ML18005A615
| ML18005A615 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 09/16/1988 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18005A614 | List: |
| References | |
| 50-400-88-17, NUDOCS 8810030293 | |
| Download: ML18005A615 (36) | |
See also: IR 05000400/1988017
Text
ENCLOSURE
BOARD REPORT
U.S.
NUCLEAR REGULATORY COMMISSION
REGION II
SYSTEMATIC ASSESSMENT
OF LICENSEE
PERFORMANCE
NRC INSPECTION
REPORT
NUMBER
50-400/88-17
Carolina
Power
and Light Company
Shearon
Harris Unit
1
July 1,
1987 - June
30,
1988
33 f0030293
3809 1 6
ADOCK 05000400
I.
INTRODUCTION
TABLE OF
CONTENTS
Pacae
II.
CRITERIA
III.
SUMMARY OF
RESULTS
A.
B.
Overall Facility Performance
Facility Performance
Summary
IV.
PERFORMANCE ANALYSIS
A.
B.
C.
D.
E.
F
~
G.
H.I.
J.
K.
L.
Plant Operations
Radiological Controls
Maintenance
Surveillance
Fire Protection
Emergency
Preparedness
Security
Outages
guality Programs
and Administrative Controls
Affecting guality
Licensing Activities ..
Training and gualification Effectiveness ....
Engineering
Support
~
~
~
~
~
~
~
0
~
~
~
~
~
6
10
12
14
16
18
20
22
23
25
28
29
V.
SUPPORTING
DATA AND SUMMARIES
32
A.
B
~
C.
D.
E.
F.
G.
H.I.
J.
K.
Licensee Activities
Inspection Activities
.
Investigation
Review
~ .
Escalated
Enforcement Actions
Management
Conferences
Confirmation of Action Letters ..
Licensee
Event Reports
Licensing Activities
Enforcement Activities
Effluent Summary for 1987
0
~
~
~
0
~
~
~
~
~
~
~
32
33
33
33
33
34
34
34
35
35
36
I .
INTRODUCTION
The
Systematic
Assessment
of Licensee
Performance
(SALP) program is
an
integrated
NRC staff effort to collect available observations
and data
on
a periodic
basis
and
to evaluate
licensee
performance
based
on this
information.
The
program
is
supplemental
to
normal
regulatory
processes
used to determine
compliance with
NRC rules
and
regulations.
The
SALP program is intended
to
be sufficiently diagnostic
to provide
a
rational
basis
for allocating
NRC
resources
and
to provide
meaningful
guidance to licensee
management
in order to promote quality and safety of
plant construction
and operation.
An
NRC
SALP Board,
composed
of the staff members
listed below,
met
on
August 25,
1988, to re'view the collection of performance
observations
and
data
to assess,.licensee
performance
in accordance
with guidance
in
NRC
Manual
Chapter
0516,
"Systematic
Assessment
of Licensee
Performance".
A
summary of the guidance
and evaluation criteria is provided in Section II
of this report.
This report is the
SALP Board's
assessment
of the licensee's
safety
and
management
performance
at- Shearon
Harris Unit
1 for
the
period July 1,
1987,
through June
30,
1988.
SALP Board for Shearon
Harris Unit 1:
C.
W. Hehl,
Deputy Director, Division of Reactor Projects
(DRP),
Region II
(RII), (Chairman)
A.
R. Herdt, Chief, Engineering
Branch,. Division of Reacto}
Safety
(DRS), RII
D.
M. Collins, Chief,
Emergency
Preparedness
and Radiological Protection
Branch, Division of Radiation Safety
and Safeguards,
RII
D.
M. Verrelli, Chief, Reactor Projects
Branch 1,
DRP, RII
E.
G.
Adensam,
Director, Project Directorate II-1, Office of Nuclear
Reactor
Regulation
(NRR)
G.
F. Maxwell, Senior Resident
Inspector,
Shearon Harris,
DRP, RII
B.
C. Buckley, Senior Project Manager,
Project Directorate II-l, NRR
Attendees
at
SALP Board Meeting:
P.
M. Madden, Acting Chief, Technical
Support Staff (TSS),
DRP, RII
R.
E. Carroll, Project Engineer,
Project Section. 1A,
DRP, RII
W. Bradford, Senior
Resident
Inspector (Selectee),
Shearon
Harris,
DRP, RII
II .
CRITERIA
Licensee
performance is assessed
in selected
functional areas
depending
on
whether
the facility has
been
in the construction,
preoperational,
or
operating
phase
during
the
SALP review period.
Each
functional
area
normally represents
an area
which is significant to nuclear safety
and the
environment,
and
which is
a
normal
programmatic
area.
Some functional
areas
may not
be
assessed
because
of little or
no licensee activity, or
because
of
a lack of meaningful
NRC observations.
Special
areas
may
be
added to highlight significant observations.
One or more of the following evaluation criteria was
used to assess
each
functional area;
however,
the
SALP Board is not limited to these criteria
and others
may have
been
used
where appropriate.
A.
B.
C.
D.
E.
F.
G.
Management
involvement in assuring quality
Approach
to
the
resolution
of technical
issues
from
a
safety
standpoint
Responsiveness
to
NRC initiatives
Enforcement history
Operational
and construction
events (including response
to, analysis
of, and corrective actions for)
Staffing (including management)
Training and qualification effectiveness
Based
upon the
SALP Board
assessment,
each
functional
area
evaluated
is
classified
into one of three
performance
categories.
The definitions of
these
performance
categories
are:
~Cate or
1:
Reduced
NRC attention
may
be
appropriate.
Licensee
management
attention
and
involvement
are
aggressive
and oriented
toward nuclear safety;
licensee
resources
are
ample
and effectively
used
such
that
a
high
level
of
performance
with respect
to
operational
safety or construction quality is being achieved.
~Cate or
2:
NRC attention
should
be
maintained
at
normal
levels.
Licensee
management
attention
and
involvement
are evident
and
are
concerned
with nuclear safety;
licensee
resources
are
adequate
and
are
reasonably
effective
such that satisfactory
performance
with
respect
to
operational
safety
or construction
quality is
being
achieved.
t
Cate<aCor
3:
Both
NRC- and
licensee
attention
should
be
increased.
Licensee
management
attention
or
involvement
are
acceptable
and
considers
nuclear
safety,
but
weaknesses
.are
evident;
licensee
resources
appear
to
be strained
or not effectively used
such that
minimally satisfactory
performance with respect
to operational
safety
or construction quality is being -achieved.
The functional
area
being
evaluated
may
have
some attributes
that would
place
the
evaluation
in Category
1,
and others that would place it in
either Category
2 or 3.
The final rating for each
functional
area
is
a
composi.te
of the attributes
tempered
with the judgment
of. NRC management
as to the significance of individual .items.
The
SALP Board
may also include
an appraisal
of the performance
trend of a
functional
area.
This performance
trend will only be
used
when both
a
definite trend of performance within the evaluation period is discernable
and
the
Board believes
that continuation
of the trend
may result in
a
change of performance
level.
The trend, if used, is defined as:
~Im rovin
Licensee
performance
was determined
to
be improving near the
close of the assessment
period.
~Declinin
Licensee
performance
was
determined
to
be declining near the
close of the assessment
period.
III. SUMMARY OF
RESULTS
A.
Overall Facility Performance
Shearon
Harris
has
been
operated
in
an overall
safe
and effective
manner
during its first year
of full
power
operation.
Major
strengths
were identified in the areas
of maintenance,
surveillance,
security,
outages,
and training.
There
were
no
major
weaknesses
identified in any functional area.
Although,
nonconservative
managem'ent
decisions
and
numerous
operator
errors
occurred
during
the first half of the
assessment
period,
continued
operation
at
power with corrective
action
feedback
has
reduced
this
experience-related
trend
dramatically.
Harris
has
developed
an
adequate
health
physics
program.
As,yet,
though,
the
staff
and
management
have
not
been
challenged
on
the
program
implementation
by an extended
outage
or
a significant health
physics
related modification or event.
Maintenance
continues
to be
a strong
area
at
Harris,
with
an
aggressive
maintenance
effort.
The
surveillance
program is well established
and
has
proven to
be very
effective.
Implementation
of
the
fire
protection
program
was
adequate,
except for several
procedural
deficiencies.
An emergency
response facility appraisal
and two routine evaluations
demonstrated
that,
although
additional
training
was
needed
in
accident
dose projections,
emergency
planning at Harris was managed
satisfactorily,
with
more
challenging
scenarios
than
previously
observed.
Harris
has
aggressively
resolved
those
security
problems
which occurred
shortly after plant licensing.
Plant
management
is
very
responsive
in
reporting
security
concerns
and
has
placed
increased
oversight
in the security
area.
Although Harris
has
not
conducted
a
refueling
outage
yet,
plant
outage
personnel
have
demonstrated
good
planning,
coordination
and
implementation
on
several
other
shorter
and
less
challenging
outages
~
Plant
reliability increased
due
to the modifications
implemented
during
these
outages
~
The quality assurance
attitude
and implementation at Harris is quite
good.
Normally, activities
are
accomplished
right the first time.
Feedback
on problem areas
generally results
in improved performance.
6
The licensing
group,
both in the
company office and at the Harris
site,
have,
with
some initial difficulty, made
the transformation
from
a pre-licensing
organization
to
an effective
power operation
licensing organization.
Licensing actions
are generally timely and
the relationship with the
NRC Licensing Project Manager is effective
and professional.
Training
was
obvious
in all technical
areas.
In
earlier
problem
areas,
particularly
in
the
area
of operations,
training
was
used
to
reduce
errors
and
to
increase
personnel
knowledge
and sensitivity to safety.
Engineering
support
has
been
very active during this assessment
period,
especially
in the imple-
mentation
of the
Equipment gualification
program.
The
design
and
engineering
organizations
are still in transition
from pre-licensing
and are expected
to continue to improve.
B.
Facility Performance
Summary
The
performance
categories
for the cur'rent
and previous
SALP period
in each functional
area
are
as follows:
Functional
Area
'August 1,
1986
June
30
1987
July 1,
1987
June
30
1988
Trend
Plant Operations
Radiological
Controls
Maintenance
Surveillance
Fire Protection
Emergency
Preparedness
Security
Outages
guality Programs
and
Administrative Controls
Affecting guality
Licensing Activities
Training and gualification
Effectiveness
Engineering
Support
Preoperational
and Startup
Testing
Construction Activities
2
2
1
1
1
2
2
NR
2
12.
2
2
1
1
2
2
1
1
2
2
N/A
N/A
Improving
Improving
Note:
NR = Not Rated
IV.
PERFORMANCE ANALYSIS
A.
Plant Operations
l.
Analysi s
Ouring this assessment
period,
inspections
were performed
by the
resident
and
regional
inspection
staffs.
The
i'nspections
included:
system
walkdowns;
procedure
reviews;
personnel
interviews;
housekeeping;
observations
of reactor
startups
and
plant
shutdowns;
operations
at
power;
and
control
room
activities which included operator
demeanor,
plant transients,
routine valve lineups,
and log keeping.
The inspectors
noted that during abnormal
conditions (ie.,
such
as
when
one of the
main feedwater valves failed closed or when
the
main
tu'rbine
automatic
controls
became
operations
personnel
have
been
quick
to
use
available
information and procedures
to stabilize
and control
the plant.
This
includes
the
use
of the
readi'ly available
control
room
drawings
which
are
always
maintained
current.
Routine
operational
activities were carried
out by the operators
in
a
very professional
manner.
The uniform policy for control
room
operators'ress
continues
to help distinguish
those
operators
who are
on duty in the control
room.
Shift foreman's
logs
have
been
reviewed daily
and
have
been
found to
be consistently
legible and clearly reflect the status of the plant.
Normally,
the
number of plant annunciators
which were in alarm or disabled
were
minimized
and
generally
consistent
with existing
plant
operating
conditions.
During plant
system
walkdowns,
valves
were found to be properly aligned
and positioned.
Additionally,
all
observed
or
malfunctioning
equipment
had
deficiency tags
attached
and work requests
initiated.
This is
indicative
of operations
personnel
properly controlling the
status
of the plant
systems.
The plant
has
been
kept
very
clean.
A description
of the
plant trips
which occurred
during this
rating period is provided in Section V.J.
Of the six reactor
trips, five were
automatic
and
one
was manually initiated.
One
trip was due to equipment failure,
one was
due to design error,
one
was
due to inadequate
procedure
controls,
one
was
due to
non-licensed
operator
error,
and
two
were
due
to
licensed
operator
errors.
The
equipment
failure
was
addressed
by the
licensee's
predictive
and preventive
maintenance
programs.
The
design
problem
was
corrected
and
evaluated
by
the
design
engineering
group.
For
the
remaining
instances,
licensee
management
provided corrective
measures
which should reduce
the
plant trips caused
by personnel
error.
These
measures
included
intensified "real time" training for the operators
to acquaint
them with revisions to procedures
and lessons
learned
which have
resulted
from plant events
and incidents'lso,
in some
cases
disciplinary action (includ'ing leave without pay) was taken
when
operators failed to follow procedures.
During
the
previous
evaluation
period
the plant
experienced
several
reactor t~ips which were attributed to problems with the
condensate
and
systems.,
The
licensee
recognized
a
need to collect the reactor trip data for analysis,
and
a task
force
was formally chartered
to review
and
recommend reliable
improvements
for
the
secondary
plant.
The
task
force
recommended
permanent
changes
to the
condensate
and
systems
to alleviate the secondary
plant transients.
During
an
October
1987
outage,
the
task
force
recommendations
were
implemented.
During
the
months
following
the
plant
modifications,
the
plant
performance
significantly increased,
with
no reactor "trips being attributed
to
secondary
system
interaction.
Plant
. management
involvement
in
routine
and
nonroutine
activities became
more effective during this period.
This was
demonstrated
by their involvement in daily coordination meetings
to evaluate all plant off-normal conditions,
any
LCO conditions
which could
to
a
shutdown,
plant conditions
which could
potentially affect operations,
and prioritization of maintenance
activities.
Management
has
remained
responsive
to
items of
concern
expressed
by
the
NRC
and
they
maintain
good
communications with the public and local authorities.
A review of the
LERs indicated that the licensee
submitted
about
twice as
many
LERs in the first six months
as
an
average
plant
and
was about average for the
second six months.
This level of
reportable
events
is consistant
for
a
new plant
and
shows
an
improving
trend.
Several
of
the
LERs
were
tentatively
classified
as significant by the Office of Analysis for Events
and
Opertional
Data
(AEOD)
screening
process.
These
LERs,
discussed
in Section IY.L of this report, reflect deficiencies
in design,
installation,
and fabrication which are within the
range
of startup
problems
at
new
plants.
Generally,
the
reportable
events
were
caused
by
personnel
errors
and
administrative
oversights
which were
amenable
to correction
by
increased
familiarity with
operating
the
plant
and
more
attention to detail.
The types of personnel
errors
and administrative oversights that
caused
the majority of the
LERs included missed
survei llances,
improper valve restoration
lineup, miscues
during test or plant
evolutions.
Two events
involved
opening
one of the air lock
doors while the other door was not secure.
Overall,
the
LERs
were
submitted
in
a
timely
fashion
and
generally
provided
sufficient
information
to
understand
the
event
and the unde~lying causes.
The
number of violations listed below does not indicate
a long
term poor operations
performance
record.
The majority of the
violations occurred in the first part of the assessment
period,
with
a reduction
in the
number of violations
noted
toward the
end of the period.
Nine violations were identified.
P
Severity
Level
IV violation occurred
when
a plant operator
allowed
low pressure
safety
injection to occur during
a
normal plant shutdown.
(400/87-26-01)
.
Severity
Level
IV violation for personnel
pulling the wrong
fuse during
a clearance,
which resulted
in a reactor trip.
(400/87-26-02)
C.
Severity
Level
IV violation
occurred
when
an
operator
failed to follow procedure
when returning
a compressed air
valve to normal service.
(400/87-31-01)
Severity
Level
IV violation for failure
to correctly
interpret Technical Specification
requirements
when leaving
a
steam
generator
blowdown
valve
stuck
open
with the
reactor operating at power for 29 days.
(400/87-34-01)
e.
Severity
Level
IV violation for the shift foreman allowing
reactor
vessel
head
vent
valves
to
be
manipulated
even
though
the
valves
were
known
to
operate
improperly.
(400/87-37-01)
Severi ty
Level
IV
viol ati on
for fa i lure
to fol 1 ow
operations
procedures
by incorrectly positioning
steam" dump
controls during
a reactor
heatup.
(400/87-40-02)
h.
l.
Severity
Level
IV violation for failure to promptly update
an
emergency
operating
procedure,
to
comply with
commitments.
The revision was necessary
to assure
that the
RHR system
could supply sufficient cooling water to
keep
the reactor
vessel
core
covered
during
a
LOCA event which
may
result
in
only
one
pump
to
be
available.
(400/88-06-01)
Severity
Level
IV violation for failure to control plant
system configuration during
a test of the "A" train Solid
State Protection
System;
the "A" train was tested
when
"B"
train equipment
was inoperable.
(400/88-11-01)
Severity Level
V violation for failure of the shift foreman
to report within four hours
an
ESF actuation
to the
NRC
Duty Officer.
(400/87-31-02)
Conclusion
Category:
2
Trend:
improving
10
3.
Recommendations
An improvement
during the
assessment
period
was
recognized
in
this area
based
on
a reduction
in violations during the
second
half of the period,
an increased
emphasis
on personnel
training,
and the extended
periods of plant operation.
Continued
emphasis
should
be placed
in this functional
area.
NRC staff resources
applied to the routine inspection
program should
be maintained.
B. 'adiological
Controls
1.
Analysi s
During the assessment
period,
inspections
were performed
by the
resident
and
regional
inspection staffs.
Regional
inspections
included
two radiation
protection,
one radiological effluents,
one chemistry,
and
a confirmatory measurements
inspection
using
the
Region II
mobile
laboratory.
These
inspections
were
supplemented
by
the
resident's
routine
evaluation
of
the
day-to-day radiation work practices at the site.
The licensee's
health physics
(HP) and radwaste staffing levels
were appropriate
and
compared
well to other utilities having
a
facility of similar size.
An adequate
number of ANSI qualified
technicians
were available
to support operations.
Although the
health physics staff continued to be supplemented
by the
use of
eighteen
contractors,
the licensee
plans to eliminate,
by early
1989,
the
use of contract
HP personnel
durihg normal operations.
This was to be accomplished
by hiring six additional technicians
and qualifying twelve individuals
who
were
in the
licensee's
health physics training program.
The
knowledge
and
experience
level 'of the
HP,
radwaste,
and
radioactive
material.
transportation
personnel
continued
to
increase
during the
assessment
period
and is considered
good.
The staff
has
a
low turnover rate
and
the
general
employee
'adiation
protection
training
program
was
adequate.
The
technician training program
was accredited
by the Institute of
Nuclear
Power Operations
(INPO) on September
25,
1986.
The performance of the radiation protection staff in support of
routine operations
was
adequate.
However,'he
response
of the
radiation
protection
staff to radiological
control
problems
associated
with outages
is yet to be determined
since the first
refueling
outage
is
scheduled
for late July 1988,
which is
outside the
SALP period.
The licensee's
radioactive
material
transportation
program
was.
adequate,
as
were
the radiation
work permit
and respiratory
protection
programs.
No
internal
contaminations
or
administrative
or regulatory
occurred
during the
11
assessment
period.
The
licensee
did experience
87 personnel
contaminations
during
1987,
48
of
which
were
skin
contaminations.
The remaining
39 were clothing contaminations.
From
January
1,
through
June
30,
1988,
the
licensee
had
experienced
a total of
11 skin
and
39 clothing contaminations.
The
number of personnel
contaminations
is typical for a plant of
similar size
and age.
Licensee
management
support
of,
and
involvement
in,
the
radiation
protection
program
was
adequate.
The radiological
preparations
and
planning for the first refueling
outage
in
July 1988,
appeared
to
be
generally
complete
and
thorough.
Licensee
management
placed
emphasis
on keeping
worker doses
as
low as
reasonably
achievable
(ALARA), following procedures,
and
complying with good radiation control practices.
During calendar
year
1987,
the licensee's
collective
dose
was
33 person-rem
which was well below the
PWR national
average
of
368 person-rem.
The low collective dose
was attributable to the
fact that the facility is relatively new and that there
was
no
refueling outage
during this period.
The collective
dose
goal
for 1988,
was set at 260 person-rem with 200 person-rem of that
total
planned for the first refueling outage.
As of June
30,
1988,
the licensee
had expended
7 person-rem.
Liquid and
gaseous
radioactive effluents
were within the
dose
limits specified in the Technical Specifications
and 40'FR
190,
and within the radioactivity concentrations
specified in 10 CFR 20.
Concentrations
did not
exceed
the
Appendix I
ALARA limits.
No
abnormal
liquid or
gaseous
releases
were
reported during 1987.
A summary of 1987 effluents is listed in
Section
V.K of this report.
The chemistry
program
has
become
very effective.
The licensee
has
made
good
use of contract
chemistry
personnel,
as well
as
resources
from the corporate
training center.
In the future,
however,
the
licensee
plans
to
lessen
the
dependency
on
chemistry
contractors.
Since this plant
was
designed
in the
early
1970's,
some
of
the
physical
facilities,
such
as
laboratories,
are state-of-the-art
where
as other areas,
such
as
sample
rooms,
are
not.
However,
this
has
not
affected
acceptable
performance
by the licensee.
This was re-emphasized
by the
good
agreement
shown
between
the
licensee's
and
NRC's
sample
results
for the
NRC radiological
and
nonradiological
(chemistry) confirmatory measurements
programs'uring
calendar
year
1987,
the license
disposed
of
a total of
3,700 cubic
feet
of
solid
radioactive
waste
containing
2.6 curies
of radioactivity.
This
was
well
below
the
national
average
of 6,590 cubic feet for a single unit site, but
as stated earlier, there
was
no major outage during the period.
12
The
goal
established
for 1988
was
set at 6,500 cubic feet,
of
which 4,200 cubic feet of solid radioactive waste (including dry
active waste
shipped for supercompaction)
containing
1.37 curies
of activity had been
shipped
as of June
30,
1988.
The increased
volume of waste
shipped
in
1988
was
due to the fact that the
licensee
held
some
shipments
over from 1987.
In early 1988,
the
licensee
began
an aggressive
program to eliminate the practice
of taking
in unnecessary
items/material
into
the
controlled
area.
This was done in
a attempt to reduce
the total
volume of
waste
generated
at the facility.
In
December
1987,
the
licensee
maintained
5,200
square
feet
( 1. 1i>) of the total radiation control
area
(RCA) as contaminated
(excluding the containment).
The actual
area
being controlled
at
the
end
of
the
assessment
period
was
approximately
2,425
square
feet (0.5') of the
RCA.
No violations or deviations
were identified.
2.
Conclusion
Category:
2
3.
Recommendations
NRC staff resources
applied to the routine inspection
program
should
be maintained.
C.
Maintenance
Analysi s
During this assessment
period, inspections
were performed
by the
resident
and
regional
inspection
staffs.
The scope'f
the
inspections
included:
process,
tracking
and
implementation
of
work requests;
observation
of
maintenance
and
surveillance
testing;
witnessing
preventive
maintenance
activities,
and
modifications
and troubleshooting.
Maintenance
continues
to
be
a strong
area at Harris, with an
aggressive
maintenance
effort.
The
licensee's
work request
process
appeared
to
work very well
during this
evaluation
period.
The site-wide priority system
and
management
controls
that implement the priority system
have assured
that the safety
significance
and importance of each job are clearly communicated
and that
resources
were
applied first to the
most
important
tasks.
or malfunctioning
equipment
observed
during'ystem
walkdowns all
had
a deficiency tag attached
and
a work
request initiated.
All station requirements
had
been
adhered
to
in the
issuance
and completion of these
work requests.
High
13
priority items
were
completed
in
a timely manner;
however,
several
low priority items took longer to complete.
Early
in
the
assessment
period,
the
methods
used
to track
maintenance
trends
were
not
formal.
The
individual
system
engineer
made
the
determination if a fai lure
mechanism
was
repetitive
and warranted consideration
for generic applicability
or inclusion in the preventive
maintenance
program.
The lack of
a formal
program
produced
a subjective
situation that
may have
caused
errant decisions
when
a
new or
backup
system
engineer
made
the repetitive failure decision
and
as
such,
may not have
been
aware of the
number of fai lures.
Accordingly, the licensee
has
developed
procedural
controls
to continue
improving its
maintenance
feedback
program.
The
program
is
being
used
extensively
to
document
items
needing
attentions
Providing
documented
procedural
controls for the
feedback
program
has
aided
the program in that various affected departments
must
now
formally respond
to items of concern
which were identified by
the program.
Maintenance
personnel
evaluated
approximately
3000 plant system
valves
and
have
included
them
on the valve list for the "live
load"
program.
The "live load"
program
was designed
to reduce
the likelihood of valve packing
leakage
and valve stem binding.
The licensee
began this
program at the
end of the
assessment
period
and
plans
further
implementation
on
selected
valve's
during the July 1988 refueling outage.
The
maintenance
staff
continues
to
use
the
utility's
computerized
automated
maintenance
management
system
as
a part
of their maintenance
program.
This system
has
proven to be very
valuable
to maintenance
personnel,
in that its uses
included:
initiating
and
tracking
woi"k request
status,
planning
and
scheduling
work, and review 'of historic maintenance
records.
The licensee
has
appointed
a full time crew of instrumentation
and
control
technicians
to
perform all
of
the
maintenance
surveillance
tests
associated
with
the
reactor
protection
system.
The crew also
has
been
responsible
for conducting all
of the corrective
maintenance
on the protection
system.
Having
a single dedicated
crew for this
system
has
provided
improved
consistency
in preventive
and
corrective
maintenance
and
has
made the
system
more reliable.
Post-maintenance
activities'er e routinely inspected.
With the
exception of the violation identified below, testing
was
found
to
be
appropriate
for
the
maintenance
performed
and
was
conducted
in accordance
with written procedures.
Overall, Harris appears
to
have
a comprehensive
and aggressive
maintenance
program,
and
seems
to
be very
much
aware of
NRC
concerns
and initiatives.
One violation was identified.
Severity Level
IV violation for maintenance
personnel
failing to
follow
procedure
when
several
steps
in
a
maintenance
surveillance
test
procedure
on
an
emergency
diesel
generator
fuel
nozzle
were
not
completed
and
no justification
was
documented.
Also, while conducting
a reactor
coolant
system
isolation
valve test,
the test
procedure
was
changed
without
first obtaining
an
approved
temporary
change.
Both of these
were
documented
as
one
example of personnel
failing to follow
procedure
while
conducting
maintenance
activities.
(400/87-38-01)
2.
Conclusion
Category:
I
3.
Recommendations
A high level of performance
was
achieved
in this area.
It is
recommended
that
NRC staff
resources
applied
to
the
routine
inspection
program
be reduced.
Surveillance
l.
Analysi s
During this assessment
period,
inspections
were performed
by the
resident
and
regional
inspec'tion
staffs.
The
licensee's
survei
1 1 ance
schedul e
was
regul arly
eval uated
to
veri fy
survei1 lance
testing
was
performed "as
scheduled,
testing
was
conducted
in accordance
wit,h approved
procedures,
and the test
results
were
promptly
reviewed
by
super'vision.
The
routine
inspections
included
witnessing
surveillance
testing
for
electrical
systems,
pump
and
valve
in-service
testing,
mechanical
systems,
and instrumentation
systems.
Early in the first fuel cycle, the licensee's
performance
of and
procedures
for core
power distribution
monitoring,
reactor
coolant
system
leakage evaluation,
and thermal
power monitoring
and evaluation
were reviewed.
It appeared
that the licensee
had
demonstrated
a
good
understanding
of this
portion
of
the
surveillance
program.
The
licensee's
procedures
were
well
planned,
technically
accurate
and indicated
evidence
of prior
planning.
15
The
licensee
has
improved its
surveillance
test
scheduling
program.
The
program
has provided
a very reliable schedule for
routine surveillance
tests,
periodic tests
and
any additional
tests
which
may
have
been
requested.
Records
show that less
than
15 of the routine
13,000
survei llances
were
not completed
as
scheduled
during thi s
SALP period.
The daily surveillance
test
schedules
are
the
responsibility
of
the
licensee'
Regulatory
Compliance
personnel.
These
schedules
are regularly
discussed
at
each
morning meeting with the various
department
managers'ssurance
of quality,
including
management
involvement
and
control
was
evident.
In particular,
review of the
previous-
pressurizer
safety
valve
set
point test
results
indicated
evidence of prior planning.
Each pressurizer
safety
valve
was
tested
by the vendor with both nitrogen
and hot wa.er
so that in
future testing,
appropriate
compensations
can
be
made
when only
y single
medium is utilized.
This will provide flexibility and,
therefore,
simplify testing.
Once the valves
are
contaminated,
the
vendor will no
longer
be able to perform this function.
The licensee
is committed to ASME OM-1 for safety valve testing
and is currently establishing
a set point testing
program.
Review of completed
startup test
procedures
for the 75,
90 and
100% power plateaus
was completed during this appraisal
period.
All tests
were
conducted
in
a timely
and
acceptable
manner.
When required, test
changes
were properly approved,
retests
were
performed,
and
changes
or relaxations
in performance criteria
were justified.
One test,
the loss of 100io'f electrical
load,
was deleted following approval
by the
NRC.
The efforts involved
in the deletion
process
demonstrated
that the
licensee
had
a
good understanding
of the technical
issues
involved.
The licensee
also established
a program which is in response
to
the erosion/corrosion
experienced
by another
Region II licensee
on
the
main
system
piping.
This
program
was
implemented
in the fall of 1987 by the licensee
during
a brief
outage'he
program was developed
and implemented
in accordance
with Electric Power Research
Institute
(EPRI) guidelines.
Also
during this
outage
the
licensee
successfully
completed
the
required
local
leak rate
testing
for. all of the
individual
containment
isolation
valves.
To
assure
survei llances
are
performed within their required
time
frame,
management
plays
an
active role at the daily morning meeting
where the surveillance
schedule
is discussed.
No violations or deviations
were identified.
2.
Conclusion
Category:
1
j
16
3.
Recommendations
A high level of performance
was
achieved
in this area.
It is
recommended
that
NRC staff resources
as applied to the routine
inspection
program
be reduced.
E.
Fire Protection
1.
Analysi s
During this assessment
period,
inspections
were conducted
by the
resident
and regional
inspection staffs to review the licensee's
implementation
of the fire protection
program
and followup on
. previously identified enforcement matters.
The
licensee
has
issued
revisions
to
procedures
for the
administrative
control
of fire
hazards
within
the
plant,
surveillance
and maintenance
of the fire protection
systems
and
equipment,
and
organization
and training of the
plant fire
brigade.
These
procedures
were
reviewed
during
the
staff
inspections.
With the exception
of Fire Protection 'rocedure
Fire
Protection
Mitigating Actions,
all
of
the
procedures
appeared
to meet the
NRC requirements
and guidelines.
Review of procedure
showed that it was inadequate.
This
was identified as
a violation (b. below).
The staff inspectors
also reviewed the licensee's
implementation
of fire prevention
administrative
controls
and
surveillance
procedures.
This review
showed that the inspections
and tests
were being performed in accordance
with requirements,
except for
that required
by procedure
FPT-3302,
Main Drain Test Auxiliary
Building quarterly
Interval.
Review of inspections
and tests
required
by this procedure
showed that six systems
on the 190',
268'nd 305'levatjons
of the Reactor Auxiliary Building were
not tested
between
February 4,
1987
and August 28,
1987.
This
exceeded
the
quarterly
interval.
This
was identified
as
a
violation (a. below).
During
a walkdown inspection
by the staff, housekeeping,
control
of combustible
and
flammable materials
in safety-related
areas
were
found
to
be
satisfactory.
The
fire
protection
extinguishing
systems
(except
as
previously
noted),
fire
detection
systems
and fire barrier assemblies
protecting plant
systems for safe
shutdown
were also found to be functional.
The technical
support staffing for the fire protection
program
is adequate
to accomplish the goals without excessive
overtime.
The
licensee's
fire
protection
staff's
authorities
and
responsibilities
are
clearly
defined.
The
organization
and
staffing levels along with the training and drill frequency for
the fire brigade
members
met the
NRC guidelines.
It was
noted
17
during this
assessment
period that the
response
time for the
site fire brigade within the power block and outside
and
power'lock
has
improved.
The
improvements
are
attributed
to the
purchase
and
use of equipment carts,
one for each
elevation
in
each building,
and improved hose
houses.
The in-place equipment
carts
are
packed
with the
required
inventory
to fight
a
potential fire, and minimize the distance that equipment
must
be
carried.
The
new
hose
houses
have
improved the
response
time
outside
the
power block because
the
hoses
are preconnected,
as
opposed
to the old hoses
that required
numerous
connections
to
reach the nearest
building.
The
most recent
audits
and
gA surveillance
reports of the fire
protection
program were conducted within the specified frequency
and
appeared
to
cover all
essential
elements
of
the fire
protection
program.
These
audits
identified
some
. minor
discrepancies.
The licensee
appeared
to
be taking appropriate
corrective actions
on these audit findings.
Management
involvement
and control
in assuring
quality in the
fire protection
program
appeared
to
be
adequate
except for the
inadequacy
noted
earlier
regarding
administrative
procedure
The
licensee's
approach
to resolution
of technical
fire protection'ssues
indicates
an understanding
of issues
and
is
sound
and timely.
Responsiveness
to
NRC initiatives
are
timely
and
thorough.
When
violations
do
occur
effective
corrective
action
is promptly taken.
Fire protection related
events
and discrepancies
identified by the licensee
are properly
analyzed
and promptly reported
and effective corrective actions
are taken.
Two violations were identified.
a.
Severity
Level
IV violation
for
failure
to
perform
quarterly
surveillance
of the
multicycle
and
preaction
sprinkler
systems
on the 190', 268'nd 305'levations
of
the reactor auxiliary building.
(400/88-01-01)
b.
Severity
Level
V
violation
i'nvolving
an
inadequate
procedure
for
implementing
mitigating
actions
for
inoperable fire suppression
systems.
(400/88-01-02)
2.
Conclusion
Category:
2
3.
Recommendations
'n apparent
complacency
on the part of the licensee,
resulted
in
a lower category rating in this area.
Increased
emphasis
by the
licensee
is
warranted.
NRC staff
resources
applied
in the
18
routine inspection
program should
be mai'ntained
~
F.
Emergency
Preparedness
1.
Analysi s
During this
assessment
period,
inspections
were
performed
by
resident
and
regional
inspection
staffs.
The
regional
inspections
included
two routine inspections
and
an
emergency
response facilities (ERF) appraisal.
The licensee
had established
an effective emergency notification
and
communication
system,
consisting
of procedures,
equipment,
and trained staff to
make appropriate
notifications of offsite
agencies.
These
systems
included
the
Emergency
Notification
Systems
(ENS);
a
dedicated
Selective
Signaling
System;
and
backup
equipment
that
included
radio,
a
private
telephone
exchange,
a
microwave
system
and
commercial
telephones.
The
public
prompt notification
system,
consisting
of sirens
and
tone-alert radios,
was kept maintained
and tested.
The licensee
effectively implemented this program.
The
licensee
implemented
an
effective
system
for
emergency
detection
and classification,
based
primarily
on
the fission
product
barrier
concept,
but
also
including
anticipatory
initiating
conditions.
The
licensee's
protective
action
decision
making
was
based
on
NRC
criteria.
Individuals
responsible
for making protective action
recommendations
were
clearly identified.
The
licensee
demonstrated,
during
walk
throughs,
the ability to promptly identify and classify events
and
the
ability
to
make
appropriate
protective
action
recommendations.
The
licensee
maintained
an
effective
system
for
assuring
appropriate
onsite staffing
and for augmenting
onsite staff in
the event of an emergency.
The licensee
implemented
a system to
notify staff
when
needed,
including
pagers
and
a "call in"
program.
The
licensee's
unannounced
drill
of
shift
augmentations
showed
staff
could
arrive
onsite
within
an
appropriate
time after being notified at
home to respond to the
si te.
The licensee
maintained
an offsite dose
assessment
system that
included
computerized
dose evaluations
based
on measurements
of
effluents, plant parameters,
primary coolant activity levels
and
offsite monitoring results.
Source
terms
. were
developed
via
computer
evaluation
of post
accident
sample
results
of the
reactor
coolant,
containment
atmosphere
or containment
sump.
manual
methods
were used-to
develop
source
terms
using
other
plant parameters.
As
a backup for computerized
dose
assessment,
the
licensee
maintained
a
manual
system.
During
a
routine
19
inspection, it was
noted that there
was
a
need for additional
training
in
use
of
dose
assessment
procedures
by
both
radiological
personnel
and
reactor
operators
(who would
make
initial dose projections).
The dose calculations
were performed
slowly and resulted
in erroneous
doses
in two of three walk-
throughs.
Initially, the licensee
indicated that the expediency
of
these
calculations
was
not
relevant,
as
there
was
no
requirement
stating
dose projections
had to be calculated within
a
specified
time
period.
Further
discussions
between
the
licensee
and
Region II management
resulted
in the
licensee's
acknowledgement
of the
need for timely dose
projections.
The
licensee
then
pursued
aggressive
training
and
procedural
corrective actions that were found to be fully adequate
during
a
subsequent
follow-up inspection.
The
licensee
was
slow to
implement'
periodic
maintenance
program
on
Technical
Support
Center
(TSC)
door
seals.
The
licensee
agreed,
in June of 1986,
to perform
such
maintenance.
In August
1987,
the licensee
could not confirm whether
such
a
program
had
been
implemented.
In September
1987,
the licensee
implemented
a procedure
to routinely test
the
TSC pressure
and
habitability
systems.
The
TSC is powered
by two separate
sources.
In preparation for
the
ERF Appraisal,
the
licensee
determined
the
need
for
an
additional
power source
in the event of
a station blackout
and
determined
that
a
vendor-supplied
diesel
generator
could
be
supplied
and
made operational
in approximately
25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />.
The
licensee
agreed
to reanalyze
the
need for an additional
power
supply given the potential
impact of loss of
TSC function
on
station blackout.
The Emergency Operations Facility (EOF) is located approximately
3,400
meters
from the plant.
The. facility is
equipped
with
emergency
ventilation
(HEPA and charcoal)
to maintain the area
under positive pressure.
This degree of protection
exceeds
NRC
criteria,
which specifies
the
need
for only
HEPA filters.
The
licensee's
evaluation
of direct radiation
dose
showed
doses
would be maintained
below
GDC 19 criteria.
During the
recent
emergency
exerci se,
the
ventilation failed to
achieve
the
specified
0. 125 inches
of water differential
pressure.
The
licensee
identified
an
inleakage
path
from the filter train
drain
valves.
The
licensee
committed
to install
isolation
valves
on the drain lines.
1
The
licensee
implemented
an
appropr iate
public
information
program
that
included
dissemination
of
a public information
brochure
in
the
form of
a
calendar,
placement
of
public
information decals
on public telephones
and information signs.
In addition,
the
licensee
conducted
annual
media
education
20
seminars
and
distributed
special
information
brochures
to
school s.
The resident
inspector
observed
the routine
licensee
emergency
preparedness
training drills and
observed
limited portions of
the
annual
exercise.
The licensee's
performance
during
these
routine drills and
the exerci se
demonstrated
the capability to
implement
the
emergency
plan.
The
exercise
included
participation
by corporate
staff
and
management.
The
scenario
for
the
emergency
exercise
was
significantly
improved
as
compared with the
1987 exercise.
The
licensee
has
conducted
annual
audits
of
the
emergency
preparedness
program
by
the
Corporate
equality
Assurance
Department.
In addition,
the
licensee
evaluated drills
and
exercises
to identify areas
where
improvements
are
necessary.
Findings are tracked to completion of corrective actions.
No violations or deviations
were identified.
2.
Conclusion
Category:
2
3.
Recommendations
NRC staff resources
applied to the routine inspection
program
should
be maintained.
Security
1.
Analysi s
During
the
evaluation
period,
four routine
inspections
were
conducted
by region-based
inspectors
and additional evaluations
were conducted
by the resident inspector.
The
licensee
has significantly improved its compliance
record
since
the
last
period
through
increased
management
oversight
of
the
security
program,
plant
employee
security
education
and
increased
experience
on the part of the security
force.
The
one violation identified resulted
from
a misinterpretation
of the
term
"emergency
vehicle" following a
severe
snowstorm.
The violation does
not represent
either
a programmatic
breakdown
or
a lack of sensitivity to regulatory requirements.
The
licensee
aggressively
attacked
and
solved'hose
security
problems
which arose
shortly after licensing
through
a multi-
disciplined security task force.
These
problem areas
related to
21
vital
area
barriers,
compensatory
measures,
the
security
computer
system,
and removal of badges
from the Protected
Area.
Licensee
performance
in these
areas
during the
SALP 'period
has
been
noteworthy.
An On-Shift Training
Program
has
been
implemented
to enhance
security
force training.
This
program
has
provided
security
personnel
with some
200 training sessions
and
an equal
number of
security force drills.
Additionally, increased
tactical
force
and leadership
development
exercises
have
been
implemented.
The
licensee
is
examining
techniques
and
equipment
to
further
enhance
the effectiveness
of the tactical training program.
In
addition
to
the
Security
Training
Program
and
the
establishment
of the multi-disciplined
security
task
force,
management
involvement in this area
has
also
been
evidenced
by
the following:
( 1) quarterly
meetings
with corporate
security
are
attended
by all
three
CP&L nuclear
plant site
security
supervisors,
during which they
share
lessons
learned,
discuss
security
problems
and
encourage
uniform compliance
with
new
regulations;
and (2) the site security
supervisor
and security
chief are directly involved to provide oversight
on routine
and
nonroutine
events.
Where
needed,
and
as
appropriate,
these
individuals contact other on-site
and off-site security groups.
The
licensee
was
very
responsive
to
NRC
concerns
and
the
security program
has excellent
support at the plant
management
level
.
One violation was identified.
Severity
Level
IV violation for failure to search
vehicle
and
driver prior to entry into Protected
Area (400/88-05-01).
Conclusion
Category:
1
Recommendations
Although outside
the rating period,
the recent security access
control
problem
at
the Harris facility warrants
mentioning.
Accordingly,
increased
attention
in this
area
should
be
considered
to assure
performance
does not decrease
over the next
assessment
period.
NRC staff resources
applied to the routine
inspection
program should
be maintained.
22
H.
Outages
1.
Analysi s
During this assessment
period,
inspections
were performed
by the
resident
and regional
inspection staffs.
The licensee
formed
an outage
management
team in June
1987.
The
team was created
as
a support unit to aid other units within the
project's
organization.
The
team participated
in the
planned
outage
which was
conducted
during October
1987
and the forced
outage
which
was
conducted
during
March 1988.
During
the
October
outage
some
major
modifications
were
made
to
the
secondary
plant
systems
and
components.
These
included:
( 1) trimming the main feedwater
pump impellers; (2) changing
the
settings
on the main feedwater
pump low suction pressure
switch;
(3) modi.fying the air boosters for the main feedwater regulating
valves;
(4) removing
one
stage
from each
of the
heater
drain
pumps;
(5) modifying the main feedwater
pump recirculating flow
control line valves
(added flow restrictors);
(6) increasing
the
pressure
settings
for the
main
suction
which feeds
into the condensate
booster
pump control circuit; (7) adding
a
time
delay
to
the
condensate
booster
pump
high
discharge
pressure trip signal;
and other changes
to the controls for the
condensate
and main feedwater
pumps.
The
March outage
lasted approximately
one week and was required
in order to replace five of the bellows for the main turbine low
pressure
extraction
steam lines which failed during normal
power
operation.
.The licensee
determined
that all
eighteen
of ,the
bellows will be replaced
during the
upcoming refueling outage
with bellows that are manufactured with improved materials.
In
addition
to
replacing
the
five bellows,
some
of the
main
condenser
tubes required plugging,
as they were
damaged
when the
bellows failed.
Additional outages,
in excess
of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />,
occurred in order to
co~rect
problems
with
steam
generator
blowdown
valves
(July 16-22,
and September
12=14,
1987),
and to correct
a design
and analysis deficiency relating to the single failures
assumed
in
DC power supplies
(September
15-25,
1987).
During
the
outages
discussed
above,
the
outage
management
organization
coordinated
the efforts of the various
departments
involved to make certain the schedule
was realistic
and adhered
to, that necessary
personnel
and materials
were. available,
and
that inspections
'were conducted
by the site
gC department.
The
licensee
uses
the
Operating
Experience
Feedback
system
to
identify industry events
with potential
safety significance
to
the plant.
The licensee
has taken action
on potential
problems
in
advance
of the
issuance
of
a regulatory
mandate
to take
23
action.
Two
examples
include
the
short
term
inspections
of
reactor trip breakers
done in the October
1988 outage
and prior
to the
issuance
of
and
the
plan for
an
inspection
of the
incore
guide
tubes
in the first refueling
outage
in advance
of the issuance
Regional
based
outage
inspection
activity
involved
the
licensee's
as
a special
inspection
of the activities in response
to
From these
inspection efforts,
the inspectors
concluded
that the licensee
has
adequate
programs,
procedures,
and staffing in the areas
of
ISI and
IST.
In all areas
inspected,
the licensee
demonstrated
excellent
responses
to
NRC initiatives.
No violations or deviations
were identified.
2
~
Conclusion
Category:
1
3.
Recommendations
It was noted,
that while
a category
1 rating
was
assigned
to
this functional
area,
the licensee
had not
been
challenged
by
the
problems
associated
with
a refueling outage.
Accordingly,
NRC staff resources
applied to the routine inspection
program
should
be maintained.
I. 'uality Programs
and Administrative Controls Affecting Quality
l.
Analysi s
During this assessment
period,
inspections
were performed
by the
resident
and
regional
inspection
staffs.
Additionally,
a
Quality Yerification
Inspection
was
performed
during
this
assessment
period.
For the purpose of this assessment,
this area is defined
as the
ability of the
licensee
to identify
and
correct
their
own
problems.
It
encompasses
all
plant activities,
all
plant
personnel,
as well
as
those
corporate
functions
and
personnel
that provide services
to the plant.
The plant and corporate
staff have responsibility for verifying quality.
The rating in
this
area
specifically
denotes
results for various
groups
in
achieving quality,
as well as the performance of the
QA staff in
verifying that quality.
The content of the audit reports
and their related checklists
have
been
demonstrating
improvement
during
the
assessment
period.
The specifics
as to what
was
examined,
how examined,
sample
size
considered,
accept/reject
criteria
used,
and
the
acceptability
of the
audited
items
are
now routine checklist
comments.
The site
survei1 lance
group
performs
approximately
25<o
performance
based
type
inspections
(identifying safety-
related
hardware
problems).
An increase
in the percentage
of
performance
based
inspections
has
been
noted during the review
period.
Nanagement
has
become
more
active
with promptly correcting
identified problems.
This was demonstrated
by the project Vice
President
requiring that all
requests
for extending
response
times for Nonconformance
Reports receive his personal
approval.
This has
been effective in reducing
the
nunber nf requests
for
extensions.
The
resident
inspector,
as
part
of routine
inspections
in
various site activities,
evaluated
the administrative
controls
which may affect quality at the site.
The specific points which
were evaluated
included:
site
gC inspection
and surveillance
of
operations
and
maintenance
activities, control of nonconforming
materials
and
conditions,
gC holdpoint instructions,
and
the
licensee's
corrective
action
as it affects
repeat violations.
With the exception of the two violations discussed
below,
these
areas
appeared
satisfactory.
The first of the
violations
occurred
as
a result of the licensee
allowing repeated
breaching
of the containment building integrity.
The
second resulted
from
the
licensee's
fai lure to
take
prompt corrective
action
on
conditions
adverse
to quality.
This violation involved
a
known
problem with valves
installed
in
the
reactor
coolant
vent
system.
In June
1985
and
February
1987,
the
pl.ant experienced
problems with some of these
vent valves spuriously opening while
being tested.
The licensee
has
since
taken
steps
in an effort
to prevent these conditions
from recurring.
In
summary,
the licensee
had
demonstrated
both weaknesses
and
strengths
in identifying and correcting safety related
problems.
The ability to identify and correct safety related
problems
was
evidenced
by:
Implementation of a task force
recommended
improvements for
the
secondary
plant
(condensate
and
systems),
.
resulting in increased
plant performance, with no subsequent
trips attributed to secondary
system interaction.
Implementation
of
programs
to monitor plant
status
and
prevent
component
failures (i'
maintenance
feedback
program
and live load program),
involvement of operations
technical
support
in
plant
status
and
problems,
and
implementing
a
reactor
protection
system
specific
instrumentation
and control crew.
25
Improved
level
of operator
and
management
challenge
in
emergency drill scenarios.
The inability to either identify or once identified, correct
safety related
problems
was
shown in the following occurrences:
Inadequate
corrective action that led to repeat
breaching
of containment building integrity.
Untimely
corrective
action
in
resolving
operational
deficiencies
wi,th reactor
coolant vent system valves.
A
non-conservative
interpretation
of
Technical
Specifications
led
to
operating
with
a
stuck
open
containment isolation valve in the
blowdown
line for 29 days.
Two violations were identified.
a.
Severity
Level
IV violation for failure to prevent
a repeat
violation of breach
of the containment
building integrity
(400/87-40-01).
b.
Severity
Level
IV violation for fai lure to take
prompt
corrective
action 'on reactor
coolant
system
vent
valves
with known operational
defects
(400/87-40-03).
2.
Conclusion
Category:
2
3.
Recommendations
NRC staff resources
applied to the routine inspection
program
should
be maintained.
Licensing Activities
1.
Analysi s
The licensee
generally continued to exercise
management
control
and overview in the licensing activity area.
The licensee
had
frequent
meetings,
visits
and
management
discussions
with the
NRC staff which assisted
in
a clear
understanding
of safety
issues
and
the
need
for timely resolution.
There
was
a
reasonable
balance
between
the licensee'
resources
utilized to
improve plant performance/generation
and the resources
utilized
in the
enchancement/improvement
of overall
plant
safety.
The
licensee
recently assigned
an individual from the Central
Design
Organization
located
in Raleigh,
NC to coordinate
e'ngineering
activities with the Harris plant, to enhance
completion of plant
26
performance
objectives
from
both
safety
and
regulatory
considerations.
Although
the
licensee's
management
continued
to
be
heavily
involved, increased
emphasis
in the development
of the basis
in
a
few of
the
licensee's
initial
amendment
submittals
with
respect
to
the
"No
Significant
Hazards
Considerations
Determination"
would have further enhanced
the overall quality
of submittals.
Notwithstanding this observation,
the technical
quality
of
submittals
was
quite
good.
Moreover,
once
identified, additional
information was expeditiously provided.
During
this
assessment
period
the
licensee's
management
involvement
was
demonstrated
in various
issues
such
as its
response
to
a potential
single failure associated
with a D.C.
bus; participating
as
the
plant in removing
the
organizational
charts
from the
Technical
Specifications;
undertaking
an extensive effort to identify potentially suspect
pipe fitting material
in response
to
and
continued participation
in the Westinghouse
Technical
Specifi-
cation
Improvement
Program.
Moreover,
once
the
licensee
became
aware of the
need for the
issuance
of an
emergency
amendment
relating
to
a
diesel
generator,
coordination
was
promptly
initiated with the
NRC staff in order to provide sufficient time
to effectively process
the
amendment
request.
However,
in one
instance
a
non-conservative
interpretation
of the
Technical
Specifications
allowed
continued
operation
with
a
stuck
open
containment
isolation
valve
located
in
the
steam
generator
blowdown line for
a period of
29
days
without the
licensee
taking
compensatory
actions.
(See Violation d. in Section
IV.A
of this report.)
This indicates
there
may
not
be sufficient
controls to assure
proper management
of Technical Specification
interpretations
so that
operation
in
non-conservative
modes
without compensatory
measures
does
not occur.
The
licensee's
approach
to resolving technical
issues
from
a
safety
standpoint
was technically
sound
and
very
thorough
in
most instances.
The licensee's
management
actively pursued
an
aggressive
policy of quality control
on Technical
submittals/
amendments
which
generally
resulted
in
a quality
product.
'icensing
personnel
continued to demonstrate
a strong technical
understanding
of technical
issues
and usually were communicating
with the
NRC licensing Project
Manager
on
a daily basis.
This
interaction with the
NRC Licensing Project Manager
and other
NRC
staff resulted
in a clear understanding
of safety issues
and in
the timely submittal
of various licensing
and technical 'issues
and
minimization of
the
slippage
of mutually
agreed
upon
completion dates.
The licensee,
in cases
where generic
issues
arose,
utilized industry
owners
groups
to obtain
satisfactory
resolution.
27
The
licensee's
responses
to. NRC initiatives
were
prompt
and
generally
complete.
The licensee's
membership
in a significant
number of owners groups
was
an indication of their
commitment to
keep abreast
of acceptable
solutions of generic
issues
that were
applicable
to the Harris plant.
The licensee's
responsiveness
has
also
been
demonstrated
by timely submittals
on various
NRC
Bulletins and Generic Letters.
The licensee
promptly responded
to various
surveys, conducted during this rating period.
The technical
quality of the licensing staff assigned
to the
plant
was excellent.
There
were five full time individuals
assigned
to the various licensing activities'n
comparison
to
other facilities, the
number of licensing personnel
appeared
to
be
small;
but,
considering
their
very timely submittals
and
responsiveness
to
various
NRC initiatives,
the
number
was
adequate.
These
individuals
are
located
in
the
licensee's
corporate
headquarters
in Raleigh,
which is
.approximately
16 miles
from the plant.
This proximity to the
plant facilitated better
communication
and
understanding
of
plant objectives
and regulatory requirements.
In addition,
the
licensee
has extensive
laboratory capabilities
in the Energy
and
Environmental
Center
in very close
proximity to the
Shearon
Harris site.
These
groups
are
available
to
interface
on
licensing
issues
when
needed
and
performed quite well.
At the
end of the
assessment
period,
there
were
seven
individuals in
the
on-site
Regulatory
Compliance
Group
who
handled
the
day-to-day regulatory interface with the
NRC inspectors
and
NRC
Regional staff.
2.
No violations or deviations
were identified.
Conclusion
Category:
2
Trend:
Improving
3.
Recommendations
The licensee's
performance
in this 'functional area,
while. still
considered
good, declined early during, the
SALP period from the
previous
Category
I rating.
This decline
is attributed,
in
part, to the transition from construction
type licensing activi-
ties to operating activities.
Specifically, this was evidenced
by less
than
adequate
"No Significant
Hazards
Consideration
Determinations"
and
the
non-conservative
interpretation
of
Technical
Specifications.
The licensee's
performance
in the
latter part of the
SALP period indicates that these transitional
problems
may have
been
resolved.
28
K.
Training and Qualification Effectiveness
l.
Analysi s
Three
sets
of licensing
examinations
were administered
during
the
assessment
period.
The first of these
were
given
August
4-5,
1987,
to three Senior Reactor Operators
(SROs).
The
exams
involved all three
on the simulator
and
one
SRO oral.
All
three
passed
the respective
sections.
SRO license
examinations
were administered
November 18-19,
1987,
to four
SRO candidates.
Examination results yielded
a pass
rate
of 75io (3 of 4) for the
SRO candidates.
Initial license
examinations
were given to
11 Reactor Operators
(ROs)
and
a retake
given to one
on April 25-28,
1987, with
all of the candidates
passing their examinations.
Overall, the
pass
rate for all examinations
administered
during the
assess-
ment period was
95/o (18 of 19).
An inspection
was performed to assess
the licensee's
compliance
with Generic Letter 81-21
involving the
upper
head
voiding
during
the
Natural
Circulation
Cooldown
at
St.
Lucie.
The
inspection
reviewed the training curriculum
as well
as attend-
ance
and test
records.
The training curriculum was comprehen-
sive,
the records
were complete,
and all licensed operators
had
received
the required training in this area.
As
indicated
under
the
specific
functional
areas,
training
activities
encompassed,
to
an extent,
all
areas.
To
reduce
plant trips
caused
be
personnel
error, intensified "Real Time"
training was
used
by the Operations
group to acquaint
operators
with revisions
to
procedures
and
lessons
learned
'which
have
resulted
from plant events
and
incidents.
Training
conducted
under
the
general
employee
radiation
program,
as well
as that
given under the health physics technician's training program was
found
to
be
acceptable.
The fire
protection,
emergency
preparedness,
and
security
groups all. made
use
of frequent
trai ning
and
drills/exercises.
When
made
aware
of
the
importance for expedient initial dose calculations,
the licensee
aggressively
trained
all
applicable
reactor
operators
and
radiological
personnel.
In the
case
of security,
an on-shift
training
program
had
been
implemented
during
the evaluation
period.
Under this
new program,
some
200 training sessions
and
an equal
number of drills had
been
conducted
to enhance
security
force training.
Training program weaknesses
were identified in
the
area
of environmental
qualifications
(EQ).
In recognition
of these
weaknesses,
the licensee
had
begun
development
of
lesson
plans
for
indoctrination
and
training
of personnel
towards the
end of the evaluation period.
No violations or deviations
were identified.
29
2.
Conclusion
Category:
1
3.
Recommendations
None.
L.
Engineering
Support
1.
Analysi s
This area
was routinely evaluated
by the resident
inspector
and
the regional staff.
Also, special
inspections
were conducted
in
the areas
of equipment qualification (Eg) and design
changes.
Until early 1988,
the licensee
operated
two separate
engineering
organizations
at
the site.
One of the organizations,
Harris
Plant
Engineering
Section
(HPES),
reported
to
the
Milestone
Completion Manager.
HPES performed
as
a design
group to support
the initial start-up efforts and to complete
any remaining major
design 'efforts.
Upon completion of these
design responsibilities,
management
reorganized
the design
organization
to require that
all design efforts
be
conducted
through
the off-site Central
Design Organization.
This group
wi 11 act
as
the
A/E and
wi 11
reduce
the
licensee's
reliance
on
outside
consultants
and
temporary
personnel.
The staffing of the
engineering
design
organization
was
more
than
adequate.
The
training
and
qualification of design
personnel
was quite good
as demonstrated
by the
large
number
of design
personnel
who
have
obtained
professional
registration
by
examination
and
advanced
engineering
degrees
from accredited
universities.
Part of the
responsibilities
of this design
group
includes
managing
the
Eg
maintenance
program.
The
second
engineering
support
group
is
part
of
the
site
organization
for plant
operations.
The
group,-
Operations
Technical
Support,
reports
to the Plant
General
Manager.
This
group
has
been very active with numerous technical
issues
which
relate to the plant and its systems.
Some of the. specific areas
in
which
they
have
'provided
technical
guidance
include:
investigating
more
than
40 issues
which relate
to Limitorque-
supplied
motors;
the
erosion/corrosion
program
which
was
implemented
early during this
SALP period;
and
guidance
for
operations
technical
trends.
They provided considerable
input
to the plant maintenance
work request
system to aid in setting
up
a method for priority based
on plant safety
and reliability.
They review each
work request
to maintain
awareness
of plant
problems
and to maintain their sensitivity to the
need to assure
plant safety.
-This group has
been
very beneficial
to the
safe
operation'f the Harris plant.
30
During this
assessment
period,
several
significant deficiencies
in design, installation,
and fabrication were addressed
in LERs.
One of the significant events
was
the determination
that the
loss of a specific
DC bus coincident with loss of offsite power
would result
in isolation
of the auxiliary
system
(87-054).
Another event
involved the potential
for excessive
flow rates if only
one
low
head
safety
pump is operating
following switchover to the recirculation
mode after
a
large
break
LOCA (88-001).
In the two situations
discussed
above,
the
license'e
took
necessary
actions
to correct
the
identified
deficiencies.
A potentially more serious situation
was noted in
the
low temperature
overpressure
prctection
system
which would
automatically actuate
the relief valves
under steamline
break or
steam
generator
tube
rupture
accidents
coincident
with
a
specific single failure (88-011).
The automatic
arming of the
protection
system
was
removed to correct this situation.
In
March 1988,
a
special
inspection
team
evaluated
the
licensee's
program.
The
points
evaluated
during
the
inspection
included:
. the
licensee's
implementation
of
10 CFR 50.49, plant walkdown inspections
of electrical
equipment
within the
scope of 10 CFR 50.49,
and
a follow-up on previously
identified
EQ deficiencies.
The
team
found
the
licensee's
programs
and procedures
for the
EQ program to be acceptable
and
no violations were identified by the inspectors.
Licensee
management
appeared
to
be
sensitized
to
the
significance
and
importance
'of having
an
adequate
EQ Program.
The
licensee
identified during
the
entrance
meeting
several
planned
EQ program enhancements
(some of which were in-progress
during the inspection)
which were to be incorporated into the
Program
lessons
learned
from the Brunswick and
Robinson
NRC
Audits.
This information would enhance
Harris
EQ. procedures
and
data
packages,
and
increase
awareness
training for plant
personnel.
In most
cases,
licensee
responses
to
NRC initiatives
on
issues (i.e.,
IENs/IEBs) have
been timely with technically
sound
and
thorough
responses.
One
exception
was
the
licensee's
failure to identify and establish qualification of crimped type
connectors
in Limitorque dual voltage motors.
The
EQ maintenance
program was reviewed
by examining maintenance
procedures,
maintenance
histories
of
equipment,
and
preventive maintenance
schedules.
These
documents
were compared
with the
requirements
set
forth
in
the
Qualification
Data
Packages
(QDPs)
and
were
found
to
be
well
organized
and
controlled,
as well as,
accurate
and acceptable.
The
schedule
for replacement
of EQ equipment at the
end of its qualified life
was
also
reviewed
and
found acceptable.
Problems
previously
identified in the
EQ maintenance
area
were corrected
in a timely
manner.
31
During
the
later
part
of
1987,
a
special
gA effectiveness
inspection
reviewed
the
area
of design
changes,
Inspectors
reviewed
17
design
changes,
reviewed
engineering
and
10 CFR 50.59 evaluations,
performed
some
system walkdowns,
and reviewed
Design
basis
documentation
was
also
reviewed
and
determined
to
be excellent.
In all, the
Design
Change
program
was considered
to be adequately
controlled,
with
the exception of one design
change that did not provide adequate
detail
of protective
and control
functions for fuse
removal.
This
lack
of
detai l
caused
a
A violation
(identified as
a.
below) was issued
in this area.
A review of IE Bulletin 85-03
program indicated
some corporate
" involvement
in site activities
in that
problems
encountered
during
the
performance
of other
CPE L facility Bulletin 85-03
programs
have
also
been
evaluated
for applicability to Shearon
Harris.
For example,
the circuit logic problem associated
with
DC motor operated
valve actuators
was originally identified at
the Brunswick facility, but was also
found to
be applicable
at
Shearon
Harris.
The procedures
that
govern
the Bulletin 85-03
program
were well stated,
controlled,
and explicit. .It was
apparent
that
when
IE Information Notices
were
issued
that
address
motor
operated
valve
problems,
the
licensee
revised
applicable
procedures
to
recognize
the
IE Information
Notice
condition.
The licensee's
development of the
program
was viable but lacked thoroughness
in that motor operated
valve
operation
at
degraded
voltages
and
testing
for inadvertent
backseating
should
have
been
considered
but
were
not.
The
bulletin program action
items
by the
licensee
were
completed
prior to the bulletin deadlines.
The final response
was
due by
January
1988,
and the
Shearon
Harris final response
was
issued
on March 1987.
During the evaluation period,
two inspections
were conducted
by
regional
based
inspectors
to followup on allegations
pertaining
to alleged
improper design
practices.
None of the allegations
were substantiated.
These allegations
concerned
improper design
verification practices
in design of structural
steel.
During
the inspection effort,
one violation was identified concerning
fai lure tn follow design
control
procedures
in design of cable
tray supports.
This violation was not directly related
to the
allegations.
Licensee
management
was extensively
involved in design
review
activities required to resolve the concerns
(allegations).
This
involved retaining consultants
to perform
an
independent
study
of structural
steel
design methodology,
and assigning
personnel
to
perform
in-depth
review
of
structural
steel
design
calculation
and prepare alternate calculations.
Decision making
in
these
activities
was
at
a
level
which
ensured
adequate
management
review.
Records
(design calculation
packages)
were
complete,
well
maintained,
legible
and
retrievable.
The
32
licensee's
approach
to resolution of the concerns
from a safety
standpoint
demonstrated
a clear understanding
of the issues,
and
a
technically
sound,
conservative
and
thorough
approach.
Responsiveness
to these
NRC initiatives resulted in timely
resolution of the concerns.
Two violations were identified.
a.
Severity Level
IV violation for failure to provide adequate
detail
of. protective
and
control
functions
for
fuse
removal.
(400/87-38-02)
b.
Severity
Level
IV violation for design engineering failing
to identify the
reasons
why the
design
basis
accident
temperature
values
were
changed
when calculating
thermal
stresses
in the containment
building for
LV-66,
a
cable
tray riser frame.
(400/87-41-02)
2.
Conclusion
Category:
2
Trend:
improving
3.
Recommendations
NRC staff resources
applied to the routine inspection
program
should
be maintained.
V.
SUPPORTING
DATA
A.
Licensee Activities
The plant operated
in its first fuel cycle throughout the assessment
period.
The plant
achieved
commercial
operation
on
May 2,
1987,
prior to the beginning of the assessment
period,
and operated
at
an
coverall
availability of
83 percent
and
a capacity
factor of
80
percent.
The operation
included
two periods of continuous
operation
in excess
of 120 days.
Outages
in excess
of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />
occurred
in
order to correct problems with steam generator
blowdown valves (July
16-22,
and
September
12-14,
1987),
to correct
a design
and analysis
deficiency relating to the
single
failures
assumed
in
power
supplies
(September
15-25,
1987),
and to correct failure of turbine
extraction
steam bellows (March 20-27,
1988).
Each of these
outages
was initiated by
a controlled
shutdown of the plant.
A scheduled
outage
was
conducted
October
9-November
7,
1987.
The
purpose of the outage
was to complete
visual
inspection
of snubbers
required
by Technical Specifications,
to complete other survei llances
which would allow continued
operation
to the
scheduled
refueling
outage,
and to install major modifications to the main feedwater
and
.condensate
systems.
The latter item completed the
implementation
of
33
recommendations
of
a licensee
task force which was initiated during
the power ascension
test
program to investigate and'esolve
the root
cause
of control
instabilities
in
the
and
condensate
systems.
The net result of these
changes
was
improved reliability
from these
secondary
systems.
Consequently,
none of the six reactor
trips which occurred
in the twelve months of this
SALP period
were
due to secondary instabilities.
B.
Inspection Activities
During the
assessment
period,
routine inspections
were performed
by
the
resident
and
regional
staffs.
Special
team
inspections
were
conducted
in
the
areas
of
Equipment
gualification
and
guality
Assurance
effectiveness.
An emergency
response
facilities appraisal
was conducted during the partial participation
emergency
exercise.
C.
Investigation
Review
None
D.
Escalated
Enforcement Actions
1.
Civil Penalties
No escalated
enforcement
actions
were issued during this period.
2.
Orders
None
E.
Management
Conferences
September
17,
1987
Management
meeting
at
Bethesda,
to
discuss
the Technical
Specification
improvement
program
as it relates
October
1,
1987,.
Management
meeting
at
the
Harris
Energy
and
Environmental
Center for a discussion
of the
Board assessment.
October
21,
1987
Enforcement
Conference, at
Region II to discuss
the
loss of steam
generator
blowdown isolation
capability
between
August
13
and
September
13,
1987,
and
a technical
meeting
at
Region II to
discuss
a
power
design
problem
affecting
auxiliary
flow.
(SL
IV violation
issued.)
34
November 20,
1987
I
June
7,
1988
Enforcement
Conference
at
Region II to review
operator
actions
during
the
conduct
of
a
Technical
Specification
surveillance
test of the
reactor
coolant
system
vent
valves.
(SL
IV
violations issued.)
Management
meeting
at
Region II
to
discuss
identified problems
at all three
CP&L sites
and
to
reveal
plans
and establish
goals
to achieve
overall excellence.
F.
Confirmation of Action Letters
None
G.
Licensee
Event Reports
(LERs)
During the
assessment
period,
43
LERs for the unit were
issued
and
analyzed.
The distribution of these
events
by cause,
as determined
by the
NRC staff,
was
as follows:
Cause
Component Failure
Design
Cause
Number
10
Number
Construction,
Fabrication,
or
Installation
Personnel
- Operating Activity
Maintenance Activity
Test/Calibration
Personnel
- Other
Out of Calibration
Other
43
TOTAL
H.
Licensing Activities
Licensing
actions
during this assessment
period included:
Initial
Test Program, Quality Assurance
Program,
Accumulator Instrumentation,
Reactor
Coolant System
Vent Valves,
and
ASME Section
XI Relief.
35
There were five license
amendments
issued.
One, involving the diesel
generator,
was
an
emergency
amendment.
The others
involved the
system
vent block valves,
removal
of organizational
charts
from TS, storage
and handling of higher enriched fuel,
and the
physical security plan.
In support of the licensing activities, thirteen meetings
took place
to discuss
licensing
issues
and
other
matters
such
as
AFW System
Logic Changes
and Natural Circulation Cooldown Analysis.
I.
Enforcement Activity
FUNCTIONAL
AREA
NO.
OF DEVIATIONS AND VIOLATIONS IN EACH
SEVERITY LEVEL
Dev.
V
IV
III
II
I
Plant Operations
Radiological Controls
Maintenance
Surveillance
Fire Protection
Emergency
Preparedness
Security
Outages
Licensing
guality Programs
and
Administrative Controls
Affecting (}uality
Training
Engineering
1
8
1
1
TOTAL
2
15
During this
assessment
period
the plant. experienced
four reactor
trips with reactor
power greater
than
15/<.
July 9,
1987 - Operations
personnel
pulled the wrong fuse which
caused
the closure of feedwater regulating valve for "C"
(S/G), resulting in an automatic reactor trip
from 100io power due to S/G low-low level coincident with steam
flow/feed f1 ow, mi smatch.
36
August 4,
1987 - Following repairs to instrument air dryer
18,
incorrect clearance
valve lineup resulted in inadvertent
isolation of instrument air compressors
which allowed
various valves to close resulting in main feedwater
pump
trips followed by an automatic reactor trip from 100/.'ower
due to S/G feedwater/steam
flow mismatch coincident with low
S/G water levels.
November 8,
1987 .- Control switch for condensate
recirculation
valve was incorrectly positioned
causing
condensate
pump,
condensate
booster
pump,
and main feedwater
pump to trip, .
resulting in loss of all feedwater,
and
a manual reactor trip from 22,". power.
Parch 9,
1988
Loose
end cap
on
a replaceable
fuse caused
the
"B" feedwater regulatory valve to fail shut,
causing
a low
S/G water level.
Reactor trip from
100K< power followed, due
to
a feedwater/steam
flow mismatch coincident with low S/G
,water level.
One reactor trip occurred with reactor
power less
than
15:o as
identified below:
November 7,
1987 - Due to an inadequate
procedure,
an incorrect
setting
on steam
pressure
control.ler caused
excessive
and rapid cycling of the
steam
dump valves, resulting in an
automatic reactor trip from 4.5Fo power due to low main
steam
line pressure
on "A" S/G.
One reactor trip occurred with the unit subcritical
as indicated
below:
September
24,
1987
While implementing
a plant modification
on
a process
instrumentation
control cabinet,
the wrong
fuse
was
removed
due to i.nadequate
design information.
This
caused bistable
PS-447E to be deenergized,
resulting in an
automatic reactor trip.
K.
Effluent Summary for 1987 - Activity Releases
(Curies)
1.
Gaseous
Effluents
Fission
and Activation Gases
Iodine and Particulates
1.17
E+3
4.43
E-6
2.
Liquid Effluents
Fission
and Activation Products
9.08 E-1
1.96
E+2