ML17347B555
| ML17347B555 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 01/10/1990 |
| From: | Blake J, Girard E, Hallstrom G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17347B553 | List: |
| References | |
| 50-250-89-48, 50-251-89-48, NUDOCS 9002130217 | |
| Download: ML17347B555 (47) | |
See also: IR 05000250/1989048
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-250/89-48,
and 50-251/89-48
Licensee:
Florida Power
and Light Company
9250 West Flagler Street
Miami, Fl 33102
Docket. No.: 50-250
and 50-251
License Nos.:
DRP-31
and DRP-41
Facility Name:
Turkey Point
3 and
4
Inspection C~ t+ Octqber
30 - November
17,
1989
Inspectors:"
,-E,
Gi
.i-
.-- .:-'(/
Approv d b :-
- '=
J.
ake,
Chief
a
rials and Processes
Section
.
Di ision of 'Reactor Safety'
/o
Dat
Signed
/
Date Signed
/ /0
F>u
Date Signed
SUMMARY
Scope:
This announced
inspection
examined
the licensee
corrective actions initiated in
response
to
NRC
Maintenance
Team
Inspection
50-250,251/88-32,
conducted
November
28-December
16,
1988;
Independent
Management
Assessment
Commitments
related to maintenance
and licensee
action
on previous inspection findings.
Results:
The
team concluded
that the licensee
had developed
and implemented corrective
actions
to
address.
all
of the
maintenance
related
weaknesses
that
were
identified in the
NRC Maintenance
Team Inspection.
Significant improvement
was
observed
in all areas.
In particular,
the inspectors
noted
improvements
in the
following:
(1)
Plant
and
equipment
condition,
stemming
from
an
ongoing
upgrade
program.
(2)
Engineering
support,
especially
system
and reliability engineering,
which have only recently
been
developed
and begun to function.
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(3)
Parts availability and control
(4)
Development
of,and hiring for permanent
staff positions to replace
contractors
in
important
maintenance
support
functions,
such
as
Health Physics
and System Engineering.
(5)
An increased,
and apparently
more effective,
gC staff.
(6)
Planning
and scheduling
rel'ated
changes
which have
reduced delays to
maintenance activities.
The
improvements
which
have
occurred
appear
to
be
largely
the result
of
management's
selection
of
appropriate
personnel,
proper
assignment,
of
responsibilities,
and
especially,
to
management's
monitoring
of
the
improvements
and holding individuals personally
accountable.
Plant management
appears
adequately
supported
in all their actions
by Corporate
management
which
has allocated
large resources
to improvements.
t
Although it appears
that the licensee
program to minimize parts availability
delays
has made-significant
progress,
additional efforts are required to reach
their objective.
I
With regard
to the
plant
and
equipment
condition
and
engin'eering
support
improvements
referred to above, it should
be
recognized
these
require further
attention.
Plant
and equipment condition still appear
substandard
and
many of
the
added
engineering
support
personnel
are
relatively
inexperienced.
Reliability and
systems
engineering
programs
that were undertaken
in the past
year will likely require
some refinement.
The following violation was identified during this inspection:
89-48-01,
Drawing Discrepancies,
paragraph 2.c.(2)(b).
REPORT
DETAILS
Persons
Contacted
G. Banquer,
Corporate
Maintenance Staff
"W. Bladon, Superintendent
of Quality Assurance
L. Bossinger,
Planning
Support
Group Supervisor
Electrical Maintenance
R. Bumgarner,
Safety Supervisor
~D. Chancy, Director, Nuclear
Licensing
"J. Cross,
Plant Manager
~T. Diliard, Manager of Nuclear Maintenance,
Corporate
J.. Donis, Operations
Support Supervisor,
Technical
Department
R. Earl, Quality Control Supervisor
J. Ferrore,
Procurement
Document
Revie'w Team Supervisor
- T. Finn, Assistant Operations
Superintendent
S.
Franzone,
Lead Licensing Engineer
"J. Gianfrancesco,
Assistant
Maintenance
Superintendent
~J. Goldberg,
Executive Vice President,
Florida Power
8 Light Company
P.
Hansen,
Mechanical
Engineer
G. Harley, Instrumentation
and Control
( IKC) Planning Coordinator
- K. Harris, Site Vice President
~J. Hartzog,
Corporate
Licensing Engineer
E.
Hayes,
IKC Department
Supervisor
"G. Heisterman,
Assistant Superintendent
Electrical Maintenance
M.
AJ
G.
"H.
8'G
K.
A.
R.
R.
B.
J.
"R.
"M.
"R.
"M.
"W.
Herfurth,
System Engineer,
Instrument Air System
Kaminskas,
Technical
Department
Supervisor
Kenney,
Production Supervisor,
Mechanical
Maintenance
Koron,
I8C Projects
Coordinator
Korte, Nuclear Energy Corporate
Safety Supervisor
Max, System Engineer,
Instrument Air System
Paduano,
Corporate Technical
Manager
Pierce,
Operations
Superintendent
Powell, Regulatory
Compliance Supervisor
Regal,
Technical
Supervisor
Corporate
Maintenance
Remington,
System
Performance
Supervisor
Ray, Nuclear Job Planning
System Coordinator
Rose,
Design Control Supervisor
Seay,
Planning Supervisor
Sharpe,
Assistant
Superintendent,
Planned
Maintenance
Group
(PMG)
Sharp,
Plant Engineer Electrical Maintenance
Sontag,
Assistant
I8C Department
Supervisor
Stanton,
Reliability Engineer -
Taylor, Procedure
Upgrade
Program Superintendent
Thompson,
Engineering Supervisor,
Mechanical
Maintenance
Wade,
Eng>neering
Project Supervisor - Plant Support
Wayland,
Maintenance
Superintendent
Williams, Spare
Parts
Task Force Chairman
NRC Resident
Inspectors
"T. McElhinney, Resident
Inspector
"G. Schnebli,
Resident
Inspector
"Attended Exit Interview
2.
Licensee
Response
to
1988
NRC Maintenance
Team Inspection
(92701,
62700
and 62702)
The
NRC inspectors
examined
the actions
which the licensee
had taken to
address
apparent
maintenance
weaknesses
identified
in
a
1988
NRC
Maintenance
Team Inspection
(MTI) of Turkey Point.
(The subject
MTI was
documented
in
NRC Report
50-250,251/88-32,
dated
April 4,
1989.)
That
inspection
concluded,
based
on
the
weaknesses
observed,
that
Turkey
Point's
implementation of maintenance
was poor.
In the current
inspection
the
NRC inspectors
verified that the licensee
had documented
actions to respond
to each of the weaknesses
identified in
the
1988
MTI.
Then,
for the
weaknesses
that
were
the
more
important
contributors
to the
poor
maintenance
rating,
they
examined
details of
corrective
actions
taken
and
of their
effects.
Additionally,
the
inspectors
examined
several
maintenance
areas
that
were
not
reviewed
extensively in the MTI, e.g.,
post maintenance
testing.
The
maintenance
areas
and
weaknesses
inspected
and
the
NRC inspectors
findings are described
below.
Direct Measures
Direct
measures
utilized to
assess
plant
maintenance
in the
MTI
included historical data
and observations
of plant conditions during
wal,kdown inspections.
(1)
Hi stor ical
Data
The
most
significant
weakness
quoted
by
the
MTI for the
historical data
was the high forced outage rate.
The inspectors
could not assess
changes
in this indicator for recent operation
due to the effects of extensive
planned
and
unplanned
outage
work conducted
during the past year.
A review and discussion
of recent
forced outages with licensee
personnel
and the
NRC resident
inspectors,
however,
suggested
an
improvement in the performance of Unit 3.
Unit 4 had been in an
outage
much of the time since
the
MTI and
had experienced
two
forced
outages
since its startup
in May 1989,
suggesting
less
satisfactory
performance.
The inspectors
found that the licensee
had completed
a number of
important equipment
upgrades
which should contribute to improved
equipment availability,
and,
thus,
to
a reduced
forced: outage
.
rate.
Examples
included
valve
packing
improvements,
Residual
Heat
Removal
(RHR)
Pump
seal
modifications,
and
Containment
Cooling Heat
Exchanger
replacements.
It was also
evident that
resources
have
been
allocated
for further
improvements.
The
licensee
recently
announced
plan's for an eleven
month shutdown
late in 1990 to upgrade
aging equipment.
The inspectors
observed
considerable
engineering effort added to aide in identifying and
accomplishing
equipment
improvements
to increase
plant performance.
All of the above
should begin to be reflected in a reduced
forced
outage rate.
In addition to
a high'forced outage rate,
two other historical
weaknesses
were
noted in the
MTI.
These
were
high
personnel
radiation
exposures
and
excessive
out of service
control
room
instruments.
Data
at
the
time
of
the
MTI
suggested
that
radiation
exposures
were being
reduced
and
subsequent
licensee
data
confirms
very significant
continuing
improvement
(32io'eduction
between
1988
and
1989).
The
number of control
room
instruments
out-of-service
is still high,
but
licensee
data
shows
an
improving
trend.
The
inspectors
noted
continued
emphasis
on
improvements,
with frequent
reporting
of
open
control
room instrument-related
work orders
as
an indicator for
measuring
progress.
Plant Walkdown Inspection
The weaknesses
identified in the
MTI as
a consequence
of plant
walkdowns
for
observation
of
equipment
conditions
were
as
follows:
(a)
The
generally
unsatisfactory
equipment
and
housekeeping
conditions that existed in the plant.
(b)
(c)
Long-standing
inadequate
equipment identification tagging.
Evidence
of insufficient
worker
pride
or
"ownership"
interest
in
the
condition
of plant
and
equipment,
as
indicated
by
evidence
of
unsatisfactory
maintenance
practices
and the presence
of graffiti.
(d)
Insufficient/infrequent
licensee
supervisory
and
system
engineer
walkdowns to assess
plant conditions.
In the current inspection
the
NRC inspectors
conducted
walkdowns
and observed
plant conditions
and various maintenance activities
on at
least
five separate
occasions.
Most plant
areas
were
entered
(The
containment
was
omitted
due
to difficulties in
entry
during
plant
operation.)
Both 'NRC
inspectors
had
participated
in the
MTI and were able to discern
many improve-
ments
since then.
There
had
been
a
reduction
of contaminated
floor
space
with
. cleanup
and
application
of coatings
to
aid
in maintaining
cleanliness
in both
contaminated
and
non-contaminated
areas.
Contaminated floor space
was tracked
as
a performance
indicator
(included in the
licensee
daily "Plan of the
Day Report" ) with
reduction goals
and management
responsibility
and accountability
assigned
and monitored.
'
Equi pment
Excessive
equipment
equipment
ments
was
appearance
was
generally
improved
since
the
MTI.
lubrication was not observed
as formerly.
Additional
had
been
cleaned
and
painted
since
the
MTI
and
previously painted
as part of recent
plant improve-
being maintained.
Numerous
minor deficiencies
in plant
equipment
conditions
were
still observed.
Most were small leaks in non-safety
systems
and
only
a
very
few
had
not
been
identified in licensee
work
requests.
No
long-standing
work
requests
were
noted.
The
majority of those
examined
were dated
1989,
while
a very few
dated
back to 1987.
This suggested
that the actions to identify
and correct the. deficiencies
were largely in response
to recent
actions
taken to improve overall plant appearance
and
equipment
conditions,
rather
than
being
deficiencies
that
had
been
accumulated
and not corrected
because
of individually low safety
and reliability significance.
Licensee
actions
to ensure
proper equipment identification tags
was obvious
as
many temporary tags
were apparent
even
on items
of minor importance.
A check of equipment
tagging entries
on
walkdown log sheets
5610-TE-4510
and
4512,
conducted April 19,
1989,
and
May 31,
1989, respectively,
showed that the incorrect
'ags
specifically noted in the
MTI had
been
corrected.
These
tagging
discrepancies
were
cited
in
NRC
violation
'250,251/88-32-01.
Little graffiti was
observed.
Several
supervisors
were
seen
checking
plant
areas.
The
inspectors
found
that
specific
checklists
had
been
developed
for
use
by
supervisors
in
inspecting
areas
and
several
examples
of completed checklists
were verified.
Interviews
with
systems
engineers
indicated
they
were
now
walking down their systems
on
a planned periodic basis.
Records
of
several
of
these
walkdowns
were
verified
by
the
NRC
inspectors.
Maintenance
observed
in progress,
as for example
on charging
pumps,
was
being
performed
in
a well-organized
manner
with
location cleanliness
maintained
and tools and equipment
kept in
a generally orderly manner.
Workers
and
Health Physics
personnel
interviewed
stated their
general
agreement
with plant condition
improvements
and worker
morale appeared
good.
ll
A
II
The inspectors
considered
that all of the significant weaknesses
in
this
area (i.e., Direct Measures)
were being properly addressed,
but
that further efforts to upgrade plant conditions were
needed.
While
overall
plant
condition,
as
observed
in
walkdowns,
was clearly
improved, the forced outage rate performance indicator's status
could
not
be
assessed
accurately
for
improvement
due
to recent
lengthy
outages.
It appeared,
however, that the licensee
had
been taking the
actions
needed
to assure
equipment reliability and reduce
the forced
outage rate.
b.
Management
Organization
and Administration
For this area
the MTI's principal
concern
was inadequate
allocation
of resources
as indicated
by the following apparent
weaknesses:
(I)
Excessive
overtime
for
QC inspectors
(estimated
50%
on
the
average)
(2)
Excessive
use of contractors for Health Physics
(HP) and Systems
Engineering
support functions
(3)
Insufficient engineering
support
and
QC inspectors
(4)
Delays
due to parts unavailability
In the current
NRC inspection it was
found that the licensee
had
developed
measures
which addressed
and
had resulted
in significant
reduction of each
of the weaknesses.
With regard to
QC inspectors,
which is discussed
in detail in 2.c.(4) below, increases
in the staff
and changes
in the
QC program to better allocate inspection
personnel
were
noted.
The
number of Systems
Engineers
had
been
increased
to
improve engineering
support
and contract
system engineering
personnel
were being eliminated,
as discussed
in 2.c.(2).
Discussions
with
personnel;
including
one contractor,
indicated that the contract
personnel
were
being
eliminated
and
would
no
longer
be
used
in
routine circumstances.
As noted in 2.e.,
a program instituted
by the licensee
to minimize
parts
availability
problems
appears
to
be
effective,
though
additional efforts will be required to achieve
an acceptable
status.
I
Technical
Support
The elements
of technical
support which contained 'apparent
weaknesses
that contributed to the poor rating were implementation of corporate/
internal
communication,
engineering
support,
quality control
and
(personnel)
safety;
and the
absence
of any program for or
use
of
probabi listic ri sk
assessment
(PRA) .
In the current
inspection,
weaknesses
for these
elements
were
re-examined.
In addition,
the
inspectors
further
examined
the integration of regulatory
documents
into the maintenance
process
and the licensee's
preventive/predictive
maintenance
as
elements
of
technical
support.
The
inspectors
findings for each
element
are described
below.
( 1)
Internal/Corporate
Communication
The MTI'identified two weaknesses, for this element.
(a)
The'ack
of management
tours/walkdowns
of the plant for
'irect
communication
through
observation
of maintenance-
related activities
and
conditions
and
interaction
with
plant personnel.
(b)
The
apparently
poor
communication
between
Corporate
engineering
and
the
plant
on
technical
. problems
as
evidenced
by
poor
communications
related
to
a rust
and
. debris
inspection
conducted
in
response
to
With regard
to (a),
in the current
inspection
the inspectors
found that various walkdowns were being performed
by managerial
and
systems
engineering
personnel.
The
NRC inspectors
examined
procedure
O-ADM-008, which specifies
the performance
of manager
and
supervisor
walkdowns
and
the activities
to
be
observed.
Walkdown deficiency tracking lists (entitled
"Management
walkdowns
Trending .Data)
covering
the
period
of August 18-October
27,
1989,
were
verified
by
the
inspectors.
System
Engineers
walkdown records
were verified as
indicated
in 2.a.
above.
It
appeared
to
the
NRC
inspectors
that
the
walkdowns
were
contributing to
a better
understanding
of,
and to improvements
in plant conditions.
The
NRC
inspectors
further
examined
the
apparently
poor
communications
between
Corporate
engineering
and
the
plant
referred
to in (b)
by reviewing both subsequent
communications
on
the
rust
and
debris
inspections
and
by, reviewing
Corporate/plant
communications
in
addressing
other
similar
technical
issues
(as
described
in
(7)
below).
The
NRC
inspectors
found that the original communication
problem example
apparently
had
been
corrected
and that, for the
other
issues
checked,
there
were satisfactory
communications.
An example of
erroneous
internal
communications
associated
with
design
verification testing of GL88-14 valves
was
found,
however,
as
described
in (7) below.
(2)
Engineering
Support
The significant weakness'es
perceived
by the MTI for engineering
support
included
inadequate
specifications
o'f post modification
testing details,
inadequate
application
of
system
engineering
concepts
and evidence that recurring equipment deficiencies
were
not being corrected.
(a)
Post Modification Testing
In response
to the
concern
expressed
in the MTI, licensee
personnel
indicated that
the
MTI team
had
reviewed their
less
complex Design Equivalent Engineering
Packages
(DEEPs)
rather
than their more
complex
Engineering
Packages
(EPs)
and that,
since
the
DEEPs
were
non-complex,
specification
of their
ordinary
post
maintenance
testing
had
been
sufficient to demonstrate
adequate
function and operability.
However,
they revised
procedure
gI-3.7,
Design
Equivalent
Changes,
to clarify the testing
requirements.
The
NRC
'inspectors
reviewed gI-3.7 (7/89), three
examples
of post
modification testing
selected
and provided
by the licensee
and
two recent
examples
selected
by the
NRC inspectors
themselves
(Plant
Change/Modifications89-068
for
containment
sump solenoid valve replacement
and
89-373 for
modification to
Residual
Heat
Removal
valves to -preclude
hydraulic
lock).
Based
on their
review
the
inspectors
found no deficiencies
in the post modification testing.
(b)
System Engineering
The
MTI concluded that system engineering
concepts
had
not'een
adequately
implemented
as it was
found that
the
licensee's
system
engineer s
generally
had
not
become
adequately
fami liar with their
systems,
were
working
on
problem
components
rather
than
systems,
had
not received
adequate
training,
were
insufficient
in
number,'ad
poorly-defined responsibilities,
were not readily provided
with system work order
and failure information,
and about
,half of them were contractors.
In the current inspection
the
NRC inspectors
reexamined
the
licensee's
system
engineering
program
implementation
through interviews with the responsible
supervisor
and five
system
engineers,
review of examples
of records
of their
system
walkdowns
(September
1989 walkdowns for 480V Motor
Control, Center,
Reactor
Coolant
Systems
and August
1989
walkdowns for Auxiliary Feedwater
and
Reactor
Coolant
Systems),
review of
procedures
for
their duties
and responsibilities
and for performance
of
root
cause
analyses
(0-ADM-501
and
509
and
Technical
Department
Instruction
TDI-SE-004),
review of root cause
analyses
(RCA
89-015
and
ERT
89-013),
and
Limiting
Condition for Operation
(LCO)
hours
data
on
Main
Steam
Isolation
Valves
(MSIVs) used'y
a
system
engineer
in
assessing
MSIV performance.
Some
of the
NRC inspectors
positive findings were
as follows.
Procedures
defining
system
engineer
responsibilities
" had
been
implemented.
The
number of system
engineers
had
been
increased
to
about
29
and all but
3 were
now licensee
employees
rather than contractors.
This was adequate
to resolve
the
,MTI
concern
regarding
insufficient
system
engineers
and having too many contractors.
The licensee
had training plans set
up for the system
engineers
and
a number were currently in training.
The
systems
engineers
were actively participating in
system
problems
through
system walkdowns,
involvement
in root
cause
analyses,
arid receipt
and
review of
failure information.
Negative aspects
of the current
systems
engineering
program
implementation
noted
by the
NRC inspectors
included:
< The
relatively
short
time
the
program
had
been
operating.
The limited experience
and training of many of the
systems
engineers.
Some
had received
no turnover from the, previous
system
engineers.
Malkdowns had only been in affect for
a few months
on
many of the systems.
In reviewing system
and design engineering
involvement in a
hydraulic
lock failure of
Residual
Heat .Removal
(RHR)
System valve MOV-4-751 (documented
in Licensee
Event Report
50-251/89-04),
the
NRC inspectors
discovered
errors
on the
(c)
involved drawings,
Operating
Diagrams
5610-TE-4501
Sheet
1
and
-4510
Sheet
2.
The
4501
drawing depicted
the Unit 4
RHR hot leg suction
coming from the
Loop Chot leg whereas
it actually
comes
from
Loop
A.
The
4510
drawing
gave
incorrect flow directions
and
drawing references
from the
line
containing
valve
MOV-4-751.
These
drawings
are
utilized by Operations
personnel
and
they,had
failed to
identify or obtain correction of drawings.
The licensee's
explanation
was that Operations
personnel
were
so familiar
with the actual
locations of the involved components that
they
probably
never
referred
to
the
subject
drawing
locations.
The
drawing
errors
were
corrected
before
completion of the current inspection
and the plant manager
agreed
to perform
a further review for identification and
correction
of
any
similar
drawing
discrepancies.
The
drawing
discrepancies
identified
by
the
NRC inspectors
appear
to
be
a
violation
of
Appendix B,
'Criterion
V
requirements
to
assure
that
activities
affecting
quality
shall
be
prescribed
by .drawings.
(Violation 250,'51/89-48-01,
Drawing Discrepancies).
Failure to Correct Recurring
Equipment Deficiencies
The
NRC inspectors
determined
that the licensee
has taken
actions
to assure
recurring
equipment
deficiencies
are
properly corrected.
Primary
among
these
actions
is their
now implemented
system
engineering
program referred to in
(b)
above.
Also
the
licensee's
predictive/preventive
maintenance
program
is
utilizing reliability
centered
maintenance
concepts
to
aid
in
addressing
recurring
problems.
The licensee
was already
aware of many of their
recurring
problems
and
had
instituted modifications
to
correct
them.
Examples
examined
by
the
NRC
inspectors
included
Pump
seal
modifications to prevent
excessive
leakage
and installation of Intake Cooling Water chemical
injection
to
preclude
degradation
of
Component
Cooling
Water
Heat Exchangers.
The
NRC inspectors
verified that the licensee
had
a plan,
including
a schedule,
to generally
upgrade plant condition
and
eliminate
recurring
equipment
deficiencies.
This
upgrading
plan
was
documented
to
the
Maintenance
Superintendent
in
a
memorandum
from the
Plant
Manager
entitled
"Plant
Material
Upgrade
Program
1990"
dated
October
31,
1989.
Further,
of three
recurring
problems
10
referred
to in the
MTI, two appear
to have
been corrected
and the third largely corrected with final correction to be
complete
by the end of 1990.
Acknowledgement of Risk Significance in the Maintenance
Process
In the
MTI
an
element
of maintenance
was evaluated
that
was
entitled
"Inspect
the
Role of Probabilistic
Risk Assessment"
(PRA) in the
maintenance
process.
It was
intended
that
the
licensee's
use of
a
PRA in planning,
scheduling,
prioritizing
and performing maintenance
work be assessed
as
an element which
the
NRC considered
important to the maintenance
process.
The
MTI found that the licensee
did not use
PRA information or even
have
a
for
their
plant.
Subsequently,
the
NRC
has
acknowledged that application of other risk assessment
processes
utilized by the licensee
should
be considered
in judging their
maintenance.
In
the
current
inspection
the
NRC
inspectors
briefly examined
the overall status of Turkey Points
use of risk
assessment
in their maintenance.
They found that the licensee
has
committed to
have
a
PRA completed
and in use
by June
30,
1991.
The licensee
has
begun
using reliability assessments
that
give priority to planned
maintenance
and modifications
intended
to reduce
unplanned
days off line.
Additionally,
LCO hours are
considered.
Reliability Centered
Maintenance is beginning to be
employed.
Guidance
procedures
have
been
developed
for risk
analysis
in the design modification process.
The
inspectors
concluded
the
licensee
had
- undertaken
the
initial implementation
of
a program that would wholly address
NRC concerns
regarding their application of risk assessments
to
maintenance.
Quality Control
The examination of Quality Control
(QC) during the
MTI revealed
weaknesses
associated
with the
lack of
manpower
(i.e.,
insufficient
QC inspectors
and attendant
excessive
overtime-
estimated
at
50/,
on the
average)
and apparent
inadequate
peer
inspection
by the
maintenance
journeymen.
The insufficient
manpower
was exhibited
by craft complaints of excessive
delays
for inspection
of
QC hold points together with the fact that
available
QC inspectors
were five or- less
for all activities
other
than receipt
inspection.
The inadequate
peer
inspection
was evidenced
through observation
of less than adequate
control
of cleanliness
by the craft. during work which required opening
of the Reactor Coolant System.
was
reexamined
during
this
inspection
to
provide
an
opportunity
to
review
corrective
actions
and
a
current
assessment
of this
element.
The
inspectors
held di scussions
.
11
with cognizant
QC and craft personnel
and examined
documentation
as follows:,
IMA Commitments
(Commitments 'based
on recommendations
of
an
Independent
Management
Appraisal
that
was
conducted
between
December
1987
and March 1988)
140 - Emphasis
on QA/QC
143
Increase
of QC inspections/surveillance
Pareto
(root
cause
analysis
method)
data
package
on
field. performance
monitoring
Pareto
analysis
of recurring problems identified during
inspections/survei llances (i .e.,
root" cause
of
high
QC.
reject rates)
trend
analysis
report
from inspections/surveillances
during week of September
25 to October 1,
1989
QC trend data for month of September,
1989
trend
analysis
report
from inspections/surveillances
conducted
in the third quarter of 1989
Blanket
Purchase
Order
B89950
9000
for additional
inspectors
during outage
During examination of the above the inspectors
noted apparently
adequate
corrective actions
as follows:
Reduction of
QC overtime
from about
50% during the MTI to
37% for January
1989
and to
7% for
September
1989).
The
reduction
of
QC overtime
has
been. accomplished
through
allocation/hiring additional staff (from allocation of 6,
with
5 positions filled during
the
MTI to
a
present
allocation
of ll with
8 positions filled and
active
solicitation for
3 additional
permanent
inspectors
and
a
blanket
Purchase
Order for
3 additional
inspectors
during
.outage)
together
with more effective
use of personnel
to
increase field performance
(inspections
and surveillances)
Increased
field
inspections
and
surveillances.'or
example, total
QC activities increased
from 376 during last
quarter
of
1988 to
544
during first quarter
of
1989.
During this
same
period
surveillances
increased
by
26%
without decreasing
the necessary
inspections.
The increase
in surveillances
was partly due to increased
manning levels
but was primarily a directed
increase
in response
to the
12
analysis
of the field monitoring functions.
Discussions
.
with craft
personnel
indicated
there
were
no
longer
significant job delays resulting
from
a lack of timely (}C
inspections.
Adequate
peer
inspections.
Indirect evidence
of improved
peer
inspections
was obtained through
a detailed
review of
the licensee's
trend analysis of gC findings for the third
quarter
1989.
Indications are that these
gC activities are
conducted
very
thoroughly
and
lack
of
adequate
peer
inspection
was not evident for the discrepancies
identified
during
gC inspection activities.
The
inspectors
concluded
that
corrective
actions
have
been
sufficient to resolve
MTI concerns
regarding
gC at Turkey Point
Nuclear
Plant
(TPN).
Emphasis
on
gA/gC
has
been
further
fostered
by plant management
in response
to IMA commitments
140
and
143.
(5)
Safety
Review of Maintenance Activities (Personnel
Safety)
The MTI judged the licensee's
implementing actions to insure the
safety of maintenance
personnel
to be poor.
Their judgement
was
based
on the following perceived
weaknesses:
'I
(a)
Inadequate
attention
to fire hazards
as
observed
by team
members
in the welding
shop
(b)
Poor
safety practices
with regard
to the
use of air tools
and safety belts
as
observed
in the team's
tours of 'the
plant
(c)
Above aver'age
Industrial Safety Lost Time Accident Rate
(d)
The
licensee
did not determine their Lost Time Accident
Rate for Personnel
Involved in Maintenance
for comparison
with industry averages.
The
NRC inspectors
toured
the plant
and
observed
maintenance
activities in the current inspection
on at least, five occasions.
No evidence
of poor safety practices like those referred to in
(a)
and (b) were observed.
These
tours
included
two visits to
weld shops.
The inspectors
reviewed the
TPN Industrial Safety
Lost
Time Accident
Rate
and
found that
the
running
average
showed
no lost time accidents
since April 1988.
With regard to
TPN's failure to determine their "Lost Time Accident
Rate for
Personnel
Involved in Maintenance,"
as referred to in (d), the
licensee
responded
that thi s data
was
no longer being
used
by
the industry
as of the
end of 1988.
The licensee
had
several
13
personnel
safety
performance
indicators
they
were
tracking
closely - e.g.,
lost
time injuries
were
being
tracked
by
department.
Licensee
personnel
reported
that
beginning April
1989
root
cause
of injuries
was
being
analyzed
by the site
safety
organization
using
a
Corporate
accident
investigation
process.
The
NRC
inspectors
verified
the
manual
for this
process.
The inspector
s also
found that specific
supervisors
has
been
made individually accountable
for important aspects
of
personnel
safety.
The
NRC inspectors
did
see
a
few minor infractions of safety
rules while on their tours,
such
as
an instance
of not wearing
a
hard hat where requi red (the conditions in the area did not make
this
a significant hazard)."
However,
the inspectors
generally
concluded that their previous concerns with regard to personnel
safety practices
appeared
to have
been resolved.
Preventive/Predictive
Maintenance
An
examination
of preventive/predictive
maintenance
was
not
completed
in sufficient depth during the
MTI for inclusion of
this
function
in
the 'xamination
of
engineering
support.
Therefore,
preventive/predictive
maintenance
was
thoroughly
examined
during
this
inspection
to
provide
separate
and
additional
data
in reassessing
this element.
Preventive/predictive
maintenance
at
TPN is the responsibility
of
the
Planned
Maintenance
Group
(PMG).
PMG historically
provided
predictiVe
maintenance
(vibration
monitoring,
oil
analysis
and
on
most
plant equipment.
now
also
supplies
maintenance
support
in
areas
of root
cause
analysis
to prevent failure recurrence
on major plant equipment;
i.e.,
reduction
of plant
LCO
hours,
together
with
use
of
Reliability Centered
Maintenance
(RCM) techniques
to identify
preventive maintenance
requirements
on selected
plant equipment;
i.e.,
reduce
unplanned
days off line.
The
inspectors
examined
procedures,
had
discussions
with
cognizant
licensee
personnel,
and
exami'ned
documentation
to
assess
whether predictive/preventive
maintenance
appeared
to be
adequately
controlled
and
implemented.
Procedures
and
documentation
examined were's
follows:
Procedures
0"ADM-705
0-ADM"706
Planned
Maintenance
Program
Predictive Maintenance
Program
14
0-ADM-710
Processing,
Schedul ing,
and
Upgrading
Preventive
Maintenance
Documents
0-ADM-711
0-ADM-712
0-ADN-716
Vibration monitoring
Lubricating Oil Sample
Processing
Infrared Thermography
Documentation
Logic Flowchart
on Root Cause
Analyses
by
Logic Flowchart
on Reliability Centered
Maintenance
Process
Pareto
analyses
package
to
improve
equipment
reliability thru
RCM Techniques
(Copes-Vulcan valves)
Quality Investigation
Story (QIS) data
package
on
3B
Steam
Generator
Pump
Operational
Problems
(combination
of
vibration/lubrication
problems
requiring
complex
analyses
and
PC/M modifications to
resolve)
QIS data
on
attempt
to
increase
Mean
Time
Between
Failure
( single
point failures)
by identification/
criticality ranking of TPH critical components
Examples
of
Interdictions
to correct
discrepant
equipment conditions
(1)
excessive
thermal
aging of 13 reactor protection
relays (Units
3
8 4)
(2)
thermal
anomalies
on
the
U3
main
power
transformer
due to failed cooling oil circulating
pump.
(3)
ineffective cooling coil of normal
containment
coolers
in Unit 4.
Examples
of
vibration
analyses
which
allowed
corrective actions to prevent catastrophic
failures
(1)
damage
to
impeller,
seal
end
bearings
on
Condensate'ump
2A
(2)
defective top motor bearing
on Condensate
Pump
3A
15
(3)
damaged
roller
thrust
bearing
on
Auxiliary
Pump
A turbine
(4)
defective
inboard
bearing
on
Component
Cooling
Mater
Pump
3A
After examination of the above the inspectors
concluded that the
items
reviewed
indicated
a
strong
and
well
implemented
predictive/preventive
maintenance
program.
However,
the
inspectors
expressed
some
concerns
regarding
the
need
for
a
formal requirement
in 0-AON-711 that the
PNG vibration analysis
program properly inform inservice testing
program
personnel
on
evidence
of vibration in the alert
ranges
on- ASME components.
The inspectors
also
noted
need
for further details
regarding
specifics
on
oil
sample
analyses
to
be
conducted
under
0-ADM-712.
Cognizant
licensee
personnel
agreed
and
provided
acceptable
revisions
of
0-ADM-711
and
0-ADM-712 for
the
inspectors'eview
prior to the
end of this inspection.
(7)
Integrate
Regulatory
Requirements
During
an
MTI examination related to the integration of changes
to regulatory documents
into the maintenance
program,
there
was
a
concern
identified
regarding
inadequate
plant/corporate
communication
associated
with Generic Letter 88-14
on instrument
air systems.
The
inspectors
examined
procedures,
held
discussions
with
cognizant
licensee
personnel,
and
examined
documentation
to
assess
whether
changes
to regulatory
documents
appeared
to
be
properly integrated
into the maintenance
program.
Licensee
Res
onses
to IE Bulletins
Response
No.
Issued
Comments
88-04
6/16/89
Potential
safety-related
pump
Loss
due
to
miniflow design conditions.
The licensee's
response
was completed after
receipt of pertinent, vendor design data
and
covers the question of hydraulic instability
(need
for adequate
miniflow capacity)
and
potential
for deadheading
for the
Safety
Injection,
RHR, Containment
Spray, Auxiliary
(AFM)
and
Boric
Acid Transfer
(BATF)
pumps'iniflow
capacity
was
adequate
for all,pumps
and,
under worst case
conditions,
only the
BATF pumps
have
a
16
Licensee
Res
onses
to IE Bulletins (cont'd)
Response
No.
Issued
Comments
potential for deadheading.
This possibility
has
been
precluded
through
corrections
to
operating
procedures.
88-08
5/4/89
Thermal
stresses
in piping connected
to the
Reactor
Coolant
System
(RCS)
which
could
lead to unisolable leaks..
The licensee
identified potential locations
and committed to additional
NDE examinations
for welds in portions of the charging
pump
.
to pressurizer
auxiliary
spray
line,
and
charging
pump for "C" hotleg.
88-11
5/31/89
Pressurizer
Surge
Line Thermal Stratifica-
tion
which
could
damage
surge
line
integrity.
The
licensee's
response
noted
their
participation
in
the
owners
group's
program
to
perform
a
generic
evaluation
of
this
issue
and
present
justification for continued
operation until
completion of all plant specific actions
by
January
1991.
89-1
.
6/19/89
Failure
of
steam
generator
mechanical
plugs
due to potential
inadequate
heat treatment.
The
licensee's
response
verifies that
six
plugs
from heat
4523 are installed
in the
Unit 3
"C"
steam
generator
and
two plugs
from heat
4523 are installed in the Unit 4
"A"
steam
generator.
The
plugs will be
replaced
during the next refueling outage.
Licensee
Res
onses
to
NRC Generic Letters
Response
Issued
Item
3/10/89
Instrument
Air
Supply
Systems
Probl ems
Affecting Safety-Related
Equipment
17
Licensee
Res
onses
to
NRC Generic Letters (cont'd)
No.
Response
Issued
Item
A weakness
regarding
lack of communication
between
plant
and
corporate
personnel
associated
with
was
identified
during the MTI.
Therefore,
licensee
actions
in
response
to
GLSS-14
were
examined
in
considerable
additional detail'uring this
inspection.
The results
are reported
below:
The
inspectors
did not identify any other
examples
of apparent
lack of communication
between plant and corporate
personnel
during
this
inspection
except
as
noted
below
relative to work order DI-3304.
Additional
documentation
associated
with
examined
during
this
inspection
included
plant
procedures
and
drawings,
plant
work
orders,
test
results,
audit
reports
and correspondence.
During the examination,
the inspectors
noted
the following:
Another
example
apparent
lack
of
internal
communication in that internal
correspondence
regarding
completion of
work
associated
with
DI-3304
was
inaccurate
in that the required
design
basis
verification
testing
was
not
completed for all valves listed
on the
work order.
Flow Control Valves (FCVs) and Pressure
Control
Valves
(PCVs)
not tested
are
listed below:
FCV"""113A
FCV""-113B
FCV-"-114B
PCV-"-605
PCV-*-455A
PCV"*"455B
to Blender
Borated water
to Change
Pump
Diluted flow
to VCT
RHR Ht. Exchanger
Bypass
PZR spray
PZR spray
FC
FC
FC
FC
FC
18
Licensee
Res
onses
to
NRC Generic Letters (cont'd)
Response
Issued
Item
Cognizant
licensee
personnel
informed
the inspectors that licensee identifica-
tion of the lack of testing
noted
above
would
have
occurred
during
their
independent
gA verification of actions
in
response
to
NRC commitments,
which
is required prior to the submittal of a
final response
on GL88-14 to
NRC.
valves
without
filter
regulators
and filter-regulators not in
PM program.
The
inspectors
noted that
some
valves
(containment
purge valves
and main feed
check
valves)
were
not
protected
by
individual
filter
regulators.
Cognizant
licensee
personnel
responded
that final evaluation
of air quality
limits was not complete,
but that tests
completed
together
with
preliminary
.vendor information did not indicate
any
immediate operability problems.
The inspectors
were
informed that
some
filter regulators
were
not presently
included
in
. the
program
pending
evaluation
of air quality tests
and
receipt
of
vendor
information
to
establish
the
most
efficient
frequency.
Lack of tests
to validate Unit 4 Main
Steam
Isolation
Valve
(MSIV)
size at 85 psig minimum
During review of the design
bases
for
Unit 4
the
inspectors
noted
differences
between
valves
stated
in
PC/M
No.88-245 for
Unit 4
(80 scfh
at
85
psig)
versus
those
stated
on
PC/M No.85-135
for Unit 3
backup
of
100 scfh at
100 psig).
The inspectors
requested
additional
verification
of
Unit 4 sizing data
since Plant
Change
19
Licensee
Res
onses
to
NRC Generic Letters (cont'd)
No.
Response
Issued
Item
GL89-4
10/3/89
Modification (PC/M) No.88-245 inferred
that
80 scfh
and
85 psig
were
design
limits.
The
inspectors'eview
of
calculation MIZ-165-02 revealed that
an
design
pressure
of 100 psig
was
used
in the design.
However,
the
calculation anticipates
a minimum of 85
psig to assure
MSIV closure within'ive
seconds.
The inspectors'further
noted
that this anticipated
minimum pressure
was
not verified during completion of
preoperational
testing
(procedure
0800.213)
since
those
tests
were
conducted
at
normal
system
pressure
(100
psig)
rather
than
85
psig
~
Cognizant
licensee
personnel
provided
correspondence
verifying
and
Bechtel
Power
Corporation
(BPC)
agreement
that calculation
MIZ-169-02
will be revised
and reviewed to assure
that
any additional
necessary
testing
is completed.
Guidance
of Developing Acceptable Inservice
Testing.
GL89-4
provided
the
latest
guidance
on
NRC positions
associated
with
relief requests
from
ASME Section
XI
Code
Requirements
on the inservice
testing
(IST)
of
pumps
and
valves.
The
licensee's
response
notes that conformance
with GL89-4
will require revision of nearly all present
TPN IST surveillance
procedures.
Therefore,
full conformance will not be obtained until
tests
performed after July 1,
1990.
Safety
Related
Motor Operated
Valve Testing
and Surveillance.
expands
the
scope
of
licensee
programs
for
MOV testing
and
surveillance
which
was originally required
by
to
now
include
all
safety-related
and
position-changeable
MOVs.
the
inspectors
examined details associated
with MOVs to
20
.
Item
Licensee
Res
onses to
NRC Generic Letters (cont'd)
Response
No.
Issued
assess
whether
management
had
expanded its
concern
to addressing
MOV problems.
The
FPL response
to GL89-10 was not required
prior
to this
inspection.
However,
the
inspectors
examined
the
latest
informal
draft together with supporting documentation.
The inspectors
found that the
licensee
had
anticipated
and
completed
several
actions
associated
with
prior.
to
its
issuance.
Cognizant
licensee
personnel
noted
that
considerable
costs
have
been
associated
with
work
completed
to
date.
Further, that strong
FPL management
support
has
been
.provided
in
completing
those
activities.
The
expanded
testing
program at
TPN includes:
1)
development
of a design basis including
the manufactured
stem thrust value for
each valve
2)
verification of switch settings
3)
administrative
control
of
switch
setting
by an engineering
drawing
4)
performance
of
delta-P
testing
for
valves which will not place the unit in
an
LCO or unreviewed
safety
question
concern
5)
and
MOV user group recommendations,
data
bases
and
trending
information
will be incorporated
as applicable.
The
inspectors
noted
.that
had
required
revision
or generation
of sixteen
procedures,
expansion
of
the
program
by
nearly
400
percent,
and
considerable
additional
costs;
i.e.,
56
man-rem
and.
96
man-hours
for each first
round test
per
MOV,
7
personnel
per test
(technicians,
engineers,
'HP), etc.
The
21
Licensee
Res
onses
to
NRC Generic Letters (cont'd)
Response
Issued
Item
inspectors
concluded that management
concern
and support, for
MOV testing
was sufficient
to resolve
any
NRC concern.
The
inspectors
further
concluded
that
licensee
actions associated
with integration
of regulatory documents
were above average.
d.
Work Control
In the
MTI, three
elements
of Work Control contributed to
a poor
rating.
These
were
implementation
of work order
control,
job
planning
and ma.intenance
procedures.
In the current inspection
these
were
reexamined
to determine
whether
the
licensee
had
undertaken'ctions
to obtain
improvements
and whether the actions
were effective.
The
inspectors
reviewed
licensee
actions
relative
to work order
control
and job planning together
and examined
maintenance
procedures
as
a separate
topic.
Work scheduling,
which was not rated in the MTI
was examined together with work control
and job planning.
C
Also
examined
separately
were
the work controls
on maintenance
in
'rogress
and
post
maintenance
testing.
Neither of these
had
been
rated in the MTI.
The inspectors
conducted
thei-r examination of these
elements
through
interviews with planners,
scheduling
and craft personnel;
through
observation
of the
development/preparation
of
a Plant
Work Order
(PWO)
and of
use
of the
involved data
bases;
through
review of
completed
PWOs
and
Plan of the
Day (PODs);
and through attending
a
POD morning meeting.
Findings are described
below:
(1)
Work Order Control, Job Planning
and Scheduling
The significant
concerns/weaknesses
described
in MTI findings
and the
NRC inspectors
current
inspection
findings relative to
each
are
as follows:
ff
accessing
the job planning
system
data
bases
to identify
whether
a job was
rework,
was
becoming
a trend or if the
job
had
been
performed
previously
under
a different
classification.
The
NRC inspectors
perceived that this was
at
least
partially
due
to
inadequate
or
insufficient
.training.
22
Current ins ection findin
s
The licensee
analyzed
these
concerns
and responded
to them with actions which included
development
of
a checklist
to
aid
in
planning
PWOs;
modification of the planning
system
to permit identifica-
tion
of
multiple
component
failures
under
one
PWO
(previously only one
was identified to the
PWO
and
thus
other s corrected
could not
be readily called-up
from the
computerized
work history
system);
modification
of the
system to permit
a search for "root-cause
component"
in the
data
base;
advising
planners
of their responsibilities
to
identify
rework
and
directing
them
to
submit
PWOs
identified as rework to the maintenance
engineers
for root
cause
analy'ses;
conducting additional
planner training and
developing
a
planner
training
course;
hiring additional
planners;
and issuing
a revised planning
system
manual for
reference.
From their review of these
licensee
a'ctions,
observations
of
planning
reviews
of
PWOs
and
from interviews,
the
inspectors
determined
that
the
licensee's
actions
had
resulted
in
improvement.
Some
minor
concerns
were
identified,
however.
First,
the
licensee
had lost several
of the
maintenance
engineers
who
performed
root cause
analyses. of recurring
equipment
failures.
(They
were
attempting
to
hire
replacements.)
Second,
the
equipment
history
records
entered
in the past
lack details
and
easy
accessibility
.
(The
inspectors
were
informed that
only
1988
and
1989
records
were readily accessible
in the data
base - though
entries
back
to
1986 could
be obtained,
access
now took
longer
and they were generally
not, checked.)
not
be
readily
ascertained,
making it difficult to
accurately
assess
the maintenance
backlog.
Current ins ection findin
s
Licensee
personnel
reported
that
a daily
summary
report
had
been
developed
which
provided
accurate
information
on
backlog
to
planning
supervisors.
Based
on
the inspectors
review of licensee
backlog
information
and
discussions
with
scheduling
personnel
the inspectors
found no further
cause for concern
regarding this matter.
N~ii
E
inaccurate
and the
causes
of these
discrepancies
were not
being recognized
or corrected.
In particular,
bottlenecks
caused
by
some
of the
smallest
organizations
were
not
acknowledged.
23
Current ins ection findin s - The inspectors
examined
the
1989 estimated
versus
actual
man-hours
for the Electrical
and
18C .Maintenance
Departments.
The estimated
hours
were
ll'nd .18%
low,
respectively.
They
judged
the
18%
difference to be excessive,
but not of great concern
as the
numbe'r
or trend of open
maintenance
PWOs did not appear
excessive.
The
inspectors
were
informed there- had
been
significant .improvements
in
estimates
between
1988
and
1989.
Craft
personnel
and
planners
interviewed
by
the
inspectors
attributed
the. improvement
to
improved
parts
availability,
improved
support,
and
(especially)
reduction of waiting time for clearances.
One craft person
also noted better
supervision
as
a reason.
The principal
negative
factor
indicated
was still parts availability
(though
greatly
improv'ed).
Other
negative
factors
mentioned
included
insufficient
supervisors,
increased
paperwork
and getting
clearances
lifted.
The
inspectors
found
that
PWO
forms
and
the
associated
procedure
(0-ADM-701) required
discrepancies
between
estimated
and
actual
man-hours
to be explained
when they differed by more
than
20% but that,
based
on their review of PWOs, this was
not
being
done.
This
appears
to
have
only
minor
'ignificance
as
a
safety
issue
but is certainly
not
in
agreement with,the plant manager's
expressed
intent which
is to have "verbatim compliance" with procedures.
(d)
~TI
i
i -"P0
"(GO)ii bh
licensee
to indicate
important daily work activities did
not provide
information
needed
to fully understand
the
schedule
priorities
and
the
problems
that
had
to
be
resolved= to accomplish
the schedule.
Current ins ection findin
s - The inspectors
attended
one
licensee
morning
meeting
in
which
the
items
were
reviewed
by
management
personnel.
Also,
the
inspectors
examined
several
PODs during their inspection.
They found
the
POD greatly
improved.
It appeared
to communicate all
of the
more
important information
needed
for managers
and
supervisors
to
understand
the
status
of
plant
work
priorities
and
important
problems requiring attention
and
resolution.
Of particular significance
were
items
added,
such
as
a
three
day 'schedule
of
'maintenance
work,
procurement
status,
control
room
green
tag
(deficiency)
status-report
and contaminated floor space
status.
(e) ~li
i
-A
k
1
k
,.the
planning
procedure
(0-ADM-701)
contributed
to
a
planners
erroneous
closure of an instrument deficiency.
In
starting to plan correction of the deficiency the planner
went to observe
the
instrument.
He
examined
the
wrong
instrument
(whose identification
was missing)
and fai ling
to observe
any deficiency
he coded or closed out the
PWO as
"finished."
Had
he
cancelled
the
work order
as
being
invalid the originator of the
PWO would have
been contacted
to verify the
absence
of the deficiency
and the error in
checking
the
wrong
instrument
would likely
have
been
recognized.
This matter
was identified
as
part of
NRC
violation 250,251/88-32-02,
Procedural
Related Deficiencies.
In
a written response
to this violation included in a May
1989 letter
to the
NRC,
the
licensee
stated
that their
corrective
steps
included instructing planning supervisors
'hat
PWOs'ere
not to
be
closed
out if no
work
was
performed
but
were
to
be
processed
for cancellation
and
that 0-ADM-701 had
been revi sed to reflect this.
Cu'rrent ins ection findin s
Through
interviews
with
planning
personnel
and
review
of
O-ADM-701,
the
NRC
inspectors verified the stated corrective actions.
W
J
W
d
being completely
entered
in the computerized
work history
data
base,
though this
was
required
by procedure.
Data
entry technicians
without any related training
or
formal
guidance
were
determining
what
information
would
be
entered.'his
matter
was cited
as part of the violation
referred to in (e) above.
In the
same
response
referred to
in (e) the licensee
stated that their'orrective
action was
to revise the
PWO procedure
(0-ADM-701) to state
that the
relevant
Journeyman's
Work Report data would be entered
by
a designated
data technician.
Current ins ection findin s
The inspectors
found that the
procedure
revision
had
been
made
as
stated.
Planners
stated
that the data entry clerks
had
been
instructed
to
enter either the
complete
Journeyman
Work Report data or
the
relevant
data.
Also,
they
were
to
consult
with
planning
personnel if there
was
any question
of what to
enter.
A check of entries
in the computer data
base for a
sample
of about
10
1989
PWOs
found the data
entry clerks
were
entering
relevant
data
from the
Journeyman's
Work
Reports.
However,
the
inspectors
noted
another
concern.
Of 12 completed corrective maintenance
(trouble
and break-
down)
PWOs
reviewed,
cause
did
not
appear
adequately
addressed
on nine (e.g.,
on
WA 89102200738,
89103020073
and
891025090638).
Also,
in
one
instance
35
PWO steps
were
used
to
prescribe
the
work
to
be
performed
(on
WA
891025090638).
It appeared
to the
inspectors
that
such
extensive
prescription of work should
have
been
specified
through
an approved
procedure.
The
PWO procedure
(0-ADM-701) requires
an entry of a best
estimate
of the
root
cause
of the
problem
found.
The
25
procedure
also
provides
examples
of cause
entries.
These
examples
did not appear
to
be actual
root causes
and the
inspectors
considered
that they represented
an
inadequacy
in the procedure.
The inspectors
found that the licensee's
work order control
and job planning
had been
improved significantly since the
MTI.
The
number of planners
had increased,
the planners
had additional
experience
with the system,
checklists
were
being
used
to
assure
correct
PWO data
entries,
further
improvements
had
been
made to the planning
systems,
parts
availability
and information
had
improved
and
communica-
tions
were better.
Also,
the
licensee
appeared
to have
taken
the
necessary
actions
to assure
proper
scheduling.
Additional
improvements
were
seen
as
being
needed
in
-identifying
and
recording
(on
PWOs)
the
root
cause
of
equipment failures whose significance level
was insufficient
to trigger
a
formal
analysis.
The work order
procedure
(0-ADM-701)
gave
inadequate
guidance
on
root
cause
identification.
The loss of several
maintenance
engineers
was also of concern.
(2)
Maintenance
in Progress
Several
examples of maintenance
in-progress
were observed
by the
inspectors
(e.g.
Unit
3
Charging
Pump
C fluid drive repair,
Unit 4
intake
Cooling
Water
Pump
C
inspection
and
stud
replacement
for
same
pump).
The maintenance
observed
appeared
to
be properly performed
in accordance
with the
PWO specified
requirements.
Work appeared
well organized,
properly controlled
and calibrated
tools were
employed (e.g.,
dial indicators for
Charging
pump
alignment),
and cleanliness
was maintained.
No
matters of concern
were noted.
(3)
Post Maintenance
Testing
The inspectors
examined
the licensee's
procedural
requirements
for post maintenance
testing
and the records of post maintenance
tests
performed
on
12
PWO examples
(those
referred to in (1)
above).
The inspectors
found that the
programmatic
procedure,
AP-0190.28
was thorough
and technically adequate
but that it was
somewhat
complex to use
and could be improved by rewrite to the
Procedure
Upgrade
Program style.
Each of the
PWOs
reviewed
by
the
inspectors
was
found to
have
performed
the
proper
post
maintenance
tests.
(4)
Maintenance
Procedures
Weaknesses
were
identified
during
the
MTI associated
with
procedures.
These
included
inadequate
procedures (for example,
O-PMM-022.3 which apparently resulted
from an inadequate
review/
26
validation process),
and
a lack of procedures (for example,
on
motor maintenance,
testing
molded-case
circuit breakers
and
sampl ing plant
breathing
air ),
and
a
lack of conformance
to
procedures
(for example,
0-ADM-701
on canceling
[coding out]
work orders,
required receipt
inspections
for ASME code parts,
and maintenance
of QA records
fQP 13. 1. 17..1
and O-HPA-003]).
Violations associated
with the
above
included 250,251/88-32-02
through
04.
The licensee's
response
to the
MTI violations was transmitted to
Region II nn May 4,
1989.
The inspectors
completed verification
of actions
reported
in the licensee's
response
together with
review of actions to correct other
weaknesses
identified in the
MTI report.
Regarding
the testing/validation
process,
enhanced
controls
pertaining to actual-use
validation for new procedures
were
incorporated
in the latest revision of 0-ADM-100.
Each
new
maintenance
procedure
must
be clearly marked
to indicate
"
that it has
not
been first-use validated
and
an attached
validation feedback
form (attachment
7 of ADM-100) must
be
completed
by
the
craft
performing first
use
of the
procedure.
The form, provides for comments relative to any
problems
as well as
suggested
solutions.
Improved
checklists
for
new
and
revised
procedures
to
ensure
adequate
procedure
evaluation
by originators
ahd
technical
reviewers
are
now
included
in
0-ADM-100
(attachments
3,
4 and 5).
Training
has
been
provided to procedure writers
on the
use
of these- checklists
as well
as
general
principals of good
procedure writing.
A
new
departmental
instruction
(TDI-PUP-001)
has
been
issued
which requires
a review of plant changes
by both an
operations
and
a maintenance
procedures writer.
Maintenance
management
has
encouraged
craftsmen
to provide
feedback
on procedure
problems.
0
Procedure
0-PMM-022 '
Deficiencies
in
O-PMM-022.3
were
the first part
of
violation 250,251/88-32-02.-
The procedure
was
revised to
delete
the
requirements
for
chromate
water
and
major
modifications.
Also,
the
licensee
identified
the
root
cause
of the earlier deficiency
as failure to ensure that
plant
changes
and
modifications
(AP-0190. 15)
were
also
reviewed
and
coordinated
with the
procedures
they might
27
affect.
Figure J of AP-0190. 15'(System
Acceptance
Turnover
Sheet)
was
revised
to
ensure
that all
procedures
not
required
for acceptance/turnover
but
requi ring revisions
due to the modifications involved also
be listed.
The
inspectors
concurred
with the
licensee
corrective
actions
and this part of violation
250,251/82-32-02
is
'onsidered
closed.
Testing molded-case circuit breakers
Maintenance
instruction
MI-E-023. 1
has
been
developed
for
periodic
inspection
and
testing
of
molded-case
circuit
breakers.
The licensee
plans to,test
10 of molded-case
circuit breakers
associated
with Appendix
R for protecting
safe-shutdown
capabilities
during
the
forthcoming
Unit 3
outage.
The
remaining
breakers
will
be
tested
in
subsequent
outages.
Similar testing will be conducted for
Unit 4 commencing
the next Unit 4
outage'ailure
to have procedures
to test breathing air quality
This
deficiency
was
the
second
part
of
violation
250,251/88-32-02.
The
licensee
issued
procedure
0-SMM-101. 1,
Grade
D Breathing Air Periodic
Testing,
and
completed initial sampling
and testing
of breathing
air
quality prior to this inspection.'The
inspectors
reviewed
the test results
and
noted that
Grade
D or better quality
breathing air was verified.
However,
the inspectors
noted
deficiencies with 0-SMM-101. 1 as issued.
The
licensee
initiated
actions
to
adequately
revise
0-SMM-101. 1
during
and
immediately
subsequent
to this
inspection.
This item is considered
closed.
Lack of procedural
requirements
for periodic retraining of
contract
HP personnel
This
deficiency
was
the
third
part
of
violation
250,251/88-32-02.
The licensee
issued
on March 8,
1989,
a
corporate
recommended
practice
(RP:
HP-001)
providing
guidelines for training and qualification of ANSI contract
technicians.
Procedure
O-ADM-360,
Health
Physics
'epartment
Personnel,
Training
and gualifications,'as
revised
to include contract
HP technician
training
and
certification requirements
(Sections
5.2 and 5.3).
The
inspectors
concurred
with the
licensee's
corrective
actions.
This item is considered
closed.
28
e
Lack of conformance with existing procedures
There
were
two
examples
of these
types
of deficiencies
associated
with violations.
The first deficiency
was
the
lack of conformance
with
0-AOM-701 in improperly
concealing
(coding-out)
a
work
order 'when
no work was done.
This item was the final part
of violation
250,251/88-32-02.
The
second
example
was
inadequate
receipt inspections
(RIRs R87-7772
and
RGG-3842)
for cleanliness
inspection
of ASME Code
Parts.
This was
considered
violation
250,251/88-32-03.
The
licensee's
corrective
actions
for
the
former
were
examined
and
determined
satisfactory
by the inspectors
as
described
in
. paragraph
2.d( 1)(f) above.
Regarding
the latter,
licensee
corrections
included
revision
of plant Quality Control
Department
Instruction
7. 1
and, technique
sheet
7. 1
to
referen'ce
ANSI 1145.2.2-1972
as
the
receipt
inspector's
cleanliness
standard
when
no specific criteria is available
.or indicated in the inspection
plan.
Additionally, the
use
of sampling
was prohibited
as
an inspection
technique
on
'SME
parts,
10 CFR 21 orders,
or
EQ parts.
The
inspectors
agreed
that these
corrective
actions
were
sufficient
to
, resolve
NRC
concern.
Violation
250,251/88-32-03
is considered
closed.
Failure to maintain temperature
and humidity daily records
for the Class
B storage
warehouse
as
QA records
This item was the first part of violation 250,251/88-32-04
and
demonstrated
a
lack of conformance
to corporate
procedures
QP 13. 1 and
17. 1.
The
licensee
had
maintained
these
records
but,
due to
mi sinterpretation
of the corporate
QA manual,
they- were not
being
maintained
as'A
records.
Corrective
actions
included revision of the nuclear stores
QA records list to
include Class
B warehouse
temperature
and humidity records
as
QA records
and the transfer of all historical
records to
the
QA records
storage facility.
The inspectors verified the transfer of 1989 records to QA
storage
and
agreed that corrective actions
were sufficient
to
resolve
any
NRC
concern.
This
item is
considered
closed.
Failure to maintain qualification records for contract
personnel
in an approved cabinet
29
This item was
the last part 'of violation 250,251/88-32-04
and
demonstrated
a
lack of
conformance
with
procedure
O-HPA-003.
Licensee
corrective
actions
included
transfer
of the
records
identified during the
MTI to approved
storage
and
revision of 0-ADM-360 to clarify record
keeping
require-
ments (Sections
2.2 and 5.7).
The
inspectors
reviewed
corrections
to
0-ADM-360
and
verified the transfer
to plant
QA record
storage
of the
certification records
for contract
HP personnel
which were
not properly stored during the MTI.
Violation 250,251/88-32-04
is considered
closed.
After examination
.of all
elements
listed
above,
the
inspectors
concluded
that
considerable
improvements
had
been
made
by
the
licensee
in
the
area
of
maintenance
procedures.
Maintenance
procedures
of TPN are presently
considered
above
average.
Materials Control
Materials
control
weaknesses
identified during
the
MTI were all
associated
with spare
parts.
Problems
of obtaining
and maintaining
adequate
inventories
of
spare
parts
caused
attendant
delays
in
completing
scheduled
work.
The
inspectors
completed
a
reexamination
of the
issues
associated
with spare
parts during this inspection.
The reexamination
included
discussions
with cognizant
licensee
personnel
and
examination
of
documentation
regarding
licensee corrective actions.
The
lic'ensee
completed
several
actions
intended
to
improve
communications
as well as coordination.
Four
maintenance
personnel
were
reassigned
in January
1989
to
identify parts
needed for the next Unit 3 refueling outage
(February
1990)
and initiate requisitions
to obtain
the
necessary
parts.
By
this
inspection,
80% of the
10,000 line items
had
been
tagged
as
material
committed
to the
Unit 3 outage.
The
remaining
20K were
being
evaluated
against
the
outage
final work
scope
to expedite
delivery of the required parts.
A
TPN Quality
Improvement
Program
(QIP)
team
was
assembled
on
April 13,
1989,
to improve the current situation
and track results.
This QIP team includes
members
from engineering,
stores,
purchasing,
QC, maintenance
and construction.
30
Beginning June
1989,
the parts
team leader
began holding twice daily
'eetings
with other
discipline
coordinators
to
address
real
time
parts issues.
Parts
issues
are
now included during daily Plan of the
Day (POD)
meetings
to
ensure'dequate
communication
and
necessary
decisions
by
upper
plant
management.
Licensee
corrective
actions
have
resulted
in cancellation
of
1, 185
obsolete
line
items
in 1989.
An additional
193 line items are in process
of
deletion.
Untraceable
inventory
and
surplus
- material
existed
and
was
identified by PC/M number
and
PO number rather than the uniform
stores
catalogue
numbering
system.
One thousand
three
such line
items
were identified
and
are
in process
of being disposed
or
included
in stores
inventory.
The continued
use of
PC/M type
numbering
systems
has
been disallowed.-
Inadequate
procedural
controls to ensure
systematic
update
on
repeat violation of minimum inventory requirements
The
TPN gIP team also identified examples
of zero parts
on hand
as
a
problem.
One
countermeasure
was to review stores
parts
inventory for line items purchased
more than
once per year.
Other resources
allocated to resolve parts
problems included:
The
maintenance
personnel
expediting
Unit 3
refuel
parts
previously- listed.
Reassigned
stores
personnel
to
expedite
the
Unit 3
refuel
committed materials
tagging.
Supplements'o
engineering
staff to reduce
procurement
backlog
and
issue
PDRT guidelines
(From April 1989 to September
1989,
engineering
procurement
backlog,
went from 740 to 225 items.
The
goal is
a one-month working backlog of around
200 items
and was
- reached
in November 1989).
Engineering
is
reviewing
the
present
44 generic
procurement
evaluations
to ensure
agreement with the
new
PDRT guidelines.
Purchasing
has
obtained
blanket
POs
from
for
guality Level-l,
2
and
3 items.
Delay times
have
been
reduced
from 42 days to zero for requisition to purchase
order issuance
on these
items.
Number of stores
line items
below minimum dropped
from 5, 154
items in May 1989 to 4,509 in September
1989.
POs are
issued
on
2,001 of the 4,509 items.
31
The
number
of
PWOs
awaiting parts
dropped
from over
300
in
Oecember
1988 to
a low of 176 in October
1989.
The proportion of procurement
requests
for items
needed
on
an
urgent basis
has dropped
from a peak of 44M in March 1989 to 25';
in
September
1989
due
to the availability of more
parts
in
stores.
Average
time
from issuance
of parts
to
issuance
of purchase
orders
has
decreased
from 111.5
days
as, of March 1,
1989,
to
79. 1 days
as of, October
1,
1989.
The present
goal is an average
procurement
time of 60 days.
I
The inspectors
concluded that licensee
corrective actions associated
with'pare parts
have
been effective in eliminating or minimizing the
majority of the weaknesses
previously identified.
f.
Personnel
Control
The weaknesses
of concern
in the
MTI included
the lack of regular
personnel
performance
appraisals,
a
high
maintenance
personnel
turnover rate,
high overtime rates,
and excessive
use
of contract
personnel.
Based
on discussions
with maintenance
craft
and
foremen
the
NRC
inspectors
determined
that performance
appraisals
had
now generally
been brought up-to-date.
The
personnel.
turnover
rate still
appeared
high.
The
licensee
reported
the following maintenance
turnover rates:
mechanical
- 20;;,
el ectri cal
-
10'<,
and
Instrumentation
and
Contr ol
(1&C)
24%.
Overall, these
appeared
a little worse than reported in the MTI.
The
licensee
noted that for the mechanical craft over half the turnover
was the result of entry level personnel,
most of whom moved to other
plant positions.
They also stated that about half the
14C losses
had
been
to
Nuclear
Operator
training
and
that
new
experience
and
education
requirements
would preclude
that
movement
in the future.
To assure
sufficient IEC personnel
there
had been
an overhii e of 10.
The
inspectors
talked
to
about
eight craft (all either
IKC or
Mechanical
Maintenance)
and
found that
morale
appeared
reasonably
good.
Several
noted that overtime
had
been
reduced.
Licensee
data
showed
overtime rates
which still appeared
high to the inspectors.
There did appear
to
be
some
improvement,
but it was difficult to
evaluate
because
of outage affects earlier this year.
With
regard
to
use
of contract
personnel
the
MTI specifically
criticized the
use of excessive
contractors
for engineering
support
functions,
such
as
system engineers,
and for health physics
support.
As noted in 2.a.
above,
the
licensee
has
eliminated
most of the
system
engineering
contractors.
Discussions
between
the
NRC
32
inspectoi
s
and
HP personnel
in'dicated that
HP contractors
were being
replaced with licen'see
personnel.
The
NRC inspectors
concluded
that
the
licensee
had
made
progress
toward resolution of the staffing
weaknes'ses
identified
by the MTI.
Overdue
performance
appraisals
and
excessive
use
of contractors
appeared
adequately
corrected
but significant efforts
were still
needed
to reduce
excessive
overtime
and turnover rates.
, 3.
Independent
Management
Assessment
( IMA) Commitments
(92701)
During their
review of
MTI items,
the
inspector s noted that
several
licensee
actions
were
a
direct
or
indirect
follow-on
to
licensee
commitments
from their IMA.
The primary area of IMA commitments
reviewed
during this inspection
included those to improve maintenance
performance,
reliability engineering,
and root cause
analyses.
The inspectors
found
that the licensee
had developed
response
actions
to address
each of the
maintenance-related
IMA commitments.
Some
IMA commitments
were verified
by direct observation
during this inspection.
These
included coordination
of efforts
to -reduce
the
backlog
of
PWOs,
Plant
Supervisor-Nuclear
monitoring the progress
of work in the field,
and day-to-day
involvement
of plant management
in maintenance activities.
Other
commitments directly
or indirectly. verified
included
those
such
as
use
of
performance
indicators,
enhancement
of reliability and root cause
analyses
within the
predictive
maintenance
functions,
selection
of
noncontract
systems
engineers,
definition of systems
engineers
duties
and responsibilities,
etc.
The
inspectors
were
informed
of documentation
verifying details
of
licensee's
actions
in
response
to all
IMA commitments.
However,
the
inspectors
only
reviewed details
associated
with commitments directly
related to the areas
reported
above.
The inspectors
did not identify any
case
of
inadequate
or
missing
licensee
actions
for the
individual
commitments
reviewed.
The inspectors
concluded that the licensee
has taken action in response
to
all
IMA commitments
and these
actions
have
been
successful
in improving
maintenance
performance, reliability engineering
and root cause
analyses.
4.
Action on Previous
Inspection
Findings (92702)
The
inspectors
examined
the licensee's
actions for the four violations
identified in
NRC Inspection
Report 250,251/88-32.
The licensee written
response
to these violations, dated
May 4,
1989,
was considered
acceptable
to Region II.
Each of the violations is being closed
as described
below.
a.
(Closed)
Violation
250,251/88-32-01,
Failure
to
Take
Prompt
Corrective Action with Regard to Equipment Identification Tagging.
This
violation
cited
the
licensee's
failure
to
promptly
and
completely
correct
previously identified inadequacies
in equipment
identification tagging.
Three
examples
of incorrect or missing
tags
were noted in the citation.
The licensee's
stated corrective actions
33
included
relabeling
of the
equipment
examples
cited,
revision of
their equipment
tagging procedure;
and wal,kdowns to identify tagging
problems.
Based
on observations
of tagging
and review of walkdown
records
described
in paragraph
2.a
~ above
and discussions
with craft,
the corr'ective actions
stated
in the licensee's
response
have
been
implemented.
(Closed) Violation 250,251/88-32-02,
Procedural
Related Deficiencies
This violation involved inadequacies
in procedures
and in compliance
with procedures.
These
inadequacies
led to a'ailure
to perform
needed
corrective maintenance
on
an instrument,
work history data not
being
entered
in
a
database,
erroneous
requirements
in
a diesel
generator
maintenance
procedure,
fai lure
to retrain
contract
technicians,
and insufficient controls
on breathing air quality.
The
corrective
actions
stated
in
the
licensee's
response
to this
violation were determined
to
have
been
implemented.
Details of the
inspectors'erification
of implementation
are described
in paragraph
2.d.(4').
(Closed)
Violation 250,251/88-32-03,
Failure
to Properly
Perform
Receipt Inspections
This
violation
involved
inadequacies
in
cleanliness
receipt
inspections
of equipment
parts.
The inspectors
determined
that the
corrective
actions
stated
in
the
licensee's
response
had
been
implemented.
Details
of their inspection
of this violation
are
described
in paragraph 2.d.(4).
(Closed) Violation 250,251/88-32-04,
gA Records
Not Properly Stored
This violation involved
a failure to properly store certain records.
The corrective
actions
stated
in the
licensee's
response
to this
violation were determined
to
have
been
implemented.
Details of the
inspectors'erification
of
implementation
are
described
in
paragraph 2.d.(4).
5.
Exit Interview
The inspection
scope
and findings were
summarized
on
November
17,
1989,
with those
persons
indicated in paragraph
1.
The inspectors
described
the
areas
inspected
and discussed
in detail the violation listed below.
This
violation involved drawing errors
discovered
by the
NRC inspectors.
The
errors
were corrected during the inspection.
The plant manager
committed
to
a review of additional
similar drawings to'ssure
that
any further
errors were identified and corrected.
Violation
250,251/89-48-01,
Drawing
Discrepancies,
para-
graph 2.c.(2)(b).
0
During the exit interview,
the inspectors
characterized
the violation as
a
non-cited
violation.
Subsequesnt
reivew
by
Region II
management
determined
that
the
issuance
of
a
Notice of Violation is appropriate.
The plant
manager
was
informed of this
new information
by phone call of
January
30,
1990.
Proprietary
information
is
not contained
in this report.
Dissenting
comments
were not received
from the licensee.
ASME-
DEEP-
GL
I8(C
LCO
MSIV-
MTI
PC/M-
PDRT-
PWO
QIP
TPN
American Society of Mechanical
Engineers
Design Equivalent Engineering
Package
Generic Letter
Health Physics
Instrument Air System
Instrumentation
and Control
Independent
Management Appraisal
Limiting Condition for Operation
Maintenance
Team Inspection
Non-cited Violation
Plant Change/Modification
Procurement
Document
Review Team
Planned
Maintenance
Group
Plan of the
Day
Probabi listic Risk Assessment
Plant Work Order
Quality Assurance
Quality Control
Quality Improvement
Program
Reliability Centered
Maintenance
Residual
Heat
Removal
Turkey Point Nuclear Plant
0