ML18005A511

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Insp Rept 50-400/88-11 on 880420-0520.Violations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Maint Observation & Emergency Response Facilities Appraisal
ML18005A511
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 06/16/1988
From: Fredrickson P, Maxwell G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18005A505 List:
References
50-400-88-11, NUDOCS 8807130322
Download: ML18005A511 (14)


See also: IR 05000400/1988011

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, NW.

ATLANTA,GEORGIA 30323

Report No.:

50-400/88-11

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC

27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

April 20

May 20,

1988

License No.:

NPF-63

Inspector

G.

F

Max

e

Date Signed

Approved by:

P.

E. Fredrickson,

Section Chief

Division of Reactor

Projects

Date Signed

SUMMARY

Scope:

This routine,

announced

inspection

involved inspection

in the areas

of Operational

Safety Verification, Monthly Maintenance

Observation,

and

Emergency

Response

Facilities Appraisal.

Results:

In the

areas

inspected,

one violation was identified

Failure to

Control

System

Configuration

During

a

Test

of

the

Solid

State

Protection

System

Paragraph

2.b.

8807l30322

880622

PDR

ADOCN. 05000400

8

PNU

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

J.

M. Collins, Manager,

Operations

G.

L. Forehand,

Director,

QA/QC

J.

L. Harness,

Plant General

Manager

C.

S. Hinnant,

Manager of Maintenance

J.

R. Sipp,

Manager,

Environmental

and Radiological

Control

D.

L. Tibbitts, Director, Regulatory

Compliance

R.

B.

Van Metre,

Manager,

Harris Plant Technical

Support

R. A. Watson,

Vice President,

Harris Nuclear Project

Other

licensee

employees

contacted

included

technicians,

operators,

mechanics,

security

force

members,

engineering

personnel

and

office

personnel.

Acronyms

and

initialisms

used

throughout

this

report

are

listed

in

paragraph

6.

2.

Operational

Safety Verification (71707,

71710,

93702)

Plant Tours

The inspector

conducted

routine plant tours during this inspection

period to verify that the

licensee's

requirements

and

commitments

were

being

implemented'hese

tours

were

performed to verify the

following:

systems,

valves,

and

breakers

required

for safe

plant

operations

were in their correct position; fire protection equipment,

spare

equipment

and

materials

were

being

maintained

and

stored

properly;

plant

operators

were

aware of the current plant status;

plant operations

personnel

were

documenting

the

status

of out-of-

service

equipment;

security

and health

physics controls

were

being

implemented

as required

by procedures;

there

'were

no

undocumented

cases

of unusual fluid leaks,

piping vibration,

abnormal

hanger

or

seismic

restraint

movements;

and all

reviewed

equipment

requiring

calibration'as

current.

Tours

of

the

plant

included

review of site

documentation

and

interviews with plant personnel.

The inspector

reviewed the shift

foreman's

log, control

room operator's

log, clearance

center tag out

logs,

system

status

logs,

chemistry

and

health

physics. logs,

and

control

status

board.

During these'ours

the iospector

noted that

the

operators

appeared

to

be alert

and

aware

of changing

plant

conditions.

The

inspector

evaluated

operations

shift turnovers

and

attended

shift briefings.

He

observed

that

the

briefings

and

turnovers

provided sufficient detail for the next shift crew.

The

inspector

verified that

various

plant

spaces

were

not

in

a

condition which would degrade

the

performance

capabilities

of any

required

system

or component.

Site security

was evaluated

by observing

personnel

in the protected

and vital areas

to ensure that these

persons

had the proper authori-

zation to be in the respective

areas.

The security personnel

appeared

to be alert and attentive to their duties

and those officers performing

personnel

and

vehicular

searches

were

thorough

and

systematic.

Responses

to security

alarm conditions

appeared

to

be

prompt

and

adequate.

b.

Solid State Protection

System Testing

On

April 22,

during

a

routine

daily

review of

EIRs,

licensee

Regulatory

Compliance

personnel

identified

an

instance

where

TS 3.0.3

was violated.

The event

occur red

on April 19, with the plant

at

100% power.

The "A" train automatic trip logic, which is part of

the

SSPS,

was

being tested.

The

SSPS test

began

at

1: 10 p.m.,

and

ended at 2:26 p.m., lasting

a total of one hour,

16 minutes.

Mhen

the

"A" train

SSPS

test

was

being

conducted,

the

following

mechanical

components

associated

with the "8" train were not fully

operable:

The

"8"

emergency

service

water

pump

had its

power

supply

circuit breaker

"racked

out".

The breaker

was

racked

out to

allow maintenance

personnel

to conduct

a loop calibration

on

a

discharge

pressure

transmitter.

This work started at 10:00 a.m.,

on April 19 and was completed at 2:35 p.m.

The

control

room "8" train

emergency filtration system

was

shutdown for preventive

maintenance

on the power breaker cubicle

and

a surveillance

test to measure

heater

capacity.

Due to the

work on

the

breaker

cubicle,

the

"8" control

room

emergency

filtration system

could

not

have

functioned until its

power

breaker

wad

reclosed.

This

work started

at

8:00 a.m.,

on

April 19 and was completed at 3:45 p.m.

The

"8" train

reactor

auxiliary

building

emergency

exhaust

system

had

two outstanding

clearances

against it.

The

work

associated

with

these

clearances,had

been 'ompleted.

The

clearance

tags

were

in

the

process

of being

removed;

at

2:56 p.m.,

on April 19 they were removed.

TS Table 3.3-3,

Action Statement

14,

Page

3/4 3-26,

allows

one of

the

two

SSPS trains to

be in the test

mode for up to

two hours,

provided

the

other train

is

operable.

If the

other train

is

inoperable,

as

on April 19,

then

TS 3.0.3,would

apply.

TS 3.0.3,

when

entered,

requires

that

the associated

Action requirements

be

completed within one

hour

or

steps

should

be

taken

to place

the

plant in

a reduced

mode.

As noted

above,

the plant

was operating

under

the condition of

TS 3.0.3

for greater

than

one

hour,

and

operators

failed to recognize

during that time that the plant

was

required

to begin reducing

power to change its mode of operation.

The inspector

evaluated

the shift foreman's

log

and

EIRs for each

time that

MST I001 (Train "A" SSPS Actuation Logic and Master Relay

Test)

and

MST I0320 (Train "B" SSPS Actuation Logic and Master Relay

Test)

were

implemented

during

the past twelve months

on the "A" and

"B" SSPS trains.

Records

show that the

"B" train

SSPS

tests

were

conducted

during

1987

on

May 15, July 26,

September

22,

November

16,

.'and during

1988

on January

18

and

March 21.

When these

tests

were

conducted,

all

of

the

associated

"A" train

SSPS

equipment

was

available for operation.

Records

indicate

that

the

corresponding

"A" train

SSPS

tests

were

conducted

during

1987

on

June

18,

August

18,

October

23

and

December

17,

and

during

1988

on

February

19.

The

"A" train test

on August

18,

1987,

was

conducted

between

8:55 a.m.

and

10:20 a.m.

The

EIR and shift foreman's

logs for the

"B" train equipment

show

that the "B" train

ESW pump was in an inoperable

status

from 8:57 a.m.,

on August 17,

1987, until 4:55 p.m.,

on August 19,

1987;

thus,

the

unit

had

entered

TS 3.0.3

during this test

also.

The

pump

was

declared

inoperable

due to

a packing

replacement

for its associated

screen

wash

pump.

The screen

wash

pump provides

seal injection flow-

for the associated

ESW pump.

Consequently,

there

have

been

at least

two separate

instances

where

the plant

was

operating

unknowingly

under

the

requirements

of

TS 3.0.3 while the

SSPS

system

was being tested.

Normally,

operations

pe'rsonnel

have

relied

on

the

following two

methods of assuring

that

a

system is not placed

in

a configuration

where

redundant

components

are

simultaneously

and/or inadvertently

out of service:

The first method

involves

the

applicatio'n

of the

Operations

Management

Manual

procedures:

OMM-001,

Rev.

4,

Operations-

Conduct of Operations,

and

OMM-003, Rev.

2, Equipment Inoperable

Record.

These

procedures

require

the shift foreman to review

Work Requests

of other activities in general,to

assure

compliance

with TS requirements.

,When carrying out this task

he normally

reviews the open

EIRs and,

when in doubt,

asks his subordinates

and peers if they

know of any

reasons

that

a job, test,

etc

,

should not be conducted.

The

second

method involves the

use of Operations

Work Procedures

when conducting

complex plant system

and logic testing.

In this

application,

an

OWP is

used

to establish initial plant/system

configuration for

a

surveillance

test;

then

once

testing

is

complete,

the

OWP returns

the plant/system

to normal.

Usually,

these

OMPs contain specific cautions either by directly cautioning

the procedure

user and/or through specific procedure application.

The procedure

may contain specific checklists or steps

which by

application

would prevent

an inadvertent

defeat of a system or

component's

safety function.

Procedure

OMM-003,

noted

under

the first method

described

above,

provides

guidance

to operations

clearance

personnel.

Its purpose is

to ensure

compliance with

LCOs.

As found in the

TS, this includes

identification,

tracking,

evaluating,

and initiating the

reports

which may be required

by the

LCOs.

However, it should

be noted that

OMM-003 does

not contain

the specific cautions

and/or checklists,

etc.,

which

may

be

contained

in

an

OWP

~

Operations

clearance

personnel

have relied

on the

OWPs to contain sufficient safety nets

to prevent

inadvertent

loss

of

two

redundant

components

during

testing.

Therefore,

they apparently

did not question

allowing the

SSPS

train

"A" tests

to

be

conducted

on

August 18;

1987,

or

on

April 19,

1988,

even

though

some

of the

"B" train

SSPS

activated

equipment

was out of service.

These

events

occurred

because

operations

personnel

did not realize

that

when- actuation

logic equipment

in

an

SSPS train is placed out

of service, all emergency

equipment for the opposite

SSPS train must

be available.

The associated

Operations

Work Procedure,

OWP-RP-17,

Reactor Protection Automatic Trip Logic,

Rev.

1,

should

have

helped

prevent

this

condition

from occurring,

but did not specifically

address

the requirement for redundant train equipment

being operable.

The inspector

evaluated, eight of the remaining

OWPs to assure that,

as

applicable,

they contained

statements

cautioning

operators

that

redundant

equipment

must

be

operable

when

the

OWPs

are

being

conducted.

Those procedures

evaluated

are

as follows:

OWP-RP-16,

Rev.

1, Reactor Trip Breaker;

OWP-AF-Ol, Rev.

1, Auxiliary Feedwater

Pump

1A-SA;

OWP-AF-02,

Rev.

1, Auxiliary Feedwater

Pump

1B-SB;

OMP-AC-01,

Rev.

1,

AC Electrical Uninterrupted

Power Supply

UPS

Channel I;

OWP-CS-Ol,

Rev.

1,

Chemical

and

Volume Control

System Charging

Pump

1A-SA;

OWP-CT-01,

Rev.

1, Containment

Spray

Pump lA-SA;

OWP-DG-01,

Rev.

1, Diesel Generator

Number

1A-SA; and

OWP-ESF-01,

Rev.

1,

ESFAS

Containment

Pressure - Circuit

Components.

The procedures

implemented

by the licensee failed to assure

that the

plant

was maintained

in

a

safe configuration

when the

SSPS

system

was .being

tested.

The

inspector

informed

the

licensee

that

the

preceding

examples

demonstrate

that procedures

for controlling tests

conducted

on

the

SSPS

system,

and

therefore

system

configuration

control

procedures,

are

inadequate.

This is

a violation, Failure

to Control

System Configuration

During

a Test

of the

Solid State

Protection

System,

50-400/88-11-01.

c.

Low Temperature

Over Pressure

Protection

On May 11, while the plant was operating at

100% power,

the licensee

made

a

10 CFR 50.72 report to the

NRC Duty Officer.

The notification

was to make the

NRC aware of a potential

unanalyzed

condition regarding

the

plant

low temperature

over pressure

protection

system

(LTOP).

The unanalyzed

condition was brought to the attention of the licensee

earlier during the day by Westinghouse

Electric Corporation

personnel,

the supplier for the plant

NSSS.

LTOP utilizes

the pressurizer

PORVs to protect

the reactor

vessel

from

overpressurization

when

the

plant

is

operating

at

low

temperatures

of 335 degrees

F or less.

The

LTOP system is not needed

when the temperature

is greater

than

335 degrees

F.

When the plant

is operating

at temperatures

greater

than

335 degrees

F,

the

PORVs

are

controlled

to

open

at

pressures

to relieve

the

RCS

pressure

during

design

transients.

Operation

of the

PORVs

minimizes

the

undesirable

opening

of the

spring-loaded

pressurizer

Code

Safety

Valves.

LTOP, at the Harris Plant,

was designed

to be automatically in effect

when the control

switches for the

two affected

PORVs are

placed

in

the

automatic

position

and

one

of the

two, affected

wide

range

temperature

detectors

indicates

a reactor coolant temperature

of 335

degrees

F or less.

The

remaining

PORV is unaffected

by the

LTOP

controls.

Likewise,

the

three

Code

Safety

Valves

are

unaffected

by the

LTOP circuit.

The Westinghouse

unanalyzed

scenario

postulated

a condition where

a main

steam line break accident or major

S/G tube

rupture

accident

coincident with

a single failure of either of the

two

LTOP

RCS wide range

temperature

channels

may allow the plant

temperature

in the affected

S/G to drop to

335 degrees

F or less,

thus

arming the

LTOP circuit in 'the faulted loop

and with the other

temperature

detector failed,

LTOP would actuate.

Thus, this would

even further drop

RCS pressure,

perhaps

into an unsafe

DNB condition.

0

To reduce

the likelihood of this condition from occurring,

on Nay

11

the

licensee

placed

the control

switches for the two affected

PORVs

in the "shut" position

and placed

caution

tags

on the

switches

to

advise

the operators

that the

two switches

must

be manipulated

from

the main control board

by the operators if they wished to

open

the

two

PORVs thus eliminating the ability of the

LTOP system to activate

these

two

PORVs if a scenario

occurred

similar to that

proposed

by'estinghouse

above.

Also, placing

these

two switches

in the "shut"

position turned off all automatic controls for these

two PORVs.

The licensee

determined

that the plant would be in

a

more suitable

condition if the

LTOP system

was electrically disconnected

from the

normal

PORV control circuit and

the

switches for the

two affected

PORVs

were

returned

to

the

"automatic" position.

On

May 13

the

control circuits for the

LTOP system

were

disconnected

(the

cards

were

unplugged)

and

the

switches

for the

affected

valves

were

returned to the "automatic" position.

Currently the licensee

plans to make

some

permanent

design

change

to

the

LTOP control

system

to allow it to

be manually turned off at

temperatures

greater

than

335

degrees

F.

The

inspector

discussed

the preceding

event with the licensee,

Region II management,

and

NRR

management.

As

a result

the inspector

'concluded

that the licensee

took satisfactory

corrective

steps

upon notification by Westinghouse

of this unanalyzed

condition.

d.

Emergency

Service Water

Pump

While the plant

was operating

at

100%

power

on

May 13,

a condition

occurred

in which both

ESW

pumps

were considered

inoperable.

This

placed the plant in

a condition

under

TS 3.0.3,

which required

the

plant to begin changing

modes within one hour.

The event lasted only

ten minutes

and therefore

the licensee

was within full compliance of

this

TS requirement.

The

NRC Duty Officer was

made

aware of this

condition by the licensee.

The event resulted

from the "A" ESM seal

water booster

pump being declared

inoperable

due to its suction

and

discharge

valves failing to properly shut,

thus

making the

"A"

ESW

pump

inoperable.

The

"B"

ESW system

had previously

been

declared

inoperable for repairs

on its

ESW booster

p'ump valves.

The techni-

cians

took

immediate

steps

to

make

adjustments

to both of the

affected

"A" ESW seal

water booster

pump valves

by cycling the valves

and flushing the valve seats.

Within ten minutes

the

"A"

ESW seal

water booster

pump,

and therefore

the "A" ESW pump,

were returned to

operable

status.

The plant

was

then

no longer operating

under

the

condition of TS 3.0.3.

Except

as

noted

in paragraph

2.b,

no other violations or deviations

were

identified in the area's

inspected.

3.

Monthly Maintenance

Observation

(62703,

37700)

The inspector

reviewed

the licensee's

maintenance

activities during this

-inspection

period to verify the following:

maintenance

personnel

were

obtaining

the

appropriate

tag

out

and

clearance

. approvals

pri'or to

commencing

work activities, correct

documentation

was available for all

requested

parts

and material prior to use,

procedures

were available

and

adequate

for the work being

conducted,

maintenance

personnel

performing

work activities

were qualified to accomplish

these

tasks,

no maintenance

activities reviewed were violating any limiting conditions for operation

during the specific evolutions;

the required

QA/QC reviews

and

QC hold

points

were

implemented;

post-maintenance

testing

activities

were

completed;

and

equipment

was

properly

returned

to service

after

the

completion of work activities.

The following specific activities

were

evaluated:

The

inspector

evaluated

work associated

with

WR 88-AKUGl and

WR

88-AKUT1 which required

unplugging

the electrical

control circuit

cards

on

the

LTOP

system.

The circuit was

located

in process

instrumentation

cabinets

PIC-8 and PIC'-5.

Once unplugged,

the cards

were

tagged

in

accordance

with

the

controlling

Administrative

Procedure

to assure

that they were properly controlled.

The

work associated

with

WR

88-ABSF5

was

evaluated.

The

WR was

generated

to require that repairs

be conducted

to stop

a body-to-

bonnet leak which developed

on

an auxiliary feedwater

system

valve.

The valve

was identified as

lAF-155,

an isolation valve associated

with the

"A" steam

generator

preheater

bypass.

The valve provides

isolation

between

the auxiliary feedwater

piping leading to the "A"

steam

generator

and the

chemical

addition

system

piping which

has

been

installed

for

the addition of hydrazine.

The

work activity

required drilling a hole in the valve bonnet

and injecting

a liquid

sealer

in accordance

with the

WR and

PCR-3068.

Upon completion of

the work the valve was tested

and returned to service.

No violations or deviations

were identified in the areas

inspected.

4.

Emergency

Response

Facilities Appraisal

(82412,

71707)

On

May 17 the licensee

conducted its annual

emergency

preparedness

exer-

cise,

which this year was

a limited scale drill.

A team of regional

based

emergency

preparedness

inspectors

were

on site to

perform

an

emergency

response facility appraisal.

e

The exercise

began

about

8:05 a.m.,

and was completed at about

1:45 p,m.

While the drill scenario

was in progress

the inspector

observed

licensee

personnel

at their exercise

stations,

both in the

TSC and in the Control

Room.

The drill started with a

RCS leak over

50

gpm in the containment building.

At about 8:24 a.m.,

an "alert" was declared,

and by 8:44 a.m.,

the

TSC was

activated.

A fire was reported

at elevation 291'n

the

Waste

Process

Building at

9:09 a.m.

The Holly Springs

Fire

Department

notification

was given

and

a simulated fire truck responded.

By 9:54 a.m.,

the plant

condition

had worsened

and the plant simulated

being in a "site emergency",

and at

10:02 a.m.,

simulated

evacuation

of the site

commenced.

Contain-

ment phase

"B" isolation

was simulated at ll:52 a.m.,

and at about

11:59

the plant

simulated

the declaration

of

a "general

emergency".

The simu-

lated conditions

then

allowed the

gradual

return of plant conditions to

normal.

The inspector

arrived in the

TSC shortly before

the

TSC

was activated

While in the

TSC the inspector

observed

the following:

Both primary personnel

and their alternates

appeared

in the

TSC very

promptly.

This allowed the

TSC to

be

ready for operation

in less

than

25 minutes.

The plant

general

manager

gave

detailed

briefings

throughout

the

drill

and

played

a

significant

role

in

keeping

the

"players"

organized

and making

sound decisions

when taking corrective

steps.

The

EOPs

and the associated

diagnostic chart were available

and were

used extensively

by TSC personnel.

The status

of the plant

and supporting drill data

were promptly and

clearly posted

on the data charts

located in the

TSC.

During

the drill there

was

a

change

in players;

the

new shift

personnel

were thoroughly briefed by those

being relieved.

The inspector

also toured

the Control

Room during the exercise,

and the

following were observed:

The

players

were well

organized

and

kept

continuous

and accurate

logs

on the simulated

changing plant conditions.

The

TS

and

applicable

procedures

and

charts

were

available

where

the players

were

assembled

and

they

were

reviewed

and

referenced

continuously

by 'the players.

The shift foreman maintained

clear

and accurate

communications

when

using

the

public

address

system

and

when

speaking

to his fellow

players.

During

the

exercise

the

inspector

reviewed

the

licensee's

documented

exercise

scenario

ayd noted that it appeared

to have

an inclusive

scheme

with an unpredictable

path.

No violations or deviations

were noted in the areas

inspected.

Exit Interview

The inspection

scope

and findings were

summarized

on

May 24,

1988, with

the Plant General

Manager,

Operations.

The inspector described

the

areas

inspected

and discussed

in detail

the inspection findings listed

above.

Dissenting

comments

were not received

from the licensee.

The licensee

did

not identify as proprietary

any of the material

provided to or reviewed

by

the inspector

during this inspection.

One violation was identified:

VIO 50-400/88-11-01;

Failure to Control

System Configuration

During

Testing of the

SSPS'

paragraph

2.b.

Acronyms and Abbreviations

CPRL

DNB

EIR

EOP

ESW

F

GPM

~

LCO

LTOP

MST

NRC

NRR

NSSS

OST

OWP

PCR

PORV

QA

QC

RCS

S/G

SSPS

TS

TSC

WR

Carolina

Power

and Light Company

Departure

from Nucleate Boiling

Equipment Inoperable

Record

Emergency Operating

Procedure

Emergency

Service Water

Fahrenheit

Gallons

Per Minute

Limiting Condition for Operation

Low Temperature

Over Pressure

Protection

Maintenance

Surveillance

Test

Nuclear Regulatory

Commission

Nuclear Reactor

Regulation

Nuclear

Steam

Supply System

Operational

Surveillance Test

Operations

Work Procedure

Plant

Change

Request

Pressure

Operated

Relief Valve

Quality Assurance

Quality Control

Reactor

Coolant System

Steam Generator

Solid State Protection

System

Technical Specifications

Technical

Support Center

Work Request