ML18009A388

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Insp Rept 50-400/90-01 on 891226-900105.Violations & One Weakness Noted.Major Areas Inspected:Plant Operations to Review Licensee Activities During Recent Reactor Startup & Subsequent Power Escalation
ML18009A388
Person / Time
Site: Harris 
Issue date: 01/17/1990
From: Dance H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A387 List:
References
50-400-90-01, 50-400-90-1, NUDOCS 9002230125
Download: ML18009A388 (9)


See also: IR 05000400/1990001

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

h

Report No.:

50-400/90-01

Licensee:

Carolin-

Power

and Light Company

P. 0.

Box

1551

Raleigh,

NC 27602

Docket No.:

50-400

License No.:

NPF-63

Facility Name:

Harris

1

I

Inspection

Conduc:ed:

Decemoer

26,

1989 - January

5.

1990

Inspectors:

Te row,

enior Resid

t

nspe

or

r rz/gc

Date Signed

Shannon,

R

ident In

ctor

l/7 o

Date Signed

I

Approved ty:

Dane

, Section Chief

Division of Reactor Projects

Date Signed

SUMMARY

Scope:

This special i nspec .ion was conducted

by the resident

i nspectors

in the areas

of plant operations,

to review the licensee's

activities during

a recent

reactor startup

and

subsequent

power escalation.

Results:

One violation was identified:

Failure to establish limiting safety

system settings for the reactor trip system,

paragraph

2.

An operational

weakness

is also identified in paragraph

2 concerning

the

disregard for abnormal

plant conditions

and indications

and lack of attention

to detai

1 by plant operators.

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PDI.

REPORT DETAjLS

Persons

Contacted

Licensee

Employees

  • G. Forehand,

Director,

QA/AC

"C. Gibson, Director, Progress

and Procedures

  • P. Hadel, Project Specialist,

Planning

"J.

Hammond,

Manaaer,

Onsite Nuclear Safety

"C. Hinnant, Plant General

Manager

"D. McCarthy, Unit Manager,

Site Engineering

"C. Olexik, Supervisor,

Shift Operations

  • H. Powell, Manager,

Training

  • R. Richey,

Manager,

Harris Nuclear Project Department

  • J. Sipp,

Manager,

Environmental

and Radiation Monitoring

"J. Smith, Supervisor,

Radwaste

Operation

"D. Tibbits, Director, Regulatory

Compliance

"R.

Van Metre, Manager,

Technical

Support

  • M. Wallace,

Senior Specialist,

Regulatory

Compliance

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistryiradiation

and corporate

personnel.

"Attended exit interview

Acronyms and initialisms used

through out this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

On December

20,

1989,

a reactor startup

was performed

and the reactor

achieved criticality at 9:47 a.m.

Power operation

(Mode 1) was

commenced

at 5: 17 a.m.

on December

22.

The plant continued in power operation for

the duration of this inspection period.

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS) and the licensee's

administrative

procedures.

On December

26,

1989, during

a review of the shift foreman's

log, the

inspector

noted that at 3:30 a.m.

on December

23,

1989,

a calorimetric

calibration

was completed for .the nuclear instruments.

The nuclear

power

range

instruments

were found to be reading significantly below actual

core

power and were subsequently

adjusted.

The logs indicated that

actual

power

was approximately

41 percent while indicated

power was

approximately

28 percent.

This condition had existed

since the reactor

startup

was performed

on December

20.

NI High Power Trip

NI Low Power Trip

NI High Positive

Rate

NI High,Negative

Rate

  • This setpoint

was required by'TS 3.7.1 for an inoperable

main

steam

safety valve.

Using the percentage

of nuclear instrumentation error,

the inspector

calculated

the error in the nuclear

power range trip setpoints

inputted

into the reactor protection

system.

The reactor tri'p setpoints,

based

on

actual

rated

thermal

power,

were calculated

to be as follows:

4

Actual

Required

by TS 2.2. 1

127

5'o'

. <87'o'

37. 5;o

<25;o"

7. 5;o

7. 5;o

<

5'he"'inspector

noted that all four nuclear

power range

channel trips greatly

exceeded

the allowable instrument drift values listed in technical

specificationC.

This condition potentially placed

the 'plant in an

unanalyzed

condition in,that the reactor protection

system would not have

tripped the reactor- as designed.

Since the power range

nuclear

instrument reactor trips listed above are identified as the primary

protective action for several

accidents listed in the

FSAR, this item

appeared

to significantly compromise- plant safety.

This concern

was

immediately brought to the attention of plant management.

The concern

was identified by the inspector

as being potentially reportable at this

time.

On December

30 and 31,

1989, further discussions

were held with the

on-duty shift foreman

and acting operations

supervisor.

These

discussions

centered

on the plant potentially operating

outside of the

design basis,

and contrary to the requirements

of TS.

The shift foreman

subsequently

initiated

a significant operational

occurrence

report

(SOOR

90-01) to initiate

a reportabi lity determination.

As of January

5, this

matter

had not been reported to the

NRC Operations

Center.

Reportabi lity

will be reviewed with the apparent violation described

in this section.

During this refueling outage,

the plant received

new fuel

and

had

implemented

a fuel load design

change.

The design

change

placed

low

reactivity fuel modules

on the periphery of the core in order to reduce

neutron flux at the reactor vessel walls.

This had the effect of

reducing

the neutron flux at the excore nuclear detectors,

and th'ereby

caused

the instrument's

to be in error in

a nonconservative

direction.

A letter from the nuclear

steam

supply vendor (Westinghouse)

dated

March 16,

1988,

warned the licensee

of how the

low leakage

loading

patterns

could impact nuclear instrument detector output currents.

This

letter'pecified that the intermediate

and

power range detectors

needed

to

be recalibrated prior to criticality.

Three related industry event

reports also discussed

various

problems with miscalibration of nuclear

detectors

and the

NRC issued

an information notice

( IEN 83-43) which

discussed

problems with miscalibration of nuclear detectors.

'

0

To address

.IEN 83-43 the licensee

deve'loped

procedure

EPT-008,

Intermedia-.

Range Detector Setpoint Determination.

The procedure

was

revised

on July 21,

1988 following the Westinghouse letter of March 16,

1988.

This procedure

required that p'rior to criticality, a calibration

adjustment

of each nuclear instrumentation

system

power range

channel

be

performed.

Procedure

EPT-008 was not implemented for the four power range nuclear

instrument

channels

but was completed for the two intermediate

range

channels.

The intermediate

range

channels

appeared

to be accurate

during

startup.

The outage

planning

schedule listed this procedure

to 'be

completed prior to startup but the partial completion of the procedure

for the intermediate

range detectors

is believed to have resulted

in the

whole procedure

being crossed off the outage

schedule

as being completed.

Although the industry event reports

had

been

forwarded to the technical

support

group

and operations

management,

operating

personnel

had not

reviewed the event reports

and

had not been trained

on this issue

by the

training deoartment.

The operations

procedure

group

was in the process

of implementing the precautions

for miscalibration of nuclear detectors

into the general

plant startup

procedures,

but the procedures

had not

been modified as of the

December

1989 startup.

TS. 3.3. 1 requires

the nuclear

power range monitors to be operable

in

Modes

1 and 2.

Failure to properly establish limiting safety

system

settings

for the reactor trip system is contrary io the requirements

of

TS 2.2. 1, 3.3. 1 and 3.7. 1 and is identified as

an apparent violation.

Apparent Violation (90-01-01):

Failure to properly establish

reactor

trip system trip setpoints.

During power escalation,

the operators

had various warnings/indications

that the

power range nuclear instruments

could be/were

in error and

reading nonconservative:

a

~

The initial point of criticality and the point of adding heat

occurred at about

one decade

lower in the source

and intermediate

ranges

than previously experienced.

This was attributed to moving

the detectors.

b.

Difficultywas experienced

with clearing the P-10 interlock (NIs >

10 percent) prior to reaching

th'e intermediate

range detector

low

power rod stop of 20 percent

and low'ower trip of 25 percent

setpoints.

Differential temperature

instruments

indicated that actual

power was

50 percent greater

than indicated

power.

A subsequent

review. of

computer data

showed that six channels

of differential temperature

measured

in percent

power exceeded

that indicated by"NI power by

50 percent at various points during the

power escalation.

d.

It was noted that turbine

power was at

39 percent with reactor

power

at 28 percent.

The operators attributed this to increased

plant

efficiency.

It appeared

that with the data available to '.he operators,

the

miscalibration of the nuclear

instruments

should

have

been detected

by

the operating staff.

The operators

should not have relied

on

a single

indication of vital plant conditions

when mul iple indications were

available.

The operators

appeared

weak in responding

to offnormal plant

conditions.

3.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1)

at the conclusion of the inspection

on January

5,

1990.

During this

meeting,

the inspectors

summarized

the

scope

and findings of the

inspection

as they are detailed

in thi s report, with particular emphasis

on the Violation.

The licensee

representatives

acknowledged

the

inspector's

comments

and did not identify as proprie ary any of the

materials

provided to or reviewed

by -he inspectors

during this

inspection.

Item Number

Description

and Reference

90-01-01

Violation-Failure to properly establish

reactor

protection

system trip setpoints

4.

Acronyms and Initialisms

EPT

FSAR

IEN

NI

NRC

SOOR-

TS

Engineering

Performance

Test

Final Safety Analysis Report

Information Notice

Nuclear Instrumentation

Nuclear Regulatory

Commission

Significant Operational

Occurence

Report

Technical Specifications