Jumper

and Wire Removal

Log;

Shift Turnover Checklist;

and selected

Chemistry/Radiation

Protection

and

Radwaste

Logs.

In addition, the inspector independently verified

clearance

order tagouts.

The inspector

reviewed procedures

AP-20, Clearance

Procedure,

and

OMM-14, Operations - Operation of the Clearance

Center, to determine

the licensee's

administrative controls regarding

equipment

clearances.

Clearances

are'prepared

by a licensed operator

and

receive

an independent verification by another licensed operator for

accuracy.

The licensee utilizes

a shift foreman designee

(licensed

senior reactor operator)

to approve -the prepared

equipment clearance

to remove the administrative

burden

on the shift foreman.

The

licensee

also utilizes

a specification appraisal

computer to generate

the required.clearances.

After approval, clearance

tags are

hung on

required

components

by trained operating

personnel

(usually auxiliary

operators).

Components

important to the safe operation of the plant

receive

an additional verification that the tags are properly hung.

These

systems

are specified in procedure

PLP-702,

Independent

Verification.

After these verifications are made,

a work group

representative

physically verifies system status

and proper

positioning of tagged

components.

Restoration

positions of tagged

components

also receive

independent

verification by licensed operators.

When work on the affected

system

is complete,

the-tags

are

removed

and the component is repositioned.

Position is independently verified if applicable.

The licensee

performs

a weekly administrative audit of the clearance

forms with the clearance

index.

A more detailed monthly audit

includes physical verification that tags are in place,

undamaged,

and components

are in the required position.

The inspector considers

the licensee's

administrative controls for equipment clearances

to be

good

and should prevent personnel

injury or equipment

damage

from

occurring

due to improper system alignment.

No violations or deviations

were identified.

Facility Tours and Observations

Throughout the inspection period. facility tours were conducted

to

observe operations

and maintenance activities in progress.

Some

operations

and maintenance activity observations

were conducted

during backshifts.

Also, during this inspection period, licensee

meetings

were attended

by .the inspectors

to observe

planning and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control room; emergency diesel

generator

building; reactor auxiliary building; waste processing

building;

fuel handling building; emergency

service

water building; battery

rooms;

and electrical

switchgear

rooms.

During these tours, the following observations

were made:

(I)

Monitoring Instrumentation - Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup, reactor operating

parameters,

and auxiliary equipment

operating

parameters

were observed

to verify that indicated

S

parameters

were in accordance

with the

TS for the current

operational

mode.

As discussed

in

NRC Inspection

Report 89-34 on December 30,

1989 the resident inspector

noted that the nuclear instrument

(NI)-44 upper

and lower comparator

channels

were placed in

bypass.

The comparator

channels

are

used to calculate

the

Quadrant

Power Tilt Ratio

(QPTR) and provide input to the

QPTR

alarm.

The inspector

was informed that during the reactor

power

increase

to 55 percent

on December 28, 1989, that the upper

and

lower QPTR channels

went into alarm.

OST-1039, Calculation of

Quadrant

Power Tilt Ratio,

was performed

on December

28, 1989,

and it indicated that the channels

were close to the alarm

setpoint.

The upper

and lower NI-44 detectors

were subsequently

placed in bypass

by operations

personnel.

Discussions

with the

operators

revealed that the NI-44 instruments

had not been

declared

inoperable,

no additional surveillance

requirements

were being performed,

and that the operator

logs did not

document

"when" and "why" the detectors

were placed in bypass.

The inspector

conducted

a review of recently completed

surveillances for calculating the Quadrant

Power Tilt (OST-1039)

including the

OST performed

on December

28,

1989.

The review

concluded that the detector current data recorded for OST-1039,

on December

28,

1989, per step 7.1,

was recorded in error by the

licensed operator.

Further discussions

with licensee

personnel

confirmed that the operator

had used the wrong scale

on the

meter to obtain the data.

With the plant operating at only

55 percent

power, the recorded current values

exceeded

the

100 percent

power normalized currents.

The normalized fractions

and average

normalized fractions should

have calculated out to

be approximately

55 percent.

A subsequent

review by two senior

licensed shift foremen failed to identify the inaccurate

data

obtained

from the control

room instrumentation.

It was also

noted that the operator

who recorded

the data

had recently

returned to shift work following assignment

to the procedure

writing group and may have been, somewhat unfamiliar in performing

this procedure.

The detector currents,

required

by step 7.1 of OST-1039,

were

improperly recorded

and

a subsequent

review by two senior

licensed shift foremen failed to identify the improperly

performed

TS surveillance.

Failure to properly perform

surveillance testing is contrary to TS 6.8.1.a

and is considered

to be

a violation.

Violation (90-02-01):

Failure to properly implement procedure

OST-1039 resulting in inadequate

QPTR data calculation.

Further review of OST-1039

by the inspector determined that the

100 percent

power normalized currents

recorded

on the

December

28,

1989 surveillance test were not the

same

as those recorded

on

subsequent

surveillances

completed during January

1990.

They

also did not correlate to current values

found at the end of

cycle two.

The procedure

used to obtain the normalized currents,

EST 717, Incore/Excore Detector Calibration, required that

reactor

power be at 75 percent to perform the calibration.

Discussions

with technical

support personnel

discovered that the

100 percent

power normalized currents

were calculated

based

on

a

35 percent flux map without utilizing procedure

EST-717.

The

inspector

concluded that plant procedures

were not utilized to

obtain the normalized current values;

Discussions

with the

discipline supervisor

indicated that

he was

unaware that

unauthorized

means

were used to obtain the normalized current

values.

The licensee

was recently issued

a violation (90-01-01)

involving the miscalibration of power range nuclear instruments

in NRC Inspection

Report 50-400/90-01.

One of the causes

for

that violation involved the failure of technical

support

personnel

to properly implement

a plant procedure.

The

inability of the technical

support staff to properly implement

plant procedures

is considered

to be

a weakness.

This problem

is not being cited in this report due to the recent

issuance of

violation 90-01-01

and insufficient time for the licensee

to

respond.

Following the receipt of the upper and lower gPTR alarms,

the

manual calculation of the

gPTR was performed.

Based

on the

manual

gPTR, operations

personnel

bypassed

the upper and lower

NI-44 channel

inputs to the

gPTR alarm circuitry.

Selective

removal of detector inputs in the

gPTR alarm circuit will

inhibit an active alarm,

and therefore sufficient justification

should

be made prior to removing any channel

from operation.

The alarm response

procedure

ALB-013-5-3 and ALB-013-5-4 both

detail bypassing

a faulty channel

and require the subsequent

removal of the channel

from service

by tripping various

bistables.

Only the bypassing

step

was completed

and no other

actions

were taken

by licensee

personnel.

By bypassing

an active detector

channel

the

gPTR comparator

circuitry was not capable of performing its intended function

which resulted in an inoperable

gPTR alarm.

With an inoperable

gPTR alarm,

TS surveillance 4.2.4.1.b requires

a manual

calculation of the

gPTR every

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above,

from 6:55 a.m.

on December 28,

1989 until approximately

2:25 a.m.

on December

30,

1989, the licensee failed to perform

the required

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> TS surveillance,

which is considered

to be

a violation.

P

(2)

Violation (90-02-02)

Failure'o calcula'te

the

gPTR as required

by TS 4.2.4.1.

Shift Staffing - The inspectors verified that operating shift

staffing was in accordance

with TS requirements

and that

control

room operations

were being conducted in an orderly and

professional. manner.

In addition, the inspector

observed shift

turnovers

on various occasions

to verify the continuity of

plant status,

operations

problems,

and other pertinent plant

information during these turnovers.

(3)

Plant Housekeeping

Conditions - Storage of material

and components

,and cleanliness

conditions of various areas

throughout the

facility were observed

to determine whether safety and/or fire

hazards

existed.

(4)

The inspector

accompanied

licensee

management

personnel

on an

inspection of the'emergency

service water building.

This team

of approximately

10 managers

was led by the plant general

manager

and focused

on the general

cleanliness

and the material

condition of equipment.

This type of management

involvement

has

had

a positive effect on plant housekeeping

and the general

good material condition of equipment.

Radiological Protection

Program - Radiation protection control

activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The inspectors

also reviewed selected

RWPs to verify that the

RWP was current

and that the controls were adequate.

Security Control .- In the course of the monthly activities, the

inspector included

a review of the licensee's

physical security

program.

The performance of various shifts of the security

force was observed

in the conduct of daily activities to

include:

protected

and vital area

access

controls; searching

of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of Closed Circuit Television

(CCTV) monitors, the

Intrusion Detection

system in the central

and secondary

alarm

stations,

protected

area lighting, protected

and vital area

barrier integrity, and the security organization interface with

operations

and maintenance.

Fire Protection - Fire protection activities, staffing and

equipment

were observed

to verify that fire brigade staffing

was appropriate

and that fire alarms, extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

3.

Surveillance Observation

(61726)

'urveillance

tests

were observed

to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following

EST-219

OST-1021

MST-E0010

OST-1090

OST-1013

EST-717

OST-1039

tests

were observed

and/or data reviewed:

t

Personnel

Air Lock Door Seals

Local Leak Rate Test

Daily Surveillance

Requirements

lE Battery Weekly Test

Spent

Fuel

Pool Cooling System quarterly Interval

1A-SA Emergency Diesel

Generator Operability Test

Incore/Excore

Detector Calibration

Calculation of quadrant

Power Tilt Ratio

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were in effect; work requests

and fire

prevention work permits,

as required,

were issued

and being followed;

quality control personnel

were available for inspection activities

as

required;

and,

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the

following maintenance

(WR/JO) activities:

Replace

exhaust

gasket

on the "B" Emergency Diesel

Generator

(EDG) in

accordance

with procedure

CM-M0150, Emergency Diesel

Generator

Cylinder Head Removal,

Disassembly

and Reassembly.

Verification of diesel fire pump battery operability in accordance

with procedure

MPT-E0019. Diesel Fire

Pump Battery Weekly Test.

Replace turbine driven auxiliary feedwater

pump exhaust rupture

disk.

Clean, inspect

and calibrate actuator for valve AF-19 in accordance

with procedure

PIC-1058, Calibration Check and Stroking of a

Milliampere Hydramotor Actuator.

Lubricate coupling on the "A" EDG auxiliary lube oil pump in

accordance

with procedure

PM-M0011, Annual Lubrication Schedule.

Repair fuel oil leak on ¹5 cylinder for "A" EDG.

4

-" 'Repair oil leak on 86 'cylinder fbr '"A"'DG'in'accordance with

procedure

CM-M0150, Emergency Diesel

Generator Cylinder Head

Removal,

Disassembly

and Reassembly.

Replace

hold-down bolts for the "A" EDG turbo-chargers

in accordance

with procedure

MPT-.M0024, Emergency Diesel Generator Turbocharger

Bracket Bolting Inspection.

Brown Boveri LK1600 Breaker Failure Testing.

No violations or deviations

were identified.

5.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential generic impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with the current

NRC Enforcement Policy.

a ~

(Closed)

LER 88-06:

This

LER reported

inoperable

emergency

service

water

systems

due to isolation valve failure.

This event

was

previously discussed

in

NRC Inspection

Report 50-400/88-03

and was

the subject of an unresolved

item (88-03-01).

The licensee

issued

a

supplemental

report dated April 15,

1988.

The inspector

reviewed

and verified implementation of the licensee's

corrective action

as

stated

in the

LER.

b.

(Closed)

LER 88-21:

This

LER reported the automatic start of an

auxiliary feedwater

pump during

a surveillance test.

This matter

was also the subject of a violation (88-25-01) discussed

in NRC

'Inspection

Report 50-400/89-25.

For record purposes

the

LER will be

closed

and corrective action tracked

by the violation.

co

(Closed)

LER 88-23:

This

LER reported that the reactor coolant

system

was not adequately

vented during

a plant outage in August,

1988.

This event was previously discussed

in NRC Inspection Report

50-400/88-25

and the licensee

has

issued

a supplemental

report dated

September

13, 1988.

The inspector reviewed and verified

implementation of the licensee'0

corrective action as stated in the

LER.

d.

(Closed)

LER 89-06:

This

LER reported

a reactor trip which occurred

on March 14,

1989 due to the loss of a main feedwater

pump.

This

event is discussed

in more detail in

NRC Inspection Report

50-400/89-06.

Corrective actions for this event

have

been

completed.

e.

(Closed)

LER 89-07:

This

LER reported

an inadvertent isolation of

the containment ventilation system

due to personnel, error.

The

e

inspector

reviewed

and verified implementation of the licensee's

corrective- action

as stated

in the

LER.

f.'Closed)

LER 89-08:

This

LER reported that testing of the thermal

overload

bypass circuit for motor operated

valve MS-72 was

inadequate.

The licensee identified this problem during an

independent

review of thermal overload

bypass testing procedures.

The inspector

reviewed

and verified implementation of the licensee's

corrective action

as stated

in the LER.

This matter is considered

to be

a licensee identified Non-Cited Violation (NCV) and is not

being cited because criteria specified in section

V.G.1 of the

NRC

Enforcement Policy were satisfied.

NCV (90-02-03):

Failure to properly test thermal overload

bypass

circuitry for valve MS-72.

g.

h.

(Closed)

LER 89-13:

This

LER reported the inadvertent actuation of

a service water booster

pump during load sequencer

troubleshooting.

The inspector

reviewed

and verified implementation of the licensee's

corrective action

as stated in the

LER.

(Closed)

LER 89-14:

This

LER reported the emergency

core cooling

system piping was not being vented periodically as required

by the

TS.

The licensee

discovered this problem during a walkdown on this

system

and associated

procedures.

The inspector

reviewed

and

verified implementation of the licensee's

corrective action

as

stated

in the

LER.

This matter is considered

to be

a licensee

identified

NCV and is not being cited because criteria specified in

section

V.G.1 of the

NRC Enforcement Policy were satisfied.

NCV (90-02-04):

Failure to periodically vent emergency

core cooling

system piping.

(Closed)

LER 89-15:

This

LER reported that the fuel handling

building equipment

hatch

was not installed during fuel movement.

This matter was previously discussed

in NRC Inspection Report

50-400/89-21

and was considered

to be

a licensee identified

violation.

The inspector

reviewed

and verified implementation of

the licensee's

corrective action

as stated in the LER.

J

~

k.

(Closed)

LER 89-16:

This

LER reported the inadvertent start of the

"B" Emergency Service

Water

Pump during testing

on the load

sequencer.

The inspector

reviewed

and verified implementation of

the licensee's

corrective action as stated in the LER.

(Closed)

LER 89-18:

This

LER reported

a manual reactor trip due to

the cable failure on

a digital rod position indicator.

The

inspector

reviewed

and verified implementation of the licensee's

corrective'ction

as stated

in the

LER.

l.

(Closed)

LER 89-19:

This

LER reported

on auxiliary feedwater

system

actuation

caused

by a miscalibrated

main feedwater

pump switch.

The

inspector

reviewed

and verified implementation of the licensee's

corrective action

as stated in the

LER.

m.

(Open)

LER 89-20:

This

LER reported that several

motor operated

valve gear

boxes

had been overfilled with grease

which damaged

= wiring and affected the operator's

environmental qualification.

The

licensee

has repaired the

damaged wiring for the identified valves

and

has

completed

an inspection of the remaining motor operators

inside the containment building and the steam tunnel.

The licensee

is planning to revise applicable maintenance

procedures

to provide

better guidance

on maintaining proper grease

levels in the limit

switch gear

boxes

and to train maintenance

personnel

on this

problem.

This matter is considered

to be

a licensee identified

NCV

and is not being cited because criteria specified in section

V.G.1

of the

NRC Enforcement Policy were satisfied.

NCV (90-02-05):

Failure to maintain proper grease

levels in motor

operated

valve gear boxes.

n.'Open)

LER 89-21:

This

LER reported

an auxiliary feedwater

system

actuation

caused

by personnel

error in controlling feedwater flow.

This matter

was also discussed

in NRC Inspection

Report

50-400/89-34.

The licensee

has not yet completed all of the

corrective actions stated

in the LER.

The following items remain to

be accomplished:

Repair valve SP-226.

Revise

procedure

GP-005,

Power Operation

Mode

2 to Mode l.

to prohibit the simultaneous

transfer of all three

steam

generators

from bypass

flow feedwater control to main feed

regulating valve control.

Evaluation of the time delay relays for main feedwater

pump low

flow trip and response

time of the recirculation flow control

valve.

Training to applicable

personnel

on this event.

The

LER will remain open pending completion of this corrective

action.

o.

(Open)

LER 89-22:

This

LER reported the spurious

loss of a residual

heat

removal train during testing of interlocks.

The following

corrective action remains to be accomplished:

Revise test procedure

to ensure that the operating loop's

suction valve power supply breakers

are

open during installation

and removal of test equipment.

10

Pursue

TS changes

to eliminate the requirement for an

auto-closure

interlock.

This

LER will remain

open pending completion of this corrective

action.

p.

(Closed)

LER 89-23:

This

LER reported that power range nuclear

instrumentation

indicated non-conservatively

during a plant startup

in December,

1989.

This matter is also the subject of a violation

(90-01-01) in

NRC Inspection

Report 50-400/90-01.

For record

purposes,

the

LER will be closed

and further action tracked

by the

violation.

q.

(Open)

LER 90-01:

This

LER reported

a

TS violation regarding

response

time testing of Engineered

Safety Feature

(ESF) channels

in

a periodic rotation.

On January

5, 1990, during

a review by licensee

personnel

of procedure

NST-10645,

Group

2 of 2 Channel

RTS and

ESFAS

Response

Time Test, the licensee

discovered that testing performed

during the previous

1988 refueling outage failed to adequately

response

time test

ESF Channel III.

The other three

ESF channels

had

been tested satisfactory.

The licensee

determined that the cause for

this event

was

an inadequate

change to the surveillance

procedure,

which has subsequently

been revised.

Training will be provided for

personnel

responsible for writing and approving procedure

changes

and

Channel III will be tested

no later than February 1, 1992.

This

matter is considered

to be

a licensee identified

NCV and is not being

cited because criteria specified in section

V.G.1 of the

NRC

Enforcement Policy were satisfied.

NCV (90-02-06):

Failure to response

time test

ESF Channel III at

the correct periodicity.

This

LER will remain

open pending completion of required training

and testing of the

ESF channel.

6.

Review of NRC Bulletins (92703)

(Open)

NRC Bulletin 88-11,

Pressurizer

surge line thermal stratification.

This bulletin alerted licensees

to the potential for thermal stratification

to exist in pressurizer

surge lines during plant heatup

and cooldown

operations,

which could result in unexpected

piping movements

and

potential

high piping stress.

The licensee

has submitted correspondence

to the

NRC dated

December

29.

1989, addressing

the actions required

by the

bulletin.

A visual inspection of the pressurizer

surge line has

been

completed with no structural

damage identified.

The Westinghouse

Owners

Group performed

a bounding evaluation of this phenomenon for several

Westinghouse

plants.

However, since this evaluation is not plant specific,

and

does not encompass

the full design lifetime of the surge line,

a

justification for continued operation of the plant was submitted.

This

justification concluded that continued plant operation

was acceptable

Cl

11

based

on the results of similar plants

analyzed

thus far, consideration of

leak-before-break

concepts,

and results of non-destructive

examinations of

other pl ant pressurizer

surge lines.

Additional

moni toring and analysi s

are presently in progress.

The licensee

plans to obtain plant specific

surge line data

and update

the stress/fatigue

analysis to ensure

compliance with code requirements.

This action is expected

to be

completed

by December

29,

1990.

The bulletin will remain

open pending

completion of this additional action.

7.

Cold Weather Preparations

(71714)

The inspector

reviewed the licensee's

preparations

and administrative

controls established

to protect plant equipment during cold weather.

The

licensee

implements

procedure

AP-301, Adverse Weather

Operations,

section

5. 1, Cold Weather Operation,

whenever

ambient air temperature

reaches

35 degrees

F.

This procedure

requires that freeze protection

devices for plant equipment

be verified operable to prevent

systems

and

equipment

from freezing.

The licensee utilizes portable

space

heaters for

critical instrumentation

cabinets without installed

space

heaters.

The

inspectors

walked through the procedure with licensee

personnel

and

observed

implementation of the procedure

during cold weather conditions.

t

No violations or deviations

were identified.

8..

Licensee Action on Previously Identified Inspection

Findings

(92702

5

92701)

a.

(Closed) Violation 88-25-01

Failure to establish

and implement

procedures.

The inspector

reviewed and verified implementation of

the corrective actions

as stated in the licensee's

response letter

dated October 26,

1988.

b.

(Closed)

Violation 89-15-01

Improper flow orifice installation.

The inspector

reviewed

and verified implementation of the corrective

actions

as stated

in the licensee's

response letter dated

September

12,

1989.

c.

(Closed)

IFI 89-03-02,

Followup on diesel

generator injection

valve holder, inspections.

The spare

and installed delivery valve

holders

were inspected

and all discrepancies

have

been resolved.

d.

e.

(Closed)

IFI 89-03-01,

Implementation of PCR 3241 to resolve

low

temperature

overpressure

concerns.

Plant change

request

PCR 3241 was

completed

and turned over to operations

on November 28,

1989.

(Closed)

IFI 89-08-02

Throttle valve position verification.

Procedure

changes

were made to the following procedures;

OST-1216,

Component Cooling Water System quarterly Operability (1A-SA and

1B-SB pumps),

OST-1316,

Component Cooling Water System quarterly

'

l '

12

'Operability

(Pump 1C-SAB), and OST-1016,

Component Cooling Mater

.

System Monthly Operability, which now include specific component

cooling water to residual

heat removal

heat exchanger

valve positions

and signoff verifications.

f.

(Closed)

Violation 89-15-02. Failure to maintain

an active senior

reactor operator license.

The inspector

rev'iewed

and verified

implementation of the corrective actions

as stated in the licensee's

response letter dated

September

20,

1989.

g.

(Closed)

IFI 88-39-01

Review findings and corrective actions for

October 30,

1988 reactor trip.

The corrective actions,

developed

from the licensee'0

task force, were implemented within the time

specified.

Items included in the corrective action program were:

maintain current system descriptions,

provide operator retraining,

provide operator aids, modify booster

pump trip settings,

and

starting of auxiliary feedwater

pumps

on

a loss of one main feedwater

pump.

h.

(Open) Violation 89-28-02:

Failure to have

an adequate

procedure

for the performance of local leak rate testing which resulted in

instrument air contamination.

The licensee

has flushed

and

decontaminated

the instrument air system.

However,

due to the

possibility of hot particles still remaining inside the system,

use

of this system

was formally prohibited for breathing air purposes

by

procedure

AP-512,

Use of Respiratory

Equipment.

The licensee

has

further revised procedure

EST-212,

Type

C Local Leak Rate Tests,

to

require that any deviation from normal

system venting and draining

practices

be covered

by a temporary

change to the procedure.

The

licensee is evaluating

over time work of personnel

involved in testing

of safety related

equipment to develop appropriate guidelines

and is

developing

a plant general

order to specify controls

and exclusions

for use of the instrument air system.

This item will remain open

pending completion of the overtime guidance

and issuance

of the

plant general

order.

9.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1)

at the conclusion of the inspection

on February

16, 1990.

During this

meeting, the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the violations addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during

this inspection.

Item Number

Descri tion and Reference

90-02-01

Violation:

Failure to properly implement procedure

OST-1039, resulting in inadequate

gPTR data

calculation,

(par agraph 2.b. (1) ) .

0

13

90-02-02

90-02-03

90-02-04

90-02-05

90-02-06

Acronyms and

AF

AP

ALB

CM

EDG

EPT

ESF/AS

EST

GP

IFI

LER

MPT

MST

NCV

NI

NRC

OST

OMM

PCR

PIC

PLP

QA

QC

QPTR

RHR

RTS

RWP

SP

TS

WR/JO

Auxiliary Feedwater

Administrative Procedure

Alarm Response

Procedure

Corrective Maintenance

Emergency Diesel Generator

Engineering

Performance Test,

Engineered

Safety Feature

Actu

Engineering Surveillance Test

General

Procedure

Inspector Follow-up Item

Licensee

Event Report

Maintenance

Performance

Test

Maintenance

Surveillance Test

Non-Cited Violation

Nuclear Instrument

Nuclear Regulatory

Commission

Operations

Surveillance Test

Operations

Management

Manual

Plant Change

Request

Process

Instrument Control Pro

Plant Program

Quality Assurance

Quality Control

Quadrant

Power Tilt Ratio

Residual

Heat Removal

Reactor Trip System

Radiation

Work Permit

Sampling

System

Technical Specification

Work Request/Job

Order

ation System

cedure

Violation:

Failure to calculate

the

QPTR as required

by TS 4.2.4.1,

(paragraph 2.b.(1)).

NCV:

Failure to properly test thermal overload

bypass circuitry for valve MS-72, (paragraph 5.f).

NCV:

Failure to periodically vent emergency

core

cooling system piping, (paragraph 5.h).

NCV:

Failure to maintain proper grease

levels in

motor operated

gear boxes,

(paragraph

5.m).

NCV:

Failure to response

time test

ESF channel III

at correct periodicity, (paragraph 5.q).

Initialisms