ML17349A226
| ML17349A226 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 05/01/1992 |
| From: | Butcher R, Landis K, Resident L, Schnebli G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17349A224 | List: |
| References | |
| 50-250-92-07, 50-250-92-7, 50-251-92-07, 50-251-92-7, NUDOCS 9205220029 | |
| Download: ML17349A226 (47) | |
See also: IR 05000250/1992007
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Licensee:
Florida Power and Light Company
9250 West Flagler Street
Miami, FL
33102
Docket Nos.:
50-250
and 50-251
Facility Name:
Turkey Point Units 3 and
4
L,icense Nos.:
and
Report Nos.:
50-250/92-07
and 50-251/92-07
Inspection
Conducted:
Febru
y 29 through April 3,
1992
I
Inspectors:
.
C. Bute er,
en'
Ress
ent Inspector
te Signe
. A. Schneb i, Resi ant Inspector
~c
, Trocine,
Re i ent Inspector
Accompanying Personnel:
N.
W. Branch, Senior Resident
Approved by:
K.
.
Lan >s,
C ief
Reactor Projects
Section
2B
Division of Reactor Projects
1
Da
e Si
ned
Dat
STgne
Inspector (Surry)
S
Date Signed
/
SUMMARY
Scope:
This routine resident
inspector
inspection entailed direct inspection at the
site in the areas
of monthly surveillance
observations,
monthly maintenance
observations,
operational
safety,
and plant events.
Results:
Within the
scope
of this
inspection,
the
inspectors
determined
that
the
licensee
continued to demonstrate
satisfactory
performance to ensur e safe plant
operations.
One violation and four non-cited violations were identified.
50-250,251/92-07-01,
Non-Cited Violation.
Failure to follow procedures
for
work on shared
systems
(paragraph
3).
50-250,251/92-07-02,
Non-Cited Violation.
Missed
post-maintenance
test
on
a
component cooling'ater
drain valve
and missed
surveillance
on the automatic
9205220029
920501
ADOCK 05000250
8
fuel
makeup valve to the
4B emergency
diesel
generator.day
tank
(paragraphs
5
~
~
and 7.b).
50-250,251/92-07-03,
Violation.
Inadequate
review of a test release
work scope
resulting in the inadvertent release
of primary coolant through the
4B charging
pump vent valve
and resulting in the contamination of two licensed
operators
(paragraph
7.a).
50-250,251/92-07-04,
Non-Cited Violation.
Establishment
of
an
inadequate
procedure
(3-PMI-072.5) resulting in the entry of Technical Specification 3.0.3
for 2 minutes
(paragraph
7.h).
50-250,251/92-07-05,
Non-Cited Violation.
Multiple discrepancies
regarding
the
control of TSAs
and controlled diagrams
(paragraph
6).
REPORT
DETAILS
1.
Persons
Contacted
l
Licensee
Employees
- T. V. Abbatiello, Site guality Manager
R. J. Earl, guality Assurance
Supervisor
R. J. Gianfrencesco,
Support Services
Supervisor
K. N. Harris, Senior Yice President - Nuclear Operations
E.
F. Hayes,
Instrumentation
and Controls Maintenance
Supervisor
R.
G. Heisterman,
Mechanical
Maintenance
Supervisor
D.
E. Jernigan,
Technical
Manager
H.
H. Johnson,
Operations
Supervisor
- V. A. Kaminskas,
Operations
Manager
J.'.
Knorr, Regulatory
Compliance Analyst
R. S. Kundalkar, Engineering
Manager
J.
D. Lindsay, Health Physics Supervisor
- G. L. Marsh, Reactor
Engineering Supervisor
L.
W. Pearce,
Plant General
Manager
M. 0. Pearce,
Electrical Maintenance
Supervisor
- T.
F. Plunkett, Site Yice President
D. R. Powell, Services
Manager
R.
N. Steinke,'hemistry
Supervisor
F.
R. Timmons, Security Supervisor
- M. B. Wayland,
Maintenance
Manager
- J.
D. Webb,
Outage
Manager (Acting)
E. J.
Weinkam, Licensing Manager
Other
licensee
employees
contacted
included
construction
craftsman,
engineers,
technicians,
operators,
mechanics,
and electricians.
NRC Resident
Inspectors
R.
C. Butcher, Senior Resident
Inspector
G. A. Schnebli,
Resident
Inspector.
L. Trocine, Resident
Inspector
Additional
NRC Inspectors
M.
W. Branch, Senior Resident
Inspector (Surry)
- Attended exit interview on April 3,
1992.
Note:
An alphabetical'abulation
of acronyms
used in this report is
listed in the last paragraph
in this report.
2.
Plant Status
Unit 3
At the
beginning
of this reporting
period,
Unit 3
was
operating
at
50 percent
power in order to permit the repair of an oil leak
on the
38 steam
generator
pump.
Unit 3
had
been
on line since
February 5,
1992.
The following evolutions
occurred
on this unit during
this assessment
period:
On February
29,
1992, at 9:20 a.m.,
power ascension
from 50 percent
'was
commenced.
On February 29,
1992, at 1:00 p.m., reactor
power reached.
87 percent,
and
reduced
power operations
at this power level
was
recommenced
in
order
to
extend
the unit run
time until the
beginning of the
August 24,
1992, refueling outage.
Unit 4
At the
beginning
of this reporting
period,
Unit 4
was
operating
at
100 percent
power
and
had
been
on line since
February 3,
1992.
The
following evolutions occurred
on this unit during this assessment
period:
On March 16,
1992, at 7:10 p.m.,
a load reduction to 50 percent
was
commenced
to facilitate the cleaning of the
4B north
and
4B south
waterboxes
and the
4A TPCW heat
exchanger.
(Refer to paragraph
7.g
for additional information.)
On March 16,
1992, at 9:00 p.m., Unit 4 reached
50 percent
power.
On March 17,
1992, at 6: 10 a.m.,
power ascension
was
commenced.
On
March 17,
1992,
at ll:25 a.m.,
Unit 4 reactor
power
reached
100 percent.
On March 25,
1992, at 3:25 p.m.,
a load reduction
was
commenced
due
to the identification of moisture
in the turbine generator
housing
causing
a
generator
field
brush
ground.
(Refer
to
paragraph 7.i for additional information.)
On March 25,
1992, at 5:50 p.m.,
the turbine generator
was taken off
line,
and the unit entered
Node 2.
On
March 26,
1992,
at
1:35 a.m.,
the
prerequisites
for entering
Mode
1 were completed,
and startup
was
commenced.
On
March 26,
1992,
at 5:55 a.m.,
the turbine generator
was
placed
back
on line.
On
March 26,
1992,
at
6:45 a.m.,
reactor
power
was
stable
at
30 percent
(chemistry hold).
C
On
March 26,
1992,
at
10: 15 a.m.,
Unit 4 received
a Train
8
safeguards
actuation
signal
and reactor trip during the performance
of
a routine surveillance
on the containment
racks.
(Refer to
paragraph 7.j for additional information.)
On March 27, 1992, at 7:40 p.m., reactor startup
was
commenced.
On
March 28,
1992, at
1:Ol a.m.,
the turbine generator
was
placed
back
on. line.
On
March 28,
1992,
at
12:40 p.m.,
reactor
power
was
stable
at
100 percent.
3.
Followup on Inspector
Followup Items
(92701)
Actions taken
by the licensee
on the item listed below was verified by the
inspectors,
(Closed)
URI 50-250,251/91-11-04
- Modification Made to Fire Water Supply
System
Without Prior
Safety Evaluation
and Without Proper
Work Process
Controls.
This
URI was .initiated following the discovery that Turkey Point fossil
construction
personnel
were accomplishing modifications to the shared fire
protection
system without adequate
coordination or controls.
The fire
protection
system is just
one of many shared
systems
between
the fossil
and nuclear units at Turkey Point.
Corrective actions consisted partly of
the following actions:
The
licensee
issued
Turkey
Point fossil
plant
administrative
procedure
FOP-ADMIN-013, Authorization of
Work Requests
on
Plant
Operating
Systems
Common to Turkey Point Fossil
and Nuclear Plants.
This
procedure
defines
the
process
for authorizing
work to
be
performed
on shared
systems,
A caution
note for design
changes
for the Turkey Point,fossil units
was
added
to- Power
Plant
Engineering
Department
(non-nuclear)
administrative
procedure
Engineering
Process
to Complete
a
Request for Engineering Assistance.
The
licensee
issued
nuclear
engineering
quality
instruction
JPN-gI
3. 1-9,
Shared
Fossil/Nuclear
Systems
(PTN only).
This
procedure
provides the requirements
for JPN review of proposed
Turkey
Point fossil
engineering
packages
on
systems
shared
between
the
nuclear
and fossil units.
A new administrative
procedure
O-ADM-216, Control of Work on Shared
Systems,
was
issued.
This
procedure
requires
the
NPS to notify
nuclear
engineering
of fossil
work requests
to
ensure
nuclear
engineering's
review of the work is complete
and that results
are
satisfactory.
PTN assumed all responsibilities
for maintenance
and operation of the
raw water system.
Nuclear engineering
up-.dated
affected
drawings with an information
statement
requiring'PS
authorization
prior to starting
work on
shared,
systems,
cross-tie
valves,
isolation valves,
and
the fire
protection
system.
Land utilization interfaces
were identified.
In the
above
noted
documents,
the licensee
identified shared
systems
and
cross-tie
connections
between
Turkey Point nuclear
and fossil units.
In addition,
as part of the industry concern
regarding
events
and prior to the
1991
dual
unit outage,
the
licensee
had
issued
a
temporary
procedure controlling work activities
such that the
had to
be informed prior to performing work in the switchyard.
This concept
has
been
made
permanent
by
issuance
of
a
procedure
change
to
procedure
0-ADM-216 which requi res
NPS approval
(written or verbal
based
on the type
of
activity)
prior
to
approving
work
in
the
Procedure
0-ADM-216 is
now titled, Control of Work on Systems
Shared
by
Turkey Point Fossil
and
Turkey Point
Nuclear
Plants,
and
Access.
Other fossil
and nuclear interface
problems that have
been identified
are
as follows:
IR 50-250,251/91-46,
paragraph
10.c, identified that during one short
time period,
three of the eight offsite power lines
were lost and
noted
that there
were
no requirements
for maintaining
a
minimum
number of- offsite power lines.
In addition, at any given time, the
nuclear operators
are not aware of how many offsite power sources
are
available
since
the switchyard status
display is in the Unit
1 and
2
(fossil) control
room.
The number of offsite power sources
to the
Turkey Point switchyard is not currently controlled
by TSs or other
regulatory requirements;
however,
the
number of offsite power sources
at Turkey Point exceeds
that found at other facilities
and appears
to
be adequate.
VIO 50-250,251/91-39-01
identified Turkey Point Unit 3 and
4 transfer
'inhibit relays
that
were
not included
in any
PM program.
These
rel ays
were
under
the
control
of
the
Protecti on
Divisi on
(non-Nuclear) of FPL,
and the
PM/C that nuclear engineering
issued
to
utilize
a
spare
set of contacts
of an existing relay failed to
identify
the
need
to test
the
dropout
time.
A
procedure
(0-PMR-005. 10,
HGA 162/TDDO Relay Calibration)
was
issued
to check
the relay every refueling outage.
TS 6.8. 1 requires that written procedures
be established,
implemented,
and
maintained
covering
the facility fire protection
program.
equality
Instruction gI 3-PTN-1,
Design Control, dated
February
26,
1991, controls
all
plant
changes
and
modifications.
Paragraph
5. 1
of
equality
Instruction gI 3-PTN-1 requires that permanent
plant changes
be controlled
by design
packages
"originated by Nuclear Engineering
(JPN).
As noted in
URI 50-250,251/91-11-04,
the modification to the fire protection
system
piping was being accomplished
by
a fossil plant engineering
package that
was
not originated
by nuclear engineering
and
pen
and ink changes
were
made
to the working copy of the engineering
package
without required
review and approval.
The failure to follow procedure
gI 3-PTN-1 is
a violation.
This violation
'will not be subject to enforcement
action
because
the licensee's
efforts
'n identifying and correcting the violation meet the criteria specified in
Section
V.G. 1 of the
This item will be tracked as-
NCV 50-250,251/92-07-01,
failure to follow procedures
for work on shared
systems.
This item is considered
to be closed.
Monthly Surveillance
Observations
(61726)
The inspectors
observed
TS required surveillance testing
and verified that
the test
procedures
conformed to the requirements
of the
TSs
testing
was
performed in accordance
with adequate
procedures;
test instrumentation
was
calibrated;
limiting conditions for operation
were met; test results
met
acceptance
criteria requirements
and were reviewed
by personnel
other than
the
individual directing
the test;
deficiencies
were identified,
as
appropriate,
and
were
properly
reviewed
and
resolved
by
management
personnel;
and
system restoration
was adequate.
For completed tests,
the
inspectors verified testing frequencies
were met and tests
were performed
by quali'fied individuals.
The
inspectors
witnessed/reviewed
portions
of the
following test
activities:
Section 7.3,
Returning
'Reactor
Trip .Breaker
A to
Service,
of
procedure
4-0P-049,
Reactor Trip Breaker Operation for Maintenance
(Refer to paragraph
7.d for additional information.)
and
Procedure
4-OSP-049. 1,
Reactor
Protection
System
Logic Test,
for
Train A (Refer to paragraph
.7.e for additional information.).
The inspectors
determined that the above testing activities were performed
in a satisfactory
manner
and
met the requirements
of the TSs.
Violations,
or deviations
were not identified.
(Refer to paragraphs
5
and 7.b for
information'egarding
a missed
post maintenance
test of a
CCW drain valve
and
a missed 'surveillance
on the automatic fuel
makeup valve to the
4B
day tank.)
.
Monthly Maintenance
Observations
(62703)
Station
maintenance
activities of safety-related
systems
and
components
were observed
and reviewed to ascertain
they were conducted
in accordance
with approved
procedures,
regulatory guides,
industry codes
and standards,
and in conformance with the TSs.
0
The following items
were considered
during this review,
as appropriate:
LCOs were
met while components
or systems
were
removed
from service;
approvals
were
obtained
prior to initiating work; activities
were
accomplished
using
approved
procedures
and were inspected
as applicable;
procedures
used
were
adequate
to control
the activity; troubleshooting
activities
were controlled
and repair records
accurately
reflected
the
maintenance
performed;
functional
testing
and/or
calibrations
were'erformed
prior to returning
components
or systems
to service;
gC records
were maintained;
activities
were
accomplished
by qualified personnel;
parts
and materials
used
were properly certified; radiological controls
were properly implemented;
gC hold points
were established
and observed
where
required;
fire prevention
controls
were
implemented;
outside
contractor
force activities
were controlled
in accordance
with the
approved
gA program;
and housekeeping
was actively pursued.
The inspectors
witnessed/reviewed
portions of the following maintenance
activities in progress:
swap out of the
4A reactor trip breaker
per
PWOs 5280/64
and 5284/84
and
procedure
0-PME-049. 1,
Reactor
Trip
and Trip Bypass
Breaker
Inspection
and
Maintenance
(Refer to paragraph
7.d for additional
information.);
replacement
of
a faulty reactor
protection
relay
(RT-6-A)
per
PWO 7138/64 (Refer to paragraph
7.e for additional information.);
and
re-termination of the
3B
ICW pump motor following replacement
due to
seal leak-off problems.
On
February
24,
1992,
during
a
gC
review of post
maintenance
work
activities,
the
licensee
discovered
that
post
maintenance
testing
performed
on valve 4-50-364
(a drain valve to the inlet waterbox of the
4B
CCW heat
exchanger)
was
not adequate
because
the work plan for the
replacement
of this quality-related
valve did not identify the guality
Group which designates
the work as
an
ASME Section
XI repair/replacement.
The
CCW heat
exchanger
associated
with this valve
(4B)
had
been
out of
service during the valve replacement
and
had
remained
so until the valve
was
tested
in
accordance
with
Section
XI
repair/replacement
requirements.
During
a subsequent
review (February
27,
1992) of similar valve repairs,
gC identified that post
maintenance
testing of valve 4-50-377
(a
4A
heat
exchanger
channel
head drain valve)
was also not in accordance
with
ASME Section
XI repair/replacement
requirements.
As with the incident
described
above,
the
work plan for the
repair/replacement
of this
quality-related
valve also
did not identify the guali ty Group which .
7
designates
the
work
as
an
ASME Section
XI repair/replacement.
In
addition, the work scope of this leak repair
was
changed
in the field from
valve repacking
to valve replacement,
and
the post
maintenance
testing
requirements
were
not revisited.
As
a result,
on October
18,
1991,
valve 4-50-377
was replaced,
but the post maintenance
testing prior to the
return of the
4A
CCW heat
exchanger
to service
was performed in accordance
with the maintenance
work package for the original work scope
(packi ng
replacement).
Therefore,
testing
in
accordance
with
Surveillance
Requirements
for Inservice Testing of ASME Code Class
1, 2,
and
3 Components,
was- not completed prior to the return of the
4A
CCW heat
exchanger
to service.
Successful
testing
of valve 4-50-377 at nominal
operating
pressure
and
temperature
in accordance
with procedure
0190.90,
ASME Section
XI Pressure
Tests for guality Group A, B,
and
C System/Components,
was
completed
on
February
27,
1992.
The event safety analysis
states
that* if there
had
been
a total failure of this valve in the
open
posi tion (The valve is
located
on
a 1-1/2 inch line.), the
4A CCW heat
exchanger
ICW flow would
have
remained
adequate
and
the
heat
exchanger
would still have
been
The licensee's
analysis
of the
missed
post
maintenance
testing. for
valves 4-50-364
and 4-50-377
concluded that the
PWOs which were generated
to replace
valve 4-50-364
and to repack
valve 4-50-377
were
planned
in
accordance
with procedure
O-ADM-701, Plant
Work Order Preparation.
The
PWO safety classification
and guality Group fields
on the
Nuclear
Job
Planning
System Total
Equipment
Data
Base identified these
valves with a
quality-related
classification
but did
not identify
a guality Group.
Procedure
0-ADN-701 does
not require guality Groups to be identified for
work that does
not meet the definition of repair or replacement
as stated
in
procedure
AP 0190.89,
ASME'ection XI
Repair/Replacement.
The
,requirements
of procedure
AP 0190.89
apply to
components
identified
as
guality Group A, B, or
C (Class
1, 2, or 3), but this was misinterpreted
by maintenance
personnel
to apply to safety-related
'components
only.
Because
these
valves
were classified
as quality related,
they
were
incorrectly
assu'med
not to meet the requirements
for guality Groups
A, B,
or C;
and therefore,
the
ISI requirements
of procedure
AP 0190.90,
Section
XI
Pressure
Tests
for
equality
Groups A,
B,
and
C
System/Components,
were not included
in the
work plan.
These,
valves
should
have
been identified
as guality
Group
C valves.
In addition,
because
the valves
in question
were not properly classified,. the
PWOs for
maintenance
on
these
valves
were
not
routed
to the
Group for
designation
of .ISI testing
requirements,
and the
PWOs did not include the
post
maintenance
testing
requirements
of
procedure
AP 0190.28,
Post
Maintenance
Testing.
Another contributing
cause
was
the failure to
revisit the post
maintenance
testing
requi rements
following a change
in
work scope.
Maintenance
personnel
have
been
trained
to verify the guality Group
designation
for
equipment
by
review
of
various
related
design
'ocumentation.
These
personnel
have also
been trained
on the
importance
of reviewing the
complete
package for -scope
changes
which could require
post maintenance
testing
changes.
In addition, quality control
personnel
have
reviewed all ready
to work
PWOs to ensure
that the guality Groups
specified
are correct.
Previous
work plans for similar quality-related
equipment
were
also
reviewed
to ensure
correct specification
of the
guality Groups,
and the records
providing the guality Group of the valves
in question
and of similar valves
have
been revised to reflect the correct
status.
The licensee
also
plans to revise
the initial and continuing
training
program for this
work group
to reflect
the
information in
LER 50-251/92-003,
Component
Cooling Water Channel
Head Drain Valves Not
Post-Installation
Tested in Accordance with Technical Specification 4.0.5.
The
inspectors
will followup
on
any
additional
corrective
actions
regarding this issue.
TS 4.0.5 requires
Class
1, 2,
and
3 components
and
IST of
Code
Class
1,
2,
and
3
pumps
and valves
be
performed in
accordance
with Section
XI of the
ASME Boiler and Pressure
Vessel
Code
and
applicable
Addenda
as required
by
except where specific
written
relief
has
been
granted
by
the
NRC
pursuant
to
Section
Preservice
Inspection,
of
ASME Section XI, Rules for Inservice
Inspection of Nuclear
Power Plant
Components
- Division 1, Article IWA-7000,
Replacements,
requires
that
prior to return to service,
a preservice
inspection
shall
be
made in
accordance
with Sections
IWD-2100,
IWE-2200,
or
IWF-2200 for the
component
or part replaced,
as applicable,
including the
joints that
connect
the
replaced
component
or part to the
system.
Table IWA-5210-1,
Reference
Paragraphs
for System
Pressure
Tests
and
Visual
Examinations
(VT-2)
Requirements,
of
Section XI,
Article IWA-5000,
System
Pressure
Tests,
requires
that tests for repairs
and
replacements
of
Code
Class
3 (guality Group C)
components
be
performed in accordance
with Section
IWA-5214, Repairs
and
Replacements.
Paragraph
(e) of Section
IWA-5214, Repairs
and Replacements,
states
that
if only disassembly
or reassembly
of mechanical joints are involved, then
a system
pressure
test in accordance
with paragraphs
(a), (b), or (c) of
Section
IWA-5211, Test Descriptions,
shall
be acceptable
in lieu of a
. system
test
in
accordance
with
paragraph
(b)
of
Section
Paragraphs
(a), (b),
and (c) of Section
IWA-5211, Test
Descriptions,
respectively
refer to
a
system
leakage
test
conducted
following opening
and
reclosing
of
a
component
in the
system
after
pressurization
to normal
operating
pressure,
a
system
functional test
conducted
to verify operability in systems
(or components)
not required to
operate
during
normal
plant operation
while
under
system
operating
pressure,
and
a
system
inservice
test
conducted
to
perform
examination
VT-2 while the
system is in service
under operating
pressure.
Contrary
to
these
requirements,
following
replacement
of
a
quality-related,
guality Group C, channel
head drain valve (4-50-377)
on
the
4A CCW heat
exchanger
on October
18,
1991,
the licensee
failed to
complete testing
in accordance
with the surveillance
requirements
for ISI
of ASME Section
XI guality Group A, B, or
C
(Code
1, 2, or 3) compon'ents
prior to the return of the
4A CCW heat
exchanger
to service.
e
This missed
post maintenance
test constitutes
one example of a violation.
(Refer to paragraph
7.b for the
second
example of this violation.)
This
violation will not be subject to enforcement action because
the licensee's
efforts in identifying and correcting
the violation m'eet the criteria
specified in Section
V.G. 1 of the
This item will
be tracked
as
NCV 50-250,251/92-07-02,
missed
post maintenance
test
on
a
CCW drain valve and missed surveillance
on the automatic fuel makeup valve
to the
4B
EDG day tank.
This item is considered
to be closed.
For those
maintenance
activities observed,
the inspectors
determined that
the activities were conducted
in a satisfactory
manner
and that the work
was
properly
performed
in accordance
with approved
maintenance
work
orders..
With the exception of the
NCV documented
above,
violations or
deviations
were not identified.
6.
Operational
Safety Verification (71707)
The inspectors
observed
control
room operations,
reviewed applicable logs,
conducted
discussions
with control
room operators,
observed
shift
turnovers,
and monitored
instrumentation.
The inspectors verified proper
valve/switch alignment of 'selected
emergency
systems,
verified maintenance
work orders
had
been
submitted
as required,
and verified followup and
prioritization of work was accomplished.
The inspectors
reviewed tagout
records,
verified compliance
with
TS LCOs,
and verified the return to
service of affected
components.
By. observation
and direct i nterviews,
verification was
made that the
physical
security
plan
was
being
implemented.
The
implementation
of
radiological
controls
and plant housekeeping/cleanliness
conditions
were
also observed.
Tours of the intake structure
and diesel, auxiliary, control,
and turbine
buildings
were
conducted
to observe
plant equipment conditions
including
potential fire hazards, fluid leaks,
and excessive
vibrations.
The
inspectors
walked
down
accessible
portions
of
the
following
safety-related
systems/structures
to verify proper valve/switch alignment:
t
g *
A and
B emergency diesel
generators,
control
room vertical panels
and safeguards
racks,
intake cooling water structure,
4160-volt buses
and 480-volt load
and motor control centers,
Unit 3 'and
4 feedwater platforms,
Unit 3 and
4 condensate
storage
tank area,
area,
,
10
Unit 3 and
4 main steam platforms,
and
auxiliary building.
The licensee
routinely performs
QA/QC audits/surveillances
of activities
required
under its
QA program
and
as
requested
by management.
To assess
the effectiveness
of these
licensee
audits,
the inspectors
examined
the
status,
scope,
and findings of the following audit reports:
Number of
Audit Number
~Findin
s
T
e of Audit
QAO-PTN-92-001
QAO-PTN-92-005
QAO-PTN-92-006
QAO-PTN-92-010
Plant Systems,
TSs 3/4.7. 1 through
3/4.7.5
Document Control
4
January
Performance
Monitoring
Audit
1
February
Performance
Monitoring
Audit
No additional
NRC followup actions will
be
taken
on
the
findings
referenced
above
because
they were identified by the licensee's
QA program
audits
and corrective actions
have either
been
completed or are currently
underway.
Plant management
has also
been
made
aware of these
issues.
On March
2 - 3,
1992,
the inspectors
performed
an audit of the licensee's
TSA program utilizing procedure
O-ADM-503, Control
and
Use of Temporary
System Alterations,
dated
January
21,
1992.
The operators
had
access
to
the correct
system
drawings either
by the set of control
room
PODs or by
the red-lined
drawings in the
TSA File in the control
room.
Three of the
fifteen
open
TSAs were walked
down.
The following discrepancies
were
noted:
The asterisk
in Enclosure
2, Safety Classification
Guidelines,
of
procedure
0-ADM-503 referred
the
reader
to the Q-List although
Section 1.9, Quality Assurance
Program,
of the
FSAR stated
that the
Plant Q-l ist was replaced with the Total Equipment Data
Base in 1990.
Paragraph
4.9 of procedure
0-ADM-503 referred to the placement
of the
Log of Operating
Diagrams
(Attachment 5) in front of the control
room
PODs to identify drawings affected
by TSAs, but it did not refer to
placement
of thi s log in front of the
POD book.
Although not
required
by the procedure,
this log was located
in front of the
book in the
~
Paragraph
5,7.4.3
of procedure
0-ADM-503 requires
that control
room
and
TSC drawings
be
red lined to reflect
new plant configurations.
Attachment
3,
TSA Log-Tracking
Sheet,
of this
procedure
contains
columns for red lining and restoration
of control
room
PODs but did
not refer to red lining and restoration of TSC PODs.
Paragraph
5.7.4.3 of procedure
0-ADM-503 requires
that control
room
and
TSC drawings
be
red lined to reflect
new plant configurations,
11
and
paragraph
5.7.4.7
of this
procedure
requires
that
the
Log-Tracking
Sheet
(Attachment 3)
then
be
updated.
The following
discrepancies
were noted:
On March 2,
1992, the control
room copy of Attachment 5, Log of
Operating
Drawings
Affected
by
TSAs,
indicated
that
six
controlled
drawings
were affected
by eight
open
TSAs, but the
seventh
column
(Control
Room
PODs,
Red
Lined
Yes/No) of
Attachment 3,
TSA Log-Tracking Sheet,
did not indicate whether
or not affected control
room
PODs were red lined for the
15 open
TSAs.
Although the
Log of Operating
Drawings Affected by TSAs provided
a reference
to the
TSA,
and
th'e
TSA file packages
contained
red-lined drawings;
the actual
control
room and
had not
been
red lined.
(By March 3,
1992,
three of eight affected
control
room
and
one of eight affected
had
been
red lined,
and the remaining
PODs in the control
room and
in- the
book
had
been
red
lined
by
March 4,
1992.
The
full-sized
PODs in the
TSC were red lined by March 9, 1992.)
During
a comparison
of the control
room
and
TSC Logs of Operating
Drawings
Affected
by
on
March 3,
1992,
the
following
discrepancies
were noted:
TSA 3-89-21-2,
which affected
sheet
3 of drawing 5610-T-E-4530,
had
been restored
on January
23,
1992,
per the control
room log,
and
no restoration
date
was indicated
on the
TSC log.
The control
room log also indicated that
TSA 4-92-47-3,
which
affected
sheet
3 of drawing 5610-T-E-4505,
had
been
implemented
on February
23,
1992,
and restored
on February
25,
1992.
This
item had not been entered
on the
TSA log.
On
March 3,
1992,
the
Log of Operating
Drawings Affected
by TSAs
identified the
drawing coordinates
affected
by
TSA 4-90-13-19 for
POD 5610-T-E-4064,
sheet
2,
as A-8.
Coordinate
A-8 of the control
room and
TSC red-lined drawings referenced
TSA 3-87-13-50 in lieu of
TSA 4-90-13-19.
TSA 4-90-13-19
was referenced
at coordinates
B-4 and
C-3
on the control
room
POD;
and although
the red lines
on the
POD were similar, it did not. reference
the
TSA number (4-90-13-19).
On March 3,
1992, while the
Log of Operating
Drawings Affected by
TSAs indicated
that coordinates
B-2 through
B-9,
E-3,
and
E-5
on
POD 5610-T-E-4530,
sheet
2, were affected
by TSA 3-90-71-23;
the red
lines
on control
room POD.5610-T-E-4530,
sheet
2, indicated affected
coordinates
B-5 through
B-9, E-3,
and
E-5.
. The red lines
had not
been
completed.
During
a walkdown of TSA 3-87-13-50,
Installation of Diesel
Driven
Air Compressors
and After Cooler s to Provide
Instrument Air, on
March 2, 1992,
the following discrepancies
were noted:
12
Tag no. 2, Diesel Air Compressor T-2,'ated
September
23,
1987,
was incorrectly hung
on diesel air compressor T-l.
The tag
on diesel air compressor
T-2 (Diesel I.A. Compressor
T-2
dated
October 28,
1988)
was
not identified
as
being tag no.
2
although
paragraph
5.1.6 of procedure
0-ADM-503 states
that
tags
shall
be
consecutively
numbered
as
Unit/Year/Code/Sequential
Number/Consecutive
Tag Number.
The tag
on diesel air compressor
T-3 dated
October 28,
1988,
was
not identified as being tag no.
3 as required
by paragraph
5.1.6
of procedure
O-ADM-503.
A large portion of the
TSA tag
hung
on diesel air compressor
T-4
was missing.
The tag
hung
on the spool
piece which replaced
the after cooler
near the Unit 3 electric instrument air compressor
was not dated
and
was
not identified
as
being
tag
no.
7
as
required
by
paragraph
5. 1.6 of procedure
O-ADM-503.
During
a walkdown of TSA 3-91-21-24,
Raw Water Storage
Tank Level
Upgrade,
on March 2,
1992, the following discrepancies
were noted:
The
tags
were
not
consecutively
numbered
as
required
by
paragraph
5.1.6 of procedure
O-ADM-503.
There
was
no tag
on the pressure
indicator for, raw water storage
tank No.
1.
The
two existing tags
had the
same description (Install Fisher
Controllers
on LK-6A and
LC-501 and Pressure
on
RWST I).
Subsequent
to the
NRC's audit of the
TSA program,
the licensee
performed
an audit of all
open
TSAs, corrected
the tag discrepancies,
and red lined
the drawings.
The licensee
also submitted
a procedure
change
request
in
order to correct
the procedural
discrepancies.
At the time of the
audit, control
room
and
TSC drawings affected
by the existing
open
had
not
been
red lined
and,
therefore,
did not conform to the recent
changes
(approximately
41 days)
in the
TSA process.
At the time of the
TSA audit,
the licensee
personnel
responsible
for TSAs stated
that
the
revised
TSA procedure
was only intended to affect newly generated
TSAs and
that the revised
process
was not intended
to include the red lining of
drawings
affected
by existing
TSAs.
However,
the inspectors
noted that
both the
PNSC
and plant management
were not aware that all
TSAs were not
going to agree with the latest procedure revision.
Following discussions
with licensee
management,
all control
room and
TSC drawings affected
by
TSAs were red lined in accordance
with procedure
0-'ADM-503.
On March 4,
5,
7,
and 9,
1992,
a partial audit of the licensee's
TSC and
control
room
drawings
was
performed utilizing procedures
AP 0190.86,
13
Document Control;
AP 0109. 1, Preparation,
Revision,
Approval,
and
Use of
Procedures;
gP
6.6,
Drawing
Control
for Operating
Nuclear
Plants;
g1-3-PTN-1,
Design
Control;
g1-6-PTN-l,
Document
Control;
(}1-6-PTN-2,
Drawing Control;
the
Controlled
Document
Status
File Listing dated
March 5,
1992;
the Controlled
JPN
Immediate Distribution Acknowledgement
List dated
February 21,
1992,
and
the
Controlled
POD/MD
Immediate
Distribution Acknowledgement List dated
February 21, 1992.
The inspectors
verified that the appropriate controlled drawings listed
on the Controlled
JPN
and
POD/MD Immediate Distribution Acknowledgement Lists were available
for control set
no.
1 in the
TSC and for control set nos.
9 through
13 and
17 in the control
room.
In the TSC, various
items listed on the breaker
list
(5610-E-0855
series)
were
spot
checked
against
the
Controlled
Document Status
File Listing.
A complete audit of the
POD book (5610-T-E
series;
5610-T-D series;
5610-,
5613-,
and 5614-T-Ll series;
and selected
P8IDs), the
Hagan prints
(5610-M-430-200 series),
the Heat Tracing System
drawings
(5610-M-420-300 series),
and
the
Instrument
Index
(5610-M-311
series)
l ocated
in
the
was
also
performed.
The
following
discrepancies
were noted.
General
Comments
Numerous
Numerous
5610-M-91
5610-M-762
Drawing titles were missing from the
Controlled Document Status File Listing.
Sheet
numbers 'were missing from the
'Controlled
Document Status File Listing.
This drawing was listed
on Controlled
JPN
Immediate Distribution Acknowledgement
List but
was
not located
in the
on
March 7,
1992.
This drawing
was
placed in
the
TSC by March 17,
1992.
On March 9,
1992, controlled file
no.
10
(Control
Room/NPS)
contained
both
revision
0
dated
April 5,
1991,
and
revision
1 dated
September
23,
1991.
This
was corrected
immediately.
Audit of the
POD Book (5610-T-E Series;
5610-T-D Series;
5610-,
5613,
and
561 - -Ll Series;
and
Se ected
P
Ds
in t e
TSC on Narc
5,
19
2
5610-T-E-4064,
sheet
3
I
Both revisions
37
and
38 were located in
the
POD book.
The full-sized drawing
located
in
the
TSC -file cabinet
was
revision 38,
and,the
Controlled
Document
Status
File Listing referred to revision 38.
Revision
37
was
removed
from the
by
. March 17,
1992.
14
5610-T-E-4064,
sheet
4
5610-T-E-4065,
sheet
2
5610-T-E-1591,
sheet
1; and
5610-T-E-1592,
sheet
1
This drawing was not located in TSC
book.
The Controlled
Document Status
File
Listing referred
to revision 30,
and
the
full-sized drawing located in the
TSC File
Cabinet
was also revision 30.
This drawing
was placed in the
POD book by March 17,
1992.
Revision
62 dated
February
21,
1992,
was
located
in
the
TSC,
but
the
Controlled
Document Status
File Listing dated
March 5,
1992,
referred
to
revision 61.
The
Controlled
Document Status
File Listing was
corrected
by March 17,
1992.
These
two drawings
were
out of order in
the
POD book.
Audit of the
Ha an Prints
5610-M-430-200 Series
in the
TSC on
Narc
5610-M-430-237,
sheet
1
5610-N-430-237,
sheet
2
5610-N-430-281,
sheet
1
5610-N-430-236,
sheet
1;
5610-N-430-237,
sheet
2;-
5610-N-430-. 238,
sheet
1;
and
5610-N-430-275,
sheet
1
This drawing was not located in the
nor was it listed
on the Controlled Document
Status File Listing.
Drawing 5610-M-430-237
only
had
one
sheet
(sheet
2 of
2) for
pressurizer
level protection channel II, and
there
should
have
been
two (sheets
1 of
2
and
2 of 2).
This drawing was placed in the
TSC and was
added to the Controlled Document
Status 'File Listing by March 17,
1992.
Revision
0 was located in the TSC, but
the Controlled
Document Status
File Listing
referred
to revision
2 and listed
no sheet
number.
The Controlled Document Status File
Listing was corrected
by March 17,
1992.
This drawing was incorrectly listed
on
Controlled
Status
File
Listing
as
5610-M-430-20430-281.
It was
also out of
order
on
the listings
The listing
was
corrected
by March 17,
1992.
Many sheet
numbers
were missing from
the controlled document status list, but
these
were of significance
because
there
was
more than
one sheet
per drawing.
15
Audit of Heat Tracin
S stem
Mare
7,
~ 1992
5610-M-420-300,
sheet
97
5610-M-420-300,
sheet
99
5610-M-420-300 Series)
in the
TSC on
Revision
2 dated
October 22,
1991,
was
located
in the
TSC,
but
the
Controlled
Document
Status
File Listing referred
to
revision
1'.
The Controlled
Document Status
File Listing
was
corrected
by
March 17,
1992.
Revision
0 dated April 26,
1985,
was
located
in TSC,
but the Controlled Document
Status
File Listing referred to revision l.
The TSC drawing was replaced with revision
1
by March 17,
1992.
Audit of Instrument
Index
5610-N-311 Series
in the
TSC on March 7,
1992
5610-M-311, cover sheet
5610-N-311,
sheet
082A
5610-M-311, sheet
249A
5610-M-311,
sheet
276
5610-M-311,
sheet
299A
This document
was
stamped
as
a
"Controlled
Document"
but did not have the
controlled
set
number
( 1) written in the
box.
Revision
17 dated April 18,
1991,
was
located
in the
TSC,
but
the
Controlled
Document
Status
File Listing referred
to
revision 18.
Page
1970 of the Drawing Index
dated
February
.7,
1992,
referred
to
revision
17.
The
TSC drawing was replaced
with revision
18
on March 17,
1992.
Revision
0 dated
February 3,
1992 was
located in the
TSC but was not listed
on the
Controlled
Document
Status
File Listing.
Page
1988
of
the
Drawing
Index
dated
February
7,
1992, referred to this document
but
had
no revision
number.
The Controlled
Document
Status
File Listing was corrected
by March 17,
1992.
Revision
19 dated
February
6,
1992,
was
located
in the
TSC,
but
the
Controlled
Document
Status
File Listing and
page
1992
of the Drawing Index dated
February
7,
1992,
both
referred
to
revision
18,
The
Controlled
Document Status
File Listing was
corrected
by March 17,
1992.
Although revision
0 was listed in the
Controlled
Document
Status
File Listing,
this drawing was
not located
in the
TSC nor
was it listed in the
Drawing
Index dated
February 7,
1992.
The Controlled
Document
16
5610-M-311,
sheet
347C
Status
File
Listing
was
corrected
by
March 17,
1992.
This drawing was listed twice on the
Controlled
Document
Status
File Listing
(correctly
on
line 02377,
page
22,
and
incorrectly as drawing 5610-M-3110311,
sheet
347C,
on
line 02372,
page 44).
The
Controlled
Document Status
File Listing was
corrected
by March 17,
1992.
At the time of this audit,
document control
was in the process
of auditing
controlled
procedures
and
was planning to audit the controlled drawings.
Subsequent
to the
NRC's partial
audit of the
control
room
and
controlled .drawings,
the licensee
performed
a complete audit of all of the
controlled drawings
located
in the control
room, TSC,
and
OSC.
All noted
discrepancies
were corrected.
An audit of the controlled drawings located
in the vault is currently ongoing.
TS 6.8. l.a
requires
that
procedures
be established,
implemented,
and
maintained
covering activities
recommended
in Appendix
A of Regulatory
Guide 1.33,
Revision
Q February
1978,
and in Section
5. 1 of ANSI N18.7-
1972Property "ANSI code" (as page type) with input value "ANSI N18.7-</br></br>1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process..
Section
1 of Regulatory
Guide 1.33,
Appendix A,
r ecomnends
the use
of administrative
procedures.
Section
5. 1 of
ANSI
N18.7 -
1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7 -</br></br>1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,
recommends
that written policies
be provided to control
the issuance
of
documents,
including'hanges,
that
prescribe
activities
affecting
safety-related
structures,
systems,
or components.
Procedure
O-ADM-503,
Control
and
Use of Temporary
System Alterations,
provides instructions for
the control
and
use of TSAs to ensure that operations
personnel
are
aware
of all changes
and to ensure
that
made to plant equipment
do not
degrade
the original design intent.
Administrative procedure
AP 0190.86,
Document Control,
and Quality Instruction
QI 6-PTN-1,
Document Control,
provide instructions for the implementation of the plant program for the
control of documents
to ensure that only up-to-date
information is used in
performing activities.
Quality Instruction
QI 6-PTN-2,
Drawing Control,
provides
requirements
to ensure
that accurate
drawings
are available
and
used
at the
user location.
Contrary to these
requirements,
numerous
discrepancies
regarding
the control of TSAs
and controlled diagrams
were
identified as
documented
above.
The multiple discrepancies
identified regarding
the control of TSAs
and
controlled
diagrams
is
a violation.
This violation is not being cited
because
the criteria specified
in Section
V.A of the
NRC Enforcement
Policy
were
satisfied.
This
item will
be
tracked
as
50-250,251/92-07-05,
multiple discrepancies
regarding
the control of TSAs
and controlled diagrams.
As
a result of routine plant tours
and various operational
observations,
the
inspectors
determined
that
the
general
plant
and
system
material
conditions
were satisfactorily maintained,
the plant security
program was
effective,
and the overall
performance of plant operations
was good.
With
17
the exception
of the
NCV documented
above,
violations or deviations
were
not identified.
7.
Plant Events
(93702)
The following plant events
were reviewed to determine facility status
and
the
need for further followup action.
Plant parameters'ere
evaluated
during transient
response.
The significance of the event
was evaluated
along with the
performance
of the appropriate
safety
systems
and
the
actions
taken
by the licensee.
The i nspectors
verified that required
notifications were
made to the
NRC.
Evaluations
were performed relative
to the
need for additional
NRC response
to the event.
Additionally, the
following issues
were
examined,
as appropriate:
details
regarding
the
cause
of the event;
event chronology; safety
system performance;
licensee
compliance
with approved
procedures;
radiological
consequences, if any;
and proposed corrective actions.
a ~
On February
23,
1992, with Unit 4 at
100 percent
power, approximately
80 gallons of primary coolant
was inadvertently
released
through the
4B charging
pump vent valve (4-276E) resulting in the contamination
of two licensed
operators
and
the Unit 4 charging
pump
room.
The
released
water
was collected in
a waste
holdup tank.
This event
occurred
during troubleshooting activities to identify the
cause of
reduced
total'charging
flow discovered
during in-service testing of
the
4A charging
pump.
The
4B charging
pump was
removed from service
due to either
suspect
back
leakage
through
the
pump or possible
relief-valve
leakage.
To determine if the recirculation
valve
(4-1316) for the
4B charging
pump was leaking through,
a test release
for troubleshooting
was generated
against
the clearance
which was in
effect for the
removal
and re-installation of the
4B charging
pump
relief valve
due to suspect
leakage.
The vent valve had
been tagged
open
as part of this clear'ance,
but the
need to remove the clearance
from the vent valve and shut it during troubleshooting activities
was
not identified.
As
a result,
the vent valve was not included
on the
test release,
and it was allowed to remain
open while the system
was
pressurized
to approximately
2500 psig
from the
4A charging
pump
discharge
The vent valve
was immediately'losed
upon discovery of the leak.
The
contaminated
personnel
and
the Unit 4 charging
pump
room were
decontaminated,
and
the personnel
directly involved with this event
received
disciplinary action.
A night order
was
issued
to all
operations
personnel
discussing
the
event,
and
the
event
was
discussed
at operations
meetings.
A Nuclear Problem Report (92-025)
was also generated.
In addition,
a quality assurance
finding was
issued
for failure to provide
a
procedure
for an activity which
affected
a safety/quality-related
system
and. presented
a
personnel
hazard.
TS 6.8. 1
requires
that
written
procedures
be
established,
implemented,
and
maintained
covering
activities
recommended
in
18
Appendix
A of Regulatory
Guide 1.33,
Revision 2,
February
1978.
Section 1.c of this Appendix recommends
administrative
procedures
for
equipment
control (e.g.,
locking and tagging).
Paragraph
5. 15.5 of
procedure
O-ADM-212, In-Plant
Equipment
Clearance
Orders,
requires
that the clearance
controller/holder shall request
a Release
for Test
and shall provide,
among other things, the reason for the Release for
Test listing the test to be performed
and
a step-by-step
description
of what clearance
order steps
need to be included
on the Release for
Test
and
the position required for the test release.
In addition,
paragraph
5. 15.12 requires
that
the administrative
RCO or qualified
operator
research
and write a Release
for Test.
Paragraph
5.15. 13
also
requires
the
ANPS/NWE to independently
review
and verify the
adequacy of the administrative
RCO's instructions
and steps
including
the releasing
order
and the
component positions.
Contrary to these
requirements,
the
need
to close
the
4B charging
pump vent valve
(4-276E) during troubleshooting activities
was not identified.
As a
result,
on February
23,
1992,
vent valve 4-276E
was not included
on
the test release
and
was allowed to remain
open while the system
was
pressurized
to approximately
2500 psig
from the
4A charging
pump
discharge
This in turn permitted the inadvertent
release
of
approximately
80 gallons of primary coolant
which contaminated
two
licensed
operators
and the Unit 4 charging
pump room.
The inadequate
review of
a test release
work scope is
a violation.
This violation
will be tracked
as
VIO 50-250,251/92-07-03,
inadequate
review of a
test
release
work
scope
resulting in the
inadvertent
release
of
primary coolant through the
4B charging
pump vent valve and resulting
in the contamination of two licensed
operators.
On March 2,
1992, at 3:00 p.m.,
the
4B
EDG was declared
when
the
licensee
identified that
a
required
surveillance
for
valve SV-4-3434B,
Auto Fuel
Makeup to the
4B
EDG Day Tank,
had
been
missed.
The licensee
entered
action statement
b for TS 3.8.1.1 which
required
demonstrating
the operability of the startup
transformers
and their associated
circuits
per
TS 4.8. 1. 1. l.a within one hour,
demonstrating
the operability of the
remaining
required
EDGs per
TS 4.8. 1.1.2.a.4 within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,
and restoring the inoperable
EDG to
status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
The startup transformers
and their
associated
circuits were verified to
be operable
at 4:05 p.m.
The
surveillance
on SY-4-3434B
was successfully
completed at 4:30 p.m.,
and
the
4B
EDG was
declared
Operability
- testing of the
4A
was
completed, at 8:43 p.m.,
and operability testing
of the
3A
EDG was completed at 2:35 a.m.
on March 3,
1992.
Solenoid
valve SV-4-3434B is
a self-enclosed
Valcor solenoid
valve
which was recently installed during the
dual unit outage
in 1991.
Required
IST would include
both
a quarterly
valve exercise
and
measurement
of valve stroke
time,
Because
the valve
has
neither
remote or local position indicating lights nor
a control
switch for
actuation
and
because it only opens
on
a low
EDG 4B day tank level
signal,
no convenient
means for measuring
stroke time exists.
Based
on this condition,
the licensee
submitted
a relief request
to delete
19
the required stroke
time test.
Via telecon
discussions
with
NRR on
December
18,
1991,
the deletion of the stroke time test
requirement
for this valve
was
denied,
and
the
NRC
recommended
that alternate
test
means
be developed.
A revised relief request specifying only a
maximum stroke
time
was
submitted
on
December 31,
1991,
and
on
January
23, 1992, the
NRC granted interim relief.
The valve exercise
test
was conducted
on the
normal scheduled
date of January
30,
1992.
However,
the valve stroke
time was not measured.
The grace period
for this
test
expired
on
February 21,
1992.
Solenoid
valve SV-4-3434A for the
4A EDG was successfully
stroke time tested
on February 21,
1992,
by installation of a jumper in the
4A EDG fuel
oil
transfer
control
logic circuitry
and
placement
of
an
accelerometer
on the valve;
however,
solenoid
valve SV-4-3434B
was
not tested
on this 'date
due to high diesel
fuel oil level
in the
4B
EDG day tank
and the impression that additional
time was available
to perform the test.
This event
was further documented
in LER 50-251/92-002,
Failure to
'easure
Stroke
Time
as
Part of Inservice Test.
According to this
LER, the licensee
plans
to revise
the surveillance
procedures
to
ensure
that all
IST requirements for valve SV-3434B are incorporated;
review all i nterim reliefs granted
on January
24,
1991,
to assure
that the appropriate
test
requirements
have
been
incorporated
into
the surveillance
procedures;
review the
IST program to assure
that
each test or exam for each
IST component is adequately
identified in
the
surveillance
tracking
system;
revise
procedures
to require
tracking of all changes
to the
IST program to assure
that changes
are
incorporated
into plant procedures;
and
examine
the review process
for the identification of coomitments
within
NRC submittals
to
identify other types of documents
were tracking of commitments
was
not
assured.
The
inspectors
will followup
on
the
licensee's
corrective actions
regarding this matter during future inspections.
TS 4.0.5 requires
1, 2,
and
3 components
and
Class
1, 2, and
3 pumps
and valves
be performed
in accordance
with Section
XI of the
ASME Boiler and Pressure
Vessel
Code
and applicable
Addenda
as required
by
except
where specific written relief has
been granted
by the
NRC pursuant to
Paragraph
IWV-3413(a),
Power
Operated
Valves, of ASME Section XI, Rules for Inservice Inspection of Nuclear
Power Plant Components,
Article 3400, Inservice Tests,
Category
A and
B Valves, states
that the limiting value of full-stroke'ime of each
power
operated
valve
be
specified
by the
owner
and
that
the
full-stroke time is
the
time interval
from initiation of the
actuating
signal
to
the
end
of
the
actuating
cycle.
Paragraph
IMV-3413(b) states
that
the
stroke
time of all
power
operated
valves
be measured
to the nearest
second for stroke times of
10 seconds
or less
or to
10 percent of the specified limiting stroke
time for full.-stroke times
longer than
10 seconds
whenever
such
a
valve is
stroke
tested.
Appendix D,
Valve
Program
Table,
of
JNS-PTN-200,
Second
Ten Year Inservice
Inspection Interval Inservice
t
20
Testing
Program Test Programs for Pumps
5 Valves, identifies solenoid
valve SV-4-34348
as
a
Class
3 (guality Group C),
Category.
B type
valve.
Contrary
to .these
requirements,
on
March 2,
1992,
the
licensee
identified that
the
measurement
of the stroke
time for
valve SV-4-3434B in accordance
with the surveillance
requirements
for
XI guality Group A, B,
o'r
C (Code 1, 2, or 3)
components
was
not performed within the surveillance
period.
The
surveillance
was
due to
be
performed
on January
30,
1992, with a
grace period expiring on February 21,
1992.
This
missed
surveillance
constitutes
the
second
example
of
a
violation.
(Refer to paragraph
5 for the first example
of this
violation.)
This violation will not be subject to enforcement
action
because
the licensee's
efforts i n identifying and correcting
the
violation meet
the criteria specified
in Section
V.G. 1 of the
NRC
Enforcement
Policy.
This
item
will
be
tracked
as
NCV 50-250,251/92-07-02,
missed
post maintenance
test
on
a
CCW drain
valve
on the automatic fuel
makeup
valve to
the
4B
EDG day tank.
This item is considered
to be closed.
At 12:55 a.m.
on March 8,
1992,
the
4A CCW/ICW basket
strainer
was
taken
out of service for backwashing
per procedure
4-0P-019,
Intake
Cooling Water System,
and Unit 4 entered
a 72-hour
LCO under action
statement
c of TS 3.7.3.
At 1:35 a.m.,
the licensee identified that
the total
ICW flow through the
CCW heat
exchangers
was less
than the
minimum flow required for CCW heat exchanger
performance capabilities
(15,400
gpm)
as
required
by
procedure
4-OP-019.
As
a result,
was entered for the heat
exchangers
not being
capable
of
removing design
basis
heat
loads
per
Backwashing of the
4A CCW/ICW basket strainer
was
commenced
at 1:45 a.m.
At 2:05 a.m.,
ICW flow through
the
heat
exchangers
was verified to
be
18,000
gpm,
and
was exited.
The
4A CCW/ICW basket strainer
was returned to service at 2:06 a.m.
At 3:00 a.m., it was determined
that no
CCW heat exchangers
were out of service
and that
TS 3.0.3 did
not apply.
This was
based
on utilization of the most recent strainer
and
heat
exchanger
performance
curves
with
the
actual
flow
( 12,700 gpm),
actual
intake
temperature
(82.9 degrees
F),
and
most
conservative
tube
resistance
factor
(.001548)
at the
time of the
event.
OTSCs
incorporating
these
curves
into plant procedures
were
approved
by the
PNSC
on March 12,
1992.
At 9:48 a.m.
on March 10,
1992,
the
4A reactor trip bypass
breaker
was closed in order to facilitate the
swap out of the
4A reactor trip
breaker.
At this
time,
Unit 4
entered
TS 3.3. 1,
item
19 of
TS Table 3.3-1,
action
statement
8, which allows
one reactor trip
breaker to be bypassed
for up to
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing per
TS 4.3. 1. 1 provided
the other trip breaker
is operable.
While in
this 2-hour
LCO, the
4A reactor trip breaker
was
removed;
and prior
to installation of the
new breaker,
an inspection of the breaker
cabinet
was
performed.
During this
inspection,
the
latching
mechanism
which was tack welded to the left side rail of the breaker
21
cabinet
was
found to
be
bent forward.
The left side rail
and
associated
latching mechanism
were replaced,
and the original breaker
was re-installed
and tested
per Section 7.3, Returning
Breaker
A to Service,
of procedure
4-0P-049,
Reactor Trip Breaker
Operation for Maintenance.
The 2-hour
LCO was exited at 11:35 a.m.
when the 4A reactor trip bypass
breaker
was closed.
A similar event
occurred
a
few years
ago
on another
breaker.
Following the previous event, all of the reactor trip breakers
were
replaced.
Placards
were installed
on the cubicle doors explaining
the correct
method of racking
the
breakers
in
and out,
and
the
procedure
was
revised
to include steps
to check
the breaker rails.
The licensee
is currently in the
process
of generating
a Nuclear
Problem Report
(92-035) to document
the results, of its investigation
regarding this matter.
The investigation results
and
any long-term
corrective actions will be reviewed during future inspections.
At 12:59 p.m.
on March 10,
1992,
the
4A bypass
breaker
was re-closed
in order to re-attempt
the
swap out of the
4A reactor trip breaker.
At this time, Unit 4 re-entered
TS 3.3.1, item
19 of TS Table 3.3. 1,
action
statement
8, .which allows
one reactor trip breaker
to
be
bypassed
for up to
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing
per
TS 4.3.1. 1
provided the other trip breaker is operable.
While in this 2-hour
LCO, the
4A reactor trip breaker
was
swapped
out
and tested.
At
1:31 p.m.,
during the
performance of procedure
4-OSP-049. 1, Reactor
Protection
System
Logic Test,
RPS trai n
A relay RT-6 failed.
This
caused
the unit to enter
a 6-hour to hot standby
LCO per the
same
TS
and action
statement.
PWO 7138/64
was
generated,
and
the faulty
relay was
removed
and replaced.
The,RPS surveillance
was
resumed
and
completed
satisfactorily,
and
the
4A reactor
trip breaker
was
returned to service at 5:58 p.m.
The relay failure was
documented
in
the
RPS failure log book for trending purposes,
and the failed relay
was
sent
to Westinghouse
for analysis
to determine
the failure
mechanism.
Preliminary investigations
indicate
the
cause
to
be
a
problem in the pickup coil.
The failed relay
had
been successfully
tested
by the
same procedure
on February
12,
1992.
The licensee
is currently in the
process
of generating
a Nuclear
Problem Report
(92-'036) to document
the results of its investigation
regarding this matter
and is planning to update this report
when the
results
of . the
investigation
are
received.
The
investigation
results
and
any long-term corrective
actions will be
reviewed during future inspections.
At 12:30 p.m.
on
March ll, 1992,
with the fossil units'tartup
transformer
out of service,
Unit
1 (fossi l) lost backfeed
from the
while working
on
a field breaker.
This
in turn
de-energized
some
auxiliary
equipment for the blackstart
diesel
generators
including the
soak
back
pumps which keep the diesel oil
warm.
As
a result,'ll five blackstart
diesel
generators
were
t
~
22
declared
out of service.
The blackstart
diesel
generators
were
returned to service
two hours later.
At 7: 10 p.m.
on
March 16,
1992,
a
load
reduction
on Unit 4
was
commenced
in order to facilitate
the cleaning of the
4A TPCW heat
exchanger
and of the
4B north
and south waterboxes.
Unit 4 reached
the
50 percent
power level at 9:00 p.m.
on the
same
day.
Power
ascension
was
commenced
at
6: 10 a.m.
on
the following day,
and
100 percent reactor
power was re-attained
at ll;25 a.m.
During the performance
of procedure
3-PMI-072.5, Turbine First Stage
Pressure
Protection
Instrumentation
Set
IV
Channel
P-3-447,
on
March 19,
1992,
channel
IV
steam
flow
transmitter
test
switches
CT-3-475,
CT-3-485,
and
CT-3-495
were placed
in the test
position.
This action took the reactor protection
steam flow input
to the
steam
flow versus
flow mismatch
to zero.
At
6:30 p.m., the Unit 3
RCO notified an
ANPS that the steam flow versus
flow mismatch reactor protection bistables
were actuating
and clearing
as
the test
was
adjusted
to change
the
steam flow for comparison
to the
programmed
flow (FT-447)
as called
for by the test
procedure.
The
ANPS observed
that the
steam flow
indications for channel
IV were indicating zero
and instructed
the
ISC supervisor to terminate
the test
procedure
and to restore
the
protection
racks
to normal.
At this time,
the
IEC supervisor
informed the
ANPS that the testing
had
been
completed
and that rack
restoration
had 'already
been
commenced.
All channels
were verified
to be in the required state, all bistables
were returned
to normal,
and
an investigation
was
commenced.
It was determined that there
were
no procedural
violations; however,
a
procedural
deficiency
was
noted.
The test
procedure
did not
recognize
that placing the
channel
IV steam
flow transmitter test
switches
(CT-3-475,
CT-3-485,
and CT-3-495) in the test position not
only affected
the
inputs for the
steam
break protection
(steam
flow compared with first stage
turbine pressure)
circuitry but also
affected
the
inputs for the
steam flow versus
flow
mismatch circuitry.
As
a result,
the test
procedure
permitted the
channel
IV steam flow channel
to reactor protection to be taken out
of service without placing
the bistables
for the
steam flow versus
flow mismatch circuitry (478A2,
488A2,
and
498A2) in the
test position
as it had
done for the
steam line break protection
circuitry.
This in turn permitted
inputs to the reactor protection
logic for steam
flow versus
flow mismatch
as
compared to
low-low steam generator level.
With the
number of operable
channels
one less
than the total
number
of channels,
TS Table 3.3-1,
item 12,
action
statement
6,
permits
continued
power operation until performance
of the
next required
analog
channel
operational
test
provided that the inoperable
channel
is placed in the tripped condition within
1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
A detailed review
of
ERDADS archival
data
by the
STA determined
that during the
day
23
shift from
1:11 p.m.
to
2:13 p.m.,
a
period of
62 minutes,
all
channel
IY steam flow protection channels
were out of service without
bistables
478A2,
488A2,
and
498A2
being
placed
in the
tripped
position.
Because
these
bistables
were not placed in the tripped
position within 60 minutes,
an entry into TS 3.0.3'as
required,
but
the
out of service
condition
was
not discovered
by the day-shift
operating
crew.
Therefore,
according to
ERDADS data,
TS 3.0.3 should
have
been
entered
at 2: 11 p.m.
and exited at 2: 13 p.m.
No load
reduction
had
been initiated.
The peak-shift crew made the necessary
notifications
per
procedure
AP 103. 12, Notification of Significant
Events to NRC.
TS Table 3.3. 1, item 12,
Steam
Generator
Water Level--Low Coincident
With Steam/Feedwater
Flow Mismatch,
which is applicable -while the
unit is in Modes
1 and 2, states
that the total
number of channels
is
level
and
2 steam/feedwater
flow mismatch
channels
in each
s'team
generator.
With the
number of operable
channels
one
less
than the total
number of channels,
action statement
6 of this
TS
permits
continued
power operation
until
performance
of the
next
required analog
channel
operational
test provided that the inoperable
channel
is placed in the tripped condition within
1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
TS 6;8. 1
requires
that written procedures
be established,
implemented,
and
maintained
covering
activities
recommended
in
Appendix
A of
Regulatory
Guide 1.33,
Revision 2,
February
1978.
Section B.b of
this
Appendix
recommends
implementing
procedures
for
each
surveillance
test,
inspection,
or 'calibration
required
by
TSs.
Section B.b( l)(l) of this
Appendix also
recommends
that specific
procedures
for surveillance tests,
inspections,
and calibrations
be
written
for
tests
and
calibrations.
Paragraph
1. 1
of
procedure
3-PMI-072.5,
Turbine
First
Stage
Pressure
Protection
Instrumentation
Set
IV Channel
P-3-447,
states
that this procedure
provides
the instructions,
steps,
and data
necessary
to ensure
proper
calibration
and functional testing of the protection instrumentation
set
IY associated
with turbi'ne first stage
pressure.
Paragraph
1. 1. 1
of this
procedure
states
that all associated
instruments/components
are
contained
in channels
P-3-447,
Turbine First Stage
Pressure;
F-3-475,
Steam
Generator
3A Steam
Flow; F-3-485,
Steam
Generator
3B
Steam
Flow; and F-3-495,
Steam
Generator
3C Steam
Flow.
Contrary to
these
requirements,
procedure
3-PMI-072.5
was
not
adequately
established
in that it did not recognize that placing the channel
IY
steam
flow transmitter
test
switches
(CT-3-475,
CT-3-485,
and
CT-3-495) in the test position'ot only affected
the
RPS inputs for
steam
break
protection
(steam
flow versus first stage
turbine
pressure)
circuitry but also affected
the
RPS inputs for steam flow
versus
mismatch.
As
a result,
the channel
IY steam flow
protection
channel
to reactor protection
w'as
taken
out of service
without placing
the bistables
for steam
flow versus
flow
. mismatch
(478A2,
488A2,
and
498A2) in the tripped position.
Because
these
bistables
were
not
placed
in the
tripped position within
60 minutes
as
required
by
TS
Table 3.3-1,
item 12,
action
statement
6, Unit 3 inadvertently
entered
TS 3.0.3 for
2 minutes
on
~
~
24
March 19,
1992.
The unit was operating at
87 percent
power at the
time of this event.
The establishment
of
an
inadequate
procedure
(3-PMI-072.5) is
a
violation.
This violation will not be subject to enforcement
action
because
the licensee's
efforts in identifying and correcting
the
violation meet
the criteria specified
in Section
V.G. 1 of the
NRC
Enforcement
Policy.
This
item
will
be
tracked
as
NCV 50-250,251/92-07-04,
establishment
of
an
inadequate
procedure
(3-PMI-072.5) resulting in the entry of TS 3.0.3 for 2 minutes.
This
item,is considered
to be closed.
At 3:25 p.m.
on March 25,
1992,
a Unit 4 load reduction
was
commenced
due to the identification of moisture
in the generator
housing
causing
a generator field brush
ground following a
heavy rain storm.
The turbine generator
was taken off line,
and the
unit entered
Mode
2 at
5:50 p.m.
The prerequisites
for entering
Mode
1 were completed at 1:35 a.m.
on March 26,
1992,
and the turbine
was
placed
back
on line at
5:55 a.m.
Mode
1
was
entered
at
5:56 a.m.;
and at 6:45 a.m.,
30 percent
reactor
power
was
achieved
and maintained for a chemistry hold.
The licensee
attributed
the actual
leakage
to
be the result of
a
failure of the sealing materials
inside the exciter housing.
This
permitted
a low pressure
area at the bottom of the northeast
side of
the housing to suck in rain water from the outside.
This problem had
been
identified
by the
system
engineer
during
a routine
system
walkdown in November
1991.
A
PWO was
issued
at that time.
This
PWO
was placed
on hold for an outage but was not identified on the
SNOW
list for Unit 4.
The inspectors will follow up
on any additional
corrective actions
taken
by the licensee.
At 10: 15 a.m.
on
March 26,
1992,
Unit 4 received
an inadvertent
train
B safety injection signal
and
subsequent
reactor trip during
the
performance
of
a routine
monthly surveillance
per
procedure
OP 4004.4,
Containment
Isolation
Racks
gR50
and
gR51 Periodic Test.
At the time of this event, Unit 4 was in the process
of returning to
full
power following
a
shutdown,
and
reactor
power
was
being
maintained
at approximately
28 percent for
a
30 percent
chemistry
hold.
Test steps
1 through
4 of procedure
OP 4004.4,
which tested
the actuation
of individual test
switches
at
each
rack,
had
been
completed;
but the
performance
of item
1 in step
5 resulted
in -a
2-out-of-3
10 percent
high containment
pressure
safety injection and
containment
phase
A isolation
signal
to train 4B.
The
4B train
equipment
responded
as required.
Step
5
of
procedure
OP 4004.4
tests
the
2-out-of-3
logic for
10 percent
high containment
pressure
and calls for the operator
to
depress
the
two
push
buttons
"in pairs."
A single
pushbutton
actuates
two
type
CR2940
switch
blocks
ganged
in parallel.
Therefore,
each
pushbutton
has
two contact
sets.
One contact
set
25
actuates
the logic,
and
the
other
blocks
the
high
containment
pressure
signal.
This process
requires-that
the block contacts
open
prior to or .simultaneously
with the logic contacts:
Subsequent
testing
in
the
QR51 rack
revealed
that
for all
three
test
pushbuttons,
the actuating
contacts
operated
prior to the blocking
contacts.
One of the
three
switches
(TS-1)
was
disassembled,
examined,
and
compared
to
a
new switch.
The old switch
showed
a
travel difference of 0.027 inches
between
the
2 contact sets,
and the
new switch
showed
no measurable
travel difference
between
contact
sets.
The licensee's
inspection
also
found that
the actuation
contact set
was intermittently sticking open
due to
a cocked internal
contact
arm.
In addition,
these
switches
had
previously
been
analyzed
for failures
in
4-KV circuit
breakers
by
Root
Cause
An'alysis89-016.
This analysis
concluded
that
2000 cycles
was
a
conservative
point at which to replace
the switches.
The switches
in
question
have
been
cycled approximately
36 times per year since
1972
for a total of less
than
1000 cycles.
The licensee
attributed
the
cause
of this event to
be either the
actuating
contacts
operating prior to the blocking contacts
in both
switches
or to the sticking of the actuating
contact
on
one switch
(TS-1)
combined
with the
subsequent
actuation
of the other test
switch (TS-3).
Both causes
were primarily due to wear
and aging of
the test
pushbuttons
which were original plant equipment
and
have
been in service for over
20 years.
Another contributing factor was
that
the test
procedure
called for the test
pushbuttons
to
be
depressed
"in pairs" in lieu of pushing
one,
holding it, and
then
pushing the second.
Prior to restart,
the licensee
replaced
the test switches
in the
QR50
and
QR51 racks
on Unit 4.
In order to prevent aging from creating
a
problem
on
Unit 3;
procedure
OP 4004.4
was
revised
to
avoid
simultaneous
switch
actuation
and
to confirm switch
status
via
indicating lights.
Procedure
4004.4
was. also successfully
performed
for racks
QR50
and
QR51
on Unit 4.
In addition,
the
licensee
performed
walkdowns of other
systems
(RPS,
SI,
EDG,
AMSAC, control
room vertical
panels
and
control
boards,
and
AFW) in order
to
identify other
applications
of this type of switch.
The licensee
plans
to evaluate
these
applications
to determine if switch testing
or replacement
is warranted:
Long-term corrective
actions
may
include further
enhancements
to
OP 4004.4
to verify status
lights
when releasing
test
pushbuttons
prior to the next performance
of the procedure
on Unit 3, contacting
the
switch
manufacturer
(GE)
concerning
observed
switch
design
changers,
evaluation of a possible test circuit enhancement
that will
separate
the block and test .switches,'valuation
of the
adequacy
of
the
DDPS reporting logic for single train actuation
and provision of
recommendations,
and replacement
of the Unit 3 QR50
and
QR51 switches
during the next outage of sufficient duration.
The inspectors will
26
followup on'ny additional
long-term corrective
actions
regarding
this event.
Reactor startup
was
commenced
at 7:40 p.m.
on March 27,
1992.
Mode
2
was entered
at 8:00 p.m., criticality was achieved at 8: 12 p.m.,
and
Mode
1
was
entered
at
11:40 p.m.
during the turbine roll.
The
turbine generator
was placed
on line at 1:01 a.m.
on March 28,
1992,
and
100 percent reactor
power was achieved at 12:40 p.m.
on the
same
day.
Portions of the startup
were observed
by the inspectors.
One violation was identified.
8.
Exit Interview (30703)
The
inspection
scope
and findings
were
summarized
during
management
interviews
held
throughout
the reporting period with the Plant
General
Manager
and selected
members of his staff.
An exit meeting
was conducted
'n
April 3,
1992.
The areas
requiring management
attention were reviewed.
The licensee
did not identify as proprietary
any of the materials
provided
to or reviewed
by the inspectors
during this inspection.
Dissenting'omments
were not received
from the licensee.
Violations or deviations
were not identified.
The inspectors
had the following findings:
Item Number
Descri tion and Reference
50-250,251/92-07-01
50-250,251/92-07-02
50-250, 251/92-07-03
50-250,251/92-07-04
NCV - Failure to follow procedures for work
on shared, systems
(paragraph
3).
NCV - Hissed post maintenance
test
on
a
drain
valve
and
missed
surveillance
on
the
automatic
fuel
makeup
valve to the
4B
EDG day
tank (paragraphs
5 and 7.b).
VIO - Inadequate
review of a test release
work scope resulting
in the inadvertent
release
of primary coolant
through
the
4B charging
pump
vent valve and resulting in the contamination of
two licensed
operators
(paragraph
7.a).
NCV - Establishment
of an inadequate
procedure
(3-PHI-072.5) resulting in the entry of
TS 3.0.3 for 2 'minutes
(paragraph
7.h).
50-250,251/92-07-05
NCV - Multiple discrepancies
regardina
the
control
of
and
controlled
diagrams
(paragraph
6).
27
Administrative
ATWS Hitigation System Actuation Circuitry
Assistant Nuclear Plant Supervisor
Administrat'ive Procedure
American Society of Hechanical
Engineers
Anticipated Transient Without Scram
ADH
AHSAC
ANPS
ASHE
CFR
F
FOP
FT
Genera
ectric
gpm
Gallons
Per Hinute
ILC
ICW
IR
IS I
JPN 'uno Project Nuclear
KV
LCO"
LER
NRC
NWE
OP
OTSC
PME
PMR
PNSC
psig
PTN
PWO
QAO
QI
QR
Instrumentation,and
Control
Intake Cooling Water
Inspection
Report
Inservice Inspection
Inservice Testing
Kilovolt
Limiting Condition for Operation
Licensee
Event Report
Non-Cited Violation
Nuclear Plant Supervisor
Nuclear Regulatory
Commission
Office of Nuclear Reactor Regulation
Nuclear Watch Engineer
Operating
Procedure
Operational
Support Center
Operations
Surveillance
Procedure
On-the-Spot
Change
Preventative
Maintenance
Preventative
Haintenance-Electrical
Preventative
Maintenance-Relay
Plant Nuclear Safety Committee
Plant Operating
Diagrams
pounds
per square
inch gauge
Plant Turkey Nuclear
Plant
Work Order
Quality Assurance
Quality Assurance
Organization
Quality Control
Quality Instruction
Quality Related
Component
Cooling Water
Code of Federal
Regulations
Emergency
Response
Data Acquisition Display System
Fahrenheit
Florida Power
5 Light
MIN Fossil Plant Administrative Procedure
Final Safety Analysis Report
Flow Transmitter
1
El
4
28
RCO
SNOW
TPCW
TS
TS
Reactor Control Operator
Reactor Protective
System
Raw Water Storage
Tank
Safety Injection
Short Notice Outage
Work
Turbine Plant Cooling Water
Technical Specification
Test Switch
Temporary
System Alteration
Technical
Support Center
Unresolved
Item
Violation