ML18004B850

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Insp Rept 50-400/87-16 on 870406-10.No Violations Noted. Major Areas Inspected:Review of Startup Tests Completed at 50% & 70% of Rated Power & Licensee Response to IE Info Notices
ML18004B850
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 05/11/1987
From: Burnett P, Jape F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18004B849 List:
References
50-400-87-16, IEIN-86-014, IEIN-86-14, IEIN-87-005, IEIN-87-5, NUDOCS 8706150233
Download: ML18004B850 (9)


See also: IR 05000400/1987016

Text

PS AEVI,

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATL AN TA, G E OR GI A 30323

Report No.:

50-400/87-16

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC

27602

Docket No.:

50-400

Facility Name:

Harris

1

License No.:

NPF-63

Inspection

Conducted:

April 6 - 10,

1987

Inspector:

P.

T.

Bu ne t

Date Signed

Approved by

F. Jape,

Chief

Engineering

Branch

Division of Reactor Safety

Date Signed

SUMMARY

Scope:

This routine,

unannounced

inspection

addressed

the review of startup

tests

completed at 50 and

75 percent of rated

power and licensee

response

to IE

Information Notices.

Results:

No violations or deviations

were identified.

870eisoaaa

87asco

PDR

ADOCK 05000400

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REPORT DETAILS

Persons

Contacted

Licensee

Employees

  • R. A.

J.

L.

"H.

W.

J.

M.

R. J.

"G. L.

  • J

L

  • A. J.
  • C
  • C. E.
  • J.

R.

  • J.

H.

R.

B.

  • W. R.

R.

R.

Watson,

Vice President,

Harris Nuclear Project

Wills, Plant General

Manager

Bowles, Director, Onsite Nuclear Safety

Collins, Manager,

Operations

Duncan,

Test Program

Development

Engineer,

Technical

Support

Forehand,

Director Quality Assurance/Quality

Control

Harness,

Assistant Plant General

Manager,

Operations

Howe, Regulatory

Compliance

McKensie, Principal Quality Assurance

Engineer

Rose, Jr., Quality Assurance

Supervisor

Sipp,

Manager

EERC

Smith, Operations

Support Supervisor

Van Metre,

Manager,

Technical

Support

Wilson, Principal Engineer,

Technical

Support

Wojonarowski,

Reactor

Engineering

Leader, Technical'upport

Other

licensee

employees

contacted

included

shift

foremen,

startup

engineers,

control

room

operators,

and office personnel.

NRC Resident

Inspectors

G.

F. Maxwell, Senior Resident

Inspector

S.

P. Burris, Resident

Inspector

  • Attended exit interview

Exit Interview

The inspection

scope

and findings were

summarized

on April 10, 1987, with

those

persons

indicated in paragraph

1 above.

The inspector described

the

areas

inspected

and

discussed

in detai

1

the

inspection

findings.

No

dissenting

comments

were received

from the licensee.

Proprietary material

was not reviewed in the course of the inspection.

Licensee Action on Previous

Enforcement Matters (92702)

(Closed)

Violation 86-96-01:

Inadequate

procedure

for measuring

reactor

coolant

system

leakrate.

The

inspector

reviewed

the

revised

procedure

OST-1026,

and

analysed

survei llances

performed

under it using

micro

computer

program

RCSLK9,

from the

NRC Independent

Measurements

Program.

Six

completed

copies

of

OST-1026,

Reactor

Coolant

System

Leakage

Evaluation,

which were performed in early March,

1987,

were reviewed,

and

0

0

the results

compared with calculations

using

RCLSK9.

(System temperatures

ranged

from 345 to 571

F, all at 2235 psig.)

Agreement for both gross

and

unidentified leakage

was within 0.2

gpm in all cases.

In those

cases

in

which there

was

no net change

in reactor

coolant

system

average

temperature

there

were

no differences

in the gross

leakage

calculations.

The

small

differences

that

arose

when

there

were

changes

in

average

temperature

derived

at least

in part

from the licensee

correcting for both

system

volume

and coolant density

changes,

while

RCSLK9 accounts

only for the

latter.

Whether

the

vessel

and

piping actually

respond

to changes

in

coolant temperature

in the time frame of the test is open to question.

4.

Unresolved

Items

No unresolved

items were identified during this inspection.

5.

Fifty Percent

Power Tests

(72608)

a.

9105-S-01,

Calibration of Steam

and Feedwater

Flow Instrumentation

at

Power -

50% (Retest)

was

performed

March

13,

1987

and accepted

on

April 7,

1987.

The level

2 acceptance

criterion for the

feedwater

flow transmitter signals

was that they agree within

5% of full scale

d/p of the special test instruments.

This is

a large

number, of the

order of

61

inchs-water,

and

about

one-third

the

reading

at

50%

power.

However,

the

acceptance

criterion

in 9107-S-03

(90%

power

data)

is

no discrepancy

in excess

of 0.5% full scale d/p (approxi-

mately

6. 1

inches

water)

special

test

instrument

accuracy

(1.4 inches - water).

This will translate

to

about

1% instrument

error at full power, which, if attained will be acceptable.

b.

9105-S-05,

Core

Performance

at

50%

Power,

was

completed

on

February

21,

1987,

and

the resul ts were

approved

on March 3,

1987.

The

heat

flux hot

channel

factor

and

nuclear

enthal py ri se

hot

channel

factor each satisfied its technical

specification limit at

50

and

75% power, thus justifying escalation

of power to the

75% testing

plateau.

The maximum quadrant

power tilt ratio was 1.007, well below

the limit of 1.02.

The INCORE-calculated

average

reaction rate error

was 4.7%, again, well below the level

2 acceptance

criterion of 10%.

The reaction

rate error is the difference

between

predicted

power

production

in an

assembly

and the

measured

value.

Determination of

control

rod position

by use of the

incore

nuclear

instruments

was

also

demonstrated

to agree within

12 steps

with main control

board

indications.

The

review included

the

following procedures,

which were

performed

in

support of this test:

(1)

FMP-101 (Revision 2), In-Core Thermocouple

and Flux Mapping,

(2)

EST-710 (Revision 3), Hot Channel

Factor Tests,

(3)

EST-722

(Revision

0),

Control

Rod Position

Determination

Via

Incore Instrumentation,

and

(4)

EPT-052

(Revision

0),

Power

Range

Heat

Balance

Via Precision

Calorimetric.

9105-S-06,

Thermal

Power Measurement

and Statepoint

Data Acquisition

at

50%

Power

(Retest

2)

was

performed

on

March 13,

1987

and

the

results

accepted

on April 7,

1987.

The

test

had

no

level

1

acceptance

criteria

and

was judged

successful

when acceptable

data

were obtained,

submitted for use

in other tests,

and

thermal

power

calculated.

9105-S-07,

NIS Overlap Verification,

Power

Range

Calibration

and

Setpoint

Adjustment -

50%

was

completed

on

February

23,

1987

and

approved

on

March 3,

1987.

Adjustment of all

four

power

range

nuclear

instruments

was within two percent

of the indicated thermal

power

as determined

by test

procedure

9105-S-06.

Plots of chamber

current versus

power at zero,

30,

and

50% thermal

power all appeared

to be linear.

9105-S-09,

Power

Coefficient

at

50%

Power,

was

performed

on

February

22,

1987,

and the results

were

accepted

on

March 3,

1987.

Xenon stability during the test

was confirmed by use of the computer

code

EXSPACK, which indicated that prior to starting the test

xenon

was changing

by about 6pcm/hr.

The total reactivity worth of xenon

was about

2450

pcm.

The initial thermal

power

was determined

using

procedure

OST-1004,

Power

Range

Heat Balance-Daily Interval.

9105-S-11,

Loss of Feedwater

Heaters

Test at

50% Power,

was performed

on

March 29,

1987

and

the results

accepted

on April 7,

1987.

There

were

no level

1 acceptance

criteria.

The level

2 criterion was that

no

measurement

of feedwater

temperature

drop

more

than

44

F.

The

three

recorded

measurements

of temperature

drop were

11, 5,

and

11F;

satisfying the criterion.

9105-S-14,

Reactor Coolant

System

Flow Measurement

at

50%

Power,

was

performed

on

February

22,

1987

and

the results

were

accepted

on

February

25,

1987.

The measured

flow was

309420

gpm, which satisfied

the acceptance

criterion that flow be greater

than

298948

gpm, which

includes

allowances

for error.

Data

sheet

10.3

and

acceptance

criterion 7.2. 1 indicate the flow rate is 309970

gpm, in contrast to

the value

above

from section

1 of the procedure.

The data

used were

obtained

from test procedure

6105-S-06.

Data sheet

10. 1 demonstrates

that the

average

reactor

coolant

system

(RCS) temperature

and

steam

generator

and pressurizer

levels were stable

over the period of the

test.

The final determination of reactor coolant

system flow will be

performed

using

a precision

heat

balance

once

the reactor

achieves

100% rated thermal

power.

0

h.

9105-S-18,

Preliminary

Incore/Excore

Calibration,

was

performed

on

February

22,

1987 and accepted

on March 3,

1987.

Performance

at this

power

level

precedes

the

Technical

Specification

requirement

to

perform at

75% power.

Hence,

the use of only two quarter-core

flux

maps

at

only

two different axial flux differences

is acceptable.

This test

provided

an opportunity

to

make

practical

use

of the

engineering

and

. maintenance

surveillance

tests

(ESTs

and

MSTs,

respectively) that were to be applied in the required surveillance.

No violations or deviations

were identified.

Seventy-five

Percent

Power Tests

(72616)

Several

70% power tests

were left to

be performed at the

time of

this'nspection.

Most of the

completed

tests

were

in the

review cycle.

However,

data

from the

incore-excore

calibration test at

75% power were

available,

and

the

inspector

performed

independent

calculations

of the

least

squares fit of axial offset to chamber current'or

each of the eight

chambers.

Exact

agreement

on zero-offset,

full-power current,

slope,

and

correlation coefficient was obtained in every case.

Five data pairs

were

used

in

each

calculation

and all correlation coefficients

were greater

than 0.995.

No violations or deviations

were identified.

7.

Licensee

Followup of IE Information Notices (92703)

IE

INFORMATION NOTICE NO. 86-14:

PWR AUXILIARY FEEDWATER

PUMP

TURBINE

CONTROL

PROBLEMS

and

IE

INFORMATION NOTICE NO. 86-14,

SUPPLEMENT

1:

OVERSPEED TRIPS

OF

AFW,

HPCI,

AND RCIC

TURBINES have

been

considered

by

the

licensee.,

The

review of

the

original

notice

was

completed

on

April 16,

1986

and

the

review of the

supplement

was

completed

on

January

19,

1987.

Based

upon

discussions

with

representatives

of

Woodward

Governor

and utilities experiencing

mechanical

overspeed

trips

from oil pressure

in the governor,

licensee

engineers

concluded

that

no

similar

mechanism

existed

at

Harris.

They did,

however,

identify

a

potential for condensate-buildup-induced

overspeed trips and

made specific

recommendations

for corrective action.

The modification portion of the

corrective action

had not been

implemented at the time of this inspection.

Overspeed

trips of the turbine driven

AFW pump

were

experienced

during

the remote

shutdown

and loss of offsite power tests.

Initially the

cause

was assigned

to

a loose electrical

speed

probe

connection.

Maintenance

findings and post-maintenace

testing

appeared

to justify that conclusion.

Subsequently,

additional

overspeed

trips were experienced,

and they were

ascribed

to

condensate

buildup in the

steam

supply lines.

Currently,

the

condensate

is being drained

several

times

per shift in response

to

annunciator

alarms,

and the recent experience

has sensitized

the operators

to the

need for prompt response

to the alarms.

Corrective

modifications

are

currently

being

planned.

The

need

for

modifications to eliminate

condensation

in the

steam

supply line to the

pump turbine

stems

from the current practice of keeping

the

steam

supply

valve closed.

This results

in unheated

line length of over

100 feet in

which

steam

leakage

past

the

supply

valve

can

condense

without being

drained

by automatic action.

If the supply were controlled at the turbine

governor valve,

there

would be less

than three feet of line to heat

on

pump start,

and condensation

in the remainder of the

steam line would be

forced through

the condensing

pot drains

by

steam pressure.

Apparently,

the decision

to control

steam

at

the

supply

valve

was

made

to avoid

performing high energy line break analysis

to the

100 plus feet of steam

line

between

the

supply

valve

and

the

governor

valve.

Subsequent

discussions

with members, of the Plant Systems

Branch,

NRR

confirmed that

classifying the

steam line as

a non-high energy line in the current

mode

of operation

was acceptable.

IE

INFORMATION NOTICE NO. 87-05:

MISWIRING IN WESTINGHOUSE

ROD

CONTROL

SYSTEM was

reviewed

by the licensee,

who prepared

a test

procedure

to

determine if the

problem

existed

at Harris.

That test,

EPT-041T,

was

performed

on March 30,

1987.

A review of the

completed test

procedure

confirmed that it was

responsive

to the

concern

expressed

in the notice

and that the wiring error did not exist

in the Harris

1

rod control

system.

No violations or deviations

were identified.