ML18004B933

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Insp Rept 50-400/87-31 on 870720-0820.Violations Noted.Major Areas Inspected:Response to Safety Issues,Operational Safety Verification,Monthly Surveillance Observation,Monthly Maint Observation & Open Items
ML18004B933
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 09/08/1987
From: Burris S, Frederickson P, Maxwell G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18004B931 List:
References
50-400-87-31, IEB-81-03, IEB-81-3, NUDOCS 8709140315
Download: ML18004B933 (16)


See also: IR 05000400/1987031

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/87-31

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,,

NC

27602

Docket No.:

50-400

Facility Name:

Shearon

Harris

1

Inspection

Conducted:

July 20 - August.,20,

1987

\\

Inspectors:

5

'U ~" ~

G.

F.

Maxwe

License No.:

NPF-63

q)C> Iq

ate

igne

rri.s

Approved

b

.

re nc son,

ection

se

Division of Reactor

Projects

ate

igne

ish

ate

s

e

SUMMARY

Scope:

This routine,

announced

inspection involved inspection in the areas of

Open

NRC Items,

Survey of Licensee's

Response

to Selected

Safety Issues,

Operational

Safety Verification, Monthly Surveillance

Observation,

and Monthly

Maintenance

Observation.

Results:

Two violations were identified - "Incorrect Position of a Compressed

Air Valve During Clearance

Restoration"

- Paragraph

5.b.(4),

and "Failure to

Report

an

ESF Activation Within Four Hours" - Paragraph

5.b.(5).

8709i40315

870908

PDR

ADOCK 05000+00

8

PDR

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees

G.

G.

J.

M.

G. L.

L. I.

G. A.

D. L.

R. B.

R. A.

J. L.

Campbell,

Manager of Maintenance

Collins, Manager',

Operations

Forehand,

Director,

QA/QC

Loflin, Manager, Harris Plant Engineering

Support

Myer, General

Manager, Milestone Completion

Tibbitts, Director, Regulatory

Compliance

Van Metre, Manager, Harris Plant Technical

Support

Watson,

Vice President,

Harris Nuclear Project

Willis, Plant General

Manager,

Operations

Other

licensee

employees

contacted

included

technicians,

operators,

mechanics,

security

force

members,

engineering

personnel

and office

personnel.

2.

Exit Interview

The inspection

scope

and findings were summarized

on August 24,

1987, with

the Plant General

Manager,

Operations.

No written material

was provided

to the licensee

by the resident

inspectors

during this reporting period.

The licensee

did not identify as proprietary any of the materials

provided

to or reviewed

by the resident

inspectors

during this inspection.

The

violations identified in this report

have

been

discussed

in detail with

the licensee.

3.

Open

NRC Items

(92701,

36100)

a

~

(Closed)

NRC Circular 80-CI-13 "Grid Strap

Damage in Westinghouse

Fuel

Assemblies".

The inspectors

evaluated

the site fuel handling

procedure,

FHP-001,

Rev.

0,

"Handling Limitations for

New

and

Irradiated

Fuel

Assemblies",

and fuel management

procedure

FMP-107,

Rev.

0, "Irradiated

Fuel

Visual Inspection".'he

inspectors

found

the procedures

addressed

the Westinghouse

recommendations

identified

in Circular 80-CI-13.

Procedure

FHP-001

contained

the

recommended

precautions

to aid in

minimizing corner-to-corner

interaction

between grid assemblies.

The

procedure

included

a fuel

handling

sequence

which should

generate

only side-to-side

contact

between

the assemblies.

Procedure

FMP-107

provided detailed instructions

concerning

visual

,inspections

to

be completed

on fuel assemblies.

The instructions

included requirements

that the assembly

be inspected

and the results

documented

to record

the condition of the grids.

Based

on the

procedure

evaluation

and

interviews

with those

responsible

for

implementing

the

procedures,

the

inspectors

concluded

that

the

licensee

has considered

the recommended

actions

described in Circular

80-CI-13.

This item is closed.

(Closed)

10 CFR Part 21 Item P2185-01,

"AAF Intake Silencer

TDM or

FTDM for Diesel Generators".

The inspectors

evaluated

the licensee's

documentation

concerning this Part

21 item which was communicated

to

the

NRC by the vendor,

American Air Filter Company

(AAF).

In

September

1985,

the

licensee

received

a letter

from the

NRC

stating that the supplier of the air silencers

for the Harris Plant

emergency

diesel

generators

had reported

a potential

manufacturing

defect in the si lencers.

The potential

defect

was described

as

"an

internal

part not being

welded into place".

The

vendor further

indicated

that

the

part

which

was

not

welded

into place

was

identified as

an air baffle.

To as'sure that the potential defect

was

properly tracked

and resolved,

the licensee

documented

the vendor's

concern

on

a Nonconformance

Report

(NCR-85-1963).

In mid-October

1985,

the

licensee

dismantled

the installed air

si lencers

and

conducted

an extensive

detailed

visual

inspection of .

their internals.

The licensee's

inspectors

found that

the air

baffles located inside the air si lencers

had

been welded into place

as

required

by design

documents.

The licensee

concluded

that the

conditions

described

by AAF, in the vendor's

report to the

NRC, did

not apply to the air si lencers

which

AAF supplied for the Harris

Plant.

The licensee

closed

NCR-85-1963,

and the vendor's

Part

21

report

was

not considered

applicable

to Harris.

The inspectors

concurred with the licensee's

conclusion.

This item is closed.

(Closed)

10 CFR Part 21 Item P2184-02."Deficient

Valves for Auxiliary

Feedwater

Pump

Drive Turbine".

In

1984 the licensee

was

advised

through correspondence

from the Institute of Nuclear

Power Operations

(INPO) that

a utility had experienced

problems with a motor-operated

semibalanced

globe

valve

supplied

by Gimpel

Machine

Works/Gimpel

Corporation.

The problem was identified during operability testing

of a turbine-driven auxiliary feedwater

pump.

During the test the

turbine

steam inlet isolation valve would stop or hesitate

in the

mid-position

when the turbine

was operating

under

no load or minimum

load conditions.

The Harris

Plant

was identified

as

having

one of these

valves

installed

in the

steam

header

for the turbine-driven auxiliary

feedwater

pump.

The supplier of the turbine,

Terry,

a part of

Ingersoll-Rand,

Inc.,

advised

the

licensee

that

a design

review

revealed

that

the installed

Gimpel

valve

could

be

repaired

by

increasing

the valve closure

spring tension.

Increasing'he

spring

tension

would eliminate the possibility of the valve stalling in a

mid-position.

The valve manufacturer

supplied

an improved closing spring to replace

the existing spring

on the installed

Gimpel valve.

The

new spring

installation

was

authorized

by

Work

Request

WR/85-AKHL1.

The

installation

was

completed

and

accepted

on

November

6,

1985.

The

inspectors

evaluated

the

documentation

associated

with WR/85-AKHLl

and interviewed responsible

licensee

personnel

concerning

the spring

replacement.

This item is closed.

4.

Survey of Licensee's

Response

to Selected

Safety Issues,(TI

2515/77,

92701)

The inspectors

reviewed the licensee's

marine growth control program with

respect

to biofouling of cooling water heat

exchangers

and verified the

following:

The licensee

had

a formal program which would monitor changes

in flow

capabilities of all open-cycle

systems,

including those closed-cycle

systems

which were capable of being cross-connected

to the open-cycle

systems.

The

program

included

monitoring

the

pressure

drop

instrumentation,

temperature'instruments,

and visual inspections

of

the heat exchangers

on a routine basis.

The licensee's

program identified above

was routinely reviewed

and

evaluated

against

design considerations

to ensure that any potential

marine

growth would be detected

prior to loss of

a heat exchanger

required

by safety equipment.

Incorporation of lessons

learned

from events

at other facilities was

conducted

by operations

personnel.

Specific

procedures

for the

degradation

of heat

exchangers

due to marine

growth

do not exist,

because

the licensee

considers

blockage of flow from.marine growth to

be

a loss of the heat exchanger.

The licensee

performs

routine periodic inspections

of the service

water

and fire protection

systems

in accordance

with its documented

surveillance testing

program.

During this

review the

inspectors

reviewed

IE Bulletin 81-03,

"Flow

Blockage of Cooling Water to Safety

Components

by Coribicula Sp. (Asiatic

Clam)

and Mytilus

Sp.

(Mussel)", which was closed in

ISE Report 84-14.

The licensee

continues

to maintain

surveillance

for the control

and

removal of any identified marine growth at the Shearon Harris Plant.

5.

Operational

Safety Verification (71707,

71710)

a ~

Plant Tours

The inspectors

conducted

routine plant tours during this inspection

period to verify that the licensee's

requirements

and

commitments

were being

implemented.

These

tours

were performed to verify that

systems,

valves

and breakers

required for safe plant operations

were

in their correct position; fire protection equipment,

spare

equipment

and

materials

were

being

maintained

and

stored

properly;

plant

operators

were

aware of the current plant status;

plant operations

personnel

were

documenting

the status

of out-of-service

equipment;

security

and

health

physics

controls

were

being

implemented

as

required

by procedures;

there

were

no undocumented

cases

of unusual

fluid leaks,

piping vibration, abnormal

hanger

or seismic restraint

movements;

and all

reviewed

equipment

requiring calibration

was

current.

II

Tours

of the

plant

included

review of site

documentation

and

interviews with plant personnel.,

The inspectors

reviewed the shift

foreman's

log, control

room operator's

log, clearance

center tag out

logs,

system

status

logs,

chemistry

and health

physics

logs,

and

control status

board.

During these

tours the inspectors

noted that

the

operators

appeared

to

be alert

and

aware of changing

plant

conditions.

The inspectors

evaluated

operations

shift turnovers

and

attended

shift briefings.

They observed

that the briefings

'and turnovers

provided sufficient detail for the next shift crew.

The inspectors

verified that various

plant

spaces

were

not in

a

condition which would degrade

the

performance

capabilities of any

required

system or component.

This inspection included checking the

condition of electrical

cabinets

to ensure

that they were free of

foreign and, loose debris, or material.

Site security

was evaluated

by observing

personnel

in the protected

and vital

areas

to

ensure

that

these

persons

had

the

proper

authorization to be in the respective

areas.

The security personnel

appeared

to be alert

and attentive to their duties

and those officers

performing

personnel

and

vehicular

searches

were

thorough

and

systematic.

Responses

to security

alarm conditions

appeared

to be

prompt and adequate.

The inspectors

observed

that the licensee

had

established

additional

active

and

passive

security

measures

at the

correct levels, to be consistent with NRC Information Notice 87-27.

b.

Plant Events

(1)

On July 22,

1987

the licensee

notified the

NRC Duty Officer

concerning

an event that resulted

in an automatic actuation of

the engineered

safety features.

When the event occurred,

the

reactor

was critical and stable at approximately

two percent

power with the

"B" main feedwater

pump supplying feedwater to

the

steam

generators.

The

licensee

reported

that

the

motor-driven auxiliary feedwater

pumps

(AFW) started at

5 a.m.

as

a result of the "B" main feedwater

pump tripping.

Upon

losing

the

main

feedwater

pump,

both

of

the

electrically-driven

AFW

pumps

started,

as

expected.

The

operators

maintained

steam generator

water level with the

AFW

pumps until the

"A" main feedwater

pump was started.

The

AFW

pumps

were then

secured

and the

AFW system

was returned

to its

normal

emergency

standby condition.

The licensee first reported that the event

was initiated by the

circuit breaker for the

"B" main feedwater

pump motor tripping,

due to overcurrent.

However, the inspectors

were informed that

after

the

maintenance

technicians

inspected

and

tested

the

pump's

protective circuitry,

they

determined

that it was

unlikely that it tripped

on overcurrent.

The

inspectors

evaluated

the site electrical

drawings for the circuit breaker

and noted the following:

When the overcurrent relay energizes it causes

contacts

to

close which lockout the circuit breaker

once it has tripped

open.

The lockout device would then require resetting

before the

breaker could be operated

again.

The inspectors

interviewed the responsible

technicians

and were

told that the lockout device

was not activated

when the circuit

breaker tripped.

Based

on this observation

and the electrical

tests

which were conducted

on the

pump motor

and its circuits,

the technicians

determined that the main feedwater

pump did not

trip on overcurrent.

The circuit tests

and inspections

revealed

that

a mechanical

fastener

on the valve linkage for the "B" main

feedwater

pump recirculating

valve

had vibrated

loose.

The

loose

valve

linkage

caused

a false

valve position to

be

indicated.

The false indication resulted

in a feedwater

pump

low flow alarm followed by a low feedwater

pump flow trip.

On July 23,

1987 the licensee

contacted

the

NRC and provided

a

correction to the initial report of this event.

The licensee

has

documented

the event

on

a Licensee

Event Report identified

as LER-87-46.

On July

24,

1987

the

licensee

experienced

a

loss

of the

Emergency

Response

Facility Information System

(ERFIS) computer.

The licensee

informed the inspectors

that the plant

had

been

experiencing

a "random" fault on the

"A" train

ERFIS computer.

The fault

had

been

identified

as

an input/output

processor

failure

in

the

"A" Central

Processor

Unit

(CPU),

which

effectively locked

up the ability of the computer to update, the

CRT (cathode

ray tube) monitors.

A lockup of one of the trains

of ERFIS will automatically shift the input/output to the other

train".

However,

a

computer

operator

was

in the

process

of

performing

a routine surveillance

on train "B" and therefore

the

automatic shift over did not occur.

Prior to this event the

licensee's

computer

personnel

were able to correct

the lockup

problems

by restarting

the

ERFIS program within 15 minutes.

The

0'

Plant

Emergency, Plan

allowed the licensee

15 minutes

to

be

without .the

ERFIS computer,

however,

on this date

the computer

operator

was unable to restart

the system within the specified

time.

The licensee

declared

an Unusual

Event at 1:15 a.m.

and

notified the appropriate

federal,

state

and local officials.

The

ERFIS computer

was returned'o

service at 1:42 a.m.

and the

licensee

began

an investigation

of the

cause

and corrective

actions for this event.

Subsequent

to this event the licensee

revised its

Emergency

Pl'an, in accordance

with 10 CFR 50.54q.,

to allow an hour time period prior to making

a determination of

an

Unusual

Event

for all

future

computer

failures.

Acceptability of this

change will be reviewed during subsequent

inspections.

On July 25,

1987, at about

1:45 p.m.,

the site experienced

a

loss

of both trains

of the

ERFIS

computer.

The

licensee

declared

an

Unusual

Event,

and notified the appropriate

local,

state

and federal

agencies.

The "A" train of the

ERFIS computer

was repaired

and the site terminated

the

Unusual

Event at 1:58

p.m.

On July 27,

1987 the licensee

removed

both trains of the

ERFIS

computer for troubleshooting.

The troubleshooting

was performed

to try to locate

the

cause

of the previous

computer failures.

Removal

from service of the

ERFIS computer

was coordinated with

local, state

and federal

agencies

prior to system

deenergi zing.

Th'e troubleshooting

was

completed

and both

ERFIS trains

were

returned to service.

On July 31,

1987

the licensee

identified

a problem with the

containment

wide range level

(CWRL) instrumentation.

The

CWRL

system

is divided into

"A" and

-"B" trains

which

meet

the

redundant train requirements.

Operations

personnel

noted that

the

"A" train instrument

pegged

low and that there

was

an alarm

condition

on the

computer monitoring system.

The operations

section

generated

two Work Request

and Authorizations

(87-AYJT1

and

87-AYJU1) to locate

and correct these

problems.

With both

trains of the instruments

out of service, it placed the plant in

a

48-hour

Limiting Condition for Operation

(LCO)

action

statement

in

accordance

with Technical Specification (TS) 3.3.3.6.b.

Licensee

Instrumentation

and Control personnel

found

that the "8" train instrument loop had

a short to ground

between

a potentiometer

and metal

housing,

which was repaired,

allowing

the

"B" train to be returned to service.

Correction of the "B"

train

ended

the 48-hour

LCO.

However, with only one loop of

instruments

available,

TS 3.3.6.a specifies

that the inoperable

loop must

be returned to service within seven

days, or the plant

must be in Hot Standby within the following six hours,

and in at

least

Hot Shutdown within the following six hours.

While operations

personnel

were reviewing the probable

causes

for the

"A" train failure, engineering

personnel

were reviewing

a Plant

Change

Request

(PCR),

PCR-2138,

which would replace

the

control

room meter with one capable of receiving direct signals

from

a sensing

device.

The analysis for the

PCR was

based

on

the following facts:

Location of the

detectors

inside

containment

would not

allow repairs

due

to high radiation

levels while the

reactor

was at power operation.

The

CWRL instrumentation

system

was

not normally

used

during routine plant operation.

A local

instrument in the reactor auxiliary building was

available

during all operational

and accident

phases

to

monitor the water level in the containment pit.

System reliability would not

be affected

by this change,

and

a

safety

evaluation

would

be

completed

prior to

implementation of the

PCR.-

The licensee

obtained

the replacement

meter

and

performed all

necessary

certifications

to ensure

that

the

meter

met site

specifications.

The

inspectors

evaluated

the

maintenance

activities

associated

with the

Work Request

(87-A2AG1) which

replaced

and calibrated

the sensing

device,

as specified in

PCR-2138,

and they found that the work performed

appeared

to be

satisfactory.

(4)

At 9:54 p.m.

on August 4, 1987, while the reactor

was operating

at

100

percent

power,

personnel

error

caused

the plant to

experience

a reactor trip when

the "B",train compressed

air

system

was

being

returned

to its

normal

valve lineup.

The

compressed

air system is composed

to two separate

trains,

each

consisting

of an air compressor,

an air dryer tower, support

equipment,

valves

and piping.

The

"A" train compressed

air

system

was out of service, with the

"B" train system supplying

plant air loads.

A clearance

was required to allow maintenance

personnel

to replace

the desiccant

material

in the

"B" air

dryer.

The clearance

(OP-87-1418)

removed

the

"B" air dryer

from service

by electrically isolating

the air dryer

power,

closing

the isolation

valves

and

opening

the

bypass

valve.

Bypassing

the air dryer allowed the

"B" train compressed

air

system to remain in service,

supplying all plant air loads.

When restoring the "B" train air dryer to service,

the clearance

center

mistakenly identified that the air dryer outlet valve

(1IA-852) was to remain closed.

With the air dryer outlet valve

shut

and

the air dryer

bypass

valve shut,

no flow path

was

available for compressed

air.

Based

on

a low air alarm in the

control

room,

the

control

operator

instructed

the auxiliary

operator

to

investigate

the

cause

for the

loss

of air.

Subsequently,

the

reduced

air

pressure

to

feed

flow

control 1 er

reduced

the

capabi lity to control

feed flow,

therefore

the

turbine

load

was

reduced.

During the

load

reduction

the plant experienced

a loss of both heater

drain

pumps

and

a trip of the "A" main feedwater

pump, resulting in an

automatic

runback.

After the runback,

the reactor tripped

on an

"A" steam generator

low level, coincident with a feed flow/steam

flow mismatch.

The "A" steam

generator

level

decrease

was

due

to the turbine throttle valves closing,

thereby

causing

the

steam

header

pressure

to increase

which led to a steam generator

shrink (decrease).

All safety

systems

started

as required.

The inspectors

reviewed

the

circumstances

leading

up to this

event

and

determined that the clearance

center operator failed

to appropriately

identify the correct position of

an outlet

valve

(1IA-852)

on

the

restoration

section

of clearance

OP-87-1418

in accordance

with Operations

Procedure

OP-151-01,

Compressed

Air System Operation, while returning the

system to

service.

The inspectors

informed licensee

management

that

failure to show the correct operational

position of this valve

on the

clearance

procedure

was

a violation of Administrative

Procedure

AP-020, Clearance

Procedure,

and will be identified as

"Incorrect Position of a Compressed

Air Valve During Clearance

Restoration"

50-400/87-31-01.

(5)

During the restart

of the plant

on the morning of August 5,

1987, at approximately 2:Ol a.m., following the reactor trip the

previous

day,

the

plant

experienced

an

actuation

of the

engineered

safety

features

(ESF)

s'stem.

While approaching

Mode

2 (Start-up)

from Mode

3 (Hot Standby),

the plant lost the

running

"A" main feedwater

pump which generated

an

ESF signal

for the standby motor-driven

AFW pumps to start

and supply the

necessary

steam

generator

feed

requirements,

as

designed.

Preliminary investigations .by the licensee

determined that the

cause for the main feedwater

pump trip was

due to high discharge

pressure..

The inspectors

interviewed licensee

personnel

and reviewed the

licensee's

documentation

for this event,

which included

Work

Request

and Authorization 87-AY2Rl, instrument calibration data

sheets,

and the initial Licensee

Event Report information.

The

inspectors verified that the licensee's

evaluation of this event

correctly identified the

reasons

for the main feedwater

pump

tripping.

The

inspectors

determined

that

the

event

was

initiated

due to incorrect settings

on the main feedwater

pump

discharge

pressure

switches.

These incorrect settings

were

a

result of the pressure

sensors drifting out of calibration.

9

The

event

was

evaluated

by

the

licensee

as

a

four-hour

reportable

event

under

the

requirements

of

10 CFR 50.72..

However, the licensee

did not make the

"Red Phone" call to the,

NRC Duty Officer until approximately

9:44

a.m.

on August 5,

1987.

When

the

inspectors

inquired

about

the

licensee's

allowing nearly eight

hours to

pass

prior to reporting

the

event,

they were'nformed

by responsible

licensee

supervision

that failure to report this event within four hours

was

due to

personnel

incorrectly interpreting the reportable

requirements

of 10 CFR 50.72.

Additionally, the interpretation error was

a

result of not distinguishing this event

from the reactor trip

which occurred at 9:54 p.m.

on August 4,

1987.

The inspectors

informed

licensee

management

that

fai lure

to

make

the

appropriate

event

report

within

the

four-hour

reporting

requirement

is

a violation of

10 CFR 50.72,

and will be

identified

as "Failure to Report

an

ESF Actuation Within Four

Hours" (50-400/87-31-02).

On

August

10,

1987

the

licensee

experienced

a loss of the

capability

to

collect

weather

data

from

the

onsite

meteorological

weather station

and therefore declared

an Unusual

Event at 5:36 a.m.

State

and local officials were notified in

accordance

with the

Emergency

Plan requirements,

and the Unusual

Event

was terminated at 9:00 a.m.

The cause of the event

was

attributed to the

power supply breaker for the meteorological

tower

modem

tripping.

The

breaker

was

reset

and

the

meteorological

tower station

was

placed

back in service.

The

licensee

is evaluating this event to determine

the root cause

for the loss of the power supply breaker.

On

August

15,

1987

the

licensee

identified that

the

ERFIS

computer

was

not

updating

plant

parameters,

as

designed.

Operations

personnel

initiated an investigation to determine

the

cause

and to correct the problem.

Plant management

declared

an

Unusual

Event at 4:41 a.m. in accordance

with the Emergency

Plan

and notified all appropriate

agencies.

The event

was terminated

at 5:15 a.m.

On August

15,

1987 the plant experienced

a loss of the

ERFIS

computer

and declared

an Unusual

Event at 12:15 p.m.

All local,

state

and federal

response

organizations

were notified within

the required

time period.

The licensee

repaired

the computer

and

returned it to service,

terminating

the

Unusual

event at

1: 12 p.m.

Both of the

ERFIS events

which occurred

on August

15

were attributed

to

a defective electrical

card in the

"B"

computer circuit.

The card provided

a path for the high speed

data link connecting

the

"A" and

"B" computers.

The computer

technicians

replaced

the

card

on the afternoon

of the 15th.

Replacement

of the defective

card appears

to have corrected

the

cause of these

two Unusual

Events.

0

10

Two violations were identified in the areas

inspected.

6.

Monthly Surveillance

Observation

(61726)

The inspectors

witnessed

the licensee

conducting maintenance

surveillance

test activities

on safety-related

systems

and

components

to verify that

the

licensee

performed

the activities

in

accordance

with licensee

requirements.

These observations

included witnessing selected

portions of

each

surveillance,

review of the surveillance

procedure

to ensure

that

administrative

controls

were in force,

determining

that approval

was

obtained

prior to conducting

the surveillance test

and the individuals

conducting

the test

were qualified in accordance

with plant-approved

procedures.

Other

observations

included

ascertaining

that

test

instrumentation

used

was

calibrated,

data

collected

was within the

specified

reauirements

of Technical

Specifications,

any

identified

discrepancies

were properly noted,

and the systems

were correctly returned

to service.

The following specific activities were observed:

The inspectors

reviewed

the test procedure

and witnessed

maintenance

personnel

during the

performance

of Maintenance

Surveillance

Test

MST-I-0001, Rev. 3, Train "A" Solid State Protection

System Actuation

Logic and Master

Relay Test.

This test verified operation of the

reactor trip breaker,

reactor trip bypass

breaker

and verification of

the

P-4 permissive.

MST-I-0001 also verified the requirements

of

Technical Specifications 4.3.2. 1, Table 4.3-2,

Sections

1.b, 2.b,

3.a.2, 3.a.3, 3.b.2, 3.c.2, 3.c.3, 4.b, 5.a, 5.c, 6.b, 6.d, 6.g, 7.a,

8.a

and 8.b.

Portions of Technical Specifications 4.3. 1. 1, Table

4.3-1,

Sections

20,

21

and

22

were

also verified during

the

performance

of this test.

FSAR commitments

3. 1.17-002, 7.3.2-044,

7.3.2-049,

7.3.2-051

and 15.0.6-003

were verified upon completion of

the test

and acceptance

of the test results.

The inspectors

obtained

a copy of the

MST procedure

and reviewed the

procedure

to ensure

the following:

a current

copy of the procedure

was

being

used

by personnel

performing the test; prerequisites

for

the test were met prior to commencing

the test; maintenance

personnel

performing

the

test

were

familiar with

the

precautions

and

limitations;

communications

for the

completion of the test

were

established

as required;

special

tools

and

equipment

were properly

obtained

and calibrated

as required;

acceptance

criteria were clearly

understood

by test

personnel;

procedural

steps

were

clear

and

progressed

logically throughout the testing

sequence;

data collected

by the test personnel

were formally documented

in the test procedure;

and all test data

sheets

were attached

to the test after completion

for proper review and acceptance.

The inspectors

witnessed

maintenance

and operations

personnel

during

the performance

of the

MST to verify that:

personnel

performing the

required activities were qualified to accomplish

the task; operations

personnel

performing selected

test portions

were

aware of any test

requirements

which would impact test results;

and personnel

involved

in the test

maintained

a professional

attitude

during

the test

performance.

Maintenance

personnel

completed

the test in accordance

with testing

requirements

specified

in the

procedure

and

documented

-the test

results

for acceptance/rejection

by plant

management.

All areas

observed

by the inspectors

appeared

to be satisfactorily performed

by

maintenance

and operations

personnel.

The inspectors

witnessed

portions of Operational

Surveillance

Test

OST-1026,

Rev.

2, Reactor

Coolant

System

Leakage

Evaluation - Daily

Modes

1-2-3-4.

The licensee

performed the test to verify that the

unidentified leakage

and identified leakage

of the reactor coolant

system

was within the

values

specified

in Technical Specification 4.4.6.2. 1.d.

Verification of these

leakages

is

accomplished

by

performing

an inventory water balance of the reactor

coolant system.

The inspectors

verified that operations

personnel

were in compliance

with the procedure,

in that test prerequisites

were met and signed

off prior to

data

collection;

precautions

and limitations

were

reviewed

by the necessary

operations

personnel

prior to starting the

test; operations

personnel

performed

and signed off on each

procedure

step

as required;

operations

management

reviewed

and verified that

the

test

data

and

calculations

met

the

acceptance

criteria

established

in the

procedure;

and

mathematical

review of the

calculations

used

for

determination

of

the

identified

and

unidentified leak rates

appeared

to be correct.

Portions

witnessed

and

reviewed

by the inspectors

appeared

to

be

completed in accordance

with site approved

procedures.

No violations or deviations

were identified in the areas

inspected.

7.

Monthly Maintenance

Observation

(62703,

62700,

37700)

The inspectors

reviewed

the licensee's

maintenance activities during. this

inspection

period to verify the following:

maintenance

personnel

were

obtaining

the

appropriate

tag

out

and

clearance

approvals

prior to

commencing

work activities, correct

documentation

was available for all

requested

parts

and material prior to use,

procedures

were available

and

adequate

for the work being

conducted,

maintenance

personnel

performing

work activities were'ualified to accomplish

these

tasks,

no maintenance

activities

reviewed

were violating any limiting conditions for operation

during the specific evolutions;

the required

QA/QC reviews

and

QC hold

points

were

implemented;

post-maintenance

testing

activities

were

completed,

and

equipment

was

properly

returned

to service

after the

completion of work activities.

Maintenance activities were evaluated for the "B" main feedwater

pump

motor.

The maintenance

was

performed to determine

and correct the

cause

for the motor's circuit breaker tripping open.

The work was

0

12

authorized

by

Work

Request

WR-87-AXMN1.

Maintenance

personnel

determined

that the circuit breaker

tripped

open

due to incorrect

signals

received

from the

feedwater

flow circuit.

The incorrect

signals

were

caused

by

a loose fastener

located

on the feed

pump's

recirculating valve.

The fastener

was tightened

and the

pump

was

returned to service

on July 23,

1987.

CL,

Maintenance

acti vities

were

evaluated

for the

repl acement

and;>

calibration of the containment

wide range

sump level instrument..-,Thh>

work was authorized

by WR-87-A7AG1, which implemented

a Plant

Change':

Request

PCR-2138.

The

new level instrument

was installed

and pllce4.";

into service

on August 7, 1987.

r

Maintenance

activities

were

evaluated

for the

"A" main feedwater

pump,

which tripped

and

caused

an

ESF actuation.,

The work w9

authorized

by WR-87-AYZRl.

The

pump trip was

caused

by incorrect

settings

on the feedwater

pump discharge

pressure

switches

PS-2100Al,

2100A2

and

2100A3.

The

switches

were readjusted

and returned

to

service.

On August

7

and

8,

1987

the licensee

removed

the plant from the

electrical grid and placed the plant in Mode

2 (Start-up).

The plant

was placed in this

mode to allow maintenance

activities

on the main

turbine.

The maintenance

was authorized

by Work Request

WR-87-k CPl.

The inspectors

evaluated

the work associated

with the

Work Request.

The

maintenance

was

required

to repair

a

steam

leak.

The leak

developed

around

the weld which fastened

a three

inch drain line to

the main steam line for governor valve k'4.

The leaking weld was

ground out

and replaced

by qualified welders

using

a site

weld procedure

which

was

reviewed

and

accepted

by

Westinghouse.

Upon completion the weld was inspected

both visually

and by magnetic particle testing.

No violations or deviations

were identified in the areas

inspected.