ML17349A723

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Insp Repts 50-250/93-01 & 50-251/93-01 on 930101-29. Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety & Plant Events
ML17349A723
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 02/17/1993
From: Butcher R, Landis K, Schenbli G, Trocine L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17349A721 List:
References
50-250-93-01, 50-250-93-1, 50-251-93-01, 50-251-93-1, NUDOCS 9303020265
Download: ML17349A723 (35)


See also: IR 05000250/1993001

Text

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UNITEDSTATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/93-01

and 50-251/93-01

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-250

and 50-251

License Nos.:

DPR-31

and

DPR-41

Facility Name:

Turkey Point Units 3 and

4

Inspection

Conducted:

January

-29,

1993

Inspectors:

.

C. Butche

, Senior Resident

Inspector

M (7

Da

Si

ned

(7

0

. A. Schnebl

, Resi

nt Inspector

Dat

Si

ned

C

~

~

. Trocine, Resident

Inspector

Date Si

ned

Accompanying Personnel:

R. Freudenberger,

Resident

Inspector,

Crystal River

J. J.

Lenahan,

Reactor Inspector,

Engineering

Branch,

Division of Reactor Safety

R.

P. Schin, Project Engineer,

Division of Reactor

Projects,

RII

Approved by:

K. D. Landis, Chief

Reactor ProjectsSection

2B

Division of Reactor Projects

/7 N

Date Signed

SUMMARY

Scope:

This routine resident

inspector inspection

involved direct inspection at the

site in the areas of monthly surveillance observations,

monthly maintenance

observations,

operational

safety,

and plant events.

Backshift inspections

were performed

on January

6, 7,

and

18,

1993.

Results:

In the operations

area,

several

major plant status

changes

were accomplished

in a professional

and controlled manner,

including two Unit 3 and

one Unit 4

shutdowns

and their subsequent

startups.

Two areas of concern

were identified

l

involving the inadvertent

opening of a power operated relief valve

(paragraph

'F303020265

9302f7

PDR

ADOCK 05000250

6

PDR

0

e

2

8.c)

and the iso1ation of the containment

spray

pumps in the wrong mode of

operation

(paragraph

S.d) which indicates

a lack of attention to detail.

In the maintenance

area,

several

equipment failures required plant shutdowns

for repairs,

inc1uding rep1acement

of 38 moisture separator

reheater

drain

line, repair of an unisolable leak on Unit 3 pressurizer

spray line,

and the

repacking of 4A steam generator

feed regulating valve.

Maintenance for the

three short notice outages

was conducted

in a safe, efficient manner,

and the

units were returned to service within the scheduled

time.

In the safety assessment/quality

verification area,

an issue

was identified

concerning

a failure to implement measures

to assure

vendor supplied materials

conform to procurement

documents

(paragraph 8.e).

In the engineering

and technical

support

area,

a weakness

was identified

concerning minor inaccuracies

on drawings which is

a repetitive problem

(paragraph 7.c).

Within the scope of this inspection,

the inspectors

determined that the

licensee

continued to demonstrate

satisfactory

performance to ensure

safe

plant operations.

One violation was identified.

In addition, the licensee,

through self assessment,

took prompt action to correct the two

non-cited violations:

Non-Cited Violation 50-250,251/93-01-01,

failure to maintain pressurizer

pressure

below 375 psig resulting in the inadvertent

opening of a power

operated relief valve (paragraph 8.c).

Violation 50-250,251/93-01-02,

failure to follow procedures

in the area of

conduct of operations resulting in the isolation of containment

spray prior to

reactor coolant

system temperature

going below 200'

(paragraph 8.d).

Non-Cited Violation 50-250,251/93-01-03,

failure to implement measures

to

assure

that the wet annular burnable absorber

assemblies

conformed to

procurement

documents

(paragraph

S.e).

i

REPORT DETAILS

Persons

Contacted

Licensee

Employees

T. V.

H. J.

R. J.

R. J.

R.

D.

E.

F.

R.

G.

P.

C.

D.

E.

H. H.

V. A.

J.

E.

J.

E.

R. S.

J.

D.

L.

W.

H. 0.

T.

F.

D.

R.

R.

E.

R.

N.

F.

R.

R. J.

H.

B.

E. J.

Abbatiello, Site guality Hanager

Bowskill, Reactor

Engineering Supervisor

Earl, quality Assurance

Supervisor

Gianfrencesco,

Support Services

Supervisor

Gill, Chief Civil Engineer

Hayes,

Instrumentation

and Controls Haintenance

Heisterman,

Hechanical

Haintenance

Supervisor

Higgins,

Outage

Hanager

Jernigan,

Technical

Hanager

Johnson,

Operations

Supervisor

Kaminskas,

Operations

Hanager

Kirkpatrick, Fire Protection/Safety

Supervisor

Knorr, Regulatory

Compliance Analyst

Kundalkar,

Engineering

Hanager

Lindsay, Health Physics Supervisor

Pearce,

Plant General

Hanager

Pearce,

Electrical Haintenance

Supervisor

Plunkett, Site Vice President

Powell, Services

Hanager'ose,

Nuclear Haterials

Hanager

Steinke,

Chemistry Supervisor

Timmons, Security Supervisor

Tomonto,

Licensing Engineer

Wayland,

Haintenance

Hanager

Weinkam,

Licensing Hanager

Supervisor

Other licensee

employees

contacted

included construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

Bechtel

Employee

o G.

Thomas,

Senior Structural

Engineer

NRC Resident

Inspectors

  • R.

C. Butcher,

Senior Resident

Inspector

  • G. A. Schnebli,

Resident

Inspector

  • L. Trocine,

Resident

Inspector

Other

NRC Personnel

S. A. Varga, Director, Division of Reactor Projects

- I/II, NRR

H.

N. Berkow, Director, Project Directorate II-2, NRR

o L. Raghavan,

Project Hanager,

Project Directorate II-2, NRR

o H. Ashar,

Senior Structural

Engineer, Civil Engineering

& Geoscience

Branch,

NRR

o G. Bagchi, Chief, Civil Engineering

& Geoscience

Branch,

NRR

l

]

2.

o Y. Kim, Senior Structural

Engineer, Civil Engineering

8 Geoscience

Branch,

NRR

o J.

Lenahan,

Reactor

Inspector,

Engineering

Branch,

Region II

R. Freudenberger,

Resident

Inspector,

Crystal River

R.. Schin,

Project Engineer,

Region II

Attended exit interview on January

29,

1993

o

Attended January ll, 1993, meeting at

NRC headquarters

regarding

containment

tendon surveillance

inspections.

(Refer to paragraph

9 for

additional information.)

Note:

An alphabetical

tabulation of acronyms

used in this report is

listed in the last paragraph

in this report.

Other

NRC Inspections

Performed During This Period

Re ort No.

Dates

Area Ins ected

3.

50-250,251/93-05

January

25-29,

1993

Emergency

Preparedness

Plant Status

Unit 3

At the beginning of this reporting period, Unit 3 was operating at

100%

power and

had

been

on line since

December

6,

1992.

The following

evolutions occurred

on this unit during this assessment

period:

On January

8,

1993, at ll:15 a.m.,

a load reduction to support

flux mapping

was

commenced.

At 12:20 p.m., the licensee

began

inducing Xenon oscillations with reactor

power at 85%,

and the

load reduction

was continued at 6:00 p.m., in order to facilitate

the repair of a steam leak on

a 3B HSR drain line.

The turbine

was taken off line,

and the unit entered

Mode

2 at 7:40 p.m.

The

turbine was placed

back on line,

and Unit 3 entered

Mode

1 again

at 2:30 a.m.

on January

10,

1993.

With reactor

power at

approximately

30%,

power ascension

was ceased

at 3:30 a.m.

due to

secondary

system high cation conductivity.

Power ascension

was

re-commenced

at 12:45 p.m.,

and

100% reactor

power was achieved at

8:20 p.m.

On January

15,

1993, at 2:32 p.m.,

an Unusual

Event was declared

because

of the identification of RCS pressure

boundary leakage.

(Refer to paragraph

8.b for additional information.)

A unit

shutdown

was

commenced

at 2:35 p.m., the turbine was manually

tripped at 5:49 p.m.,

and

Mode 3 was entered

at 5:55 p.m.

Unit 3

entered

Mode

4 at 4:40 a.m.

on January

16,

1993.

At 6: 15 p.m.,

Mode

5 was entered,

and the Unusual

Event was downgraded to a non-

emergency classification.

On January

18,

1993,

at 4:55 a.m., Unit 3 entered

Mode 4.

Hode

3

was entered

at 5:05 p.m.

on January

19,

1993.

Mode

2 was entered

at 2:02 p.m.

on January

20,

1993;

and criticality was achieved at

2:28 p.m.

Unit 3 was placed

on line and

Mode

1 was entered

at

7:25 p.m.

on January

20,

1993,

and reactor

power reached

100% at

4:25 a.m.

on January

21,

1993.

Unit 4

At the beginning of this reporting period, Unit 4 was operating at

100%

power

and

had

been

on line since October 27,

1992.

The following

evolutions occurred

on this unit during this assessment

period:

On January

6,

1993, at 7:20 p.m.,

a load reduction to approximate-

ly 15% reactor

power was

commenced

in order to facilitate the

repacking of the

4A steam generator

feedwater regulation valve

(FCV-4-478).

The unit was stabilized at approximately

50

MWe at

9:45 p.m.

The turbine was tripped

and

Node

2 was entered

at 3:45

a.m.

on January

7,

1993.

Following the repair,

the turbine

was

placed

back

on line and

Mode

1 was re-entered

at 11:50 a.m.

At

12:40 p.m.,

power ascension

was ceased

and reactor

power

was

maintained at approximately

45% because

axial flux was outside of

the target

band for 73 minutes.

Power ascension

was

re-commenced

at 12:30 p.m.

on January

8,

1993,

and

100% reactor

power was

attained at 6:30 p.m.

On January

26,

1993, at 7:50 a.m.,

a power reduction

was

commenced

as

a precautionary

measure

due to a ground

on the

4A condensate

pump.

(Refer to paragraph 8.f for additional information.)

Reactor

power was stabilized at

70% at 9:40 a.m.,

power ascension

was

commenced

at 1200 p.m.,

and

100% reactor

power was attained at

5:30 p.m.

Onsite Followup and In-Office Review of Written Reports of Nonroutine

Events

and

10 CFR Part 21 Reviews

(90712/90713/92700)

The Licensee

Event Reports

and/or

10 CFR Part 21 Reports

discussed

below

were reviewed.

The inspectors verified that reporting requirements

had

been met, root cause

analysis

was performed, corrective actions

appeared

appropriate,

and generic applicability had

been considered.

Additional-

ly, the inspectors verified the licensee

had reviewed

each event,

corrective actions

were implemented,

responsibility for corrective

actions not fully completed

was clearly assigned,

safety questions

had

been evaluated

and resolved,

and violations of regulations

or TS

conditions

had

been identified.

When applicable,

the criteria of 10 CFR Part 2, Appendix C, were applied.

(Closed)

LER 50-250/92-12,

Containment

Personnel

Airlock Vent Inadver-

tently Open to Atmosphere

During Core Alterations.

This event

was previously discussed

in IR No. 50-250,251/92-28

and was

identified as

NCV 50-250,251/92-28-01.

This

LER is closed.

0,

Surveillance

Observations

(61726)

The inspectors

observed

TS required surveillance testing

and verified

that the test procedures

conformed to the requirements

of the TSs;

testing

was performed in accordance

with adequate

procedures;

test

instrumentation

was calibrated; limiting conditions for operation

were

met; test results

met acceptance

criteria requirements

and were reviewed

by personnel

other than the individual directing the test; deficiencies

were identified,

as appropriate,

and were properly reviewed

and resolved

by management

personnel;

and system restoration

was adequate.

For

completed tests,

the inspectors verified testing frequencies

were met

and tests

were performed

by qualified individuals.

The inspectors

witnessed/reviewed

portions of the following test

activities:

3-OSP-049. 1, Reactor Protection

System Logic Test, for both trains

A and

B,

and

0-OSP-025.

1 Control

Room Emergency Ventilation System Operability

Test.

The inspectors

determined that the above testing activities were

performed in a satisfactory

manner

and met the requirements

of the TSs.

Violations or deviations

were not identified.

Maintenance

Observations

(62703)

Station maintenance activities of safety-related

systems

and components

were observed

and reviewed to ascertain

they were conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and standards,

and in conformance with the TSs.

The following items were considered

during this review,

as appropriate:

LCOs were met while components

or

systems

were removed from service;

approvals

were obtained prior to initiating work; activities were

accomplished

using approved

procedures

and were inspected

as applicable;

procedures

used

were adequate

to control the activity; troubleshooting

activities were controlled

and repair records accurately reflected the

maintenance

performed; functional testing and/or calibrations

were

performed prior to returning components

or systems to service;

gC

records

were maintained; activities were accomplished

by qualified

personnel;

parts

and materials

used were properly certified;

radiological controls were properly implemented;

gC hold points were

established

and observed

where required; fire prevention controls were

implemented;

outside contractor force activities were controlled in

accordance

with the approved

gA program;

and housekeeping

was actively

pursued.

The inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

replacement

of reactor trip breakers

3A and

3B,

repacking of the

4A main feedwater regulating valve (FCV-4-478),

troubleshooting of water intrusion in thermo-lagged

terminal

box

TB-3029,

replacement

of 3B MSR drain line due to steam leak caused

by

erosion,

and

repair of pressure

boundary leakage

from a cracked weld on

a

capped fitting off the pressurizer

spray line.

(Refer to

paragraph

8.b for additional information).

At 5:20 a.m.

on January

25,

1993, the diesel

driven fire pump

and raw

water tank II were taken out of service for repair

and recoating,

respectively.

TS 3.7.8. 1 requires

the fire water supply

and

distribution system to be operable with at least

two fire suppression

pumps

(one electric driven

and

one diesel

driven) with their discharges

aligned to the fire suppression

header,

with two separate

water supplies

each with a minimum contained

volume of 300,000 gallons,

and with an

operable flow path taking suction from raw water tanks

I and II.

With

one

pump and/or

one water supply inoperable,

action statement

a. of TS 3.7.8. 1 requires

the restoration of the inoperable

equipment to operable

status within 7 days or the provision of an alternate

backup

pump or

water supply.

Alternate

pumps

and

an alternate

water supply were

provided prior to the removal of the diesel

driven fire pump

and raw

water tank II from service via the installation of a spool

piece

between

fire hydrant

13 and the screen wash/fire system crosstie line in

accordance

with O-ONOP-016.7,

Screen

Wash

Emergency

Makeup to the Fire

Protection

System at 1: 15 a.m.

on January

25,

1993.

For those maintenance

activities observed,

the inspectors

determined

that the activities were conducted

in a satisfactory

manner

and that the

work was properly performed in accordance

with approved

maintenance

work

orders.

Violations or deviations

were not identified.

7.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room operators,

observed shift

turnovers,

and monitored instrumentation.

The inspectors verified

proper valve/switch alignment of selected

emergency

systems,

verified

maintenance

work orders

had

been submitted

as required,

and verified

followup and prioritization of work was accomplished.

The inspectors

reviewed tagout records, verified compliance with TS LCOs,

and verified

the return to service of affected

components.

By observation

and direct interviews, verification was

made that the

physical security plan was being implemented.

The implementation of

6

radiological controls

and plant housekeeping/cleanliness

conditions were

also observed.

Tours of the intake structure

and diesel, auxiliary, control,

and

turbine buildings were conducted to observe plant equipment conditions

including potential fire hazards,

fluid leaks,

and excessive

vibrations.

The inspectors

walked down accessible

portions of the following

safety-related

systems/structures

to verify proper valve/switch

alignment:

4

A and

B emergency diesel

generators,

control

room vertical panels

and safeguards

racks,

intake cooling water structure,

4160-volt buses

and 480-volt load

and motor control centers,

Unit 3 and

4 feedwater platforms,

Unit 3 and

4 condensate

storage

tank area,

auxiliary feedwater

area,

Unit 3 and

4 main steam platforms,

and

auxiliary building.

a ~

The inspectors

reviewed the

FSAR and TSs in regard to the

requirements

for the

IAS,

PORVs,

and the nitrogen backup

system

for the

PORVs in conjunction with a postulated fire per

10 CFR Part 50, Appendix R.

The

PORVs were not originally designed

as

safety-related

components

(other than for RCS pressure

boundary

isolation)

as they do not perform any active safety function and

credit for their operation to mitigate design

basis

events

was not

considered

in the plant accident

analyses.

Overpressure

protection for the

RCS is provided

by the pressurizer

safety

valves.

Since the

PORVs, which are air operated

valves,

were not

originally classified

as safety-related

components,

other than fo}

RCS pressure

boundary isolation, their motive power source

was

instrument air which is

a non-safety

system.

A review of Plant

TSs supports this position

as there are

no

LCOs specified for the

PORVs during Nodes

1, 2,

or 3.

TS 3/4.4.4, Relief Valves, applies

to each remotely operated

PORV block valve which is required to be

operable to isolate

an inadvertently stuck open or leaking

PORV in

Nodes

1, 2,

and

3.

The basis for TS 3/4.4.4 states that the

opening of the

PORVs fulfills no safety-related

function and

no

credit is taken for their operation in the safety analysis for

Nodes

1, 2, or 3.

Each

PORV has

a remotely operated

block valve

to provide

a positive shutoff capability should

a relief valve

become inoperable.

I

Subsequently,

increased

emphasis

was placed

on the

PORVs to

provide overpressure

protection for the

RCS during periods of low

RCS temperature/pressure

operation.

This functional requirement

for the

PORVs is referred to as

OHS.

The operational

requirement

for the

PORVs is reflected in Technical Specification Limiting

Condition for Operation 3.4.9.3,

Overpressure

Mitigation System

(OHS), which is required to be operable

in Hodes 4, 5,

and

6 when

RCS average

temperatures

are below 275'F.

This requirement

assures

that the

RCS will be protected

from pressure

transients

which could exceed

the limits of Appendix

G to

10 CFR Part 50. If

the

PORVs are not available in this mode of operation,

the TSs

require that the

RCS

be depressurized

and

a vent path of at least

2.20 square

inches

be established.

As stated in the basis for TS 3.4.9.3,

in the

OHS mode of operation,

the PORVs'unction is to

provide relieving capability to protect the

RCS from the following

overpressurization

events:

The start of a HHSI pump and its injection into a water

solid

RCS; or

The start of an idle reactor coolant

pump with the secondary

water of the steam generators x 50'F above the

RCS leg

temperature.

In summary,

the Turkey Point TSs require that the

PORVs

be

operational

only in Modes 4, 5,

and

6 with the reactor

head

on and

the

RCS not vented.

Operation of the

PORVs in this mode of plant

operation is dependent

on the availability of either the original

non-safety related

IAS or the dedicated

backup safety related

nitrogen bottle system.

To assure that the

PORVs are available in

this mode of operation,

TS 4.4.9.3. l.d. requires that the backup

air supply system

be verified as operable

at least

once every

24

hours.

Procedure

3/4-GOP-305,

Hot Standby to Cold Shutdown,

step

5. 13

requires that prior to

RCS cooldown to less

than 276'F

and when

pressurizer

pressure

is in the range of 325 to 375 psig,

then

perform the nitrogen

backup

system leak test

and loop operability

tests

using 3/4-0SP-041.4,

Overpressure

Mitigating System Nitrogen

Backup

Leak and Function Test,

and establish

and verify OMS

operation in accordance

with 3/4-0P-041.4,

Overpressure

Mitigating

System.

Operating

Procedure

0204.2,

Periodic Tests,

Checks,

and

Operating Evolutions,

step 8.2.3.4(l)

has the

RCO check the

OHS

status

on peak

and mid shifts when the

RCS temperature

is less

than 275'F.

With respect to

10 CFR Part 50, Appendix

R requirements,

the

PORVs

are identified on the essential

equipment l~ist as defined in the

TP FSAR, Appendix 9.6A.

Drawing 5610-H-723,

Appendix

R Essential

Equipment List, lists the

PORVs

(PCV-*-455C and PCV-*-456).

The

purpose for identifying the

PORVs on the essential

equipment list

is two-fold.

First, the

PORVs are protected to ensure that

an

Appendix

R fire does not cause their spurious

opening which could

cause

primary system depressurization.

Secondly,

the

PORVs are

identified to reflect their requirement for providing

OHS

protection.

In accordance

with 10 CFR Part 50, Appendix R,

Section III.L.6, the shutdown

systems installed to meet these

postfire shutdown requirements

need not be designed

to meet

seismic Category

I criteria, single failure criteria or other

design basis

accident criteria.

This requirement is reflected in

the

TP

FSAR.

The

TP

FSAR, Appendix 9.6A presents

the fire

protection

program

as required

by 10 CFR Part 50, Appendix R.

Some of the listed assumptions

and design basis

presented

in the

fire protection

program are

as follows:

During hot standby conditions

and initial cooldown

conditions,

decay heat

removal is accomplished

by

atmospheric

dump valve operations

and

AFW turbine exhaust.

During subsequent

cooldown

and cold shutdown conditions,

decay heat

removal is accomplished

by the

RHR system,

the

CCW system,

and the

ICW system.

No design basis

accident or natural

phenomenon

shall

be

postulated

concurrently.

The single failure criterion shall not apply to the design

of the alternate

shutdown

systems

and components,

except to

account for adverse

equipment actions

caused

by the

postulated fire.

The

IAS provides filtered compressed

air to pneumatic

instruments,

controls,

and air operated

valves.

Based

on the data noted

above,

the

IAS is assumed

to be available

during the Appendix

R postulated fire and the nitrogen

backup

system is not required.

The IAS,

PORVs,

and the nitrogen backup

system

meet present

TS and

10 CFR Part 50, Appendix

R design

requirements.

By GL 90-06 dated

June

25,

1990, the

NRC advised all

PWR owners of

the staff positions relating to

PORV and

PORV block valve

reliability and additional

low-temperature

overpressure

protection

for light water reactors.

The

GL represented

the technical

resolution of two generic

issues

and included plant backfits which

were cost-justified safety

enhancements.

FPL submitted

a response

to

GL 90-06 dated

November 25,

1992,

proposing license

amendments

to resolve the generic

issues

involved.

The

NRC has not completed

review of FPL's submittal at this time.

Based

on the resolution

of the generic

issues of GL 90-06, the existing

TS and/or

FSAR

requirements

are subject to change.

The licensee routinely performs

gA/gC audits/surveillances

of

activities required

under its gA program

and

as requested

by

management.

To assess

the effectiveness

of these

licensee

audits,

the inspectors

examined the status,

scope,

and findings of the

following audit reports:

Number of

Audit Number

~Findin

s

T

e of Audit

QAO-PTN-93-038

Design Control

QAO-PTN-93-045

QA Records

QAO-PTN-93-046

Procedure

Control

No additional

NRC followup action is required.

During inspection of the fire water supply system

on January

11,

1993, the inspector

noted that valve 10-1188,

raw water booster

pump

B recirculation line isolation valve,

had about

a one-foot

length of open threaded five-inch diameter pipe extending

from it.

The inspector could look into the open pipe

and

see the disc of

the manual

gate valve.

A similar valve about two feet

above

(10-1187,

raw water booster

pump

C recirculation line isolation

valve)

had about

a one-foot length of five-inch diameter pipe

extending

from it with a bolted blank flange

on the end.

Both

valves

connected

to raw water storage

tank II through locked open

valve 10-762.

Valve 10-1188

was located

about six feet above the

base of the raw water tank,

such that if it were opened it would

drain most of the TS-required fire supply water from the tank.

The pipes connecting

each of these

valves to the raw water booster

pumps

had recently

been

removed

a part of a modification to the

fire water

and service water systems.

Valves 10-1188

and 10-1187

had clearance

tags attached,

indicating that they were to remain

in the closed position per clearance

No. 0-92-11-019-R.

Subsequent

review found that the clearance,

located in the control

room, referenced

PC/H 92-108

and stated that these

two valves were

tagged

closed for administrative control.

The inspector

asked

a licensee

engineer

who was in the area

inspecting the fire water supply system if there should

be

a blank

flange or lock on valve 10-1188.

Review of the current drawing,

which the engineer

had with him (Drawing No. 5610-T-E-4072,

Operating

Diagram, Fire Protection

System Tanks

L Pumps,

Rev.

24,

dated

November 23,

1992),

showed that valves

10-1187

and 10-1188

had

been

removed

and replaced with blank flanges.

The inspector

and engineer

noted that the drawing was in error.

Additional

review found that the drawing error had

been

made in rev.

23,

dated

November

13,

1992,

and that error had

been carried over into

rev.

24.

Rev.

22 of the drawing, which included valves

10-1187

and 10-1188,

indicated that the sections of piping including those

two valves were inside the

"Q" boundary, i.e. they were quality

related

and important to safety.

The engineer,

working with

licensee fire protection,

operations,

and engineering

personnel,

responded

with prompt interim action.

A lock was placed

on valve

10-1188 that day and

a corrected

drawing, rev. 25,

was issued that

10

same

day, January

11,

1993.

Also, licensee

engineers

conducted

a

walkdown of the piping system

shown in the drawing

and found that

there were

no other errors

on the drawing.

Later, it was

determined that

a lock was not required

on valve 10-1188

and the

lock was removed.

Although it was determined that the noted drawing error had little

safety significance, it is another

example of minor inaccuracies

on drawings.

The licensee

does

have

a program in place to replace

the existing T-E drawings with P&IDs by mid 1993.

As a result of routine plant tours

and various operational

observations,

the inspectors

determined that the general

plant

and system material

conditions were satisfactorily maintained,

the plant security program

was effective,

and the overall performance of plant operations

was good.

Violations or deviations

were not identified.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and the need for further followup action.

Plant parameters

were

. evaluated

during transient

response.

The significance of the event

was

evaluated

along with the performance of the appropriate

safety

systems

and the actions

taken

by the licensee.

The inspectors verified that

required notifications were

made to the

NRC.

Evaluations

were performed

relative to the need for additional

NRC response

to the event.

Additionally, the following issues

were examined,

as appropriate:

details regarding the cause of the event;

event chronology; safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences, if any;

and proposed corrective actions.

a ~

Step 7. 1. 18 of procedure

4-0SP-051.6,

Containment Air Lock Doors

Operability Test, requires

the outside air lock door latch of the

containment

personnel

air lock to be slowly turned toward the

unlatched position in order to verify that the door will not

unlatch.

During performance of this step at 2:30 a.m.

on

January

14,

1993, the outside air lock door latch partially moved

in the unlatched position,

and air flow was detected.

Both doors

were immediately closed,

the containment

personnel

air lock was

declared

out of service,

and action statement

b of TS 3.6.1.3

was

entered.

This action statement

required at least

one air lock

door to be maintained

closed

and required the inoperable air lock

to be restored to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or bring the

unit to at least

Hot Standby within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and in Cold

Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The interlock linkages

were adjusted,

and Section 7. 1, Containment

Personnel

Air Lock

Test, of 'procedure

4-0SP-051.6

was re-commenced

at 6:15 a.m.

This

test

was completed at 6:45 a.m.,

and the containment

personnel air

lock was returned to service at 7: 10 a.m.

b.

At 2:32 p.m.

on January

15,

1993, the licensee

declared

an Unusual

Event due to the identification of RCS pressure

boundary

leakage

11

on Unit 3.

The leak was from a cracked

weld on

a pipe cap

on the

abandoned

spray valve bypass

pipe between

the previous

A spray

valve body and the pressurizer

spray nozzle.

The licensee

commenced

a unit shutdown at 2:35 p.m.

on January

15,

1993,

and

the unit reached

Hode

5 at 6: 15 p.m.

on the following day.

NCR N-93-005 was issued to document the condition

and

PC/H 933-012

was issued to repair the leak.

After cooldown,

a more detailed

visual inspection identified the leak location

on the pipe cap to

nipple socket weld.

After the piping assembly

was removed,

microscopic examination of the failed weld revealed

ID initiated

branch cracking,

which is indicative of SCC.

Additionally,

examination

showed

inadequate

pullback between the pipe

and cap

(the cap appeared

to have

been

bottomed out on the pipe).

The

lack of pullback can cause

high localized stresses

which increases

the chances

of SCC.

Repair of the failed weld was accomplished

per

PC/H 93-012

on January

17,

1993,

and preparations

were

made to

return the unit to service

(Refer to paragraph

2 for further

information on the plant startup).

At 4:32 p.m.

on January 16,'993,

PORV PCV-3-456 momentarily

lifted once

and immediately reseated

while the licensee

was in the

process

of collapsing the pressurizer

bubble for the establishment

of a solid water condition during

a Unit 3 shutdown.

Prior to

this event,

the 3A RCP had

been secured,

and the

3B and

3C

RCP

pumps were running.

OHS was in service,

and the

3B and

3C

charging

pumps were running with a 45 gpm orifice in service.

RCS

temperature

was approximately 260'F

and stable,

and

RCS average

pressure

was approximately

315 psig.

The

NPS had cautioned

the

RCO performing the evolution to monitor

RCS pressure

and to be

prepared for solid conditions at any time because

the wide range

level could be incorrect.

This was due to the actual

RCS

temperature

being greater

than the wide range pressurizer

level

calibration temperature

of 68'F.

In order to reduce the

charging/letdown

mismatch to allow greater control while

approaching

solid conditions,

the

RCO secured

one of the two

running charging

pumps.

This action reduced

the mismatch to

approximately

20 gpm.

At this point, wide range pressurizer

level

was approximately

87%.

It increased

to approximately

88.5% and

leveled off.

With the

NPS,

ANPS,

and

STA present,

the

RCO

performing the evolution explained that

as the water level rose

and covered the vapor temperature

tap, the vapor temperature

which

read approximately 430'F would begin to decrease

rapidly and

approach

the water temperature.

The

RCO explained that

he had

recently performed this evolution and

had noticed this occurrence

well before going solid.

No change in vapor temperature

was

noted.

At approximately 4:29 p.m., pressurizer

pressure

began to

increase rapidly with wide range pressurizer

level indicating

steady at approximately

88.5%.

When this pressure

increase

was

noted

by the

RCO in charge of the unit, the

RCO performing the

evolution reached for the charging

pump speed controller and

letdown flow control valve.

Although actions

were taken to slow

the pressure

increase

by increasing

letdown flow and decreasing

12

charging flow, pressure

increased

to the point {approximately 415

psig) where

PORV PCV-3-456 momentarily cycled open

once

as

designed

and immediately reseated.

The alert annunciator

and the

PORV lift occurred simultaneously

as the

RCO was securing

the

charging

pump.

The charging

pump was subsequently

restarted,

and

RCS pressure

was stabilized at approximately

310 psig.

This event

was attributed to the wide range pressurizer

level

indicating steady at 88.5% when the solid water condition was

achieved

and to the

RCO's failure to slow the

RCS pressure

increase

in time to prevent the

OHS actuation.

As a result of

this event,

the

RCO was counselled

by Operation's

Hanagement,

and

procedure

changes

were initiated,

The licensee

plans to

incorporate

a pressurizer

level correction curve into procedures

'by February

5,

1993.

1n addition,

by February

22,

1993,

the

licensee

plans to incorporate

procedure

changes

including the

addition of requirements

to maintain

RCS pressure

between

325 and

350 psig using the highest indicated pressure,

the

recommended

method of RCS pressure

control during solid water operations,

a

caution to stop the charging

pumps if a pressure

increase

cannot

be controlled by charging

and letdown,

a caution to stop the

RCPs

if the

RCS pressure

decreases

to the

RCP No.

1 seal differential

pressure

low limit, and the requirement that

an operator

who has

been briefed by the unit ANPS to ensure

understanding will be

dedicated

to the tasks of drawing

a pressurizer

bubble or going

solid.

Operators

have also

been

scheduled

to receive

classroom

{procedure)

and simulator training on solid water operations

by

April 15,

1993,

and

an

REA has

been

submitted requesting

a

setpoint

change for the

OHS alert annunciator.

This change

would

allow the setpoint to be varied with a maximum limit dependent

on

the desired

RCS pressure.

TS 6.8. l.a requires that written procedures

and administrative

policies

be established,

implemented,

and maintained in accordance

with the requirements

and recommendations

of Appendix

A of

Regulatory

Guide 1.33,

Revision 2, dated

February

1978.

Section

1.b of this Appendix recommends that written procedures

be

established

for administrative

procedures

which include

authorities

and responsibilities for safe operation

and shutdown,

and Section 2.j of this Appendix recommends

general

plant

operating

procedures

for plant operation

from Hot Standby to Cold

Shutdown.

Paragraph

5. 1.6 of procedure

O-ADH-200, Conduct of

Operations,

requires all on-shift Operations

personnel

to be aware

of and responsible for the plant status

at all times.

Paragraph

5.14.2.2 of procedure

3-GOP-305,

Hot Standby to Cold Shutdown,

requires that pressurizer

pressure

be maintained within the range

of 325 to 375 psig for the collapsing of the pressurizer

bubble

and establishment

of a solid water condition.

Contrary to these

requirements,

on January

16,

1993, while collapsing the

pressurizer

bubble for the establishment

of a solid water

condition on Unit 3, pressurizer

pressure

was not maintained

below

375 psig.

This resulted in the inadvertent

momentary opening of

/

13

PORV PCV-3-456.

This failure to follow a procedure constitutes

a

violation; however, this violation is not being cited because

the

criteria specified in Section VII.B of the

NRC Enforcement Policy

were satisfied.

This item will be tracked

as

NCV 50-250,251/93-01-01,

failure to maintain pressurizer

pressure

below 375 psig resulting in the inadvertent

opening of a

PORV.

This item is closed.

Although the root causes

of previous inadvertent

PORV opening

events

and the more recent January

16,

1993,

event discussed

above

were unrelated;

the increased

frequency of these

types of events

has

caused

a concern regarding the lack of attention to detail.

On January

16,

1993, at approximately

11:00 p.m., the licensee

notified the

NRC of a reportable

event per

10 CFR 50.72(b)(2)(i).

The event involved the inadvertent closing of the

CSP discharge

valves

3-891A and

B prior to

RCS temperature

going less

than

200'F.

On January

16,

1993, at 9:45 p.m., during the review of

SNPO log readings,

the Unit 3 ANPS recognized that containment

spray valves 3-891A and

B were logged

as locked closed at 8:00

a.m. that

same day.

Investigation

showed that valves

3-891A and

B

were closed at 5:00 a.m.,

at the

same time the operators

isolated

the

HHSI valves,

the accumulator discharge

isolation valves,

and

other required actions

when

T average

became

less

than 380'F.

Procedure

3-GOP-305,

Hot Standby to Cold Shutdown,

paragraph

5.8.3, states

that when T average is less than 380'F,

then

among

other actions,

align the

HHSI valves,

the accumulator

discharge

isolation valves,

and other alignments in accordance

with

attachment

1, Cold Shutdown Alignment Requirements.

Reference

Step 5.8.3 of Attachment

1 requires certain valve and breaker

alignments that do not include the

CSP isolation valves.

Paragraph

5. 15.3. requires that when the

RCS temperature

is less

than 200'F,

then isolate containment

spray in accordance

with

Attachment I.

Reference

Step 5. 15.3 of Attachment

1 requires

CSP

valves 3-891A and 3-891B to be closed.

Investigation of this event

shows there

was poor communications

between the control

room

RCO and the

SNPO in the auxiliary

building.

The

SNPO possessed

Attachment

1 to 3-GOP-305;

however,

the method of communication

was inadequate

to correctly perform

the task.

The

RCO copied Attachment

1 to 3-GOP-305

and

highlighted certain

items to be accomplished

including portions of

reference

steps

5.8.3

and 5.15.3.

The

SNPO, while accomplishing

the highlighted steps of Attachment

1 to 3-GOP-305,

asked

the

RCO

if he should accomplish the remaining highlighted steps.

The

RCO

replied to the affirmative without discussing

which specific

valves were to be operated.

A second

SNPO independently verified

the highlighted valves

and breakers

on the field copy of

Attachment

1 to 3-GOP-305.

The poor communications

between the

RCO and the

SNPO led the

RCO to believe

he was accomplishing the

required

steps in proper

sequence

and the

RCO was not aware the

14

CSP discharge

valves

had

been closed.

The Unit 3 ANPS directed

the

RCO to accomplish

the steps

in 3-GOP-305 in specific order

as

plant conditions dictated

and

was not aware that the

CSP discharge

valves

had

been closed.

The

RCO on peak shift that

had Unit 3 responsibility

when Unit 3

entered

Hode

5 (<200'F) at 6:15 p.m.

on January

16,

1993, put the

CSP controls in pull-to-lock, however,

the

RCO did not direct the

isolation of containment

spray in accordance

with 3-GOP-305 at

that time.

At 9:00 p.m. the

RCO,

when ready to accomplish

step

5. 15.3 of 3-GOP-305

(which isolates

the

CSP discharge

valves)

noted that Attachment

1 was signed off and independently verified.

The

RCO in charge of Unit 3 assumed

that

a second

RCO that was

assisting

in the control

room had ordered the

CSP discharge

valves

be closed

per attachment

1

and

he therefore initialled step

5. 15.3

of 3-GOP-305

as accomplished.

At 9:45 p.m.

on January

16,

1993, the

ANPS, while reviewing the

SNPO log readings,

noted that containment

spray valves 3-891A and

3-891B were logged

as closed at 8:00 a.m.

The

ANPS recognized

that valves 3-891A and 3-891B should not have

been closed until

Hode

5 (which occurred at 6:15 p.m.)

and initiated

an

investigation which revealed

the sequence

of events previously

noted.

TS 3.6.2. 1, Containment

Spray System,

requires

in Hodes

1, 2, 3,

and

4 that two CSSs

be operable.

Action statement

b states

that

with two CSSs inoperable,

restore

at least

one

CSS to operable

status within one hour or be in at least

Hot Standby

(T average>

350'F) within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and in Cold Shutdown

(T average<

200'F) within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The

CSSs were inoperable

with the

RCS temperature

greater

than 200'F from approximately

5:00 a.m. until 6: 15 p.m. or approximately thirteen

hour s,

therefore

TS 3.6.2.1

LCO was not exceeded.

The licensee

performed

an engineering

evaluation to assess

the

impact of isolating containment

spray

on the plant's

response

to

an accident with an average

RCS temperature

of approximately 350'F

or less.

At the time the

CSPs

were isolated,

Unit 3 had

been shut

down for approximately

10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> with an average

RCS temperature

of

350'F or less.

The engineering

evaluation

noted that the analysis of the plant

response

to a

LOCA with the plant in other than

Hode

1 is not

explicitly analyzed

in the

FSAR.

Per Turkey Point's original

licensing basis, it was

assumed

that

an accident in a Hode other

than

power operation

would be bounded

by the full power event.

Westinghouse

has studied

shutdown accidents

(Hodes

3 and below)

and

has

shown that the largest credible break would be

a 6-inch

pipe break attached to the

RCS cold leg.

15

The

LOCA containment integrity FSAR analysis is performed at

100%

hot full power operation

assuming

a double

ended pipe break.

The

analysis

is performed specifically for Hode

1 operation,

because

it bounds the other

modes

and it represents

the limiting scenario

for containment integrity, in part,

because

the stored

energy in

the systems

are at their highest.

For this event,

the containment

peak pressure

and temperature

peak is turned

by the action of the

containment

heat sinks prior to the

CSS starting

and loading.

Therefore,

the

CSS function is to reduce

containment

pressure

and

temperature

and to remove decay heat.

Both the primary and

secondary

sides of the

RCS were at lower pressures

and

temperatures

than the

100% hot full power analyzed

values

when the

CSS

was isolated,

while the system stored energies

were

significantly reduced.

The effect of having the

CSSs unavailable

with the primary system at or about 350'F would be bounded

by the

assumptions

and conditions of the accident analysis,

and would not

represent

a challenge to the integrity of containment,

or

equipment qualification.

The

CSS is part of the plant's

ESF

system described

in Section 6.4 of the Final Safety Analysis

Report.

The primary purpose of the Containment

Spray

system is to

spray cool water into the containment

atmosphere

when appropriate

in the event of a

LOCA and therefore

assure that containment

pressure

and temperature limits are not exceeded.

For purposes

of

maintaining containment integrity, the three

ECCs are considered

fully redundant to the

CSS.

For purposes

of environmental

qualification, at least

one

CS pump

and two ECCs are

assumed

available to reduce the containment

temperature within the time

limits of the

Eg curve following a design basis

LOCA.

The

CSS also functions to reduce temperature

and pressure

following a Hain Steam Line Break accident.

However, for purposes

of containment design,

a

LOCA is considered limiting.

Considering

a single failure, two

ECCs

by themselves

would be sufficient to

remove decay heat at the reduced levels that correspond

to

a plant

shutdown for ten hours.

Therefore,

the

ECCs would be capable of

reducing containment

temperature

and pressure

following the

initial blowdown.

TS 6.8. 1 requires that written procedures

be established,

implemented,

and maintained covering the activities referenced

in

Appendix A of Regulatory

Guide 1.33, revision 2, February

1978.

Regulatory

Guide 1.33,

Appendix A, Section

1,

recommends

administrative

procedures

for authorities

and responsibilities for

safe operation

and shutdown.

Section 2.j also

recommends

operating

procedures

for going from hot shutdown to cold shutdown.

Administrative procedure

O-ADH-200, Conduct of Operations,

paragraph

5.6.20,

states

that communications to operating

personnel

must

be clear

and concise.

These directions shall

be

given in such

a manner that they are explicit and understandable.

This should

be verified for complex orders

and those orders that

include numbers

by having the operator

repeat

them back or by

providing written direction

so that the director is satisfied that

16

the orders

are understood.

Upon completion of the directed

evolution, the operator shall report back to the controlling

station the exact action that he/she

has taken.

General

Operating

Procedure

3-GOP-305,

Hot Standby to Cold Shutdown,

provides the

prerequisites,

precautions/limitations,

and instructional

guidance

for changing plant conditions from hot standby to cold shutdown.

Step 5. 15 states

that when the reactor coolant temperature

is less

than 200'F,

then perform the following steps.

Step

5. 15.3 then

states

to isolate containment

spray in accordance

with Attachment

1, Cold Shutdown Alignment Requirements.

However, at

approximately

5:00 a.m.

on January

16,

1993, with the reactor

coolant temperature

at approximately 350'F,

the reactor control

operator directed the senior nuclear plant operator to accomplish

the highlighted portions of Attachment

1 to 3-GOP-305.

No

explicit directions

were provided

and

no report back of the exact

action taken

was accomplished resulting in the inadvertent

isolation of the containment

spray

system prior to reactor coolant

temperature

being less

than 200'F.

This failure to follow

procedures

is

a violation and will be tracked

as

VIO 50-250,

251/93-01-02,

Failure to follow procedures

in the area of conduct

of operation resulting in the isolation of containment

spray prior

to

RCS temperature

going below 200'F.

Also, there were several

missed opportunities to have identified this discrepancy earlier.

As noted in paragraph

8.c above,

the increased

frequency of

operator errors

has

caused

a concern regarding the lack of

attention to detail.

On January

15,

1993, the licensee notified the resident

inspector

of the preliminary results of their investigation into the cause

for an unexpected

increase

in the local peaking factor and

a more

positive power distribution following the Unit 3 startup

on

December

3,

1992.

A flux map performed

on December

29,

1992, at

100% power, equilibrium xenon,

and steady state conditions

prompted reactor engineering to investigate

the cause of the

unexpected results.

Westinghouse

reviewed their manufacturing

records

and

on January

14,

1993,

confirmed that the

WABA rods were

manufactured

incorrectly resulting in the absorber centerline

being positioned

1.368 inches lower than the fuel center line.

This condition existed for both Unit 4, cycle

13 and Unit 3, cycle

13.

Unit 3 cycle

13 started

on December

3,

1992,

and Unit 4 cycle

13 started

on October 29,

1991.

Unit 4 is scheduled for a

refueling outage

(cycle 14) in April, 1993.

The

FPL fuel design

specifications

were not properly implemented

by Westinghouse

for

manufacturing the

WABAs for the

new debris resistent

fuel

assemblies.

Engineering evaluation

JPN-PTN-SEFJ-93-002,

Assessment

of Operability and Past

Performance

With Offset Wet

Annular Burnable Absorbers at Turkey Point Unit 3, Cycle 13,

and

Unit 4, Cycle 13, concluded that both Units 3 and

4 had operated

within the design basis

and that continued operation within TS

parameters

would ensure

operation within the design basis.

No TSs

were violated.

FPL is reviewing contractor

oversight activities

to determine if the manufacturing error could or should

have

been

17

identified earlier.

It appears

that the

WABA configuration for

Unit 4, Cycle

13 was sufficiently different such that

any effects

on local peaking factors

and for axial

power distrjbution would

have

been less

obvious

and more difficult to recognize.

The

recognition of the unexpected

peaking

and

a more positive power

distribution anomalies

on Unit 3 and the pursuit of a root cause

is considered

a strength.

Starting with Turkey Point Unit 3, Cycle 12, the fuel assembly

design

was modified to reduce

the probability of fuel failures.

The

DRFA design contained

a longer solid bottom endcap to reduce

debris fretting and in turn raised the fuel stack

1.368 inches.

The

DRFA fuel design

has

been incorporated

in Turkey Point Unit 3

Cycles

12 and

13 and in Turkey Point Unit 4 Cycle 13.

The

WABA rods are

used in the core for reactivity control

and to

aid in reducing

power peaking.

The Turkey Point Unit 3 Cycle

13

core contains

512

WABA rods,

each

108 inches in length

and the

Turkey Point Unit 4 Cycle

13 core contains

a total of 368

WABA

rods,

most at

126 and

some at

108 inches in length.

These cycles

were designed with the

WABA rods centered

on the fuel mid-plane.

The

WABAs provide the highest

power shaping control early in the

cycle and their reactivity control capability is reduced with

increasing

cycle operation.

Contrary to the core design

requirement that the

WABA rods

be centered

on the fuel mid-plane,

the

WABAs were manufactured

such that the absorber

length

was not

centered

on the active fuel mid-plane.

In December

1992 while performing the first 100% power

steady

state flux map at Turkey Point Unit 3 Cycle 13,

a discrepancy

between the predicted

and measured total peaking factor (Fq)

was

observed.

Subsequent

investigation of the deviation led to the

conclusion that the

WABA rods were incorrectly positioned relative

to the active fuel stack

by 1.368 inches.

10 CFR Part 50, Appendix B, guality Assurance Criteria for Nuclear

Power Plants

and

Fuel

Reprocessing

Plants, Criterion VII, Control

of Purchased

Haterial,

Equipment,

and Services,

states that

measures

shall

be established

to assure

that purchased

material,

equipment,

and services,

whether purchased directly or through

contractors

and subcontractors,

conform to the procurement

documents.

The failure to implement measures

that assure

the

WABA

assemblies

conformed to the procurement

document is

a violation.

However, this violation will not be subject to enforcement

action

because

the licensee's

efforts in identifying and correcting the

violation meet the criteria specified in Section VII.B of the

NRC

Enforcement Policy.

This item will be tracked

as

NCV 50-250,251/93-01-03,

failure to implement measures

to assure

that the

WABA assemblies

conformed to procurement

documents.

This

item is considered

closed.

18

At 11:00 p.m.

on January

25,

1993, the control

room began to shift

loads

on the

4A 4KV bus

due to the identification of a ground

on

the bus.

The ground

was isolated to the

4A condensate

pump at

11: 11 p.m.,

and the

4A condensate

breaker

was racked out at 11:20

p.m.

due to the ground.

As

a precautionary

measure

due to

inclement weather

and the possibility of losing

a second

condensate

pump,

a power reduction

was

commenced

at 7:50 a.m.

on

January

26,

1993.

Unit 4 reactor

power was stabilized at

70% at

9:40 a.m.

Power ascension

was

commenced

at 12:00 p.m.,

and

100%

reactor

power was attained at 5:30 p.m.

on the

same day.

Meeting on Results of Twentieth Year Tendon Surveillance for Units

3 and

4.

(94702)

A regional

inspector attended

a meeting held

on January

11,

1993,

in the

NRC Headquarters

office at

One White Flint North, Rockville, Maryland.

Attendees

at the meeting

are listed in paragraph

1 above.

The purpose

of the meeting

was to discuss

the results of the twentieth year tendon

surveillance results, specifically, the low lift-offvalues

measured

in

four Unit 3 and seven Unit 4 tendons,

and the licensee's

long-term

corrective actions.

The tendons with the low lift-offforces were

. retensioned

in accordance

with TS requirements.

The licensee

also

submitted special

reports

summarizing the low lift-offvalues

and

short-term corrective actions (retensioning)

as required

by the TSs.

The licensee attributed the root cause of this problem to be

underestimation

of the time-dependent

steel

relaxation values during

original design.

The original design

was

based

on steel

relaxation

values obtained

from test data which used

an ambient value of 68'F,

which was the current practice at that time.

Review of plant specific

temperature

data

shows that the average

temperature

is 90'F at the

tendon location.

Testing performed

on tendon wires for other sites

experiencing similar problems

showed that this small temperature

difference

has significant effect

on steel

relaxation values.

The

licensee

stated that re-analyzing

the predicted lift-offvalues

using

the stress

relaxation data corresponding

to

a 90'F temperature

correlates

well with the measured lift-offvalues.

The licensee

planned

long-term corrective actions

include reanalyzing the containment

using

appropriate effective prestress

forces

based

on the licensing basic

internal containment

pressure

of 55 psig.

The 55 psig containment

pressure

has

a

10% margin over the calculated

accident pressure

of 49

psig.

The licensee will submit

a report to

NRC on January

29,

1993, to

document their proposed

long term corrective actions.

Additional

reports will be submitted

as required to documet that the re-analysis

is

in compliance with FSAR commitments.

The containment post-tensioning

system meets

TS requirements,

and will be maintained

beyond the next

scheduled

surveillance.

Exit Interview

The inspection

scope

and findings were summarized during management

interviews held throughout the reporting period with the Plant General

19

Hanager

and selected

members of his staff.

An exit meeting

was

conducted

on January

29,

1993.

The areas requiring management

attention

were reviewed.

The licensee

did not identify as proprietary

any of the

materials

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

The inspectors

had the following findings:

Item Number

Descri tion and Reference

50-250,251/93-01-01

NCV - Failure to maintain pressurizer

pressure

below 375 psig resulting in the inadvertent

opening of a

PORV (paragraph S.c).

50-250,251/93-01-02

VIO - Failure to follow procedures

in the area

of conduct of operations resulting in the

isolation of containment

spray prior to

RCS

temperature

going below 200'F

(paragraph

S.d).

50-250,251/93-01-03

NCV - Failure to implement measures

to assure

that the

WABA assemblies

conformed to

procurement

documents

(paragraph

S.e).

Acronyms

and Abbreviations

ADM

AFW

ANPS

CCW

CFR

CS

CSP

CSS

DRFA

ECC

ESF

EQ

F

FCV

FPL

Fq

FSAR

GL

GOP

gpm

HHSI

IAS

-ICW

ID

IR

JPN

KV

LCO

Administrative

Auxiliary Feedwater

Assistant

Nuclear Plant Supervisor

Component Cooling Water

Code of Federal

Regulations

Containment

Spray

Containment

Spray

Pump

Containment

Spray System

Debris Resistent

Fuel Assembly

Emergency

Containment

Cooler

Engineered

Safety Feature

Environmental Qualification

Fahrenheit

Flow Control Valve

Florida Power

and Light

Peaking

Factor

Final Safety Analysis Report

Generic Letter

General

Operating

Procedure

Gallons

Per Ninute

High Head Safety Injection

Instrument Air System

Intake Cooling Water

Inside Diameter

Inspection

Report

Juno Project Nuclear

Kilovolt

Limiting Condition for Operation

20

LER

LOCA

HSR

MWe

NCR

NCV

NPS

NRC

NRR

OHS

ONOP

OP

OSP

P &ID

PC/M

PCV

PORV

pslg

PTN

QA

QAO

.QC

RCO

RCP

RCS

REA

RHR

SCC

SNPO

STA

T

TB

TP

TS

VIO

WABA

Licensee

Event Report

Loss-of-Coolant Accident

Moisture Separator

Reheater

Megawatts Electric

Non-conformance

Report

. Non-Cited Violation

Nuclear Plant Supervisor

Nuclear Regulatory

Commission

Office of Nuclear Reactor Regulation

Overpressure

Mitigation System

Off Normal Operating

Procedure

Operating

Procedure

Operations

Surveillance

Procedure

Piping and Instrumentation

Drawing

Plant Change/Modification

Pressure

Control Valve

Power Operated Relief Valve

pounds

per square

inch gauge

Plant Turkey Nuclear

Quality Assurance

Quality Assurance

Organization

Quality Control

Reactor Control Operator

Reactor Coolant

Pump

Reactor Coolant System

Request

For Engineering Assistance

Residual

Heat

Removal

Stress

Corrosion Cracking

Senior Nuclear Plant Operator

Shift Technical Advisor

Temperature

Terminal

Box

Turkey Point

Technical Specification

Violation'et

Annular Burnable Absorber