ML17347B544
| ML17347B544 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 01/22/1990 |
| From: | Butcher R, Mcelhinney T, Orlenjak R, Schnebli G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17347B542 | List: |
| References | |
| 50-250-89-52, 50-251-89-52, NUDOCS 9002010246 | |
| Download: ML17347B544 (28) | |
See also: IR 05000250/1989052
Text
1P,S REG(g,
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
lf
Report Nos.:
50-250/89-52
and 50-251/89-52
Licensee:
Florida Power
and Light Company
9250 West Flagler Street
Miami,
FL
33102
Docket Nos.:
50-250
and 50-251
Facility Name:
Turkey Point
3 and
4
License Nos.:
and
Inspection
Conducted: 'ece
ber 2,
1989 through
December
22,
Inspectors-:- ~
.
r-c- ~ c
R.
C.
cher,
nior
R
i ent Inspector
Mc-iZ.
T.
F.
cElhinne,
Resi
ent Inspector
~r
l c.i'~
G. A.
bli, Resid
t Inspector
Approved by:
R.
.
rlenjak,
ection
Ch
f
Division of Reactor Projects
1989
Date Signed
Date Signed
Date Signed
/8~
'Pd
D te Signed
SUMMARY
Scope:
This routine resident
inspector
inspection
entailed direct inspection
at the
site
in the
areas
of monthly surveillance
observations,
monthly maintenance
observations,
operational
safety,
fitness for duty training and plant events.
Results:
There
was
one violation with two examples,
two URIs**, four IFIs, and
two NCVs,
identified.
Also,
the
residents
expressed
a
concern
regarding
two
recent
events
that resulted
from operators'nattention
to detail
and the fai lure to-
maintain communications
during
EDG runs which was
a contributing factor in one
of the events.
e
" Unresolved
Items
are
matters
about
which more information is required to
determine
whether they are acceptable
or may involve violations or deviations.
. 900i22
pgp
QQIOCK
Q
50-250,251/89-52-01,
IFI.
Excessive
acceptable
leak rate
through fire
protection-PIV.
(Paragraph
2)
50-250,251/89-52-02,
IFI.
Modify procedures
to ensure
personnel
notified
of site evacuation
alarm
and evacuation
has occurred.
(Paragraph
7)
50-250,251/89-52-03,
IFI.
Verification of tygon
tubing indication for
BAST level indicator channel
check.
(Paragraph
7)
50-250,251/89-52-04,
IFI.
Initiation of
PM requirements
to prevent lint
accumulation
in laundry room.
(Paragraph
9)
50-250,251/89-52-05,
Violation,
two
examples.
Failure
to
follow
procedures
resulting in inadvertent
release
of liquid waste
from the
B. MT
(paragraph
9) and failure to follow procedure resulting in the
B
EDG speed
droop not being adjusted during
a Surveillance Test.
(Paragraph
5)
50-250,251/89-52-06,
NCV.
Failure to maintain
RCP seal injection throttle
valve closed resulting
in
an inadvertent 'increase
in
RCS level while in
Mode 5.
(Paragraph
3)
50-250,251/89-52-07,
NCV.
Failure
to incorporate
required testing
into
plant procedures
for ICW isolation valves
4-4882
and
4-4883 to
TPCW heat
exchangers.
.(Paragraph
3)
50-250,251/89-52-08,
~
Followup
on investigation
of
NCR 86-421 being
closed without required actions
being completed.
(Paragraph
4)
50-250,251/89-52-09,
URI.
Followup
on
licensee's
corrective
actions
regarding failure to establish
TS required fire watch in time following
Auxiliary Building evacuation.
(Paragraph
9)
REPORT DETAILS
Persons
Contacted
Licensee
Employees
T. Abbati el 1 o,
equal ity Assurance,
Supervi sor
J.
W. Anderson, guality Assurance
Supervisor
J. Arias, Technical Assistant to Plant Manager
"L. W. Bladow, equality Assurance
Superintendent
R.
M. Brown, Health Physics
Supervisor
J.
E. Cross,
Plant Manager - Nuclear
R. J. Earl, guality Control Supervisor
T. A. Finn, Assistant Operations
Superintendent
S.
M. Franzone,
Lead Engineer
S.
T. Hale,
Engineering Project Supervisor
- K. N. Harris, Vice President
G. Heisterman,
Electrical Assistant
Superintendent
- RE J. Gianfrencesco,
Assistant
Maintenance
Superintendent
~V. A. Kaminskas,
Technical
Department
Supervisor
J.
AD Labarraque,
Senior Technical Advisor
G. Marsh,
Reactor
Engineering
Supervisor
- R. G. Mende, Operations
Supervisor
"L. W. Pearce,
Operations
Superintendent
D. Powell, Regulatory
and Compliance Supervisor
K. Remington,
System
Performance
Supervisor
G.
M. Smith, Service
Manager - Nuclear
F.
H. Southworth,
Assi stant to Site Vice President
R.
N. Steinke,
Chemistry Supervisor
J.
CD Strong,
Mechanical
Department
Supervisor
"G.
S. Warriner, guality Control, Supervisor
M. B. Wayland,
Maintenance
Superintendent
J.
D. Webb, Assistant Superintendent,
Planning
and Scheduling
Other
licensee
employees
contacted
included
construction
craftsman,
engineers,
technicians,
operators,
mechanics,
and electricians.
- Attended exit interview on December '22,
1989.
Note:
An Alphabetical Tabulation of acronyms
used in this report is
listed in paragraph
11.
Followup on Items of Noncompliance
(92702)
A review
was
conducted
of the following noncompliances
to assure
that
corrective actions
were adequately
implemented
and resulted
in conformance
with regulatory
requirements.
'erification
of corrective
action
was
achieved
through record reviews,
observation
and discussions
with licensee
personnel.
Licensee
correspondence
was evaluated
to ensure
that the
e
'responses
were timely and that corrective actions
were implemented within
. the time periods specified in the reply.
(Closed) Deviation 50-250,251/88-36-02.
Failure to have
a test
program
as
required
by the
FSAR to demonstrate
conformance
to design
and
system
readiness
requirements
for the Fire Protection
System.
On
October
29,
1988,
an event
occurred
where
a portion of the fire main could not
be
isolated
due to leaking PIVs.
This condition resulted
in both fire pumps
being
declared
OOS.
The
licensee
in
response
to this
event
issued
Surveillance
Procedure
Fire Main Post
Indicator
Valve
Leak
Test
and
System
Flush,
dated
June
29,
1989.
The inspector
reviewed
the
procedure
and found the licensee's
method for determining
PIV leakage
to
be acceptable
for those
leak rates
less
than
50
gpm.
The basis for the
maximum allowable
leakage
rates
for the
specific fire main isolation
valves
identified
in
Enclosure
1 of the
procedure,
were
established
through
the
use of
a computer
model.
The
computer
model
evaluates
the
various sprinkler system
demands,
hose
stream flow, and pressure
require-
ments,
flow paths,
fire
pump
flow and
pressure
requirements
and
then
calculates
the
remaining
system
flow which could
be lost due to system
leakage
without
the fire
suppression
(water)
system
being
declared
The inspector
reviewed the computer
model calculation results
for PIV-23 and PIV-33,
and
found the results
to
be reasonable,
based
on
fire suppression
system
water flow demands
in the event that
a fire were
to occur concurrent
wi,th
a pipe break requiring
PIV-23 or PIV-33 to
be
isolated.
The inspector
in reviewing,
O-OSP-016.38,
found the five gallon
bucket
and stop watch leak rate measuring
method f'r leak rates
less
than
50
gpm to
be feasible.
However, for leak rates
in excess
of 50
gpm this
, method
could not
be easily
implemented.
For example,
PIV-33
has
a leak
rate of 590
gpm, this would require
118 five gallon 'buckets of water to be
collected
in
a
one
minute
time frame.
In response
to this concern
the
.
licensee
initiated
a request
for -procedure
review
and
provided
a draft
revision of procedure
O-OSP-016.30
to
the
inspector
for review.
The
licensee
draft'rocedure
includes
provision for calculating
flows in
excess
of 50
gpm using data gained
by Pitot Tube
Flow measurements.
The
inspector
agrees
that
the
l.icensee
through
the
implementation
of this
revised draft test
procedure
can
demonstrate
system
design
conformance.
This item is closed.
However, the inspector is still concerned
that with
established
acceptable
leak rates
in excess
of the Jockey
Pump Capacity
and with
a pipe break in the
underground fire main, both fire pumps
may
still have to
be placed
in order
to facilitate repairs.
This is
identified as IFI 50-250,251/89-52-01,
exce'ssive
design acceptable
leakage
rates
through
PIVs may require total fire suppression
system to be placed
.
OOS to facilitate repairs
in the event of fire main pipe break.
(Closed) Violation 50-250,251/88-21-01.
Concerning
the Failure to Follow
Procedure
to Place Transfer Switches
on Channel
IV for Steam Generator
"B"
Testing.
In order to prevent recurrence,
the licensee
modified procedures
of this nature
during which incorrect
channel
selection
could place
the
unit in a transient to have the channel
selections
independently verified
by
a qualified operator.
In addition,
identification labeling
of the
subject
equipment
was modified to reflect the protection
channel
numbers.
This item and
LER 50-251/88-10,
(discussed
in paragraph
4) are closed.
(Closed)
Violation
50-250,251/89-12-03.
Failure
to fol low
procedur es
resulting
in
valve
201B
being
open
and
draining
water
to
the
containment
sump.
The licensee,
in response
to this violation, performed
a review of procedure
AP-0103.4,
In Plant
Equipment
Clearance
Orders,
to
determine
procedure
adequacy with respect
to vent and drain
hose install-
ation and vent/drain valve manipulations.
In order to prevent recurrence,
the
licensee
revised
procedures
3/4-0P-41.8,
Filling and
Venting
The
and 3/4-OSP-041. 1, Reactor
Coolant
System
Leak Rate
Calculation.
Procedure
3/4-OSP-041. 1,
was
revised
to incorporate
the
requirement
to visually
inspect
vent
and
drain valves'ith
hoses
connected
to assure
no
leakage
is occurring.
In addition,
the inspector
verified that procedure
3/4-0P-41.8
was
revised
to require that
whenever
RCS 'filling and
venting
operations
are
occurring that
one
containment
pump
and
one
channel
of
level
indication
be
The
inspector
found the licensee's
actions
in response
to this violation, to be
satisfactory.
This item is closed.
(Closed)
Violation
50-250,251/89-18-01.
Fai lure
to
fol low
procedure
resulting
in
the
inadvertent
actuation
of Train
A Safeguards.
The
licensee,
in response
to this violation, placed
warning
signs
inside
the
safeguard
racks of both units
and at the
power supply breakers
to these
racks.
The warning signs inside the safeguard
racks state that installing
fuses
FU4 or
FU3
may result
in
an
SI being
generated.
This sign also
references
that
procedure
3/4-0NOP-049,
Re-energizing
Safeguards
Racks
After Loss of Single
Power
Supply,
should
be utilized when installing
these
fuses.
The sign at the
power
supply
breakers
identifies
to
the
operator that closing these
breakers
can also result in an SI signal.
In
addition,
the licensee
revised the standard
clearance, for this activity in
the plant clearance
network to require that procedure
3/4-ONOP-049 is to
be
used
when releasing
clearances
associated
with the
safeguards
racks.
The inspector
found the licensee's
corrective actions associated
with this
event to be satisfactory.
This item is closed.
Followup
on
Inspector
Followup
Item(s),
Inspection
and
Enforcement
Information Notice( s),
IE Bulletin(s) (information only), IE Circular(s),
and
NRC Request(s)
(92701).
(Closed)
URI 50-250,251/88-11-01.
Evaluate
Licensee's
Method of Testing
Check
Valves to
Meet
the
Requirements
of
Code
Section
XI.
The
inspector
reviewed
OP-0209. 1,
Valve Exercising
Procedure,
dated
May 17,
1989,
to determine, that
LHSI pressure
boundary isolation
4-876A,
B, and
C, are included in their
Valve Exercising
Program.
These
valves
are classified
as
valves
which cannot
be exercised
during plant
.operations
and
have
been
included in Appendix
B to OP-0209 '
as valve
which are
required to
be exercised full open
whenever
a unit is in Cold
Shutdown.
The inspector
also verified that the licensee
had developed
a
method for determining
the flow split between
v'alves
4-876B
and
C,
and
incorporated
the
method
into the
procedure.
The licensee's
corrective
actions
and
code
test
requirements
associated
with
check
.valves
is
consistent with the requirements
of ASME Boiler Pressure
Code,
Section XI,
Division I,
Subsection
IWV,
1980 Edition through Winter
1981
Addenda;
IWV-3520, Tests for Check Valves.
This item is closed.
(Closed)
URI 50-250,251/89-12-02.
This item concerned
RCP seal injection
throttle valve 4-297A being
opened contrary to
GOP 4-305,
Hot Standby
to
. Cold Shutdown.
This resulted
in
an
increase
in the reactor, drain
down
water level
with Unit
4 in
Mode
5.
Investigation
revealed
that
work
needed
to
be
done
on
4-297A during the outage'herefore,
the clearance
boundary
was modified and the tag
on 4-279A was
removed to allow the work
to
be
done.
When
the
maintenance
was
completed,
the
clearance
was
released
prior to re-tagging
and reclosing
4-279A allowing water from the
CVCS to enter
the
RCS through the
RCP.
The Unit 4
RCO noted the increase
in level
and
promptly identified the
source
of inleakage.
Valve 4-279A
was closed
and tagged
as required.
The fai lure to reclose
and tag 4-279A,
as specified
by
GOP 4-305, after maintenance
was
completed
constitutes
a
violation of
TS 6.8. 1.
However,
this violation
meets
the criteria
specified in
Appendix
C,
Section V.A,'herefore,
no notice of
violation will be
issued.
The
licensee
was
in the
process
of and is
continuing to'eview the
equipment
clearance
procedure
and training of
personnel
to prevent recurrences.'his
item is closed
and will be tracked
as
NCV 50-250,251/89-52-06.
(Cl osed)
50-250,251/89-24-03.
Resoluti on
of
Document
Contr ol
Discrepancies.
During
the
same
time
frame
the
document
control
discrepancies,
noted
in
NRC
IR 89-24
were identified,
the
licensee
was
conducting
a
QA Audit in the
same
area.
The
inspector
reviewed
the
results
of
QA Audit Report
QA-O-PTN-89-988,
dated
May 23,
1989,
which
covered
the audit conducted
on May 11,
1989 thru May 22,
1989, in the area
of Document Control.
Based
on the inspectors
review,
the
scope
of the
document discrepancies
identified by
NRC IR 50-250,251/89-24
were included
in the findings of the licensee's
audit report.
The inspector
reviewed
the
response
to the audit report
and QI-6-PTN-1,
Document Control, dated
August 17,
1989,
and
AP 0190.86,
Document Control, dated October 27,
1988.
The inspector
found response
to this audit report to be satisfactory
and
the
scope
of the
QI was consistent
wi,th the
scope
of the
AP governing
document control.
This item is closed.
(Closed)
IFI
50-250,251/88-30-06.
Corrective
Actions
to
Prevent
Overload
From
ICW
Pump
Auto Start
During'ccident
Conditions.
The
licensee
implemented
PC/M 88-393,
ICW Overcurrent Trip, which modified the
control
circuits
of
the
ICW
pumps
to
defeat
the
overcurrent trip
auto-start
interlocks
between
the
pumps.
This
modification,
as
implemented,
prevents
the train "B" EDG from potentially being overloaded
during
a
DBA concurrent
with
a loss of off-site power.
The inspector
reviewed
the
PC/M
and
verified this
modification
was
completed
on
November
17,
1988. This item is closed.
(Closed)
IFI 50-250,251/88-39-02.
Resolution of Root
Cause
for Unlanded
Spade
Connection
in the
EDG Control Panel.
The. licensee,
under
PWO 5390,
ER69 relanded
a pair of wires to the
ES 200
relay and the
EZ
40
relay.
The
cause
of this condition
was attributed to the routing
and
pulling of
cable
B4B0698P
inside
the
control
panel.
During
the
installation
of this cable,
the
cable
rubbed
up against
the affected
stake-on
push type lugs,
causing
these
wire connections
to
become
loose.
The inspector
agrees this was the most probable
cause for this condition.
This item is closed.
(Closed) IFI 50-250,251/88-40-03.
Followup on Licensee's
Determination of
the
Cause
For
Leakage
Through
Seal
Table
Conduit at J7
and J12.
The
licensee
had Westinghouse
perform
a failure analysis
on the Unit 3 leaking
conduit
guide
tubes.
The
inspector
reviewed the Westinghouse
Analysis
dated
March 13,
1989.
The analysis
concluded that the type of
cracking
observed
is
indicative
of
transgranular
stress
corrosion
cracking.
In addition,
the analysis identified that the localized pitting
on
the
shoulder
and
socket
outside
diameter.
surfaces
is indicative of
attack
from a corrodant
such
as chlorides.
The metallographic analysis of
the
fracture
face
and
the
crack tip region
revealed
were
present.
This chloride contamination,'long
with the subject
tubes
being
wetted
from the
leaks
observed
on the
swage
lock fittings., coupled with
the
stresses
from the
service
pressure
and
from the
cold
worked
microstructure
promoted
this
transgranular
stress
corrosion
cracking
failure.
The cracks
propagated
from this outside diameter
surface
in the
shoulder
and
socket
region to the. inside diameter.
The inspector
agrees
with the results of the licensee's
analysis.
This item is closed.
(Closed)
URI 50-250,251/89-45-05.
This
item
concerned
the failure to
perform quarterly
IST for
ICW isolation valves
4-4882
and
4-4883 to the
TPCW heat
exchangers.
The
cause
of this
event
was
determined
to
be
personnel
error.
0190. 15,
Plant
Changes
and Modifications
(PC/M),
Figure J,
System Acceptance
Turnover
Sheet,
required
the
PUP coordinator
to list all procedures
not required
for
system
acceptance/turnover,
but,
required revision.
This section
.was
marked
N/A by the
PUP coordinator.
The need to revise
OP 209. 1, Valve Exercising Procedure,
was identified by
PUP
on October 26,
1988'n June
27,
1989,
a Request for Procedure
Review
was initiated by
PUP group to revise
OP 209. 1.
However, during the review.
process,
comments
concerning
test
frequencies
were not
resolved
at
the
reviewer level.
This
was
not elevated
to higher levels of management.
Therefore,
the testing
was not done prior to the
due date
of August
1,
1989.
The failure to
perform
the
ASME,
Section
XI, testing
of valves
4-4882
and
4-4883,
constitutes
a violation of
The inspectors
determined
this violation
met
the criteria
specified
in
Appendix C, Section
G. l. for a Licensee Identified NCV.
The basis for the
determination
was
as follows:
(a) the licensee identified the 'violation,
(b) the violation was classified
as Severity Level IV, (c) the event
was
reported
to
the
NRC via
LER 50-251/89-13,
(d)
the
licensee
initiated
corrective
" actions
which included
adding
the
valves
to
OP
0209. 1
on
October
24,
1989,
counseling
the
personnel
involved
and .initiating
a
review of procedures
requiring revision for PC/Ms to identify any other
needed
procedure
changes,
(e) the violation,was
not willful and,it could
not
have
been
prevented
by corrective actions for,a previous violation.
The inspectors. mentioned
in IR 50-250,251/89-45,
other recent
examples
of
failure to incorporate
design
requirements
into plant procedures.
The
root causes
for those
events
was inadequate
administrative controls,
where
in thi s
case,
the
administrative
controls
were
adequate
but
were
not
implemented.
Therefore,
the
corrective
actions
for
the,
previous
violations
would
not
have
prevented
this
occurrence.
50-250,251/89-45-05
is closed
and this
item will
be
tracked
as
50-250,251/89-52-07.
(Closed)
IFI 50-250,251/89-12-01.
Possible
Improper Oil Level in the
Governor.
The
licensee,
in
response
to this
item,
revised
the
PWO
guidance
associated
with checking
the oil levels
in the
AFW governors.
The
guidance
presently
utilized provides
a definition with regard
to
normal
levels
under
standby
and
operating
conditions.
The
inspector
reviewed
PWO
69-8207,
69-7458,
and
69-7459
and verified this
revised
guidance
was being properly incorporated
in the
PWO work descriptions.'n
addition,
the
licensee
incorporated
caution
notes
into
the
surveillance
procedures
with regard to the actions to be taken if the oil
level in the governor is not within its normal level range.
The inspector
reviewed
3-OSP-075. 1,
and
4-OSP-075. 1,
both
dated
July ll,
1989,
and
verified this guidance
was properly incorporated
into these
procedures.
The inspector
found the licensee's
corrective actions
to be satisfactory.
. This item is closed.
(Closed)
IFI 50-250,251/89-18-03.
Recurrence
of Voids in the
~
The
licensee
performed
an
investigation
of
the
sudden
pressurizer
level
decreases
which occurred
onJanuary
25,
1989,
and March 9,
1989, while the
reactor
was in
Mode
5, depressurized
and vented.
The inspector
reviewed
the
results
of
the
licensee's
investigation.
This
investigation
determined that
a gradual
increase
in pressurizer
level occurred prior to
each
event
along
with
a
subsequent
pressurizer
level
decrease
of
approximately
2.4%.
The licensee
determined this condition is indicative
of dissolved
gas being released
into the reactor vessel
and forming
a void
in the reactor
head area.
The gas formation in the
head
area is caused
by.
the nitrogen cover gas
on the
VCT being entrained
by the charging flow and
being
released
when
the
flow velocity
and
pressure
decreases
in the
, reactor.
The
licensee's
investigation
also
determined
that
venting of the reactor
head
area
is restricted
by the resistance
of the
head vent orifice and the loop seal
which is incorporated
in the head vent
system
design
configuration.
Based
on this
investigation it
can
be
concluded that the increase
in pressurizer
level is
a result of gas void
formation
in the
reactor
head
area
and
the
sudden
drop in pressurizer
level
can
be attributed to sudden
venting of collected
gas in the reactor
head
area.
The
licensee
based
on
the
results
of their investigation
revised
procedures
3/4-0P-041.7,
Draining The Reactor Coolant System,
and
attachment
to
3/4-OSP-201. 1,
RCO Daily Logs.
The
inspector
reviewed
procedures
3/4-0P-041.7,
dated
June
29,
1989,
and
3/4-OSP-201. 1,
Attachment
7,
dated
June
29,
1989,
and
determined
the
investigation
recommendations
associated
with establishing
and maintaining
a reactor
head
vent path
had
been
incorporated.
In addition,
the
inspector
has
determined
the corrective
actions
are
satisfactory
and
reactor
vessel
level perturbations
under similar operating conditions which were present
on January
25
and
March 9,
1989,
should
be reduced
as
a result of 'these=-
actions.
This item is closed,
Onsite
Followup
and
In-Office Review of Written
Reports
of Nonroutine
Events
and
10 CFR Part 21 reviews (92700/90712/90713)
The
Licensee
Event Reports
and/or
10 CFR Part 21 Reports
discussed
below
were
reviewed
and
closed.
The
inspectors
verified
that
reporting
requirements
had
been
met,
root
cause
analysis
was performed,
corrective
actions
appeared
appropriate,
and
generic
applicability
had
been
considered.
Additionally, the inspectors
verified that the
licensee
had
reviewed
each
event,
corrective actions
were
implemented,
responsibility
for corrective
actions
not ful.ly completed
was clearly assigned,
safety
questions
had
been evaluated
and resolved,
and violations of regulations
or
TS conditions
had
been identified.
When applicable,
the criteria of
10 CFR 2, Appendix C, were applied.
(Closed)
50-250,251/P2186-03.
This deficiency
involved
damage
to
wire insulation for Limitorque
DC Motors manufactured
by Peerless-
Winsmith.
The failure mechanism
was attributed
to insulation
damage
due
to bending during field installation
and setup.
FPL experienced
a failure
of a Peerless
Winsmith
DC motor
on Unit 3
AFW Steam
Supply
MOV-3-1403,
in December
1986.
Root cause
analysis
determined
the lead wire failures
were due to mechanical
damage
during packaging,
shipping,
or installation.
The
licensee
performed
inspections
and testing
of all
the
subject
motors which indicated
no damaged
lead Hires.
NCR 86-421
was written to
address
this
problem.
Engineering
resolution
required
the
plant
to
replace
MOV-3-1403 with a qualified motor and to return
any
spare
motors
to the
vendor for lead wire sleeving.
The licensee identified two spare
motors with suspect
serial
numbers.
One spare
motor was in the Electrical
(}C locker and the other spare
motor was located in the nuclear warehouse.
The
NCR was
closed
out
due to MOV-3-1403 being
replaced
and
the
spare
motors
being returned to the vendor for electrical
lead replacement.
The
~ inspectors
verified that
MOV-3-1403'as
replaced
by
reviewing
the
completed
work order
and
performing
a field walkdown.
The
inspectors
could
not verify the
spare
motors
were
returned
to the
vendor.
The
licensee
determined
that this task
was not completed contrary to the
disposition.
One spare
motor
was still in the nuclear warehouse,
without
any
gC
hold
tags
to
prevent
field installation.
The
licensee
was
investigating
how the
NCR was closed without all of the required
actions
completed.
The inspectors will'ollowup on this investigation.
This item
will be tracked
as
URI 50-250,251/89-52-08.
(Closed)
50-250,251/P2185-02.
Concerning
a defect
in
TEC Model 914-1,
Acoustic Valve Flow Monitor Modules.
A Safety Evaluation
was conducted
by
the licensee
.and documented
in JPE-L-85-42,
dated
January
15,
1986.
The
evaluation
concluded
the concern
was not
a substantial
safety hazard.
The
inspectors
reviewed
the
and
O-PMI-041.5,
Safety
Valve, Position
Indicator
Instrumentation
Channel
S-6303 Calibration which performs, the
calibration
and functional testing of this system.
This item is closed.
(Closed)
LER 50-251/88-10.
Concerning
the Failure to Follow Procedure
to
Place
Transfer
Switches
on
Channel
IV for Steam
Generator
"8" Testing.=
This
issue
is
discussed
and
closed
in
paragraph
2,
Violation
50-251/88-21-01.
Thi s i tern i s closed.
Monthly Surveillance
Observations
(61726)
The
inspectors
observed
TS
requi red surveillance
testing
and verified:
The test procedure
conformed to the requirements
of the
TS,
testing
was
performed in -accordance
with adequate
procedures,
test instrumentation
was
calibrated,
limiting conditions for operation
were met, test results
met
acceptance
criteria requirements
and were reviewed
by personnel
other than
the
individual directing
the
test,
deficiencies
were
identified,
as
appropriate,
and
were
properly
reviewed
and
resolved
by
management
personnel
and
system restoration
was
adequate.
For completed tests,
the
inspectors
verified testing frequencies
were met and tests
were performed
by qualified individuals.
The
inspectors
witnessed/reviewed
portions
of
the
following test
activities:
3-0SP-050.2
Residual
Heat
Removal
Pump Inservice Test.
3-SMI-04. 16
Tavg and Delta - T Protection
Channel
T-3-412,
T-3-422,
and T-3-432 Analog Test.
O-OSP-074.3
Standby
Pumps
Availability Test.
O-OSP-023.1
Diesel Generator Operability Test.
On
December
21,
1989,
the operators
tested
the
B
EDG in accordance
with
0-OSP-023. 1, Diesel
Generator
Operability Test,
dated
June
22,
1989.
The
inspectors
noted
the
speed
droop setting
on the
EDG governor
was set at
zero.
Step
7.2.21
of the
procedure
required
the
operator
to set
the
governor
speed
droop control to
30 on the droop scale.
The
NPO notified
the Unit 3
RCO and the droop was set at 30 as required.
While setting the
droop,
the
EDG load decreased
to 900
KW which invalidated the test.
The
licensee
decided
to
run
the
EDG for one
hour
as
recommended
by the
manufacturer'.
After the
engine
was
shut .down,
the operability test
was
performed successfully.
The failure to set the
speed
droop as required
by
0-OSP-023. 1,
constitutes
a violation of
TS 6.8. 1.
This is the
second
instance of operators
inattention
to detail this inspection
period, with
the first being the release
of the incorrect liquid waste tank.
This item
is discussed
in paragraph
9.
The
inspectors
also
noted
that
constant
communications
were
not established during'his test.
Good communication,
between
the
RCO and
NPO could have prevented this problem from occurring.
The licensee
is considering
using
the Alternate
Shutdown
Communications
headsets
in
the
future.
This violation is
the
-second
example
of
50-250,251/89.-52-05.
6.
Monthly Maintenance
Observations
(62703)
Station
maintenance
activities of safety related 'systems
and
components
were
observed
and
reviewed
to ascertain
that
they
were
conducted
in
accordance
with approved
procedures,
regulatory guides,
industry codes
and
standards,
and in conformance with TS.
The following items
were considered
during this review,
as appropriate:
LCOs
were
met while
components
or
systems
were
removed
from service;
approvals
were
obtained
prior
to initiating
work;
activities
were
accomplished
using
approved
procedures
and
were
inspected
as applicable;
procedures
used
were
adequate
to control
the activity;
troubleshooting
activities
were
controlled
and
repair
records
accurately
reflected
the
maintenance
performed;
functional
testing
and/or
calibrations
were
performed prior to returning
components
or systems
to service;
gC records
were
maintained;
activities
were
accompli shed
by qualified
personnel
parts
and materials
used
were properly certified; radiological controls
were properly
implemented;
gC hold points
were established
and
observed
where
required;
fire
prevention
controls
were
implemented;
outside
contractor
force activities
were
controlled
in
accordance
with the
approved
gA program;
and housekeeping
was actively pursued.
The
inspectors
witnessed/reviewed
portions of the following maintenance
activities in progress:
Repair of 4-942Y cracked weld.
0
10
Troubleshooting
Unit 4 Containment
Personnel
Hatch Interlocks.
Repair of Unit 4 Main Condenser
Tube Leak.
Troubleshooting
3A HHSI pump breaker.
Replacing
prop spring in the
3A HHSI pump breaker.
On December
7,
1989,
the licensee identified
a cracked weld on the branch
connection
to drain
valve
4-942Y in the safety injection
system.
This
section of piping provides
a minimum recirculation
flowpath for the
for pump testing
and to protect the
pump in the event the
pump discharge
valve failed to
open
upon starting
the. pump.
The license'e
performed
an
engineering
assessment
of
operability
to
allow isolation
of
the
recirculation
flowpath to facilitate repair of the
cracked
weld.
The
repaired
wa's tested
satisfactorily
and the
system
was returned
to
normal configuration
on December
12,
1989.
No violations or deviations
were identified in the areas
inspected.
7.
Operational
Safety Verification (71707)
By observatio'n
and direct interviews,
verification
was
made
that
the
physical security plan was being
implemented.
Plant
housekee
in /cleanliness
conditions
and
implementation
of
p
g
radiological controls were observed.
Tours of the
intake structure
and diesel, auxiliary, control
and turbine
buildings were conducted
to observe
plant equipment
conditions
including
potential fire hazards,
fluid leaks
and excessive
vibrations.
The
inspectors
walked
down accessible
portions of the following safety
related
systems
to verify operability and proper valve/switch alignment:
The inspectors
observed
control
room operations,
reviewed applicable
logs,
conducted
discussions
with control
room
operators,
observed
shift
turnover s
and confirmed operability of instrumentation.
The
inspectors
verified the operability of selected
emergency
systems,
verified that
maintenance
work orders
had been
submitted
as required
and that followup
and prioritization of work was
accomplished..
The
inspectors
reviewed
tagout records, verified compliance with TS
LCOs
and verified the return
to service of affected
components.
A and
B
Control
Room Vertical Panels
and Safeguards
Racks
ICW Structure
4160 Volt Buses
and
480 Volt Load and
Unit 3 and
Platforms
11
Unit 3 and
4 Condensate
Storage
Tank Area
AFW Area
Unit 3 and
4 Main Steam Platforms
Auxi l i a ry
- Bui 1 di ng
The inspectors
reviewed the licensee's
test of the site evacuation
alarm.
Procedure-
0-OSP-200. 1,
Schedule
of
Plant
Checks
and
Survei llances,
requires
the
noted test
be
conducted
at
11:45
a.m.
every
Wednesday.
0-OSP-200. l.references
procedure
OP-0204.2,
Periodic
Tests,
Checks
and
Operating
Evolution.
Section
8.4.6
of
OP
0204.2,
lists
the
site
evacuation
alarm lights to check to ensure
proper light operation.
The
inspectors
positioned
themselves
outside
the
protected
area
and
near
personnel
trailers
and the construction tool
room to determine if the site
evacuation
alarm
was
audible.
The
alarm
was
barely
audible
in
some
locations
and inaudible at other locations.
The inspectors
reviewed the
security
procedure
SFI
6307,
Emergency
Procedures
Security
Force
Requirements,
and
although
Security
makes
a
sweep
of the
general
area
following the initiation of. a site evacuation
alarm, there is no specific
guidance
to
do
a .detailed building by building check to ensure
personnel
have
evacuated
the
area.
The
licensee
committed
to
revise
security
procedures
to ensure that all personnel
in the area
are
aware of any site
area
emergency
or general
emergency
declaration
and/or
a site evacuation
alarm.
Also, following any site
evacuation
alarm,
a
sweep
of the -area
(building by building) will be accomplished
to ensure all personnel
have
evacuated
as
necessary.
The modification of procedures
to accomplish
the
notification of personnel
of any site
emergency
and/or site
evacuation
will be IFI 50-250,251/89-52-02.
Other specific
areas
such
as the Scout
Camps, Air Force
Sea
Survival
Training
School,
recreation
areas,
boat
ramps,
and
the
cooling
canal
system
are
specifically
addressed
in
EPIP 20110, Criteria For and Conduct of Owner Controlled Area Evacuation,
and are accomplished
by detailed security procedures.
The inspectors
noted
a concern
regarding
the
use of
a level
hose
on the
BAST.
The licensee'ses
these
level
hoses
to perform the weekly channel
check required
by
TS 4. 1. 1,
item
14.
These
hoses
are
connected
to the
drain line at the bottom of each tank
and
are
routed
up the
side of the
tank where tape
marks are provided indicating percent level for the tanks.
The
channel
check is performed
in accordance
with
OP
0204.2,
Periodic
Tests,
Checks,
and
Operating
Evolutions.
The
procedure
directed
the
operator to compare
the control
room tank level indication with the local
indication.
The operator
may
use
the level
hose if the ultrasonic level
indicator is inoperable.
The operators
had
been
using the level
hose
due
.
to
the ultrasonic
indicators
not working properly for
some
time.
The
acceptance
criteria was 10:o'f span
between indicators
(685 gallons).
The
inspectors
questioned
how the
temporary
level indicators
were installed.
Drawing 5610-T-E-4505,
sheet
5, revision
5,
contained
a note mentioning
the
tygon tubing
used for local
level indication.
The tubing note
was-
added to the drawing in
1983 during
an as-built walkdown.
Investigation
by the licensee
could not find any engineering
documents
that approved
the
12
use of the tygon tubing for level indication.
The licensee
indicated that
the tank markings
would
be verified and the temporary
level indicators
will be controlled via the
TSA process.
The licensee
plans to repair the
ultrasonic level indicators during the next outage with vendor assistance.
The inspectors will followup the licensee's
actions to verify the accuracy
of the tank markings
and the control of the temporary installation.
This
item will be tracked
as IFI 50-250,251/89-52-03.
No violations or deviations
were identified in the areas
inspected.
Licensee
Fitness for Duty Training (TI 2515/104)
The resident
inspectors
attended
one licensee initial training session
for
supervisors
which
was
approximately
8
hours
in duration,
one. training
session
for general
employees
which was approximately
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> in duration
and
one followup training session
for supervisors
which was approximately
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />
in duration.
The licensee's
supervisory
and/or general
employee
training sessions
also qualify personnel
for escort duties.
Copies of the
licensee's
FFD program for the Nuclear Energy Department
were
used
as the
basis
for the training
session
with the stipulation
the
FFD program
was
still
under
Corporate
Nanagement
review
and
minor
changes
could occur
since the
FFD program is to be implemented
on January
3,
1990.
Personnel
are to
be notified of any
changes
made to the
FFD program
subsequent
to
the training.
Also discussed
was
the
and
when,
in
general,
an
.
employee
becomes
ineligible for the
EAP.
An
experienced
policeman,
associated
with
a
Vice/Narcotics
strike
force,
supplemented
the
instructors
and
was very effective in making employees
aware of the
need
for an
FFD program.
No deviations or violations were identified.
Plant Events
(93702)
The following plant events
were reviewed to determine facility status
and
the
need
for further
followup action.
Plant
parameters
were evaluated
during transient
response.
The significance
of the event
was
evaluated
along with the
performance
of the
appropriate
safety
systems
and
the
actions
taken
by the
licensee.
The
inspectors
verified that
required
notifications were
made
to the
NRC
~
Evaluations
were performed relative
to the
need for additional
NRC response
to the event.
Additionally, the
following issues
were
examined,
as
appropriate:.
Details
regarding
the
cause of the event;
event chronology; safety
system performance;
licensee
compliance
with approved
procedures;
radiological
consequences,
if any;
and proposed corrective actions.
On
December
2,
1989,
with Units
3
an'd
4 operating
at
100%
power,
the
Unit 4
RCO attempted
to fill the cold leg SI accumulators
using-the
4A HHSI
pump.
The
RCO noted that motor
amps went to zero approximately
one
second
after starting.
The
pump was declared
OOS and
a work request
was
13
initiated
for
electrical
maintenance.
Investigation
by
electrical
maintenance
revealed
a broken prop spring
on the
4KV breaker.
The spring
was replaced
and the
pump returned
to service
on
December
3,
1989.
The
licensee'ent
the broken prop spring to
a metallurgical
expert for failure
analysis.
The licensee
believes
that fatigue
was
the failure mechanism.
The breakers
for the
pumps
had experienced
a high number of cycles
compared
to the other
4KV breakers,
therefore,
the licensee
decided
to
replace
the
prop springs for the other three
pump breakers.
These
breakers
are General
Electric Magna Blast breakers.
GE recommended
that
a
modification to the breakers
be
done to
add
a
second
prop spring.
indicated this was not
a requirement but only a recommendation,
therefore,
continued
operation
with only
one
prop
spring
was
acceptable.
The
licensee
was considering
implementing this modification during
an
outage
of sufficient length.
On December
10,
1989, at 2:45 a.m., with Unit 4 at
100% power,
a unit load
reduction
was
commenced
due
to
a
main
condenser
tube
leak.
Load
was
'educed
to approximately
20% and the ruptured tube
and six adjacent
tubes
were
plugged.
The
unit
returned
to
100%
power
at
4:00
a.m.,
on
December
13,
1989.
On December
14,
1989, with Unit 3 at
100% power, the
3C
ICW pump failed to
start.
Investigation of the
pump breaker
revealed
the white light was out
and the charging springs
were discharged
which indicated
DC charging
power
was not available.
The licensee identified that the cause
was that closing
fuses
were not fully engaged.
The fuses
were
engaged
and
the
pump
was
cycled successfully
and returned to service later that day.
The licensee
checked
the
fuses
for,. t'e
other
4KV breakers
and
no
problems
were
identified.
On December
15,
1989, at 6:01 a.m., with Unit 3 at
100% power,
the
NPO was
in the
process
of hanging
a
clearance
on
the
3A=- HHSI
pump
4160 volt
breaker
3AA13,
when
the
3A HHSI
pump inadvertently started.
The Unit
3
RCO noted the
3A HHSI pump red
run light was lit and notified the
PS-N.
Normal plant conditions
were verified and since
RCS pressures
were normal,
'o SI flow to the reactor vessel
occurred.
The
3A HHSI
pump
was
secured
from the control
room at 6:08 a.m.
The
3A HHSI pump was placed in pull to
lock with the breaker closing fuses
removed
and
a caution tag
hung stating
to
keep
the
3A
pump
in pull to lock until electrical
department
completes
troubleshooting
and repair.
The licensee notified the
NRC of
a
significant
event
per
6:53
a.m.
Subsequent
investigation
has
led
the
licensee
to
conclude
the
NPO inadvertently
contacted
the
manual
close
button
on breaker
3AA13 while removing
the
control
power fuses inside the breaker
cubicle for the clearance.
On December'5,
1989,
at
1:47 p.m.,
a fire was reported
in the
laundry
room in the auxiliary building.
The fire team was dispatched
and the fire
extinguished
at
1:50
p.m.
The
cause
of
the fire
was
an
excessive
accumulation of lint on top of a dryer.
The dryer was turned
on and the
14
heaters
ignited the lint.
The local breakers
to the dryers were opened,
and cleaning of lint accumulation
was initiated.
The
STA report'f this
event
recommended
that periodic
inspection/cleaning
of the
dryers
be
.initiated as
a
PM measure.
The licensee's
actions
to 'prevent
recurrence
will be followed up as IFI 50-250,251/89-52-04.
On December
18,
1989, at 2:55 a.m;,
a
SNPO notified the
PS-N the
B MT had
been
inadvertently
released
rather
than
the
B
WMT as authorized
by
LRP
89-641.
The
MT capacity is 10,000 gallons versus
a
WMT capacity of 5,000
gallons.
The
SNPO
had received
the
LRP
and correctly
logged that
the
discharge
was to"be
from the
B WMT.
The
SNPO then obtained
procedure
OP
5163.2,
Waste
Disposal
System
-
Controlled
Liquid
Release
to
the
Circulating Water,
and proceeded
to follow Section
8. 1, Controlled Liquid
Release
from Monitor Tanks,
rather
than
Section
8.2,
Controlled
Liquid
Release
from
Waste
Monitor
Tanks
(Radwaste
Building).
Investigation
showed the
B MT had
been
sampled at 10:45 p.m.,
on December
17,
1989,
and
the
PS-N
then
requested
that
an
LRP
be
prepared
for the
B
MT.
A
comparison
of the
B
MT (LRP 642)
versus
the
B
WMT (LRP 641)
gave
the
following results:
B MT
B WMT
Specific Activity
Specific Activity (after
dilution-non-gaseous)
Specific Activity (after
Dilution-'gaseous)
R-18 Background
cpm
R-18 Setpoint
cpm
6.351E-7
4.071E-10
9.705E-11
3.9K
8.9K
1.057E-5
6.776E-9
1.404E-6
4.2K
10K
TS 6.8. 1 requires that written procedures
and administrative policies
shall
be established,
implemented
and maintained that meet or exceed
the
requirements
and
recommendations
of Appendix
A of
Regulatory
Guide 1.33'nd
Sections
5. 1
and
5.3 of ANSI N18.7-1972.
Section
5. 1 of
ANSI N18.7-1972 requires that procedures
be followed.
Operating
Procedure
5163.2,
Waste
Disposal
System
-
Controlled
Liquid
Release
to
the
Circulating
Water,
Section
8.2,
Controlled
Liquid Release
from
Waste
Monitor Tanks
(Radwaste
Building), provides di rections for the release
of
liquids from the
WMT.
Nuclear Chemistry procedure
NC-44, Preparation
of a
Liquid Release
Permit, provides instructions for preparation
of an
LRP for
a controlled radioactive liquid discharge
to the circulating water.
On
December
18,
1989,
a
liquid release
was
performed
per
Section
8. 1,
Controlled Liquid Release
from Monitor Tanks,
of
OP 5163.2,
resulting
in
the inadvertent
release
of the
B MT liquid waste for which no
LRP had been
issued.
The inspectors
determined
that this release
did not exceed
NRC
requirements.
Failure to follow procedure
OP 5163.2 to release
the
B WMT
will be identified as the first example of violation 50-250,251/89-52-05.
On December
18,
1989 the licensee
reported
an Unusual
Event in accordance
with Emergency
Plan Implementing
Procedure
20101, Duties of Emergency
E
V
0
0
15
Coordinator,
dated
November
7,
1989,
Category
20,
Loss
of Engineered
Safety
Features/Fire
Protection.
The
licensee
determined
that
on
December
1,
1989,
the hourly roving fire watch for the Auxiliary Building
'as
not performed at the 4:00 p.m.
and 5:00 p.m. intervals.
The Auxiliary
Building had been
evacuated
as
a precautionary
measure
due to an alarm
on
the plant gas
vent monitor
and
an air sample.
The roving fire watches,
which were in place to cover approximately
31 fire protection
impairments,
did not resume until the 6:00 p.m. interval.
TS 3. 14 required that
a fire
watch
patrol
be
established
within
one
hour
when
fire
detection
instrumentation
is lost.
The inspectors
were evaluating this event at the
end
of
the
inspection
period
and will followup
on
the
licensee's
investigation
and corrective actions.
This item will be tracked
as
50-250,251/89-52-09.
On
December
19;
1989, at 2:29 p.m., feeder breaker
41406
on the
4F
LC to
the
4E
MCC tripped.
This disabled'he
Unit
4 intake
screens
and
the
differential pressure
started
increasing.
A load reduction
was initiated
at
4:00
p.m.
and
power
was
reduced
to
89%.
Electrical
maintenance
restored
'power to the
4E
MCC and is initiating a clean
up of the
MCC to
prevent recurrence.
On
December
19,
1989,
at
5:45
p.m.,
the
Unit
4
RCO reported
high
conductivities with an
upward trend.
At 5:55 p.m.,
a load reduction
was
initiated to reduce
power to less
than
50% to facilitate
removing
the
water
boxes
from service.
= The
4B north, and
4B south water
boxes
were
initially removed
from service
but it was later determined
the
leak
was
most likely from the
4A .water
boxes.
The
4B north
and
4B south water
boxes
were
retur'ned
to service.
At 4:20 a.m.,
on
December
20,
1989,
a
load reduction to
30% was initiated.
The licensee is currently trying to
identify the source of the leak.
10.
Exit Interview (30703)
The
inspection
scope
and
findings
were
summarized
during
management
.
interviews
held throughout
the reporting period with the Plant Manager
Nuclear
and selected
members of his staff.
An exit meeting
was
conducted
on
December
22,
1989.
The
areas
requiring
management
attention
were
reviewed.
No proprietary
information
was
provided
to
the
inspectors
during the reporting period.
The inspectors
had the following findings:
50-250,251/89-52-01,
IFI.
Excessive
acceptable
leak rate
through fire
protection
PIV.
(Paragraph
2)
50-250,251/89-52-02,
IFI.
Modify procedures
to,ensure
personnel
notified
of site evacuation
alarm and evacuation
has occurred.
(Paragraph
7)
50-250,251/89-52-03,
IFI.
Verification of tygon
tubing
indication for
BAST level indicator channel
check.
(Paragraph
7)
50-250,251/89-52-04,
IFI.
Initiation of
PM requirements
to prevent lint
accumulation
in laundry room.
(Paragraph
9)
16
50-250,251/89-52-05,
"'Violation,
two
examples.
Failure
to
follow
procedures
resulting in inadvertent
release
of liquid waste
from the
B MT
(paragraph
9) and fai lure to follow procedure resulting in the
B
EDG speed
droop not being adjusted
during Surveillance
test.
(Paragraph-
5)
50-250,251/89-52-06,
NCV.
Failure
to
maintain
seal
injection
throttle
valve
closed
resulting
in
an
increase
in
level while in
Mode 5.
(Paragraph
3)
50-350,251/89-52-07,
NCV.
Failure
to incorporate
required testing into
plant procedures
for
ICW isolation valves
4-4882
and 4-4883 to
TPCW heat
exchangers.
(Paragraph
3)
50-250,251/89-52-08,
URI.
Followup
on investigation of
NCR 86-421 being
closed without required, actions
being completed.
.(Paragraph
4)
50-250,251/89-52-09,
URI.
Followup
on
licensee's
corrective
actions
regarding failure to establish
TS required fire watch in time following
Auxiliary Building evacuation.
(Paragraph
9)
and Abbreviations
ADM
ANSI
BAST
CFR
cpm
EP IP
gpm
ICW
IFI
Administrative
American National
Standards
Institute
Administrative Procedures
American Society of Mechanical
Engineers
Boric Acid Storage
Tank
Code of Federal
Regulations
c'ount per minute
Containment
Spray
Pump
Chemical
and
Volume Control
System
Design Basis Accident
Employee Assistance
Program
Emergency
Diesel
Generator
Emergency
Plan
Implementing
Procedures
Engineered
Safeguards
Florida Power
8 Light
Final Safety Analysis Report
General
Operating
Procedure
Gallons
Per Minute
High Head Safety Injection
Health Physics
Health Physics
Network
Intake Cooling Water
Inspector
Followup Item
17
IR
'CO
LER
LHSI
LRP
NRC
ONOP
OP
PC/M
PMI
PS-N
PUP
PWO
QI
RCO
SNPO
Tavg
TPCW
TPNP
TS
WMT
Inspection
Report
Inservice Testing
Load Center
Limiting Condition for Operation
Licensee
Event Report
Low Head Safety Injection
Liquid Release
Permit
Motor Control Center
Motor Operated
Valve
Maintenance
Procedures
Monitor Tank
Non-conformance
Report
Non-Cited Violation
Nuclear Plant Operator
Nuclear Regulatory
Commission
Off Normal Operating
Procedure
Out of Service
Operating
Procedure
Operations
Surveillance
Procedure
Plant Change/Modification
Post Indicator Valve
Preventive
Maintenance
Preventive
Maintenance
Instrumenta
Plant Supervisor
Nuclear
Procedure
Upgrade
Program
Plant Work Order
Quality Assurance
Quality Control
Quality Instruction
Reactor
Control Operator
Reactor
Coolant
Pump
Reactor
Coolant
System
Safety Evaluation
Safety Injection
Senior Nuclear Plant Operator
Shift Technical
Advisor
Temperature
Average
Reactor
Coolan
Turbine Plant Cooling Water
Turkey Point Nuclear Plant
Technical Specification
Temporary
System Alteration
Unresolved
Item
Volume Control
Tank
Waste Monitor, Tank
tion
t System
~ I
I