ML17347B544

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Insp Repts 50-250/89-52 & 50-251/89-52 on 891202-22. Violations Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety,Fitness for Duty Training & Plant Events
ML17347B544
Person / Time
Site: Turkey Point  
Issue date: 01/22/1990
From: Butcher R, Mcelhinney T, Orlenjak R, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17347B542 List:
References
50-250-89-52, 50-251-89-52, NUDOCS 9002010246
Download: ML17347B544 (28)


See also: IR 05000250/1989052

Text

1P,S REG(g,

e:=:.'<

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATL AN TA, G Eo R G IA 30323

lf

Report Nos.:

50-250/89-52

and 50-251/89-52

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-250

and 50-251

Facility Name:

Turkey Point

3 and

4

License Nos.:

DPR-31

and

DPR-41

Inspection

Conducted: 'ece

ber 2,

1989 through

December

22,

Inspectors-:- ~

.

r-c- ~ c

R.

C.

cher,

nior

R

i ent Inspector

Mc-iZ.

T.

F.

cElhinne,

Resi

ent Inspector

~r

l c.i'~

G. A.

bli, Resid

t Inspector

Approved by:

R.

.

rlenjak,

ection

Ch

f

Division of Reactor Projects

1989

Date Signed

Date Signed

Date Signed

/8~

'Pd

D te Signed

SUMMARY

Scope:

This routine resident

inspector

inspection

entailed direct inspection

at the

site

in the

areas

of monthly surveillance

observations,

monthly maintenance

observations,

operational

safety,

fitness for duty training and plant events.

Results:

There

was

one violation with two examples,

two URIs**, four IFIs, and

two NCVs,

identified.

Also,

the

residents

expressed

a

concern

regarding

two

recent

events

that resulted

from operators'nattention

to detail

and the fai lure to-

maintain communications

during

EDG runs which was

a contributing factor in one

of the events.

e

" Unresolved

Items

are

matters

about

which more information is required to

determine

whether they are acceptable

or may involve violations or deviations.

. 900i22

pgp

QQIOCK

Q

50-250,251/89-52-01,

IFI.

Excessive

acceptable

leak rate

through fire

protection-PIV.

(Paragraph

2)

50-250,251/89-52-02,

IFI.

Modify procedures

to ensure

personnel

notified

of site evacuation

alarm

and evacuation

has occurred.

(Paragraph

7)

50-250,251/89-52-03,

IFI.

Verification of tygon

tubing indication for

BAST level indicator channel

check.

(Paragraph

7)

50-250,251/89-52-04,

IFI.

Initiation of

PM requirements

to prevent lint

accumulation

in laundry room.

(Paragraph

9)

50-250,251/89-52-05,

Violation,

two

examples.

Failure

to

follow

procedures

resulting in inadvertent

release

of liquid waste

from the

B. MT

(paragraph

9) and failure to follow procedure resulting in the

B

EDG speed

droop not being adjusted during

a Surveillance Test.

(Paragraph

5)

50-250,251/89-52-06,

NCV.

Failure to maintain

RCP seal injection throttle

valve closed resulting

in

an inadvertent 'increase

in

RCS level while in

Mode 5.

(Paragraph

3)

50-250,251/89-52-07,

NCV.

Failure

to incorporate

required testing

into

plant procedures

for ICW isolation valves

4-4882

and

4-4883 to

TPCW heat

exchangers.

.(Paragraph

3)

50-250,251/89-52-08,

URI

~

Followup

on investigation

of

NCR 86-421 being

closed without required actions

being completed.

(Paragraph

4)

50-250,251/89-52-09,

URI.

Followup

on

licensee's

corrective

actions

regarding failure to establish

TS required fire watch in time following

Auxiliary Building evacuation.

(Paragraph

9)

REPORT DETAILS

Persons

Contacted

Licensee

Employees

T. Abbati el 1 o,

equal ity Assurance,

Supervi sor

J.

W. Anderson, guality Assurance

Supervisor

J. Arias, Technical Assistant to Plant Manager

"L. W. Bladow, equality Assurance

Superintendent

R.

M. Brown, Health Physics

Supervisor

J.

E. Cross,

Plant Manager - Nuclear

R. J. Earl, guality Control Supervisor

T. A. Finn, Assistant Operations

Superintendent

S.

M. Franzone,

Lead Engineer

S.

T. Hale,

Engineering Project Supervisor

  • K. N. Harris, Vice President

G. Heisterman,

Electrical Assistant

Superintendent

  • RE J. Gianfrencesco,

Assistant

Maintenance

Superintendent

~V. A. Kaminskas,

Technical

Department

Supervisor

J.

AD Labarraque,

Senior Technical Advisor

G. Marsh,

Reactor

Engineering

Supervisor

  • R. G. Mende, Operations

Supervisor

"L. W. Pearce,

Operations

Superintendent

D. Powell, Regulatory

and Compliance Supervisor

K. Remington,

System

Performance

Supervisor

G.

M. Smith, Service

Manager - Nuclear

F.

H. Southworth,

Assi stant to Site Vice President

R.

N. Steinke,

Chemistry Supervisor

J.

CD Strong,

Mechanical

Department

Supervisor

"G.

S. Warriner, guality Control, Supervisor

M. B. Wayland,

Maintenance

Superintendent

J.

D. Webb, Assistant Superintendent,

Planning

and Scheduling

Other

licensee

employees

contacted

included

construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

  • Attended exit interview on December '22,

1989.

Note:

An Alphabetical Tabulation of acronyms

used in this report is

listed in paragraph

11.

Followup on Items of Noncompliance

(92702)

A review

was

conducted

of the following noncompliances

to assure

that

corrective actions

were adequately

implemented

and resulted

in conformance

with regulatory

requirements.

'erification

of corrective

action

was

achieved

through record reviews,

observation

and discussions

with licensee

personnel.

Licensee

correspondence

was evaluated

to ensure

that the

e

'responses

were timely and that corrective actions

were implemented within

. the time periods specified in the reply.

(Closed) Deviation 50-250,251/88-36-02.

Failure to have

a test

program

as

required

by the

FSAR to demonstrate

conformance

to design

and

system

readiness

requirements

for the Fire Protection

System.

On

October

29,

1988,

an event

occurred

where

a portion of the fire main could not

be

isolated

due to leaking PIVs.

This condition resulted

in both fire pumps

being

declared

OOS.

The

licensee

in

response

to this

event

issued

Surveillance

Procedure

OSP-016.30,

Fire Main Post

Indicator

Valve

Leak

Test

and

System

Flush,

dated

June

29,

1989.

The inspector

reviewed

the

procedure

and found the licensee's

method for determining

PIV leakage

to

be acceptable

for those

leak rates

less

than

50

gpm.

The basis for the

maximum allowable

leakage

rates

for the

specific fire main isolation

valves

identified

in

Enclosure

1 of the

procedure,

were

established

through

the

use of

a computer

model.

The

computer

model

evaluates

the

various sprinkler system

demands,

hose

stream flow, and pressure

require-

ments,

flow paths,

fire

pump

flow and

pressure

requirements

and

then

calculates

the

remaining

system

flow which could

be lost due to system

leakage

without

the fire

suppression

(water)

system

being

declared

inoperable.

The inspector

reviewed the computer

model calculation results

for PIV-23 and PIV-33,

and

found the results

to

be reasonable,

based

on

fire suppression

system

water flow demands

in the event that

a fire were

to occur concurrent

wi,th

a pipe break requiring

PIV-23 or PIV-33 to

be

isolated.

The inspector

in reviewing,

O-OSP-016.38,

found the five gallon

bucket

and stop watch leak rate measuring

method f'r leak rates

less

than

50

gpm to

be feasible.

However, for leak rates

in excess

of 50

gpm this

, method

could not

be easily

implemented.

For example,

PIV-33

has

a leak

rate of 590

gpm, this would require

118 five gallon 'buckets of water to be

collected

in

a

one

minute

time frame.

In response

to this concern

the

.

licensee

initiated

a request

for -procedure

review

and

provided

a draft

revision of procedure

O-OSP-016.30

to

the

inspector

for review.

The

licensee

draft'rocedure

includes

provision for calculating

flows in

excess

of 50

gpm using data gained

by Pitot Tube

Flow measurements.

The

inspector

agrees

that

the

l.icensee

through

the

implementation

of this

revised draft test

procedure

can

demonstrate

system

design

conformance.

This item is closed.

However, the inspector is still concerned

that with

established

acceptable

leak rates

in excess

of the Jockey

Pump Capacity

and with

a pipe break in the

underground fire main, both fire pumps

may

still have to

be placed

OOS

in order

to facilitate repairs.

This is

identified as IFI 50-250,251/89-52-01,

exce'ssive

design acceptable

leakage

rates

through

PIVs may require total fire suppression

system to be placed

.

OOS to facilitate repairs

in the event of fire main pipe break.

(Closed) Violation 50-250,251/88-21-01.

Concerning

the Failure to Follow

Procedure

to Place Transfer Switches

on Channel

IV for Steam Generator

"B"

Testing.

In order to prevent recurrence,

the licensee

modified procedures

of this nature

during which incorrect

channel

selection

could place

the

unit in a transient to have the channel

selections

independently verified

by

a qualified operator.

In addition,

identification labeling

of the

subject

equipment

was modified to reflect the protection

channel

numbers.

This item and

LER 50-251/88-10,

(discussed

in paragraph

4) are closed.

(Closed)

Violation

50-250,251/89-12-03.

Failure

to fol low

procedur es

resulting

in

valve

201B

being

open

and

draining

RCS

water

to

the

containment

sump.

The licensee,

in response

to this violation, performed

a review of procedure

AP-0103.4,

In Plant

Equipment

Clearance

Orders,

to

determine

procedure

adequacy with respect

to vent and drain

hose install-

ation and vent/drain valve manipulations.

In order to prevent recurrence,

the

licensee

revised

procedures

3/4-0P-41.8,

Filling and

Venting

The

Reactor Coolant System

and 3/4-OSP-041. 1, Reactor

Coolant

System

Leak Rate

Calculation.

Procedure

3/4-OSP-041. 1,

was

revised

to incorporate

the

requirement

to visually

inspect

RCS

vent

and

drain valves'ith

hoses

connected

to assure

no

leakage

is occurring.

In addition,

the inspector

verified that procedure

3/4-0P-41.8

was

revised

to require that

whenever

RCS 'filling and

venting

operations

are

occurring that

one

containment

sump

pump

and

one

channel

of

sump

level

indication

be

operable.

The

inspector

found the licensee's

actions

in response

to this violation, to be

satisfactory.

This item is closed.

(Closed)

Violation

50-250,251/89-18-01.

Fai lure

to

fol low

procedure

resulting

in

the

inadvertent

actuation

of Train

A Safeguards.

The

licensee,

in response

to this violation, placed

warning

signs

inside

the

safeguard

racks of both units

and at the

power supply breakers

to these

racks.

The warning signs inside the safeguard

racks state that installing

fuses

FU4 or

FU3

may result

in

an

SI being

generated.

This sign also

references

that

procedure

3/4-0NOP-049,

Re-energizing

Safeguards

Racks

After Loss of Single

Power

Supply,

should

be utilized when installing

these

fuses.

The sign at the

power

supply

breakers

identifies

to

the

operator that closing these

breakers

can also result in an SI signal.

In

addition,

the licensee

revised the standard

clearance, for this activity in

the plant clearance

network to require that procedure

3/4-ONOP-049 is to

be

used

when releasing

clearances

associated

with the

safeguards

racks.

The inspector

found the licensee's

corrective actions associated

with this

event to be satisfactory.

This item is closed.

Followup

on

Inspector

Followup

Item(s),

Inspection

and

Enforcement

Information Notice( s),

IE Bulletin(s) (information only), IE Circular(s),

and

NRC Request(s)

(92701).

(Closed)

URI 50-250,251/88-11-01.

Evaluate

Licensee's

Method of Testing

Check

Valves to

Meet

the

Requirements

of

ASME

Code

Section

XI.

The

inspector

reviewed

OP-0209. 1,

Valve Exercising

Procedure,

dated

May 17,

1989,

to determine, that

LHSI pressure

boundary isolation

check valves,

4-876A,

B, and

C, are included in their

Valve Exercising

Program.

These

valves

are classified

as

valves

which cannot

be exercised

during plant

.operations

and

have

been

included in Appendix

B to OP-0209 '

as valve

which are

required to

be exercised full open

whenever

a unit is in Cold

Shutdown.

The inspector

also verified that the licensee

had developed

a

method for determining

the flow split between

v'alves

4-876B

and

C,

and

incorporated

the

method

into the

procedure.

The licensee's

corrective

actions

and

code

test

requirements

associated

with

check

.valves

is

consistent with the requirements

of ASME Boiler Pressure

Code,

Section XI,

Division I,

Subsection

IWV,

1980 Edition through Winter

1981

Addenda;

IWV-3520, Tests for Check Valves.

This item is closed.

(Closed)

URI 50-250,251/89-12-02.

This item concerned

RCP seal injection

throttle valve 4-297A being

opened contrary to

GOP 4-305,

Hot Standby

to

. Cold Shutdown.

This resulted

in

an

increase

in the reactor, drain

down

water level

with Unit

4 in

Mode

5.

Investigation

revealed

that

work

needed

to

be

done

on

4-297A during the outage'herefore,

the clearance

boundary

was modified and the tag

on 4-279A was

removed to allow the work

to

be

done.

When

the

maintenance

was

completed,

the

clearance

was

released

prior to re-tagging

and reclosing

4-279A allowing water from the

CVCS to enter

the

RCS through the

RCP.

The Unit 4

RCO noted the increase

in level

and

promptly identified the

source

of inleakage.

Valve 4-279A

was closed

and tagged

as required.

The fai lure to reclose

and tag 4-279A,

as specified

by

GOP 4-305, after maintenance

was

completed

constitutes

a

violation of

TS 6.8. 1.

However,

this violation

meets

the criteria

specified in

10 CFR 2,

Appendix

C,

Section V.A,'herefore,

no notice of

violation will be

issued.

The

licensee

was

in the

process

of and is

continuing to'eview the

equipment

clearance

procedure

and training of

personnel

to prevent recurrences.'his

item is closed

and will be tracked

as

NCV 50-250,251/89-52-06.

(Cl osed)

URI

50-250,251/89-24-03.

Resoluti on

of

Document

Contr ol

Discrepancies.

During

the

same

time

frame

the

document

control

discrepancies,

noted

in

NRC

IR 89-24

were identified,

the

licensee

was

conducting

a

QA Audit in the

same

area.

The

inspector

reviewed

the

results

of

QA Audit Report

QA-O-PTN-89-988,

dated

May 23,

1989,

which

covered

the audit conducted

on May 11,

1989 thru May 22,

1989, in the area

of Document Control.

Based

on the inspectors

review,

the

scope

of the

document discrepancies

identified by

NRC IR 50-250,251/89-24

were included

in the findings of the licensee's

audit report.

The inspector

reviewed

the

response

to the audit report

and QI-6-PTN-1,

Document Control, dated

August 17,

1989,

and

AP 0190.86,

Document Control, dated October 27,

1988.

The inspector

found response

to this audit report to be satisfactory

and

the

scope

of the

QI was consistent

wi,th the

scope

of the

AP governing

document control.

This item is closed.

(Closed)

IFI

50-250,251/88-30-06.

Corrective

Actions

to

Prevent

EDG

Overload

From

ICW

Pump

Auto Start

During'ccident

Conditions.

The

licensee

implemented

PC/M 88-393,

ICW Overcurrent Trip, which modified the

control

circuits

of

the

ICW

pumps

to

defeat

the

overcurrent trip

auto-start

interlocks

between

the

pumps.

This

modification,

as

implemented,

prevents

the train "B" EDG from potentially being overloaded

during

a

DBA concurrent

with

a loss of off-site power.

The inspector

reviewed

the

PC/M

and

verified this

modification

was

completed

on

November

17,

1988. This item is closed.

(Closed)

IFI 50-250,251/88-39-02.

Resolution of Root

Cause

for Unlanded

Spade

Connection

in the

EDG Control Panel.

The. licensee,

under

PWO 5390,

ER69 relanded

a pair of wires to the

ES 200

RPM

relay and the

EZ

40

RPM

relay.

The

cause

of this condition

was attributed to the routing

and

pulling of

cable

B4B0698P

inside

the

control

panel.

During

the

installation

of this cable,

the

cable

rubbed

up against

the affected

stake-on

push type lugs,

causing

these

wire connections

to

become

loose.

The inspector

agrees this was the most probable

cause for this condition.

This item is closed.

(Closed) IFI 50-250,251/88-40-03.

Followup on Licensee's

Determination of

the

Cause

For

Leakage

Through

Seal

Table

Conduit at J7

and J12.

The

licensee

had Westinghouse

perform

a failure analysis

on the Unit 3 leaking

conduit

guide

tubes.

The

inspector

reviewed the Westinghouse

Analysis

WCAP-12146,

dated

March 13,

1989.

The analysis

concluded that the type of

cracking

observed

is

indicative

of

transgranular

stress

corrosion

cracking.

In addition,

the analysis identified that the localized pitting

on

the

shoulder

and

socket

outside

diameter.

surfaces

is indicative of

attack

from a corrodant

such

as chlorides.

The metallographic analysis of

the

fracture

face

and

the

crack tip region

revealed

chlorides

were

present.

This chloride contamination,'long

with the subject

tubes

being

wetted

from the

leaks

observed

on the

swage

lock fittings., coupled with

the

stresses

from the

RCS

service

pressure

and

from the

cold

worked

microstructure

promoted

this

transgranular

stress

corrosion

cracking

failure.

The cracks

propagated

from this outside diameter

surface

in the

shoulder

and

socket

region to the. inside diameter.

The inspector

agrees

with the results of the licensee's

analysis.

This item is closed.

(Closed)

URI 50-250,251/89-45-05.

This

item

concerned

the failure to

perform quarterly

IST for

ICW isolation valves

4-4882

and

4-4883 to the

TPCW heat

exchangers.

The

cause

of this

event

was

determined

to

be

personnel

error.

AP

0190. 15,

Plant

Changes

and Modifications

(PC/M),

Figure J,

System Acceptance

Turnover

Sheet,

required

the

PUP coordinator

to list all procedures

not required

for

system

acceptance/turnover,

but,

required revision.

This section

.was

marked

N/A by the

PUP coordinator.

The need to revise

OP 209. 1, Valve Exercising Procedure,

was identified by

PUP

on October 26,

1988'n June

27,

1989,

a Request for Procedure

Review

was initiated by

PUP group to revise

OP 209. 1.

However, during the review.

process,

comments

concerning

test

frequencies

were not

resolved

at

the

reviewer level.

This

was

not elevated

to higher levels of management.

Therefore,

the testing

was not done prior to the

due date

of August

1,

1989.

The failure to

perform

the

ASME,

Section

XI, testing

of valves

4-4882

and

4-4883,

constitutes

a violation of

TS 4.0.3.

The inspectors

determined

this violation

met

the criteria

specified

in

10 CFR 2,

Appendix C, Section

G. l. for a Licensee Identified NCV.

The basis for the

determination

was

as follows:

(a) the licensee identified the 'violation,

(b) the violation was classified

as Severity Level IV, (c) the event

was

reported

to

the

NRC via

LER 50-251/89-13,

(d)

the

licensee

initiated

corrective

" actions

which included

adding

the

valves

to

OP

0209. 1

on

October

24,

1989,

counseling

the

personnel

involved

and .initiating

a

review of procedures

requiring revision for PC/Ms to identify any other

needed

procedure

changes,

(e) the violation,was

not willful and,it could

not

have

been

prevented

by corrective actions for,a previous violation.

The inspectors. mentioned

in IR 50-250,251/89-45,

other recent

examples

of

failure to incorporate

design

requirements

into plant procedures.

The

root causes

for those

events

was inadequate

administrative controls,

where

in thi s

case,

the

administrative

controls

were

adequate

but

were

not

implemented.

Therefore,

the

corrective

actions

for

the,

previous

violations

would

not

have

prevented

this

occurrence.

URI

50-250,251/89-45-05

is closed

and this

item will

be

tracked

as

NCV

50-250,251/89-52-07.

(Closed)

IFI 50-250,251/89-12-01.

Possible

Improper Oil Level in the

AFW

Governor.

The

licensee,

in

response

to this

item,

revised

the

PWO

guidance

associated

with checking

the oil levels

in the

AFW governors.

The

guidance

presently

utilized provides

a definition with regard

to

normal

levels

under

standby

and

operating

conditions.

The

inspector

reviewed

PWO

69-8207,

69-7458,

and

69-7459

and verified this

revised

guidance

was being properly incorporated

in the

PWO work descriptions.'n

addition,

the

licensee

incorporated

caution

notes

into

the

AFW

surveillance

procedures

with regard to the actions to be taken if the oil

level in the governor is not within its normal level range.

The inspector

reviewed

3-OSP-075. 1,

and

4-OSP-075. 1,

both

dated

July ll,

1989,

and

verified this guidance

was properly incorporated

into these

procedures.

The inspector

found the licensee's

corrective actions

to be satisfactory.

. This item is closed.

(Closed)

IFI 50-250,251/89-18-03.

Recurrence

of Voids in the

RCS

~

The

licensee

performed

an

investigation

of

the

sudden

pressurizer

level

decreases

which occurred

onJanuary

25,

1989,

and March 9,

1989, while the

reactor

was in

Mode

5, depressurized

and vented.

The inspector

reviewed

the

results

of

the

licensee's

investigation.

This

investigation

determined that

a gradual

increase

in pressurizer

level occurred prior to

each

event

along

with

a

subsequent

pressurizer

level

decrease

of

approximately

2.4%.

The licensee

determined this condition is indicative

of dissolved

gas being released

into the reactor vessel

and forming

a void

in the reactor

head area.

The gas formation in the

head

area is caused

by.

the nitrogen cover gas

on the

VCT being entrained

by the charging flow and

being

released

when

the

flow velocity

and

pressure

decreases

in the

, reactor.

The

licensee's

investigation

also

determined

that

nitrogen

venting of the reactor

head

area

is restricted

by the resistance

of the

head vent orifice and the loop seal

which is incorporated

in the head vent

system

design

configuration.

Based

on this

investigation it

can

be

concluded that the increase

in pressurizer

level is

a result of gas void

formation

in the

reactor

head

area

and

the

sudden

drop in pressurizer

level

can

be attributed to sudden

venting of collected

gas in the reactor

head

area.

The

licensee

based

on

the

results

of their investigation

revised

procedures

3/4-0P-041.7,

Draining The Reactor Coolant System,

and

attachment

to

3/4-OSP-201. 1,

RCO Daily Logs.

The

inspector

reviewed

procedures

3/4-0P-041.7,

dated

June

29,

1989,

and

3/4-OSP-201. 1,

Attachment

7,

dated

June

29,

1989,

and

determined

the

investigation

recommendations

associated

with establishing

and maintaining

a reactor

head

vent path

had

been

incorporated.

In addition,

the

inspector

has

determined

the corrective

actions

are

satisfactory

and

reactor

vessel

level perturbations

under similar operating conditions which were present

on January

25

and

March 9,

1989,

should

be reduced

as

a result of 'these=-

actions.

This item is closed,

Onsite

Followup

and

In-Office Review of Written

Reports

of Nonroutine

Events

and

10 CFR Part 21 reviews (92700/90712/90713)

The

Licensee

Event Reports

and/or

10 CFR Part 21 Reports

discussed

below

were

reviewed

and

closed.

The

inspectors

verified

that

reporting

requirements

had

been

met,

root

cause

analysis

was performed,

corrective

actions

appeared

appropriate,

and

generic

applicability

had

been

considered.

Additionally, the inspectors

verified that the

licensee

had

reviewed

each

event,

corrective actions

were

implemented,

responsibility

for corrective

actions

not ful.ly completed

was clearly assigned,

safety

questions

had

been evaluated

and resolved,

and violations of regulations

or

TS conditions

had

been identified.

When applicable,

the criteria of

10 CFR 2, Appendix C, were applied.

(Closed)

50-250,251/P2186-03.

This deficiency

involved

damage

to

lead

wire insulation for Limitorque

MOVs

DC Motors manufactured

by Peerless-

Winsmith.

The failure mechanism

was attributed

to insulation

damage

due

to bending during field installation

and setup.

FPL experienced

a failure

of a Peerless

Winsmith

DC motor

on Unit 3

AFW Steam

Supply

MOV-3-1403,

in December

1986.

Root cause

analysis

determined

the lead wire failures

were due to mechanical

damage

during packaging,

shipping,

or installation.

The

licensee

performed

inspections

and testing

of all

the

subject

DC

motors which indicated

no damaged

lead Hires.

NCR 86-421

was written to

address

this

problem.

Engineering

resolution

required

the

plant

to

replace

MOV-3-1403 with a qualified motor and to return

any

spare

motors

to the

vendor for lead wire sleeving.

The licensee identified two spare

motors with suspect

serial

numbers.

One spare

motor was in the Electrical

(}C locker and the other spare

motor was located in the nuclear warehouse.

The

NCR was

closed

out

due to MOV-3-1403 being

replaced

and

the

spare

motors

being returned to the vendor for electrical

lead replacement.

The

~ inspectors

verified that

MOV-3-1403'as

replaced

by

reviewing

the

completed

work order

and

performing

a field walkdown.

The

inspectors

could

not verify the

spare

motors

were

returned

to the

vendor.

The

licensee

determined

that this task

was not completed contrary to the

NCR

disposition.

One spare

motor

was still in the nuclear warehouse,

without

any

gC

hold

tags

to

prevent

field installation.

The

licensee

was

investigating

how the

NCR was closed without all of the required

actions

completed.

The inspectors will'ollowup on this investigation.

This item

will be tracked

as

URI 50-250,251/89-52-08.

(Closed)

50-250,251/P2185-02.

Concerning

a defect

in

TEC Model 914-1,

Acoustic Valve Flow Monitor Modules.

A Safety Evaluation

was conducted

by

the licensee

.and documented

in JPE-L-85-42,

dated

January

15,

1986.

The

evaluation

concluded

the concern

was not

a substantial

safety hazard.

The

inspectors

reviewed

the

SE

and

O-PMI-041.5,

RCS

Safety

Valve, Position

Indicator

Instrumentation

Channel

S-6303 Calibration which performs, the

calibration

and functional testing of this system.

This item is closed.

(Closed)

LER 50-251/88-10.

Concerning

the Failure to Follow Procedure

to

Place

Transfer

Switches

on

Channel

IV for Steam

Generator

"8" Testing.=

This

issue

is

discussed

and

closed

in

paragraph

2,

Violation

50-251/88-21-01.

Thi s i tern i s closed.

Monthly Surveillance

Observations

(61726)

The

inspectors

observed

TS

requi red surveillance

testing

and verified:

The test procedure

conformed to the requirements

of the

TS,

testing

was

performed in -accordance

with adequate

procedures,

test instrumentation

was

calibrated,

limiting conditions for operation

were met, test results

met

acceptance

criteria requirements

and were reviewed

by personnel

other than

the

individual directing

the

test,

deficiencies

were

identified,

as

appropriate,

and

were

properly

reviewed

and

resolved

by

management

personnel

and

system restoration

was

adequate.

For completed tests,

the

inspectors

verified testing frequencies

were met and tests

were performed

by qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

3-0SP-050.2

Residual

Heat

Removal

Pump Inservice Test.

3-SMI-04. 16

Tavg and Delta - T Protection

Channel

T-3-412,

T-3-422,

and T-3-432 Analog Test.

O-OSP-074.3

Standby

Steam Generator

Feedwater

Pumps

Availability Test.

O-OSP-023.1

Diesel Generator Operability Test.

On

December

21,

1989,

the operators

tested

the

B

EDG in accordance

with

0-OSP-023. 1, Diesel

Generator

Operability Test,

dated

June

22,

1989.

The

inspectors

noted

the

speed

droop setting

on the

EDG governor

was set at

zero.

Step

7.2.21

of the

procedure

required

the

operator

to set

the

governor

speed

droop control to

30 on the droop scale.

The

NPO notified

the Unit 3

RCO and the droop was set at 30 as required.

While setting the

droop,

the

EDG load decreased

to 900

KW which invalidated the test.

The

licensee

decided

to

run

the

EDG for one

hour

as

recommended

by the

manufacturer'.

After the

engine

was

shut .down,

the operability test

was

performed successfully.

The failure to set the

speed

droop as required

by

0-OSP-023. 1,

constitutes

a violation of

TS 6.8. 1.

This is the

second

instance of operators

inattention

to detail this inspection

period, with

the first being the release

of the incorrect liquid waste tank.

This item

is discussed

in paragraph

9.

The

inspectors

also

noted

that

constant

communications

were

not established during'his test.

Good communication,

between

the

RCO and

NPO could have prevented this problem from occurring.

The licensee

is considering

using

the Alternate

Shutdown

Communications

headsets

in

the

future.

This violation is

the

-second

example

of

50-250,251/89.-52-05.

6.

Monthly Maintenance

Observations

(62703)

Station

maintenance

activities of safety related 'systems

and

components

were

observed

and

reviewed

to ascertain

that

they

were

conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and

standards,

and in conformance with TS.

The following items

were considered

during this review,

as appropriate:

LCOs

were

met while

components

or

systems

were

removed

from service;

approvals

were

obtained

prior

to initiating

work;

activities

were

accomplished

using

approved

procedures

and

were

inspected

as applicable;

procedures

used

were

adequate

to control

the activity;

troubleshooting

activities

were

controlled

and

repair

records

accurately

reflected

the

maintenance

performed;

functional

testing

and/or

calibrations

were

performed prior to returning

components

or systems

to service;

gC records

were

maintained;

activities

were

accompli shed

by qualified

personnel

parts

and materials

used

were properly certified; radiological controls

were properly

implemented;

gC hold points

were established

and

observed

where

required;

fire

prevention

controls

were

implemented;

outside

contractor

force activities

were

controlled

in

accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The

inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Repair of 4-942Y cracked weld.

0

10

Troubleshooting

Unit 4 Containment

Personnel

Hatch Interlocks.

Repair of Unit 4 Main Condenser

Tube Leak.

Troubleshooting

3A HHSI pump breaker.

Replacing

prop spring in the

3A HHSI pump breaker.

On December

7,

1989,

the licensee identified

a cracked weld on the branch

connection

to drain

valve

4-942Y in the safety injection

system.

This

section of piping provides

a minimum recirculation

flowpath for the

CSPs

for pump testing

and to protect the

pump in the event the

pump discharge

valve failed to

open

upon starting

the. pump.

The license'e

performed

an

engineering

assessment

of

operability

to

allow isolation

of

the

recirculation

flowpath to facilitate repair of the

cracked

weld.

The

repaired

weld

wa's tested

satisfactorily

and the

system

was returned

to

normal configuration

on December

12,

1989.

No violations or deviations

were identified in the areas

inspected.

7.

Operational

Safety Verification (71707)

By observatio'n

and direct interviews,

verification

was

made

that

the

physical security plan was being

implemented.

Plant

housekee

in /cleanliness

conditions

and

implementation

of

p

g

radiological controls were observed.

Tours of the

intake structure

and diesel, auxiliary, control

and turbine

buildings were conducted

to observe

plant equipment

conditions

including

potential fire hazards,

fluid leaks

and excessive

vibrations.

The

inspectors

walked

down accessible

portions of the following safety

related

systems

to verify operability and proper valve/switch alignment:

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room

operators,

observed

shift

turnover s

and confirmed operability of instrumentation.

The

inspectors

verified the operability of selected

emergency

systems,

verified that

maintenance

work orders

had been

submitted

as required

and that followup

and prioritization of work was

accomplished..

The

inspectors

reviewed

tagout records, verified compliance with TS

LCOs

and verified the return

to service of affected

components.

A and

B

EDGs

Control

Room Vertical Panels

and Safeguards

Racks

ICW Structure

4160 Volt Buses

and

480 Volt Load and

MCCs

Unit 3 and

4 Feedwater

Platforms

11

Unit 3 and

4 Condensate

Storage

Tank Area

AFW Area

Unit 3 and

4 Main Steam Platforms

Auxi l i a ry

- Bui 1 di ng

The inspectors

reviewed the licensee's

test of the site evacuation

alarm.

Procedure-

0-OSP-200. 1,

Schedule

of

Plant

Checks

and

Survei llances,

requires

the

noted test

be

conducted

at

11:45

a.m.

every

Wednesday.

0-OSP-200. l.references

procedure

OP-0204.2,

Periodic

Tests,

Checks

and

Operating

Evolution.

Section

8.4.6

of

OP

0204.2,

lists

the

site

evacuation

alarm lights to check to ensure

proper light operation.

The

inspectors

positioned

themselves

outside

the

protected

area

and

near

personnel

trailers

and the construction tool

room to determine if the site

evacuation

alarm

was

audible.

The

alarm

was

barely

audible

in

some

locations

and inaudible at other locations.

The inspectors

reviewed the

security

procedure

SFI

6307,

Emergency

Procedures

Security

Force

Requirements,

and

although

Security

makes

a

sweep

of the

general

area

following the initiation of. a site evacuation

alarm, there is no specific

guidance

to

do

a .detailed building by building check to ensure

personnel

have

evacuated

the

area.

The

licensee

committed

to

revise

security

procedures

to ensure that all personnel

in the area

are

aware of any site

area

emergency

or general

emergency

declaration

and/or

a site evacuation

alarm.

Also, following any site

evacuation

alarm,

a

sweep

of the -area

(building by building) will be accomplished

to ensure all personnel

have

evacuated

as

necessary.

The modification of procedures

to accomplish

the

notification of personnel

of any site

emergency

and/or site

evacuation

will be IFI 50-250,251/89-52-02.

Other specific

areas

such

as the Scout

Camps, Air Force

Sea

Survival

Training

School,

recreation

areas,

boat

ramps,

and

the

cooling

canal

system

are

specifically

addressed

in

EPIP 20110, Criteria For and Conduct of Owner Controlled Area Evacuation,

and are accomplished

by detailed security procedures.

The inspectors

noted

a concern

regarding

the

use of

a level

hose

on the

BAST.

The licensee'ses

these

level

hoses

to perform the weekly channel

check required

by

TS 4. 1. 1,

item

14.

These

hoses

are

connected

to the

drain line at the bottom of each tank

and

are

routed

up the

side of the

tank where tape

marks are provided indicating percent level for the tanks.

The

channel

check is performed

in accordance

with

OP

0204.2,

Periodic

Tests,

Checks,

and

Operating

Evolutions.

The

procedure

directed

the

operator to compare

the control

room tank level indication with the local

indication.

The operator

may

use

the level

hose if the ultrasonic level

indicator is inoperable.

The operators

had

been

using the level

hose

due

.

to

the ultrasonic

indicators

not working properly for

some

time.

The

acceptance

criteria was 10:o'f span

between indicators

(685 gallons).

The

inspectors

questioned

how the

temporary

level indicators

were installed.

Drawing 5610-T-E-4505,

sheet

5, revision

5,

contained

a note mentioning

the

tygon tubing

used for local

level indication.

The tubing note

was-

added to the drawing in

1983 during

an as-built walkdown.

Investigation

by the licensee

could not find any engineering

documents

that approved

the

12

use of the tygon tubing for level indication.

The licensee

indicated that

the tank markings

would

be verified and the temporary

level indicators

will be controlled via the

TSA process.

The licensee

plans to repair the

ultrasonic level indicators during the next outage with vendor assistance.

The inspectors will followup the licensee's

actions to verify the accuracy

of the tank markings

and the control of the temporary installation.

This

item will be tracked

as IFI 50-250,251/89-52-03.

No violations or deviations

were identified in the areas

inspected.

Licensee

Fitness for Duty Training (TI 2515/104)

The resident

inspectors

attended

one licensee initial training session

for

supervisors

which

was

approximately

8

hours

in duration,

one. training

session

for general

employees

which was approximately

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> in duration

and

one followup training session

for supervisors

which was approximately

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />

in duration.

The licensee's

supervisory

and/or general

employee

training sessions

also qualify personnel

for escort duties.

Copies of the

licensee's

FFD program for the Nuclear Energy Department

were

used

as the

basis

for the training

session

with the stipulation

the

FFD program

was

still

under

Corporate

Nanagement

review

and

minor

changes

could occur

since the

FFD program is to be implemented

on January

3,

1990.

Personnel

are to

be notified of any

changes

made to the

FFD program

subsequent

to

the training.

Also discussed

was

the

EAP

and

when,

in

general,

an

.

employee

becomes

ineligible for the

EAP.

An

experienced

policeman,

associated

with

a

Vice/Narcotics

strike

force,

supplemented

the

FPL

instructors

and

was very effective in making employees

aware of the

need

for an

FFD program.

No deviations or violations were identified.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need

for further

followup action.

Plant

parameters

were evaluated

during transient

response.

The significance

of the event

was

evaluated

along with the

performance

of the

appropriate

safety

systems

and

the

actions

taken

by the

licensee.

The

inspectors

verified that

required

notifications were

made

to the

NRC

~

Evaluations

were performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were

examined,

as

appropriate:.

Details

regarding

the

cause of the event;

event chronology; safety

system performance;

licensee

compliance

with approved

procedures;

radiological

consequences,

if any;

and proposed corrective actions.

On

December

2,

1989,

with Units

3

an'd

4 operating

at

100%

power,

the

Unit 4

RCO attempted

to fill the cold leg SI accumulators

using-the

4A HHSI

pump.

The

RCO noted that motor

amps went to zero approximately

one

second

after starting.

The

pump was declared

OOS and

a work request

was

13

initiated

for

electrical

maintenance.

Investigation

by

electrical

maintenance

revealed

a broken prop spring

on the

4KV breaker.

The spring

was replaced

and the

pump returned

to service

on

December

3,

1989.

The

licensee'ent

the broken prop spring to

a metallurgical

expert for failure

analysis.

The licensee

believes

that fatigue

was

the failure mechanism.

The breakers

for the

HHSI

pumps

had experienced

a high number of cycles

compared

to the other

4KV breakers,

therefore,

the licensee

decided

to

replace

the

prop springs for the other three

HHSI

pump breakers.

These

breakers

are General

Electric Magna Blast breakers.

GE recommended

that

a

modification to the breakers

be

done to

add

a

second

prop spring.

GE

indicated this was not

a requirement but only a recommendation,

therefore,

continued

operation

with only

one

prop

spring

was

acceptable.

The

licensee

was considering

implementing this modification during

an

outage

of sufficient length.

On December

10,

1989, at 2:45 a.m., with Unit 4 at

100% power,

a unit load

reduction

was

commenced

due

to

a

main

condenser

tube

leak.

Load

was

'educed

to approximately

20% and the ruptured tube

and six adjacent

tubes

were

plugged.

The

unit

returned

to

100%

power

at

4:00

a.m.,

on

December

13,

1989.

On December

14,

1989, with Unit 3 at

100% power, the

3C

ICW pump failed to

start.

Investigation of the

pump breaker

revealed

the white light was out

and the charging springs

were discharged

which indicated

DC charging

power

was not available.

The licensee identified that the cause

was that closing

fuses

were not fully engaged.

The fuses

were

engaged

and

the

pump

was

cycled successfully

and returned to service later that day.

The licensee

checked

the

fuses

for,. t'e

other

4KV breakers

and

no

problems

were

identified.

On December

15,

1989, at 6:01 a.m., with Unit 3 at

100% power,

the

NPO was

in the

process

of hanging

a

clearance

on

the

3A=- HHSI

pump

4160 volt

breaker

3AA13,

when

the

3A HHSI

pump inadvertently started.

The Unit

3

RCO noted the

3A HHSI pump red

run light was lit and notified the

PS-N.

Normal plant conditions

were verified and since

RCS pressures

were normal,

'o SI flow to the reactor vessel

occurred.

The

3A HHSI

pump

was

secured

from the control

room at 6:08 a.m.

The

3A HHSI pump was placed in pull to

lock with the breaker closing fuses

removed

and

a caution tag

hung stating

to

keep

the

3A

HHSI

pump

in pull to lock until electrical

department

completes

troubleshooting

and repair.

The licensee notified the

NRC of

a

significant

event

per

10 CFR 50.72(b)(2)(ii) at

6:53

a.m.

Subsequent

investigation

has

led

the

licensee

to

conclude

the

NPO inadvertently

contacted

the

manual

close

button

on breaker

3AA13 while removing

the

control

power fuses inside the breaker

cubicle for the clearance.

On December'5,

1989,

at

1:47 p.m.,

a fire was reported

in the

laundry

room in the auxiliary building.

The fire team was dispatched

and the fire

extinguished

at

1:50

p.m.

The

cause

of

the fire

was

an

excessive

accumulation of lint on top of a dryer.

The dryer was turned

on and the

14

heaters

ignited the lint.

The local breakers

to the dryers were opened,

and cleaning of lint accumulation

was initiated.

The

STA report'f this

event

recommended

that periodic

inspection/cleaning

of the

dryers

be

.initiated as

a

PM measure.

The licensee's

actions

to 'prevent

recurrence

will be followed up as IFI 50-250,251/89-52-04.

On December

18,

1989, at 2:55 a.m;,

a

SNPO notified the

PS-N the

B MT had

been

inadvertently

released

rather

than

the

B

WMT as authorized

by

LRP

89-641.

The

MT capacity is 10,000 gallons versus

a

WMT capacity of 5,000

gallons.

The

SNPO

had received

the

LRP

and correctly

logged that

the

discharge

was to"be

from the

B WMT.

The

SNPO then obtained

procedure

OP

5163.2,

Waste

Disposal

System

-

Controlled

Liquid

Release

to

the

Circulating Water,

and proceeded

to follow Section

8. 1, Controlled Liquid

Release

from Monitor Tanks,

rather

than

Section

8.2,

Controlled

Liquid

Release

from

Waste

Monitor

Tanks

(Radwaste

Building).

Investigation

showed the

B MT had

been

sampled at 10:45 p.m.,

on December

17,

1989,

and

the

PS-N

then

requested

that

an

LRP

be

prepared

for the

B

MT.

A

comparison

of the

B

MT (LRP 642)

versus

the

B

WMT (LRP 641)

gave

the

following results:

B MT

B WMT

Specific Activity

Specific Activity (after

dilution-non-gaseous)

Specific Activity (after

Dilution-'gaseous)

R-18 Background

cpm

R-18 Setpoint

cpm

6.351E-7

4.071E-10

9.705E-11

3.9K

8.9K

1.057E-5

6.776E-9

1.404E-6

4.2K

10K

TS 6.8. 1 requires that written procedures

and administrative policies

shall

be established,

implemented

and maintained that meet or exceed

the

requirements

and

recommendations

of Appendix

A of

USNRC

Regulatory

Guide 1.33'nd

Sections

5. 1

and

5.3 of ANSI N18.7-1972.

Section

5. 1 of

ANSI N18.7-1972 requires that procedures

be followed.

Operating

Procedure

5163.2,

Waste

Disposal

System

-

Controlled

Liquid

Release

to

the

Circulating

Water,

Section

8.2,

Controlled

Liquid Release

from

Waste

Monitor Tanks

(Radwaste

Building), provides di rections for the release

of

liquids from the

WMT.

Nuclear Chemistry procedure

NC-44, Preparation

of a

Liquid Release

Permit, provides instructions for preparation

of an

LRP for

a controlled radioactive liquid discharge

to the circulating water.

On

December

18,

1989,

a

liquid release

was

performed

per

Section

8. 1,

Controlled Liquid Release

from Monitor Tanks,

of

OP 5163.2,

resulting

in

the inadvertent

release

of the

B MT liquid waste for which no

LRP had been

issued.

The inspectors

determined

that this release

did not exceed

NRC

requirements.

Failure to follow procedure

OP 5163.2 to release

the

B WMT

will be identified as the first example of violation 50-250,251/89-52-05.

On December

18,

1989 the licensee

reported

an Unusual

Event in accordance

with Emergency

Plan Implementing

Procedure

20101, Duties of Emergency

E

V

0

0

15

Coordinator,

dated

November

7,

1989,

Category

20,

Loss

of Engineered

Safety

Features/Fire

Protection.

The

licensee

determined

that

on

December

1,

1989,

the hourly roving fire watch for the Auxiliary Building

'as

not performed at the 4:00 p.m.

and 5:00 p.m. intervals.

The Auxiliary

Building had been

evacuated

as

a precautionary

measure

due to an alarm

on

the plant gas

vent monitor

and

an air sample.

The roving fire watches,

which were in place to cover approximately

31 fire protection

impairments,

did not resume until the 6:00 p.m. interval.

TS 3. 14 required that

a fire

watch

patrol

be

established

within

one

hour

when

fire

detection

instrumentation

is lost.

The inspectors

were evaluating this event at the

end

of

the

inspection

period

and will followup

on

the

licensee's

investigation

and corrective actions.

This item will be tracked

as

URI

50-250,251/89-52-09.

On

December

19;

1989, at 2:29 p.m., feeder breaker

41406

on the

4F

LC to

the

4E

MCC tripped.

This disabled'he

Unit

4 intake

screens

and

the

differential pressure

started

increasing.

A load reduction

was initiated

at

4:00

p.m.

and

power

was

reduced

to

89%.

Electrical

maintenance

restored

'power to the

4E

MCC and is initiating a clean

up of the

MCC to

prevent recurrence.

On

December

19,

1989,

at

5:45

p.m.,

the

Unit

4

RCO reported

high

SG

conductivities with an

upward trend.

At 5:55 p.m.,

a load reduction

was

initiated to reduce

power to less

than

50% to facilitate

removing

the

water

boxes

from service.

= The

4B north, and

4B south water

boxes

were

initially removed

from service

but it was later determined

the

leak

was

most likely from the

4A .water

boxes.

The

4B north

and

4B south water

boxes

were

retur'ned

to service.

At 4:20 a.m.,

on

December

20,

1989,

a

load reduction to

30% was initiated.

The licensee is currently trying to

identify the source of the leak.

10.

Exit Interview (30703)

The

inspection

scope

and

findings

were

summarized

during

management

.

interviews

held throughout

the reporting period with the Plant Manager

Nuclear

and selected

members of his staff.

An exit meeting

was

conducted

on

December

22,

1989.

The

areas

requiring

management

attention

were

reviewed.

No proprietary

information

was

provided

to

the

inspectors

during the reporting period.

The inspectors

had the following findings:

50-250,251/89-52-01,

IFI.

Excessive

acceptable

leak rate

through fire

protection

PIV.

(Paragraph

2)

50-250,251/89-52-02,

IFI.

Modify procedures

to,ensure

personnel

notified

of site evacuation

alarm and evacuation

has occurred.

(Paragraph

7)

50-250,251/89-52-03,

IFI.

Verification of tygon

tubing

indication for

BAST level indicator channel

check.

(Paragraph

7)

50-250,251/89-52-04,

IFI.

Initiation of

PM requirements

to prevent lint

accumulation

in laundry room.

(Paragraph

9)

16

50-250,251/89-52-05,

"'Violation,

two

examples.

Failure

to

follow

procedures

resulting in inadvertent

release

of liquid waste

from the

B MT

(paragraph

9) and fai lure to follow procedure resulting in the

B

EDG speed

droop not being adjusted

during Surveillance

test.

(Paragraph-

5)

50-250,251/89-52-06,

NCV.

Failure

to

maintain

RCP

seal

injection

throttle

valve

closed

resulting

in

an

increase

in

RCS

level while in

Mode 5.

(Paragraph

3)

50-350,251/89-52-07,

NCV.

Failure

to incorporate

required testing into

plant procedures

for

ICW isolation valves

4-4882

and 4-4883 to

TPCW heat

exchangers.

(Paragraph

3)

50-250,251/89-52-08,

URI.

Followup

on investigation of

NCR 86-421 being

closed without required, actions

being completed.

.(Paragraph

4)

50-250,251/89-52-09,

URI.

Followup

on

licensee's

corrective

actions

regarding failure to establish

TS required fire watch in time following

Auxiliary Building evacuation.

(Paragraph

9)

Acronyms

and Abbreviations

ADM

AFW

ANSI

AP

ASME

BAST

CFR

cpm

CSP

CVCS

DBA

EAP

EDG

EOF

EP IP

ES

FFD

FPL

FSAR

GE

GOP

gpm

HHSI

HP

HPN

ICW

IFI

Administrative

Auxiliary Feedwater

American National

Standards

Institute

Administrative Procedures

American Society of Mechanical

Engineers

Boric Acid Storage

Tank

Code of Federal

Regulations

c'ount per minute

Containment

Spray

Pump

Chemical

and

Volume Control

System

Design Basis Accident

Employee Assistance

Program

Emergency

Diesel

Generator

Emergency Operations Facility

Emergency

Plan

Implementing

Procedures

Engineered

Safeguards

Fitness for Duty

Florida Power

8 Light

Final Safety Analysis Report

General Electric

General

Operating

Procedure

Gallons

Per Minute

High Head Safety Injection

Health Physics

Health Physics

Network

Intake Cooling Water

Inspector

Followup Item

17

IR

IST

LC

'CO

LER

LHSI

LRP

MCC

MOV

MP

MT

NCR

NCV

NPO

NRC

ONOP

OOS

OP

OSP

PC/M

PIV

PM

PMI

PS-N

PUP

PWO

QA

QC

QI

RCO

RCP

RCS

SE

SG

SI

SNPO

STA

Tavg

TPCW

TPNP

TS

TSA

URI

VCT

WMT

Inspection

Report

Inservice Testing

Load Center

Limiting Condition for Operation

Licensee

Event Report

Low Head Safety Injection

Liquid Release

Permit

Motor Control Center

Motor Operated

Valve

Maintenance

Procedures

Monitor Tank

Non-conformance

Report

Non-Cited Violation

Nuclear Plant Operator

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of Service

Operating

Procedure

Operations

Surveillance

Procedure

Plant Change/Modification

Post Indicator Valve

Preventive

Maintenance

Preventive

Maintenance

Instrumenta

Plant Supervisor

Nuclear

Procedure

Upgrade

Program

Plant Work Order

Quality Assurance

Quality Control

Quality Instruction

Reactor

Control Operator

Reactor

Coolant

Pump

Reactor

Coolant

System

Safety Evaluation

Steam Generator

Safety Injection

Senior Nuclear Plant Operator

Shift Technical

Advisor

Temperature

Average

Reactor

Coolan

Turbine Plant Cooling Water

Turkey Point Nuclear Plant

Technical Specification

Temporary

System Alteration

Unresolved

Item

Volume Control

Tank

Waste Monitor, Tank

tion

t System

~ I

I