ML17347B120

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Insp Repts 50-250/89-18 & 50-251/89-18 on 890331-0428. Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Engineered Safety Features Walkdowns, Operational Safety & Plant Events
ML17347B120
Person / Time
Site: Turkey Point  
Issue date: 05/22/1989
From: Butcher R, Crlenjak R, Mcelhinney T, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17347B118 List:
References
50-250-89-18, 50-251-89-18, NUDOCS 8906080261
Download: ML17347B120 (19)


See also: IR 05000250/1989018

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MAR I ETTA ST R E E7, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/89-18

and 50-251/89-18

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-250

and 50-251

License Nos.:

DPR-31

and

DPR-41

Facility Name:

Turkey Point

3 and

4

Inspection

Conducted:

March 31,

1989 through April 28,

1989

Inspectors:~D

R.

C. Butcher,

Senior

Residen 'nspector

Da

e

S gned

l~L

~ ~~. se,

s

T.

F. McElhinney, Resident

Insp ctor

( WC.I.s.r-'-

$C

.,

G. A.

S

ebli

Resident

Insp ctor

Approved by

R.

.

rlenjak,

i

hief

Division of Reactor Projects

Da

e Signed

s

Date Si

ned

~

C7

te

gned

SUMMARY

Scope:

This routine resident

inspector

inspection

entailed direct inspection

at the

site

in the

areas

of monthly surveillance

observations,

monthly maintenance

observations,

engineered

safety

features

walkdowns,

operational

safety

and

plant events.

Results:

One violation was identified:

Failure to follow procedure

resulting

in the

inadvertent actuation of Train A Safeguards.

Two Inspector

Followup Items were identified:

Followup on licensee's

actions to prevent recurrence

of voids in the

RCS.

One

concern

was expressed

to licensee

management

regarding

the licensee's

program to ensure

availability of the Black Start Diesels.

This is also

identified as

an Inspector

Followup Item.

REPORT

DETAILS

Persons

Contacted

Licensee'mployees

J.

d.

A d

,

Q~

"J. Arias,

Sr

~ Technical Advisor to Plant Manager

  • L. W. Bladow, guality Assurance

Superintendent

J.

E. Cross,

Plant Manager-Nuclear

  • R. J. Earl, guality Control Supervisor

T. A. Finn, Training Supervisor

  • S. T. Hale,

Engineering

Project Supervisor

R. J. Gianfrencesco,

Maintenance

Superintendent

  • V. A. Kaminskas,

Technical

Department Supervisor

J.

A. Labarraque,

Senior Technical Advisor

R.

G.

Mende,

Operations

Supervisor

  • J.

S.

Odom, Site Vice President

  • L. W. Pearce,

Operations

Superintendent

J.

C. Strong,

Mechanical

Department

Supervisor

  • K. Van Dyne, Acting Regulatory

and Compliance Supervisor

M. B. Wayland, Electrical

Department Supervisor

J.

D. Webb, Operations - Maintenance

Coordinator

Other

licensee

employees

contacted

included

construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

"Attended exit interview on April 28,

1989

Note:

An Alphabetical Tabulation of acronyms

used in this report is

listed in paragraph

11.

Followup on Items of Noncompliance

(92702)

A review

was

conducted

of the following noncompliances

to assure

that

corrective actions

wer e adequately

implemented

and resulted

in conformance

with regulatory

requirements.

Verification of corrective

action

was

achieved

through record reviews,

observation

and discussions

with licensee

personnel.

Licensee

correspondence

was

evaluated

to

ensure

that

the

responses

were timely and that corrective actions

were

implemented within

the time periods specified in the reply.

(Closed)

Violation

50-251/87-46-01.

Failure

to

implement

approved

procedures

to control

the configuration of

a safety-related

system.

The

inspector

reviewed the licensee's

corrective actions

and verified that all

corrective actions

had been

completed.

The inspector verified that valve

3-937

had

been

removed

from the

system to prevent

inadvertent

closure.

Valve 4-937

was

removed previously.

The inspector also verified that the

valves

had

been

deleted

from

the

associated

operating

procedure

3/4-0P-064,

Safety Injection Accumulators.

This item is closed.

(Closed)

Violation 50-250,251/88-18-01.

Failure to follow procedure

in

that the

ONOP for Reactor

Control

System Malfunction was not referred to

with one

RPI reading greater, than

12 steps

misaligned with other

RPIs in

the

same

bank.

The inspector

reviewed

the licensee's

corrective actions

and verified that all corrective

actions

had

been

completed.

Procedure

3/4-OSP-201. 1,

RCO Daily Logs,

was

revised

to require

comparison

of the

RPIs to the step counters

and to calculate

the difference

between

the two.

This item is closed.

(Closed)

Yiolation 50-250,251/88-30-03.

Fai'lure to maintain

an audible

neutron

flux monitor

and

improper

use

of

a

procedure.

The

inspector

reviewed

the

licensee's

corrective

actions

and

verified that

all

corrective

actions

had

been

completed.

Procedure

3/4-0P-201,

Filling/Draining the

Refueling

Cavity

and

the

SFP Transfer

Canal

was

revised to add

an infrequent operation to raise

reactor

cavity level

and

procedure

3/4-OSP-201. 1,

RCO Daily Logs,

was revised to require

an audible

neutron

source monitor with a unit in Mode 6.

This item is closed.

(Closed)

URI 50-250,251/88-26-04.

Followup on personnel

access

control to

the

Emergency

Diesel

Generator

(EDG) area.

This event

was reviewed

by

q

Region II security

inspector

in inspection

report

50-250,251/88-31

and

resulted

in

a Notice of Violation and

impositon of civil penalty.

The

licensee's

corrective actions will be tracked

by the notice of violation.

This item is closed.

Followup on Inspector

Followup Items

( IFIs).

(Closed)

Inspector

Followup

Item

50-250,251/88-26-03.

Correction

of

nomenclature

errors

in Operating

Procedure

3/4-0P-094,

Containment

Post

Accident

Monitoring

Systems.

The

inspector

verified that

Procedure

3/4-OP-094

had

been revised to correct the identified nomenclature

errors.

This item is closed.

Onsite

Followup

and

In-Office Review of Written

Reports

of Nonroutine

Events

(92700/90712)

The

Licensee

Event

Reports

(LERs)

discussed

below were

reviewed

and

closed.

The inspectors verified that reporting requirements

had

been

met,

root

cause

analysis

was

performed,

corrective

actions

appeared

appropriate,

and generic applicability had

been considered.

Additionally,

the

inspectors

verified that

the

licensee

had

reviewed

each

event,

corrective actions

were implemented,

responsibility for corrective actions

not fully completed

was clearly

assigned,

safety

questions

had

been

evaluated

and resolved,

and violations of regulations

or TS conditions

had

been identified.

When applicable,

the criteria of

10 CFR 2, Appezdix C,

were applied.

(Closed)

LER 50-250/88-32.

Personnel

Error Results

in

Loss of Power to

Vital

Instrument

Bus

and

Automatic

Isolation

of

Control

Room

and

Containment

Ventilation.

This

event

was

reviewed

in inspection

report

50-250,251/88-39.

The

inspector

reviewed

the

licensee's

corrective

actions

and verified that all corrective

actions

had

been

completed.

Procedure

O-OP-003.3

was revised to require that the operator verify that

the inverter to

be de-energized

is not supplying

power

by checking

the

associated

ammeter prior to opening the breakers.

This item is closed.

(Closed)

LER 50-251/88-05.

Calibration of Nuclear Instrumentation

System

Power

Range

Detectors

Performed

Late

Due

to

Personnel

Error.

The

surveillance

was satisfactorily

completed

less

than

30 minutes following

the expiration of the grace period.

At the expiration of the grace period

the detectors

were declared

out of service

(OOS)

and

the unit entered

TS 3.0. 1 until the ~aillance

was completed.

The inspector

reviewed the

corrective

actions

implemented

by the licensee

and determined

they were

adequate

to preclude

future occurrences

of similar events.

This item is

closed.

(Closed)

LER 50-251/88-07.

Failure

o'f Source

Range

Neutron Flux Detector

Results

in

Subcritical

Reactor

Trip.

This

event

was'eviewed

in

inspection

report

50-250,251/88-21.

Source

Range

Detector

N-32

was

replaced

with

a

new

detector

and'

pulse

height

di scriminator

bias

potentiometer

was replaced

as

a preventive

measure.

This item is closed.

Complex Surveillance - Engineered

Safeguards

Test Review (61701)

The

inspector

reviewed

procedures

4-OSP-203. 1,

Train

A

Engineered

Safeguards

Integrated

Test,

dated April 3,

1989

and 4-0SP-203.2,

Train

B

Engineered

Safeguards

Integrated

Test,

dated

April

3,

1989.

The

procedures

were

verified

to

specify

appropriate

plant

conditions,

prerequisites

and

precautions.

The

procedures

had

received

the

appropriate

level of management

review and approval.

The above procedures

were

new in the

respect

that Train

A and Train

B tests

were

conducted

individually.

Previous tests

were conducted

on both trains concurrently.

The Train

A test

was

conducted

early

on April

14,

1989

and

several

equipment

problems

were identified, i.e

the

4C

feedwater

bypass

valve

FCV-4-499 failed to close

and the

sequence

time for load centers

4A and

4C

were

out

of tolerance

by

approximately

0.2

seconds.

Also,

not all

verifications

were

completed

due to

a five minute time limit on safety

injection

pumps

running

in recirculation.

The test

was

halted

and

maintenance

corrected

noted

discrepancies.

Train

A

was

successfully

retested

on April 14,

1989.

The Train

B test

was conducted

on April 15,

1989

and step 7.3. 15 failed because

the

containment

spray

pump

(B train)

did not actuate.

It was

found that the

B containment

spray

pump breaker

was not fully racked in.

After fully racking in the breaker,

the test

was

rerun successfully.

The acceptance

criteria were in accordance

with TS

and prescribed

a qualitative or quantitative

method for determining

the

results of the test.

Within the areas

inspected,

no violations or deviations

were identified.

Monthly Surveillance

Observations

(61726)

The

inspectors

observed

TS required

surveillance

testing

and verified:

That the test

procedure

conformed to the requirements

of the

TS, that

testing

was

performed

in accordance

with adequate

procedures,

that test

instrumentation

was calibrated,

that limiting conditions

for operation

(LCO) were met, that test results

met acceptance

criteria requirements

and

were reviewed

by personnel

other than the individual directing the test,

that

deficiencies

were identified,

as

appropriate,

and

were

properly

reviewed

and resolved

by management

personnel

and that

system restoration

was

adequate.

For completed tests,

the inspectors

verified that testing

frequencies

were met and tests

were performed

by qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

OSP-O41.4,

Overpressure

Mitigating System Nitrogen Backup

Leak and Functional -Test.

4-PMI-041.7,

RCS Temperature

Loop

B Protection

Channel

Set II

Calibration.

O-OSP-074.4,

Standby

Steam Generator

Feedwater

Pumps/Cranking

Diesels Test.

On April

5,

1989,

during

performance

of 3-0SP-041.4,

revision

dated

March 2,

1989,

Power

Operated

Relief Valve

(PORV)

455C failed to open.

The

PORV was declared

out of service

and

a Plant

Work Order

(PWO)

was

initiated.

Troubleshooting

identified that the

actuator

cover

assembly

was leaking

and the capscrews

were loose.

The capscrews

were retorqued to

228 inch-pounds

and the leakage

was

stopped.

The valve

was

subsequently

tested

satisfactorily

and

placed

back

in service.

This

same

problem

occurred

on October

2,

1988,

and is discussed

in

NRC inspection

report

50-250,251/88-30

as

Inspector

Followup

Item

50-250,251/88-30-02.

The

licensee's

corrective

actions

were to install

an ethylene-propylene

( EP)

diaphragm

in

the

PORV

actuator

and

to install

lockwashers

on

the

capscrews..

These

actions,

however,

did not

prevent

the

capscrews

from

loosening

again.

Another

problem

to

note

was that the

I&C root cause

engineers

were

not

made

aware

of the

recent

failure of the

actuator.

Therefore,

an

analysis

of the

as-found

condition

was

not

made.

The

inspectors

will

continue

followup

of

this

problem

via

IFI

50-250,251/88-30-02

'n

Apri,l

19,

1989,

the

licensee

performed

O-OSP-074.4,

Standby

Steam

Generator

Feedwater

Pumps/Cranking

Diesels

Test, for the

B Standby

Steam

Generator

Feedwater

Pump

(SSGFP).

This test

was required to be performed

during

each refueling

outage

in accordance

with Technical

Specification

(TS) section

4.21.

The

purpose

of this test

was to power the

SSGFP

from

the Cranking Diesels

and operate

the

pump to provide

feedwater

to the

Unit 4

steam

generators.

The Cranking Diesels

(Black Start)

and

SSGFPs

are not safety related,

however,

they provide

a backup

supply of electri-

city and feedwater to the nuclear units.

The licensee

experienced

problems

during the initial test

attempt.

The

operators

started

four cranking diesels

(nos.

1-4),

however,

no.

4 diesel

tripped and

none of the other diesels'reakers

closed

onto the dead bus.

A second

attempt

was

made

and this time only the 2, 3,

and

4 diesels

were

started

since

the

no.

1

diesel

had

an

outstatading

PWO for

the

auto-synchronizing circuitry.

The no.

4 breaker

closed

onto the

bus but

when the no.

3 breaker closed

a bus lockout on undervoltage

occurred.

The

test

was terminated

and electical

maintenance

began

troubleshooting

the

auto-synch circuitry.

A faulty relay

was

replaced

for the

no.

2 diesel

auto-synch circuitry and,a

run of the diesels

was, performed successfully.

The surveillance test

was run again

and the diesels

performed

as designed.

The

no.

2 breaker

closed first followed by no.

4 breaker

and

then

the

no.

3 breaker.

The

B SSGFP

was then started

and

feedwater

was

pumped to

the

Unit 4

steam

generators

until

a

level

i'ncrease

was

observed.

The

inspectors

raised

several

concerns

regarding

the operability of the Black

77>>77.

7

assumes

that

these

units

are well maintained

and available for nuclear

plant use following a loss of AC power.

The

licensee's

April

17,

1989,

letter

concerning

station

blackout

specifies that these diesels

are capable of being aligned to the emergency

buses

in approximately twenty minutes.

However,

based

on the observations

made

during this test,

the

inspectors

raised

concerns

to 'icensee

management

as to the availability of the diesels.

No violations or deviations

were identified in the areas

inspected.

7.

monthly Naintenance

Observations

(62703)

Station

maintenance

activities

on safety-related

systems

and

components

were

observed

and

reviewed

to ascertain

that

they

were

conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and

standards,

and in conformance with TS.

The following items

were

considered

during this review,

as appropriate:

That

LCOs were met while components

or systems

were

removed

from service;

that approvals

were obtained prior to initiating work; that activities

were

accomplished

using

approved

procedures

and

were

inspected

as

applicable;

that

procedures

used

were

adequate

to control

the activity;

that

troubleshooting

activities

were

controlled

and

repai r

records

accurately

reflected

the

maintenance

performed;

that

functional

testing

and/or

calibrations

were

performed

prior to returning

components

or

systems

to service; that

gC records

were maintained; that activities were

accomplished

by qualified personnel;

that parts

and materials

used

were

properly certified; that radiological controls were properly

implemented;

that

gC hold points

were established

and

observed

where required;

that

fire prevention controls

were

implemented;

that outside contractor

force

activities were controlled in accordance

with the approved

gA program;

and

that housekeeping

was actively pursued.

The

inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Repair of Unit 3 Sea]

Table Leaks.

Troubleshooting

No.

2 Cranking Diesel.

Repair Unit 3 Pressurizer

Power Operated Relief Valve Actuator.

48

RHR seal

heat exchanger

leak.

Troubleshooting

4B

Reactor

Coolant

Pump

high

bearing

temperature.

Repacking of 4B Intake Cooling Water

pump.

Due to the

problems

encountered

during the surveillance test of the

Black Start Diesels

(see

paragraph

6), the inspectors

held discussions

with responsible

licensee

personnel

and identified several

areas

of

concern:

(2)

The diesel

engines

are

maintained

by the

Nuclear

Mechanical

Maintenance

Department.

There

are

currently

two preventive

maintenance

procedures

in

use

for those

units,

MI

102014

(Black Start

Diesel

Generator Quarterly Preventive

Maintenance)

and

MI 102015 (Blackstart

Diesel

Generator

18 Month Preventive

Maintenance).

The electrical

portion of the diesel

generators,

including

the

associated

switch

gear

is

maintained

by

the

Nuclear Electrical

Department.

However, there

are currently

no

procedures

in effect for electrical

maintenance

on the units.

Since fossil

(non-nuclear)

unit

personnel

operate

the units,

deficiencies

with the units will be identified by non-nuclear

plant

personnel.

Although

def ici enci es

identified

by

the

non-nuclear

operators

are turned

over to nuclear

personnel

to

ensure

nuclear

PWOs

are

generated

to correct

the

problem,

the

inspectors

consider that the non-nuclear

operators

may not have

the "attention

to detail"

concept

for problem identification

that is instilled in the nuclear operators.

(3)

(4)

At present,

these

units

are

not

assigned

a

system

engineer.

Therefore,

the routine

system

walkdowns

required

by the

system

engineers

on

their

assigned

systems

is

not

normally

accomplished.

The

system

engineer

currently

assigned

the

Emergency

Diesel

Generators

has

taken it

upon

himself

to

periodically walkdown the cranking diesels,

however,

no formal

program or requirement

exi sts to ensure this is accompli shed

on

a routine basis.

r

The

only -required

surveillance

procedure

on

the

units

i s

O-OSP-074.4

which

loads

the

standby

steam

generator

feedwater

pumps onto the cranking diesels

every

18 months.

The licensee

stated that the non-nuclear plant normally runs the units weekly

to ensure availability.

However, there is

no formal requirement

or documentation

associated

with this.

(5)

During

the testing

witnessed

by the

inspectors,

deficiencies

were

noted

that

could

have

been

previously

identified

and

corrected if a

more

formal

program,

as discussed

in 1-4 above,

existed for these units.

These deficiencies

included:

Breaker

1W134 could not easily

be racked in by one person.

Wheels

were rusty

and the breaker

was hard to move in its

track.

, Lighting in the switch gear trailer and the engine trailers

is less

than adequate.

The

general

material

condition

of

.the

diesel s

and

switchgear

is

poor

compared

to

the

site's

emergency

diesels.

Diesels that were out of service (I and 2) were not listed

in t~~f=service

log.

During the initial performance

of the test these

two diesels

were also started.

Governor oil levels were in the low end of the sight glass.

Inappropriately rigged crankcase

pressure

indication

on the

engines

(tygon tubing and ruler).

Although the

Black Start

Diesels

installed at the site

were initially

under

the control of the fossil units for their use,

the nuclear units

also

take credit for

them

as

stated

in their

Diesel

Loading

Safety

Evaluation,

dated

June

12,

I986.

The units are not only used to power the

standby

feed

pumps via the "C" bus but can also

be

used to power the

"A"

'r

"B" busses

via the

"C" bus.

The evaluation

also

states

that

the

reliability analysis

assumes

that

these

units

are

well maintained

and

available for nuclear plant

use.

To ensure availability, maintenance

of

these

units

became

the

responsibility

of

the

Nuclear

Maintenance

Department.

Based

on

the

observ'ation

noted

during the testing

of the

units and the subsequent

discussions

with responsible

licensee

personnel,

the inspectors

consider

the licensee

should

have

a more in-depth program

for the maintenance,

surveillance,

and control of these units .

This wi 1 1

be identified as Inspector followup Item 50-250,251/89-18-02,

Followup on

licensee's

actions to ensure reliability/availability of the Black Start

Diesels.

No violations or deviations

were identified in the areas

inspected.

Operational

Safety Verification (71707)

The inspectors

observed control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room

operators,

observed

shift

turnovers

and confirmed operability of instrumentation.

The

inspectors

verified the operability of selected

emergency

systems,

verified that

maintenance

work orders

had been

submitted

as required

and that followup

and prioritization

of work was

accompli shed.

The

inspectors

reviewed

tagout records, verified compliance with TS

LCOs

and verified the return

to service of affected

components.

By observation

and direct

interviews, verification was. made

that

the

physical security plan was being

implemented.

Plant

housekeeping/cleanliness

conditions

and

implementation

of

radiological controls were observed.

Tours of the intake structure

and diesel, auxiliary, control

and turbine

buildings

were conducted

to observe

plant equipment

conditions

including

potential fire hazards,

fluid leaks

and excessive

vibrations.

The

inspector s

walked

down accessible

portions of the following safety

related

systems

to verify operability and proper valve/switch alignment:

A and

B Fmergency Diesel

Generators

Control

Room Vertical Panels

and Safeguards

Racks

Intake

Cool in~~~fructure

4160 Volt Buses

and

480 Volt Load and Motor Control Centers

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank Area

Auxiliary Feedwater

Area

Unit 3 and

4 Main Steam Platforms

On April 1,

1989,

a routine visual

inspection

of the Unit

3

seal

table

revealed

boron residue

on one of the fifty stainless

steel

guide tubes for

incore instrumentation.

The

leak

was approximately

one drop

per minute.

Further testing

has

shown indications

in other

guide tubes.

Preliminary

metallurgical

reports

from Westinghouse

have

concluded

the

indications

resulted

from transgranular

stress

corrosion

cracking.

The reports

also

indicate

the

defects

initiated

from the

outside

surface

and

was

most

likely the result

of chloride contamination.

The licensee

has efforts

under

way to determine

the

source

of the

contamination.

For further

information on this issue refer to Inspection

Report 50-250,251/89-22.

No violations or deviations

were identified in the areas

inspected.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need for further followup action.

Plant

parameters

were

evaluated

during transient

response

The significance

of the event

was evaluated

along with the

performance

of the

appropriate

safety

systems

and

the

actions

taken

by the

licensee.

The

inspector s verified that

requi red

notifications were

made to the

NRC.

Evaluations

were

performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were

examined,

as

appropriate:

details

regarding

the

cause

of the event;

event chronology; safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences,

if any;

and proposed corrective actions.

On March 31,

1989, at 1:50 p.m.,

the licensee

declared

a significant event

due to the

"ioss of emergency notification communications.

Both Unit 3 and

Unit 4 were shut

down

~

The commercial

telephone

system

was being

used

as

a

compensato

y measure.

The

Emergency

Notification

System

(ENS)

phone

failed

a

normal

co'mmunications

check.

The

ENS was restored to operation

at 10:10 p.m.

On April 9,

1989, with Unit 3 in Mode 5,

the

Reactor

Control Operator

(RCO) noticed pressurizer

level decreasing.

Printouts

showed that level

dropped

from

78.9X to

71.4%

in approximately

11

minutes.

The

RCO

increased

charging

flow and isolated

letdown which restored

pressurizer

level.

The

pressurizer

level

stabalized

and

an

investigation

was

conducted'to

identify any reactor coolant

system

leakage.

The Unit 3 pipe

and valve room, Residual

Heat

Removal

(RHR)

pump

rooms,

and the charging

pump

rooms

were

inspected

and

no

l'eakage

was identified.

Based

on all

indications,

the operators

determined that the most probable

cause

of the

decreased

pressurizer

level

was the collapsing of

a void in the reactor

vessel

head.

The gases

were formed

due to

a loop seal

in the

head

vent

piping.

The gas buildup forced water into the pressurizer

which resulted

in

a gradual

increasa ~u essurizer

level

over the previous

two days.

Eventually,

the

gas

pressure

overcame

the loop seal

enabling

the

head to

vent

and

the pressurizer

level

dropped.

After reviewing data

from the

previous

fourteen

days,

the licensee

believed that

a similar event

may

have occurred

on April 7,

1989.

A void was also

formed in Unit 4 on March 14,

1989, exhibited

by a

5% drop

in'ressurizer

level.

The inspectors will monitor the licensees

actions

to prevent recurrence

of voids in the

RCS.

This will be tracked via IFI

50-250,251/89-18-03.

On April 12,

1989, at 11:40 a.m.,

a significant event

was declared

by the

licensee

due to an inadvertent actuation of train A of Unit 4 safeguards.'

Reactor

Operator

was installing fuses

in safeguard

rack 43,

when

an

inadvertent

SI signal

was

generated.

All train

A safeguards

equipment

functioned

as

designed.

The licensee

has

a procedure

for accomplishing

the

re-energization

of safeguard

Racks.

The

operator

did not utilize

procedure

4-0NOP-049,

Re-Energizing

Safeguard

Racks After Loss of Single

Power Supply,

and the required precautions

prior to replacing

fuses

FU-3

and

FU-4

were

not

implemented.

The

licensee

is preparing

information

placards

to caution

operators

that

an

SI signal

can

be

generated

when

installing certain

fuses

and refers

to procedure

3/4-ONOP-049.

TS 6.8. 1

requires

written

procedures

be established,

implemented

and

maintained

that meet or exceed

the requirements

and

recommendations

of Section

5.3 of

ANSI N18.7-1972.

Section

5.3 of ANSI N18.7-1972

requires

nuclear

power

plants

be

operated

in

accordance

with written procedures.

Procedure

4-0NOP-049,

Re-energizing

Safeguard

Racks After Loss

of Single

Power

Supply,

provides

instructions for re-energizing

safeguard

racks without

initiating an inad'vertent

safeguards

actuation.

.On April 12,

1989,

the

operator installed fuses

in safeguard

rack 43 resulting in re-energization

of the rack and

an inadvertent actuation of Train A of safeguards,

without

following 4-ONOP-049.

The failure to follow procedures

for re-energizing

safeguard

racks will be identified as violation 50-250,251/89-18-01.

On April 21,

1989,

with both units in

a cold

shutdown condition,

the

licensee notified the

NRC of a significant event in 'accordance

with 10 CFR 50.72.b.2.iiiA.

The

event

concerned

the potential

loss

of all

three

charging

pumps

in the event of

a fire.

In the Appendix

R Safe

Shutdown

Analysis,

credit is

taken

for

one

charging

pump

per

unit

as

being

available for safe

shutdown.

This charging

pump is required to maintain

hot

standby

and

achieve

cold

shutdown

in the

event

of

a fire.

The

charging

pump takes

suction

from either the

Volume Control Tank (VCT) or

the Refueling Mater Storage

Tank

(RWST) through inter locked valves.

The

VCT valve

LCV-115C is normally

open

and

the

RWST valve

LCV-115B is

normally closed.

A fire postulated

in certain fire areas

could

cause

spurious closure of LCV-115C and loss of automatic function could prevent

opening of LCV-115B.

Should the charging

pump (which is assumed

available

for safe

shutdown)

be running,

and

a fire in a given area

cause

spurious

\\

10

closure

of

LCV-115B,

the pump'ould

be starved

of suction flow.

This

could result

in the inability of the

pump to perform its required

safe

shutdown function due,to

damage resulting

from flow starvation.

Credit is

taken in the Appendix

R Safe

Shutdown Analysis for an operator action to

mitigate the

adverse

effects of spurious

closure of LCV-115C.

However,

without

admini stra~~gnirols

or

a

permanent

design

change,

this

operator

action

may not

be

taken

in time to'revent

pump

damage.

The

licensee

plans

to

implement

the

following administrative

contr ols to

ensure

safe

shutdown capability:

a.

Establish

continuous fire watches

in Fire Areas

N (Charging

Pump

Room)

and

R

(Rod

Control

Equipment

Room),

per

Plant

Procedure

O-ADM-016.4, with

a

means

of direct

and

immediate

communication

to

the Control

Room.

As

a minimum, the fire watch is required in Fire

Area

N

when

Charging

Pump

B is

running,

and

Fire

Area

R

when

Charging

pumps

A

and

C

are

running.

However,

at

the

Plant's

discretion

and in order to provide operator flexibility, continuous

fire watches

may be established

during the operation of any

charging'umps.

Coordinate

with

Health

Physics

prior

to

establishing

continuous fire watch in fire Area

N.

b.

Upon detection

of

a fire in Fire Area

N or R, fire watch personnel

shall

immediately notify the Plant Supervisor

Nuclear (PSN).

Upon notification of a fire, Control

Room operators will immediately

secure

Charging

Pump

B if a fire is reported

in Fire Area

N and

either Charging

Pump

A or

C if a fire is reported

in Fire Area

R.

These

actions will preclude

damage

to the

charging

pumps

due

to

potential

loss

of suction.

This action will be

taken prior to

invoking

the

Hot

Standby

Procedure.

Charging

flow will then

be

reestabli shed with the alternate

charging

pump( s) to continue control

of plant operating

parameters.

d.

Change/revise

the applicable procedure(s)

and/or prepare

a temporary

procedure

to

enforce

the

requirements,

stated

herein,

until

a

permanent

plant modification is installed to remove the restriction.

10.

Exit Interview (30703)

The

inspection

scope

and

findings

were

summarized

during

management

interviews held throughout the reporting

period with the Plant. Manager

Nuclear

and selected

members of his staff.

An exit meeting

was conducted

on April 28,

1989.

The

areas

requiring

management

attention

were

reviewed.

No proprietary

information

was

provided to the

inspectors

during the reporting period.

The inspectors

had the following findings:

50-250,251/89-18-01,

Violation.

Failure to follow procedure resulting in

the inadvertent actuation of Train A Safeguards.

(Paragraph

9).

50-250,251/89-18-02,

Inspector

Fo1 l owup

Item.

Fol 1 owup

on licen see '

actions

to ensure reliability/availability of the

Black Start

Diesels.

(Paragraph

7).

50-250,251/89-18-03,

Inspector

Fol 1owup

Item.

Fol 1owup

on licensee'

actions to prevent recurrence

of voids in the

RCS.

(Paragraph

9).

Acronyms and Abbreviations

ADM

ANSI

AP

ASME

CCW

CFR

DP

ENS

FPL

FSAR

HHSI

ICW

IEB

IFI

LCO

LER

LIV

LOCA

MP

NRC

ONOP

OOS

OP

OTSC

P.C/M

PSN

PSP

QA

QC

RCO

RCP

RCS

RHR

SRO

TS

TSA

URI

Administr~

American National

Standards

In

Administrative Procedures

American Society of Mechanical

Component Cooling Water

Code of Federal

Regulations

Differential Pressure

Emergency Notification System

Florida Power

8 Light

Final Safety Analysis Report

High Head Safety Injection

Intake Cooling Water

Inspection

and Enforcement

Bul

Inspector

Followup Item

Limiting Condition for Operati

Licensee

Event Report

Licensee Identified Violation

Loss of Coolant Accident

Maintenance

Procedures

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of Service

Operating

Procedure

On the Spot

Change

Plant Change/Modification

Plant Supervisor

Nuclear

Physical

Security Procedures

Quality Assurance

Quality Control

Reactor Control Operator

Reactor

Coolant

Pump

Reactor Coolant

System

Residual

Heat

Removal

Senior Reactor Operator

Technical Specification

Temporary

System Alteration

Unresolved

Item

stitue

Engineers

letin

on