ML17352A250

From kanterella
Jump to navigation Jump to search
Insp Repts 50-250/93-21 & 50-251/93-21 on 930724-0820. Violations Noted.Major Areas Inspected:Surveillance Observations,Operational Safety & Plant Events
ML17352A250
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/17/1993
From: Butcher R, Binoy Desai, Landis K, Trocine L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17352A247 List:
References
50-250-93-21, 50-251-93-21, NUDOCS 9309280239
Download: ML17352A250 (19)


See also: IR 05000250/1993021

Text

gp,R REC(g

~o

eo

I

0

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIEITASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report Nos.:

50-250/93-21

and 50-251/93-21

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami; FL

33102

Docket Nos.:

50-250

and 50-251

License Nos.:

DPR-31

and DPR-41

Facility Name:

Turkey Point Units 3 and

4

Inspection

Conducted:

July 24

hrough August 20,

1993

Inspectors:

R.

C. Butche

, Senior

sident

Inspector

Da

Si

ned

B. B. Desai,

esi

nt I

pector

D

e

S gned

L. Trocine,

esident

In

ector.

Da e S'gned

Accompanying Inspectors:

T.

P. Johnson,

Senior Resident

Inspector,

Salem

and

Hope Creek

George Schnebli,

Resident

Inspector,

Browns Ferry

Approved by:

lk~

K. D. Landis, Chief

Da

Si

ned

Reactor Projects

Section

2B

Division of Reactor Projects

SUMMARY

Scope:

This routine resident

inspector

inspection

involved direct inspection at the-

site in the areas of surveillance

observations,

maintenance

observations,

operational

safety,

and plant events.

Backshift inspections

were performed

on

July 24-25

and 27-28

and August

1 and 16-19,

1993.

Results:

Within the scope of this inspection,

the inspectors

determined that the

licensee

continued to demonstrate

satisfactory

performance to ensure

safe

plant operations.

The .following violation was identified:

Violation 50-250,251/93-21-01,

Failure to Follow a Procedure

Resulting

in a Feedwater

Transient

and Subsequent

Reactor Trip (paragraph 8.f).

9309280239

930'F17

PDR

ADOCK 05000250

8

PDR

During this inspection period, the inspectors

had

comments

in the following

Systematic

Assessment

of Licensee

Performance

functional areas:

Plant Operations

The approach

to criticality following the Unit 4 outage

was performed in

a professional

manner with good communications

(paragraph 8.c).

A

concern

was noted regarding the performance of procedural

steps

out of

sequence,

the lack of command

and control that resulted in a feedwater

transient

and subsequent

reactor trip, and the lack of good

communications

needed to ensure that both control

room and field

personnel

were aware of the performances

of significant evolutions

(paragraph 8.f).

Engineering

A weakness

was noted in the lack of attention to detail

on the Unit 4

design

package for the elimination of the turbine runback

on

a dropped

rod (paragraph

8.e).

A strength

was also noted for Engineering's

quality perspective

in the identification of the inadvertent

removal of

a wire on the Unit 4 turbine runback circuitry during preparation for

the performance of the

same modification 'on Unit 3 (par agraph 8.e).

The following general

comment

was also noted:

Management's

decision to remove Unit 4 from service in order to

facilitate the replacement of a pressurizer

spray mini-flow bypass

valve

due to

a minor unisolable leak was conservative

(paragraph 8.c).

This

was noted

as

a strength.

The inspectors

reviewed the following outstanding

item:

(Closed)

License

Event Report 50-251/93-002,

Reactor Trip Due to Manual

Turbine Trip (paragraph

4).

REPORT DETAILS

Persons

Contacted

Licensee

Employees

Abbatiello, Site equality

Manager

Bohlke, Vice President,

Nuclear Engineering

Supe

Bowskill, Reactor Engineering Supervisor

Earl, equality Assurance

Supervisor

Geiger,

Vice President,

Nuclear Assurance

Gianfrencesco,

Support Services

Supervisor

Goldberg,

President,

Nuclear Division

Hayes,

Instrumentation

and Controls Maintenance

Heisterman,

Hechanical

Maintenance

Supervisor

Higgins,

Outage

Manager

Hollinger, Operations Training Supervisor

Hosmer, Director, Nuclear Engineering

Jernigan,

Operations

Manager

Johnson;

Operations

Supervisor

Kaminskas,

Services

Manager

Kirkpatrick, Fire Protection/Safety

Supervisor

Knorr, Regulatory Compliance Analyst

Kundalkar, Engineering

Manager

Lindsay, Health Physics Supervisor

chese,

Site Construction

Hanager

Paduano,

Acting Director, Nuclear Licensing

Pearce,

Plant General

Manager

Pearce,

Electrical Maintenance

Supervisor

Plunkett, Site Vice President

Powell, Technical

Hanager

Rose,

Nuclear Materials Manager

Steinke,

Chemistry Supervisor

Timmons, Security Supervisor

Wayland,

Haintenance

Manager

Weinkam, Licensing Manager

T. V.

W. H.

H. J.

R. J.

J.

E.

R. J.

J.

H.

E.

F.

R.

G.

P.

C.

G.

E.

J.

B.

D.

E.

H. H.

V. A.

J.

E.

J.

E.

R.

S.

J.,D.

J.

Har

H.

N.

L.

W.

M. 0.

T.

F.

D.

R.

R.

E.

R.

N.

F.

R.

H.

B.

E. J.

rvisor

Supervisor

Other licensee

employees

contacted

included construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

NRC Resident

Inspectors

R.

C. Butcher,

Senior Resident

Inspector

B. B. Desai,

Resident

Inspector

L. Trocine,

Resident

Inspector

Other

NRC Personnel

on Site

T.

P. Johnson,

Senior Resident

Inspector,

Salem

and

Hope Creek

G. A. Schnebli,

Resident

Inspector,

Browns Ferry

Attended exit interview on August 20,

1993

Note:

An alphabetical

tabulation of acronyms

used in this report is

listed in the last paragraph

in this report.

Other

NRC Inspections

Performed During This Period-

None

Plant Status

Unit 3

At the beginning of this reporting period, Unit 3 was operating at

approximately

15% power in order to facilitate the repair of a steam

leak on the

3B MSR drain line, cleaning of the

3A north and

3A south

waterboxes,

and cleaning of the 3A and

3B TPCM heat exchangers.

(Refer

to paragraphs

3 and 8.i of NRC Inspection

Report

No. 50-250,251/93-19.)

The unit had

been

on line since January

20,

1993.

The following

evolutions occurred

on this unit during this assessment

period:

At 3: 15 a.m.

on July 24,

1993,

power ascension

was

commenced

following the repair of a steam leak on the 3B MSR drain line.

In

order to facilitate cleaning of the 3A TPCW heat exchanger,

reactor

power was stabilized at

50% at approximately 6:40 a.m.

At

6:00 p.m., the licensee

commenced

a slow power increase

and

removed the

3B TPCW heat

exchanger

from service for cleaning.

This heat exchanger

was returned to service at 9:30 a.m.

on July

25,

1993.

Power ascension

from 75% was re-commenced

at

a rate of

10% per hour,

and

100% reactor

power was achieved

at 12:15 p.m.

(Refer to paragraph 8.a,for additional information.)

At 12: 15 p.m.

on July 25,

1993, Unit 3 broke the previous Turkey

Point record for continuous

days

on line.

This record

(185 days,

15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />,

and

43 minutes)

was set

on March 20,

1988.

Unit 4

At the beginning of this reporting period, Unit 4 was operating at

100%

power and

had

been

on line since June

27,

1993.

The following

evolutions occurred

on this unit during this assessment

period:

At 5:55 p.m.

on August 12,

1993,

a load reduction

was

commenced

in

order to facilitate the replacement. of the pressurizer

spray mini-

flow bypass

valve (4-524A) around pressurizer

spray valve PCV-4-

455B.

(Refer to paragraph

8.c for additional information.)

Unit

4 was taken off line and entered

Mode

2 at 8:34 p.m.,

and

Mode 3

was entered

at 8:44 p.m.

On August 13,

1993, Unit 4 entered

Modes

4 and

5 at 5: 10 a.m.

and 10:55 a.m., respectively.

Following RCS filling and venting,

RCS heatup

was

commenced

at

1:45 a.m.

on August 15,

1993.

A pressurizer

bubble

was

established

at 11:40 a.m.,

Mode 4 was entered

at 1:36 p.m.,

and

Mode

3 was entered

at 10:30 p.m.

Normal operating

pressure

(2235

psig)

and temperature

(547'F) were established

at 3:40 a.m.

on

August

16,

1993.

Reactor

startup

was

commenced

at 4:22 p.m.,

Hode

2 was entered

at 5:03 p.m.,

and critical'ity was achieved

at 5:20

p.m.

Hode

1 was entered

at 7:55 p.m., Unit 4-was placed

back on

line at 9:27 p.m.,

and reactor

power was increased

to

approximately

28K for a chemistry hold.

(Refer -to paragraph

8.c

for additional information.)

At 10:33 p.m.

on August 16, 1993,'nit

4 experienced

a turbine

trip and subsequent

reactor trip from approximately

28K power due

to high narrow range level in the

4C steam generator.

(Refer to

paragraph 8.f for additional information.)

Reactor startup

was

commenced

at 9:17 a.m.

on August 17,

1993.

Hode

2 was entered

at 9:50 a.m., criticality was achieved

at 10:04

a.m.,

Hode

1 was entered

at 1:01 p.m.,

and Unit 4 was placed

back

on line at 1:28 p.m.

Reactor

power was stabilized at

100% at 6:00

a.m.

on August 18,

1993.

(Refer to paragraph 8.f for additional

information.)

Onsite Followup and In-Office Review of Written Reports of Nonroutine

Events

and

10 CFR Part 21 Reviews

(90712/90713/92700)

The Licensee

Event Reports

and/or

10 CFR Part 21 Reports

discussed

below

were reviewed.

The inspectors verified that reporting requirements

had

been= met, root cause

analysis

was performed, corrective actions

appeared

appropriate,

and generic applicability had

been considered.

Additionally, the inspectors verified the licensee

had reviewed

each

event, corrective actions

were implemented, responsibility for

corrective actions not fully completed

was clearly assigned,

safety

questions

had

been evaluated

and resolved,

and violations of regulations

or TS conditions

had

been identified.

When applicable,

the criteria of

10 CFR Part 2, Appendix C, were applied.

(Closed)

LER 50-251/93-002,

Reactor Trip Due to Hanual Turbine

Trip.

This event

was discussed

in detail in paragraphs

3 and 10.d of NRC

Inspection

Report

No. 50-250,251/93-17

and in paragraphs

3 and 8.a

of NRC Inspection

Report

No. 50-250,251/93-19.

On June

22,

1993,

the licensee

performed

a turbine trip test

on Unit 4 while it was

operating at

100% reactor power,

and operators

were unable to

relatch the turbine trips after the successful

completion of this

test.

As a result,

a load reduction

was

commenced with the

intention of ta'king the turbine off line to troubleshoot

and

repair the turbine trip latching mechanism.

During this load

reduction,

a loss of turbine control oil pressure

occurred with

reactor

power at approximately

33%.

This in turn resulted

in a

turbine anti-motoring trip followed by a generator

lockout.

Based

on the turbine anti-motoring indication

and the generator lockout,

operators

manually tripped the turbine,

and

a subsequent

reactor

trip occurred

because

reactor

power was greater

than IÃ.

The

1.1 ~

'licensee's

subsequent

investigations

concluded that the cause

was

an inadvertent operation of the..auxiliary governor trip lever by

personnel

restoring the turbin'e controls to normal after the

turbine trip test.

As a result,

the licensee'-installed

a guard to

prevent the inadvertent operation of the auxiliary governor trip

lever.

The unrelated inability to relatch the turbine trips was

caused

by incorrect clearances

in the overspeed trip block between

the trip relay and the relay bushing

and between

the relay cup

valve and the relay cover plate.

These clearances

were corrected,

and Unit 4 was returned to service

on June

26,

1993.

This

LER is

closed.

Surveillance Observations

(61726)

The inspectors

observed

TS required surveillance testing

and verified

that 'the test procedures

conformed to the requirements

of the TSs;

testing

was performed in accordance

with adequate

procedures;

test

instrumentation

was calibrated; limiting conditions for operation

were

met; test results

met acceptance

criteria requirements

and were reviewed

by personnel

other than the individual directing the test; deficiencies

were identified,

as appropriate,

and were properly reviewed

and resolved

by management

personnel;

and system restoration

was adequate.

For

completed tests,

the inspectors verified testing frequencies

were met

and tests

were performed

by qualified individuals.

The inspectors

witnessed/reviewed

portions of the following test

activities:

procedure

3-SHI-064. 1, Accumulator Level

and Pressure

Loop Analog

Tests;

and

procedure

3-0SP-022.4,

EDG Fuel Oil Transfer

Pump

and Valve

Inservice Test.

The inspectors

determined that the above testing activities were

performed in a satisfactory

manner

and met the requirements

of the TSs.

The flow gage associated

with the

EDG fuel oil transfer

pump test

was

observed to be functioning erratically during the first run of the test.

A PWO was written to troubleshoot

and repair the gage.

The test

was

rerun satisfactorily.

Violations or deviations

were not identified.

Haintenance

Observations

(62703)

Station maintenance activities of safety-related

systems

and components

were observed

and reviewed to ascertain

they were conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and standards,

and in conformance with the TSs.

The following items were considered

during this review,

as appropriate:

LCOs were met while components

or systems

were removed from service;

approvals

were obtained prior to initiating work; activities were

accomplished

using approved

procedures

and were inspected

as applicable;

procedures

used

were adequate

to control the activity; troubleshooting

activities were controlled

and repair..records

accurately reflected the

maintenance

performed; functional testing and/or calibrations

were

performed prior to returning components

or systems- to service;

gC

records

were maintained; activities were accomplished

by qualified

personnel;

parts

and materials

used

were properly certified;

radiological controls were properly implemented;

gC hold points were

established

and observed

where required; fire prevention controls were

implemented;

outside contractor force activities were controlled in

accordance

with the approved

gA program;

and housekeeping

was actively

pursued.

The inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

cleaning of Unit 4

TPCW heat exchangers

and

troubleshooting

and weld repair of an unisolable leak on

pressurizer

spray mini-flow bypass

valve 4-524A, the bypass

valve

for pressurizer

spray valve PCV-4-455B (Refer to paragraph

B.c for

additional information.).

For those maintenance activities observed,

the inspectors

determined

that the activities were conducted

in a satisfactory

manner

and that the

work was properly performed in accordance

with approved

maintenance

work

orders.

Violations or deviations

were not identified.

Operational

Safety Verification (71707)

The inspectors

observed control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room operators,

observed shift

turnovers,

and monitored instrumentation.

The inspectors verified

proper valve/switch alignment of selected

emergency

systems,

verified

maintenance

work orders

had

been submitted

as required,

and verified

followup and prioritization of work was accomplished.

The inspectors

reviewed tagout records, verified compliance with TS LCOs,

and verified

the return to service of affected

components.

By observation

and direct interviews, verification was

made that the

physical security plan was being implemented.

The implementation of

radiological controls

and plant housekeeping/cleanliness

conditions were

also observed.

In addition, the inspectors

reviewed portions of the

licensee's

GET training program.

Tours of the intake structure

and diesel, auxiliary, control,

and

turbine buildings were conducted to observe plant equipment conditions

including potential fire hazards,

fluid leaks,

and excessive

vibrations.

The inspectors

walked

down accessible

portions of the following safety-

related systems/structures

to verify proper valve/switch alignment:

A and

B emergency diesel

generators,

Vs~

6

control

room vertical panels

and safeguards

racks,

intake cooling water structure';

4160-volt buses

and 480-volt load

and motor control centers,

Unit 3 and

4 feedwater platforms,

Unit 3 and

4 condensate

storage

tank area,

auxiliary feedwater

area,

Unit 3 and

4 main steam platforms,

and

4

auxiliary building.

I~

The licensee routinely performs

QA/QC audits/surveillances

of activities

required

under its

QA program

and

as requested

by management.

To assess

the effectiveness

of these

licensee

audits,

the inspectors

examined the

status,

scope,

and findings of the following audit reports:

Audit Number

QAO-PTN-93-013

QAO-PTN-93-014

QAO-PTN-93-015

QAO-PTN-93-016

QAO-PTN-93-018

Number of

~Findin

s

T

e of Audit

Control of Computer Software

Per

Procedure

QP 2.15

Radioactive effluents

(Process

Control

Program)

TSs 6.1, 6.2,

and 6.5.1

and

TQR 1.0

June

Performance

Monitoring Audit

Radwaste Audit

No additional

NRC followup actions will be taken

on the finding

referenced

above

because it was identified by the licensee's

QA program

audits

and corrective actions

have either been completed or are

currently underway.

Plant management

has also

been

made

aware of this

issue.

As a result of routine plant tours

and various operational

observations,

the inspectors

determi'ned that the general

plant and system material

conditions were satisfactorily maintained,

the plant security program

was effective,

and the overall performance of plant operations

was good.

Violations or deviations

were not identified.

Plant Events

(93702)

The following plant events

were reviewed to determi.ne.facility status

and the need for further followup action.

Plant parameters

were

evaluated

during transient

response.

The significance of the event

was

evaluated

along with the performance of the appropriate

safety

systems

and the actions

taken

by the licensee.

The inspectors verified that

required notifications were made to the

NRC.

Evaluations

were performed

relative to the need for additional

NRC response

to the event.

Additionally, the following issues

were examined,

as appropriate:

details regarding the cause 'of the event; event chronology; safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences, if any;

and proposed corrective actions.

'a ~

b.

C.

At 3: 15 a.m.

on July 24,

1993;

power ascension

was

commenced

following the repair of a steam leak on the

3B HSR drain line.

In

order to facilitate cleaning of the

3A TPCW heat exchanger,

reactor

power was stabilized at 5Ã at approximately 6:40 a.m.

At

6:00 p.m., the licensee

commenced

a slow power increase

and

removed the

3B TPCW heat exchanger

from service for cleaning.

This heat

exchanger

was returned to service at 9:30 a.m.

on

July 25,

1993.

Power ascension

from 75K was re-commenced

at

a

rate of i@A per hour,

and 10% reactor

power was-achieved

at 12:15

p.m.

The inspectors

witnessed portions of the power ascension.

At 1:15 a.m.

on August 3,

1993,

ISC personnel

identified that the

RC-1 relay in train

B reactor protection relay rack gR37 was in

the de-energized

(fail safe) condition.

With loop A RCS flows

greater

than

90K, the

RC-1

and

RC-2 relays should

be energized.

An investigation

was initiated,

and

a replacement

relay was found.

At 5:35 a.m. the licensee

closed reactor trip bypass

breaker

B in

order to facilitate the replacement

and testing of relay RC-1.

This action placed Unit 3 in a 2-hour action statement

per TS

Table 3.3-1,

item 19, Reactor Trip Breakers,

action statement

8.

This action statement

requires that with the number of operable

channels

1 less

than the minimum channels

operable

requirement,

the unit be in at least

Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

This action

statement

also states that

1 channel

may be bypassed for up to

2

hours for surveillance testing per

TS 4.3. 1. 1 provided that the

other channel

is operable.

The relay was replaced

and tested

per

procedure

3-OSP-049. 1, Reactor Protection

System Logic Test; the

B

reactor trip bypass

breaker

was re-opened

at 6:50 a.m.; the 2-hour

action statement

was exited.

On August 11,

1993, the licensee

performed

an operability

assessment

because

pressurizer

spray mini-flow bypass

valve 4-524A

was blowing steam out of a bellows rupture

and body-to-bonnet

0-ring leak,

and

an increase

in leakage

was noted from an

inspection

performed

two weeks prior.

The steam blowing out of

the weep hole was impinging only on the insulation of spray valve

PCV-4-455B which was located

12 inches

overhead.

The resulting

steam condensation

and boric acid crystal

accumulation

was being

deposited

on the insulation or dripping directly onto the floor.

There were

no other components

involved..

The apparent rate of

steam condensation

on the overhead

valve".insulati.on

was about

70

to 80 drops per minute,

and the results of a leak rate calculation

performed from 9:00 a.m. to 10:00 a.m.

on August ll, 1993,

were

.08 gpm gross

leakage

and

.03

gpm unidentified leakage.

This was

consistent with current

and past leakage trends which were within

TS limits.

The leakage

was minor in nature

and was coming from a

mechanical joint.

Although any increase

in the leakage

would have

been readily detectable

by

RCS leakrate calculations,

Rll/R12

levels,

and

sump level; licensee

management

elected to remove Unit

4 from service in order to facilitate the replacement

of valve 4-

524A.

This action

was conservative

and was noted

as

a strength.

. At 5:55 p.m.

on August 12,

1993,

a load reduction

was

commenced

in

order to facilitate the replacement of the pressurizer

spray mini-

flow bypass valve (4-524A) around pressurizer

spray valve PCV-4-

-455B.

Unit 4 was taken off line and entered

Mode

2 at 8:34 p.m.,

and

Hode

3 was entered

at 8:44 p.m.

On August 13,

1993, Unit 4

entered

Modes

4 and

5 at 5: 10 a.m.

and 10:55 a.m., respectively.

The inspectors

attended

many of the

ERT meetings

and followed up

on the licensee's

troubleshooting

and planning activities.

Following the replacement

of the mini-flow bypass

valve, the

RCS

was filled and vented,

a pressurizer

bubble

was established,

and

RCS heatup

was

commenced

ahead of schedule.

On August 15,

1993.

Hode

4 was entered

at 1:36 p.m.,

and

Hode

3 was entered

at 10:30

p.m.

Normal operating pressure

(2235 psig)

and temperature

(547'F) were established

at 3:40 a.m.

on August 16,

1993.

Reactor

startup

was

commenced

at 4:22 p.m.,

Hode

2 was entered

at 5:03

p.m.,

and criticality was achieved at 5:20 p.m.

Mode

1 was

entered

at 7:55 p.m., Unit 4 was placed

back on line at 9:27 p.m.,

and reactor

power was increased

to approximately

28K, for a

chemistry hold.

The inspectors

witnessed

the licensee's

approach

to criticality.

The evolution was performed in a professional

manner with good communications.

At 3:42 p.m.

on August 13,

1993,

an

IKC Specialist

experienced

respiratory

problems while picking up his children at the

licensee's

Child Care Facility.

Initial CPR was provided by

individuals in the imnediate vicinity.

The site's

medical

group

was called

and responded

in approximately three minutes.

Hetro-

Dade was also called

and arrived on site at 4:02 p.m.

Hetro-Dade

tran'sported

the individual to South Hiami Hospital of Homestead

at

4:45 p.m.,

and the individual was declared

dead at 5:20 p.m.

Preliminary results

indicated possible

asthmatic

bronchial

spasms

which may have led to cardiac arrest;

The licensee notified the

NRC Resident

Inspector at 5:30 p.m.,

and notified the

NRC Opera-

tions Center of a Significant Event per

10 CFR 50.72(b)(2)(vi) at

5:40 p.m.

Because

the fatality was not work-related,

the licensee

elected not to issue

a press

release,

and the State of Florida was

not notified.

The

NRC Resident

Inspectors will followup on the

results of the autopsy

and the 'ticensee's

investigation

as they

become available.

On August 13,

1993, the licensee identified aMisconnected

wire

associated

with the TDRL-X relay which had caused

the cycle

program in the

OThT and

OPBT turbine runback logic to become

dysfunctional.

The TDRL-X relay normally sends

a turbine runback

signal to the governor for 1.5 seconds

at

a rate of 20(C per

minute every 30 seconds until the initiating signal clears.

Mith

the wire associated

with TDRL-X disconnected,

there would be no

timing function,

and the runback would occur continuously until

the bT initiating condition clears.

The OTbT and

OPBT runback

setpoint at Turkey Point is currently the

same

as the

OThT and

OPBT reactor trip setpoints.

Therefore,

a turbine runback of any

. duration or frequency would be masked

by the reactor trip.

The licensee identified the disconnected

during

a field walkdown

to ensure similarity between

the units in preparation of Unit 3

PC/H 93-005, Elimination of Turbine Runback

on Dropped

Rod.

PC/H

92-181

had implemented this

same modification on Unit 4 during the

last refueling outage.

The licensee

had performed

a 10'FR 50.59

safety analysis of this modification.

A lack of attention to detail contributed to the problem in that

the "before" drawings were not included in the

PC/H in combination

with the implementor not correctly interpreting the

PC/H drawing.

Additionally, with the TDRL-X relay outside the scope of the

PHT,

the problem went unnoticed.

In order to address this issue,

the

licensee

developed

Condition Report

No.93-740.

As corrective action, the licensee

plans to train appropriate

personnel

on the gI requirements

with regard to "before" and

"after" drawings in PC/H packages

by approximately

September

15,

1993,

and

on reading

and interpretation

of various electrical

design

and production drawings

by approximately September

29,

1993.

The licensee

also plans to issue

a TDI by approximately

December

31,

1993, in order to clarify scope of PHT procedures.

The cognizant design engineer will be directly involved with the

preparation

and performance of PHT procedures

for complex tasks

as

determined

by engineering.

The inspectors

reviewed the licensee's

interim disposition of

Condition Report

No.93-740

and also verified that the OTbT and

OPBT runbacks

are not taken credit for in the accident analysis

and, therefore,

are not required

by TSs.

Additionally, with the

runback setpoint the

same

as the trip setpoint,

the runback

as

such serves

minimal purpose.

The inspectors

noted

a weakness

in

the lack of attention to detail

on the Unit 4 design

package for

the elimination of the turbine runback

on

a dropped rod and noted

a strength for engineering's

quality perspective

in the

identification of the inadvertent

removal of a wire on the Unit 4

turbine runback circuitry during the preparation for the

10

performance of the

same modification on Unit 3.

The inspectors

will continue to monitor licensee

performance

in this area.

Unit 4 experienced

a reactor trip from approximateTy 2N power at

10:33 p.m.

on August 16,

1993.

The reactor trip was caused

by a

tur bine trip which was caused

by high-high

SG level

(80X on narrow

range)

in the

4C SG.

A feedwater oscillation during the evolution

involving valving in of the

6A and

6B high pressur e feedwater

heaters

located

downstream of the main feedwater

pumps resulted in

the high

SG level.

Unit 4 had

been placed

on line at approximately 9:27 p.m following

the forced shutdown discussed

in paragraph

8.c of this report.

Power was increased

and held at approximately 2N for secondary

chemistry cleanup.

SG level

was appropriately

being controlled

with the feedwater flow control/regulation valves in automatic

and

one main feedwater

pump in operation.

With the

6A and

6B

feedwater

heaters still in bypass,

the next step in the evolution

was to place the two high pressure

feedwater heaters

in service.

The

ANPS for Unit 4 directed the

NWE to place the feedwater

heaters

in service in accordance

with procedure

4-0P-081.1,

Feedwater

Heater,

Extraction Steam,

Vents,

and Drains Valve

Alignment.

The

NWE, along with a balance of plant non-licensed

operator,

simultaneously initiated section 7.8, Restoration of the

6A

Feedwater

Heater

Tube Side,

and section 7.9, Restoration of the

6B

'eedwater

Heater

Tube Side, of procedure

4-OP-081. 1.

The sequence

of steps

to restore is specifically outlined in procedure

4-OP-

081. 1 with a sign-off following completion of each step.

For each heater,

the 3-way heater

bypass/normal

valve is required

by the procedure to be cracked

open off the seat followed by

verification of filling of the tube side of the heater.

Then the

tube side outlet valve is required to be slowly opened

followed by

the 3-way valve taken from the bypass to the normal position.

Performing the steps

in this sequence

would minimize changes

in

feedwater flow to the

SG.

The inspectors

noted that the procedure

was silent

on whether both the feedwater

heaters

can

be valved in

simultaneously.

Contrary to the steps outlined in procedure

4-OP-081. 1, the two

personnel

performing the feedwater lineup first cracked

open both

the feedwater tube side outlet valves

(4-30-123

and 4-30-223).

Then they opened the 3-way feedwater heater normal/bypass

valves

(4-20-121

and 4-20-221) to the normal position.

With the outlet

valves only cracked

open

and the 3-way valves

now in the normal

position (i.e. feedwater flow through the heaters)

the feedwater

flow to the

SGs started to drop

as

the= running feedwater

pump was

essentially

dead-heading.

The

RCO observed

the decreasing

SG levels

and was advised

by the

ANPS to start another condensate

pump

as. well as the other main

feedwater

pump.

The main feedwater flow control..valves

were also

taken in manual with demand for full open.

SG level recovered to

approximately

25%.

The oncoming

ANPS,

who enroute to the control

room had observed

the

NWE and the turbine operator

open the 3-way valves,

recognized

the cause of the perturbation in the feedwater

system.

He

requested

the feedwater heaters

to be unisolated.

6A feedwater

heater

was unisolated first by opening valve 4-20-223.

Feedwater

flow.was recovered,

and

SG levels started to increase.

The 4A

feedwater

pump was stopped,

and attempts

were

made to reduce

'eedwater

flow.

During this time, the

6A feedwater

heater

was also unisolated

by

opening valve 4-20-123.

This caused

feedwater flow to increase

rapidly,

and the

RCO was unable to adequately

control

SG levels.

The high-high level setpoint

was reached

on the

4C

SG causing the

turbine

and consequently

the reactor trip.

The post-trip response

by the operators

was

as expected.

The

overfeeding of SGs caused

Tave to go below the no load setpoint of

543'F.

The cooldown was slowed by shutting the HSIVs.

Letdown

was manually isolated

due to the decrease

in pressurizer

level

caused

by the cooldown.

Additionally, AFW actuation

had also

occurred following the loss of both feedwater

pumps

due to the

high-high

SG level.

A notification pursuant to the requirements

of 10 CFR 50.72 was

made in a timely manner.

The resident

inspectors

were also

notified.

The resident

inspectors

reviewed the Post Trip Review

Restart

Report

and discussed

the event with several

key utility

personnel

including the Plant Manager.

The resident

inspectors

expressed

concern

over the lack of command

and control that

resulted

in the feedwater transient

and subsequent

reactor trip

and the lack of good communications

needed to ensure that both

control

room and field personnel

were aware of the performance of

significant evolutions.

This was evidenced

by the fact that the

decision

and the subsequent

request

by the

ANPS to valve in the

high pressure

feedwater heaters

was not properly communicated to

the

RCO.

This resulted

in the

RCO not'eing fully aware of the

activities that affected his ability to control

SG levels.

Concern

over performing steps

out of sequence

was also discussed

with the licens'ee.

The licensee

was in full agreement with the concerns

expressed

by

the resident

inspectors.

Corrective actions to prevent recurrence

will.include briefing control

room supervisors

as to the need for

proper communication prior to initiation of major activities,

counseling of the operators

involved,

and review for further

enhancement

to procedure

4-0P-OSl.l in light of this event.

The

12

licensee

expects to complete these corrective actions

by. September

30,

1993.

While the licensee's. initial. corrective actions

were

prompt and thorough, this violation is being .cited because

deficiencies

in command, control,

and comaunications

allowed

a

procedural violation to escalate

into a challenge to reactor

safety

and because

a previous event also involved

a procedural

violation and

a lack of proper communication

between

operators

(VIO 50-250,251/93-01-02).

The failure to follow steps

as written

in procedure

4-0P-081.1 will be tracked

as

VIO 50-250,251/93-21-

01, failure to follow a procedure resulting in a feedwater

transient

and subsequent

reactor trip.

The resident staff observed

a majority of the activities

associated

with the reactor startup which was

commenced

at 9: 17

a.m.

on August 17,

1993.

Criticality was achieved at 10:04 a.m.,

Mode

1 was entered

at 1:Ol p.m., Unit 4 was placed

back on line at

1:28 p.m.,

and reactor

power was stabilized at

100K at 6:00 a.m.

on August 18,

1993, without any complications.

One Violation was identified.

Exit Interview

The inspection

scope

and findings were summarized during management

interviews held throughout the reporting period with the Plant General

Manager

and selected

members,.of his staff.

An exit meeting

was

conducted

on August 24,

1993.

The areas

requiring management

attention

were reviewed.

The licensee

did not identify as proprietary

any of the

materials provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comnents

were not received

from the licensee.

The inspectors

had the following findings:

Item Number

Descri tion and Reference

50-250,251/93-21-01

Strength

Weakness

Strength

VIO - Failure to follow a procedure resulting in

a feedwater transient

and subseque'nt

reactor

trip (paragraph 8.f).

Management's

decision to remove Unit 4 from

service in order to facilitate the replacement

of a pressurizer

spray mini-flow bypass

valve

due to a minor unisolable leak was conservative

(paragraph 8.c).

The lack of attention to detail

on the Unit 4

design

package for the elimination of the

turbine runback

on a dropped rod (paragraph

8.e).

. Engineering's quality perspective

in the

identification of the inadvertent

removal of a

wire on the Unit 4 turbine runback cir cuitry

~

~

0

10.

Acronyms

AFW

ANPS

CFR

CPR

EDG

ERT

F

GET

gpm

IKC

LCO

LER

HSIV

HSR

NPS

NRC

NWE

OP

OPBT

OTBT

OSP

PC/H

PCV

PHT

pslg

PTN

PWO

QA

QAO

QC

QI

QP

RCO

RCS

SG

SHI

Tave

TDI

TPCW

TQR

TS

VIO

13

during the preparation for the performance of

the

same modification. on Unit 3 (paragraph 8.e).

and Abbreviations

Auxiliary Feedwater

Assistant Nuclear Plant Supervisor

Code of Federal

Regulations

Cardiopulmonary Resuscitation

Emergency Diesel

Generator

Event Response

Team

Fahrenheit

General

Employee Training

Gallons

Per Hinute

Instrumentation

and Control

Limiting Condition for Operation

Licensee

Event Report

Hain Steam Isolation Valve

Hoisture Separator

Reheater

Nuclear Plant Supervisor

Nuclear Regulatory

Commission

Nuclear Watch Engineer

Operating

Procedure

Overpower Delta Temperature

Overtemperature

Delta Temperature

Operations

Surveillance

Procedure

Plant Change/Hodification

Pressure 'Control Valve

Post-Hodification Test

pounds per square

inch gauge

Project Turkey Nuclear

Plant Work Order

Quality Assurance

Quality Assurance

Organization

Quality Control

Quality Instruction

Quality Procedure

Reactor Control Operator

Reactor Coolant System

Steam Generator

Surveillance Haintenance

- ISC

Average Temperature

Technical

Department Instruction

Turbine Plant Cooling Water

Topical Quality Report

Technical Specification

. Violation

Delta Temperature

0

I