ML18004A547
| ML18004A547 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 09/23/1986 |
| From: | Verrelli D NRC Office of Inspection & Enforcement (IE Region II) |
| To: | |
| Shared Package | |
| ML18004A546 | List: |
| References | |
| 50-400-86-60, NUDOCS 8610060041 | |
| Download: ML18004A547 (1) | |
Text
ENCLOSURE 1
NOTICE OF VIOLATION Carolina Power and Light Company Shearon Harris Unit 1
Docket No. 50-400 License No.
CPPR-158 During the Nuclear Regulatory Commission (NRC) inspection conducted on July 20 August 20,
- 1986, a violation of NRC requirements was identified.
The violation involved failure by the licensee to comply with its drawing configuration procedures.
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions,"
10 CFR Part 2, Appendix C (1985),
the violation is listed below:
10 CFR 50.55 (f)(1) requires CP&L to implement the guality Assurance program described or referenced in the Preliminary Safety Analysis Report.
Section 1.8.5.5 of the CP&L guality Assurance Program requires that measures be established to insure that drawings are in accordance with the documented plant configuration.
Contrary to the
- above, drawings were not in accordance with the documented plant configuration in that during the week of July 28,
- 1986, the resident inspectors found the as-constructed condition of the emergency service water
- system, as described in EBASCO drawing CAR-2165-G-047, Rev.
17, CP&L Simplified Flow Diagram, CPL-2165-S-0547, Rev.
5, and FSAR drawing 9.2. 1-1, did not show piping modifications and the actual piping arrangement of the installed equipment.
This is a Severity Level V violation (Supplement II).
Pursuant to the provision of 10 CFR 2.201, Carolina Power and Light Company is hereby required to submit to this Office within 30 days of the date of the letter transmitting this Notice a written statement or explanation in reply including (1) admission or denial of the violation, (2) the reason for the violation if
- admitted, (3) the corrective steps which have been taken and the results
- achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved.
Where good cause is shown, consideration will be given to extending the response time.
Security or safeguards information should be submitted as an enclosure to facilitate withholding it from public disclosure as required by 10 CFR 2.790(d) or 10 CFR 73. 21.
FOR THE NUCLEA REGULATORY COMMISSION 8610060041
- 860923, PDR
- DOCK 05000400 PDR
)
D V
el 1 i, Chief Reactor Projects Branch 2
Division of Reactor Projects Dated at Atlanta, Georgia this 23 day oSeptember 19 86