ML17346B149

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Safety Sys Functional Insp Repts 50-250/85-32 & 50-251/85-32 on 850826-0913.Ten Potential Enforcement Findings Noted During Auxiliary Feedwater Sys Insp in Areas of Maint, Operations,Surveillance,Qa,Training & Design Changes & Mod
ML17346B149
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 10/01/1985
From: Architzel R, Callan L, Martin T, Mckee P, Morris G, Overbeck G, Shymlock M, James Smith, Walenga C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE), WESTEC SERVICES, INC.
To:
Shared Package
ML17346B148 List:
References
50-250-85-32, 50-251-85-32, NUDOCS 8510150228
Download: ML17346B149 (34)


See also: IR 05000250/1985032

Text

~

~

OFFICE

OF INSPECTION AND ENFORCEMENT

DIVISION OF

INSPECTION

PROGRAMS

Report Nos.:

50-250/85-32

and 50-251/85-32

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33101

Docket Nos.:

50-250 and 50-251

License Nos.:

DPR-31

and

DPR-41

Facility Name: Turkey Point

3 and

4

Inspection

Conducted:

August 26 - September

13,

1985

Inspectors:

L. J.

C

n, Chic

, Performance

Appraisal

Secti

, Team

eader,

IE

D. Smith, Inspection Specialist,

IE

. Martin, Inspection

Specia ist,

IE

irs

We

)

M. B.

ymlock, Seni

Resident Inspector,

Regi

n II

R.

E.

chitzel, Seni r Inspection

Specia ist,

IE

( irst Week)

/0

t I)

ate

/O

d

D te

p~ (gS

Da

e

~eS

Date

yd /

0 t

C.

G.

Wa enga,

spection

Specia ist,

IE

r

(

e ond

We k)

G.

W.

r is,

NRC Cons

tant,

Westec

Date

/o

g

Date

Date

Approved by:

~ '~M

'P i

sp

F.

c ee,

se

,

Operating

Reactor

Programs

Branch,

IE

(oer /8 v

r

85101502kB, 881001

I: '; PDR,

ADOCK 05000Q50

'DR;.

h

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~

SCOPE:

This special

announced

team inspection involved 637 inspection

hours

assessing

the operational

readiness

of the auxiliary feedwater

system.

RESULTS:

The licensee's

operational

readiness

and management

controls

as

they relate to the auxiliary feedwater

system were reviewed in six

functional areas.

The functional areas

reviewed were:

Maintenance

Operations

Surveillance

guality Assurance

Training

Design

Changes

and Modification

Additionally, 10 potential

enforcement findings were

presented

to the

NRC Region II office as Unresolved

Items for

followup.

I.

Ins ection Ob'ective

The objective of the team inspection at Turkey Point was to assess

the

operational

readiness

of the auxiliary feedwater

(AFW) system.

This

assessment

included

a determination of the following:

capability of the system to perform the safety functions required

by

its design basis;

adequacy of testing to demonstrate

that the system would perform all

of the safety functio'ns required;

adequacy of system maintenance

(with emphasis

on pumps

and valves) to

ensure

system operability under postulated

accident conditions;

adequacy of operator

and maintenance

technician training to ensure

proper operations

and maintenance

of the system;

adequacy of human factors considerations

relative to the

AFW system

(e.g., accessibility

and labelling of valves)

and the system's

supporting procedures

to ensure

proper system operation

under normal

and accident co'nditions.

II.

Summar

of Si nificant Ins ection Findin s

Section III of this report provides the detailed inspection findings

pertaining to each functional area evaluated.

The safety effects of the

more significant findings on the operational

readiness

of Turkey Point's

auxiliary feedwater

(AFW) system are summarized

below.

Safet

Effects

on the Auxiliar

Feedwater

S stem

A.

The

NRC inspection

team identified safety concerns

regarding the

ability of the

AFW system to perform its safety function in the event

of a loss of non-safety

grade instrument air.

Loss of the inst~ument

air supply to the air-operated

AFW flow control valves is an assump-

tion in the

AFW system design basis fot most analyzed

accidents

involving AFW.

To ensure that the flow control valves,

and thereby

the entire

AFW system,

continue to operate in such events,

a safety-

grade nitrogen backup system is provided.

The team determined that

this backup nitrogen system

had never

been functionallytested,

eve'n

though this system

had been substantially modified as recently as

early 1984.

The licensee

had based its procedures

and operator

training on the assumption that 15-20 minutes

were available for

operators

to take necessary

action to establish additional nitrogen

capacity

upon depletion of the first nitrogen bottle.

This would be

accomplished

by valving in additional nitrogen bottles in the event

of a loss of instrument air to the flow control valves

(FCVs).

Control

room operators

would be alerted to take action by annunciator

alarms in the control

room that indicate that the on-line nitrogen

bottles for each of four trains

(two trains per unit) had reached

a

low pressure

condition of 500 psig.

As

a result of NRC c'oncern

during this inspection,

the licensee

tested all four trains of the

nitrogen backup supply to the

AFW FCVs.

This test demonstrated

that

from the time the low nitrogen pressure

annunciator alarmed,

only 6

to 7 minutes (instead of the expected

15-20 minutes) would be avail-

able in the most limiting case

(FCVs remaining in automatic

mode).

The team further determined that correct operator

response

to

a low

nitrogen pressure

annunciator for train

1 would have

been

hampered

by

the incorrect information in the annunciator

response

procedure,

Procedure

0208.11,

which directed the operator to ignore tbe alarm if

all three train

1 nitrogen bottles were in service.

Additionally, a

review of recent design

changes

to the

AFW system indicated that the

low nitrogen pressure

annunciator

alarm setpoint

had been

reduced in

March 1984 from its original setpoint of 1000 psig to the current 500

psig.

This resulted in a significant reduction in the available time

for operator

response.

The design

change

was also performed without

an adequate

safety evaluation.

The team concluded that the weaknesses

identified above in operator

training, inadequate

procedures,

the failure to functionally test the

nitrogen backup system,

and the apparent

non-conservative

setpoint

for the low nitrogen pressure

alarm could have all contributed to a

significant risk of a, loss of AFW flow.

Specifically, the team

concluded that there

was inadequate

assurance

that the control

room

operators

would take the required actions to maintain

AFW flow within

the 6 or 7 minutes that would potential-ly be available

once the

nitrogen low pressure

annunciator

alarm was received.

The team noted

that the operators'raining

and procedural

guidance

could have

provided

a false assurance

that at least

15-20 minutes

were

available.

The team

was also concerned that,

even if operators

had

been correctly trained and had adequate

procedures,

the existing low

nitrogen pressure

setpoint of 500 psig might be too low to allow for

a reasonable

response

time for operators

to valve in standby nitrogen

bottles.

Several

operators

expressed

the consensus

that at least

IO-15 minutes should

be available to ensure

necessary

actions could

be taken.

B.

The team identified a safety concern regarding the ability of the

AFW system to perform its safety function in the event of certain

two-unit trip scenarios.

The

AFW system design description

and

design basis required that 286 gpm be supplied to each unit within 3

minutes in the event of a two-unit trip and stated that operator

action would likely be required to assure

correct flow distribution

to each unit if only one

AFW pump were available.

Specifically, the

AFW system is arranged

into two trains,

and any one train is required

by the design criteria to supply both units.

Train 2 contains only

one of the three

AFW pumps.

Consequently,

on the loss of train I,

the single

pump in train

2 is required to supply both units.

The

team determined that the control

room operators

had not been trained

for this eventuality.

In addition, the applicable

emergency

operating

procedures,

such

as

EOP 20004,

"Loss of Offsite Power," and

EOP

20007, "Total Loss of AC," made

no mention of the need to provide

a

minimum of 286

gpm to each unit within three minutes.

Without the

requisite training and procedural

support,

the team lacked confidence

that correct operator action would be taken to ensure

adequate

AFW

flow to each unit in the event of a two-unit trip with only train

2

of AFW available.

This becomes particularly important if one of the

units provided less flow resistance

to AFW, such

as would be the case

C.

if steam generator

pressures

of one unit were lower than the other

unit.

The inspection

team identified a safety concern regarding the ability

of the on-shift operators

to isolate

steam flow paths to the

environment from the affected

steam generator

in the event of a steam

generator

tube rupture.

Emergency Operating

Procedure

20003,

"Steam

Generator

Tube Rupture," directed the control

room operators

to

isolate the steam supply from the affected

steam generator

to the

AFW

turbines

by shutting the associated

motor-operated

isolation valves

using the hand switches in the control room.

The inspection

team

determined that the

AFW turbine steam supply isolation valves could

not be remotely shut from the control

room if there

was

an

AFW

actuation signal present.

The team identified that the steam supply

isolation valves were designed

to cycle open if an

AFW actuation

signal were present,

even if the control

room handswitches

were held

in the "close" position.

The licensee

had not recognized this design

feature.

Therefore,

the licensee

had not provided operator training

or adequate

procedures

to ensure that alternate

means

were taken to

isolate the

AFW steam supply from the affected

steam generator.

The

team concluded that the lack of operator

awareness

that the steam

flowpaths in question could not be isolated remotely from the control

room could have resulted in an unnecessary

and

potentially signi-

ficant radioactive release

to the environment following a steam

, generator

tube rupture.

A significant amount of time could have

been

required for the control

room operators

to first identify that the

steam supply isolation valve would not remain shut and then take

appropriate

compensatory

actions.

Effects

on Other Safet

S stems

In addition to the specific safety concerns

discussed

above that relate

directly to the operational

readiness

of the

AFW systems

the team also

identified several

general

concerns that have the potential to affect the

proper operation of other safety systems.

A.

Problems

were noted in the Turkey Point maintenance

program.

Program-

matic weaknesses

affecting quality of corrective

and preventive main-

tenance

performed

on Turkey Point safety systems

included:

The maintenance

department

had experienced

a high turnover

rate

among maintenance

technicians

which resulted in a shortage

of experienced

personnel.

The Instrumentation

and Controls

( I&C) section

was the hardest hit:

at the time of the

inspection

over half (15 of 27) of the

I8C technicians

performing surveillance testing

had and average of less

than

6$ months experience

at Turkey Point.

Maintenance

technician training had not been

conducted

since August 1984.

Management controls did not exist to ensure that safety-related

maintenance activities were performed

by qualified personnel.

On-the-job training (OJT) records or other forms of

qualification documentation

were not used

by maintenance

supervisors

as

a basis for work assignments.

Maintenance

procedures

generally lacked detail.

Complex

safety-related

maintenance activities were often considered to

be within the scope of the "skill of the trade",

and therefore

not requiring procedures.

The shortage of experienced

technicians

and lack of training referred to above

do not appear

to justify the widespread

use of "skill,of the trade"

as

a

substitute for detailed procedures.

Post-maintenance

testing requirements

were typically not

included

as part of electrical

and

IKC Plant Work Orders.

Further,

documentation of completed post-maintenance

tests for

electrical

and

IEC maintenance

were typically not pa'rt of the

retained maintenance

records.

Interviews with maintenance

department

supervisory

personnel

indi-

cated that the above maintenance

problems could have contributed to

the large backlog of safety-related

Plant Work Orders

(PWOs)

throughout both units.

This backlog was of particular concern to the

team as it applied to degraded

and malfunctioning control

room

instrumentation.

For example:

The ability of the control

room operators

to diagnose

a

steam generator

tube leak was degraded

by the fact that the

steam jet air ejector process

radiation monitors

had been out of

.

service for about six months.

The Unit 4 containment

sump high level annunciator

had been

out of service since

December

1984 due to a failed level switch.

Two of the four post-accident

monitors for containment

sump

level for Unit 4 had

been out of service since

February

1985.

A Unit 3 safety injection accumulator Hi/Lo pressure

and

Hi/Lo level annunciators

were in an alarmed condition although

the associated

pressure

and level instruments

read within their

normal bands.

Several

area radiation monitors

on both units were out of

service.

Some of the monitors

had been out of service for

greater than'six months.

AFW system nitrogen backup supply low pressure

annunciators

for nitrogen station

No.

2 were alarmed

on both units.

Nitrogen

station

No.

2 had been

removed from service since January

1985

as

a result of a design

change.

The team considers this

a

concern

because

the alarmed nitrogen low pressure

annunciators

were located adjacent

to the low nitrogen pressure

annunciators

for stations

1 and

4 and thereby could degrade

the operator's

reaction time to a valid low nitrogen pressure

alarm.

Since very

little reaction time may be available

(as little as

6 to 7

minutes) to take action to maintain

AFW flow once the low

nitrogen pressure

alarm is received,

the potential for confusion

caused

by the spurious

alarms is considered significant.

- 4.-

Both units had leaking power operated relief valves

(PORVs).

In addition, the isolation valves (block valves) for

the Unit 4

PORVs leaked

and this resulted in elevated

temperatures

downstream of the Unit 4 pressurizer

safety relief.

valves

(which share

common discharge

piping with the

PORVs).

As

a result, control

room annunciators

were alarmed, for all three

Unit 4 pressurizer

safety relief valves

downstream

temperature

elements.

This condition is significant because it could

degrade

the control

room operators'bility to identify a lifted

safety relief valve or the failure of a

PORV to reseat.

B.

Problems were noted in the Turkey Point design

change

process.

Programmatic

weaknesses

identified by the team that affect the ade-

quacy of the design

changes

and modifications to safety-related

systems

include:

The engineering

group often did not provide post-modification

testing requirements

to confirm the adequacy of the installation

to the design basis.

The team identified instances

where modifications were

installed without a detailed design analysis.

The licensee

was

found to frequently base

design

changes

on engineering

judgement

that the new design

was bounded

by the original design analysis.

Documentation justifying the engineering

judgement typically did

not exist.

Design bases for safety-related

systems

were difficult to re-

trieve.

In the absence of readily available

design

bases for

many safety-related

systems,

the team is concerned that

excessive

reliance could be placed

on engineering

judgement for

implementing design

changes

and for performing safety evalua-

tions required by 10 CFR 50.59.

The team concluded that the above

programmatic

weaknesses

in the

design

change

process potentially contributed to the following

examples of inadequate

design analysis

and design

change

implementation:

Four of six AFM system

steam supply isolation valve motor

operators

were changed

from AC to

DC motors without adequate

design analysis.

Motor overload protection for the

new

DC

motors

was not properly sized.

Further,

the

new power cables

were not properly sized to ensure

adequate

operating voltage for

the motor operators

in the event of a loss of offsite power.

The licensee

had not performed any cable sizing calculations

to

support this design

change.

The design

change to the

AFW system to provide redundant Train A

and Train

B flow control introduced the potential for common

mode failure due to control circuits from both trains

coming to

common limit switches

and

common relays.

The design

change to provide redundant

nitrogen backup

systems

-5-

to supply Train A and Train

B AFW system flow control valves

introduced

a potential for common

mode failure in the redundant

control

room annunciator circuits.

As discussed

later in this

report, the loss of these

redundant

annunciators

could lead to a

loss of AFW.

Several

problems

were identified with the modification involving

the replacement of the Unit 3 and Unit 4 safety-related

station

batteries:

no calculation

was available to substantiate

the

one

hour battery discharge profile contained in the design

specification; the factory acceptance

test failed to adequately

demonstrate

the batteries

could meet the design basis profile;

and plant procedures

and Technical Specifications

surveillance

requirements failed to recognize

the existence of the

new

battery requirements

required

by the substitution of GNB

lead-calcium batteries for the old C&D lead-acid batteries.

The

AFW system

was modified to install

a redundant

solenoid

operated

steam vent valve.

Design analysis

does not exist to

document the selection of 150 psig setpoint selection for the

pressure

switches that are used to control operation of the

valves.

The team is concerned that the

150 psig setpoint would

permit the valve to open automatically before plant cooldown

could be transferred

to the residual

heat removal

system.

The design

change to install

a redundant safety-related

conden-

sate storage

tank low level alarm introduced

a potential for an

undetected

common

mode failure.

This failure would have

been

caused

by closing

a normally open manual isolation valve.

In

addition, this valve was not administratively controlled.

The

design calculation to establish

the setpoint for the low level

alarm did not identify all the assumptions

and design inputs

used to perform the calculation.

In particular, there

was

no

evidence that the calculation considered

the net positive

suction

head

(NPSH) required to maintain

AFW pump operation.

A design analysis

did not exist to document the setpoint

selection

(500 psig) for the

AFW system nitrogen backup supply

pressure

switches.

Engineering did not provide post-

modification testing requirements,

and,

as

a result,

the

nitrogen backup system

was never adequately

tested.

The

electrical

and

I&C equipment associated

with the nitrogen

system

were not identified as safety-related

in the Turkey Point

g-List, and as

a consequence

were not being treated

as

safety-related

by the electrical

and

I&C maintenance

technicians.

III. Detailed Ins ection Findin

s

A.

MAINTENANCE

A significant weakness

noted in the Turkey Point maintenance

program

was the consistent failure to evaluate

the root cause of

equipment malfunctions

and to trend these failures to provide

input to the preventive maintenance

program.

The Plant Work

-6-

Order

(PWO) form was used to document the performance of

maintenance.

A section of this form was provided to describe

the cause or reason for the trouble found.

A review of several

hundred completed

PWO forms revealed that the cause of the

associated

equipment failure was not described

in most cases.

Interviews with maintenance

supervisory personnel

revealed that

the cause of equipment failures and the consideration of the

recur rent nature of failures are tracked informally by relying

upon the memory of maintenance

supervisors.

The equipment

history records

were not being kept current in the electrical

and mechanical

areas.

Specific examples of failures to evaluate

root causes

of equipment failures are discussed

below:

A review of the maintenance

history records,

including

PWOs

and Licensee

Event Reports

(LERs) for the auxiliary

feedwater

(AFW) system,

revealed

several

component

failures of a recurrent nature.

These included seven

separate

examples,

since January

1984, of failure of an

air-operated

AFW flow control valve to properly function "

due to water or foreign material in the instrument air

system.

In 1983,

on two separate

occasions,

two of the six AFW

steam supply motor operated

valves

(MOVs) failed to open

because

of carbon build-up on the motor operator limit

switches.

A review of the maintenance

records for the

remaining four AFW steam supply

MOVs revealed that, despite

the recent failures described

above,

one

MOV (MOV 3-1404)

had not been electrically cleaned

and inspected

since

1979.

Additional weaknesses

associated

with maintenance

on MOVs

are discussed

in Maintenance

Observations

2 and 3.

2.

A review of the maintenance activities performed

on

MOVs

indicated weaknesses

in training for repair of these valves.

Interviews with supervisory maintenance

personnel

revealed that

no training had been

conducted in either the mechanical

or

electrical

areas

covering repair of MOVs with the exception of

undocumented,

on-the-job

training and pre-maintenance

briefings.

A mock-up of a Limitorque valve operator

was

available in the training department offices but apparently

had

not been

used to train maintenance

personnel.

3.

Mechanical

maintenance

personnel

were uncertain

regarding the

type of grease

to be used in MOV gearboxes.

This was considered

a problem for two reasons.

First, the mixing of different types

of grease

in the gearbox

could cause

hardening or separation

of

the lubricant.

The potential for this exists at Turkey Point

because its preventive maintenance

instructions for Limitorque

gearboxes

specify the use of Texaco Marfac, while these

same

Limitorques have

been supplied with either Exxon Nebula

EPO or

EPI or Sun

50

EP lubricants.

Secondly,

the only Limitorque

lubricant that meets

the environmental qualification

. requirements

of 10 CFR 50.49 at Turkey Point- is Exxon Nebula

EPO

or EPI.

A program to address

these

concerns

was in progress

and

scheduled for completion

by December

1986.

The progress of this

effort will remain

an inspector followup item (50-250/8532-1;

50-251/8532-1).

4.

The licensee

has recently taken steps

to improve

MOV

reliability.

Temporary Operating

Procedure

166 was issued in

May 1985 and provide detailed instructions for troubleshooting

and repair of MOVs, including limit switches,

torque switches,

and post-maintenance

testing.

This procedure

provides specific

torque switch settings for safety-related

motor-operated

valves

and required that, during maintenance,

proper torque switch

settings

be verified by an electrical quality control inspector.

Discussions with management

representatives

revealed that the

licensee

was in the process of purchasing

new MOV test equipment

to use in improving the reliability of the MOVs.

5.

- A review of calibration records

revealed that the low pressure

alarms for the

AFW nitrogen system were not routinely calibrated

(see

Design

Changes

and Modifications Observation

5.c for

further discussion).

A search of calibration records with the

assistance

of an

IEC supervisor

revealed. that the most recent

calibration records for two of the nitrogen supply low pressure

alarm pressure

switches

(PS 2322 and

PS 2323) were dated

June

14,

1978.

In addition,

no procedure

was available for the

calibration of these alarms.

The apparent failure to establish

and implement procedures

for the calibration of the

AFW nitrogen

system low pressure

alarms

was discussed

with the licensee

and

will remain unresolved

pending followup by the

NRC Region II

Office (50-250/8532-2;

50-251/8532-2).

Due to this identified concern,

the licensee

issued

PWOs 8349

and 8350 to calibrate all four nitrogen system pressure

switches.

These calibrations

were performed

on September

9,

1985.

6.

The control

and documentation of 'sampled

post-maintenance

testing

was found to be weak.

In many cases,

neither the

post-maintenance

testing instructions nor the results of the

testing were documented

on the

PWO.

This was particularly

evident for 18C and electrical

maintenance activities.

However,

for mechanical

maintenance activities, Administrative Procedure

(AP) 0190.28,

"Post Maintenance Test Control," was.specified

on

the

PWO in most cases.

This procedure

described

most of the

testing considered

adequate

by the licensee to return mechanical

systems

to an operable status

and also provided

a form to docu-

ment the test results

as

an attachment

to the

PWO.

The apparent failure to provide adequate

instructions for

post-maintenance

testing

on some

PWOs appears

to be contrary to

AP 0190.19,

"Conduct of Maintenance

on Nuclear Safety Related

and Fire Protection

Systems,"

was discussed

with the licensee,

and will remain unresolved

pending followup by the

NRC Region II

Office (50-250/8532-3;

50-251/8532-3).

7.

A weakness

was noted in the program to return instruments

properly to service following maintenance

or calibration while

-8-

the plant was operating.

The licensee

had

a program for provid-

ing general

assurance

that instruments

inside and outside the

containment

were properly aligned

when the plant was returned to

operation

from an outage condition.

The procedures

describing

the instruments to be checked,

O-SMI-059.1 and O-SMI-059.2, were

considered

adequate,

providing a place for first and second

check verification for each applicable instrument.

However,

interviews with I8C supervisory

personnel

revealed that these

procedures

wou1d normally be used only to verify instrument

alignment at the end of an outage condition.

Instrument

line-ups were not required

by the licensee to be independently

verified following maintenance

or calibration while the plant is

in an operating status.

8.

A sample of maintenance

procedures

indicated that many complex

maintenance activities were accomplished without detailed,

step-by-step

procedures.

Instead,

these

complex activities were

considered

to be "skill of the trade".

The team considers

the

licensee's

frequent reliance

on individual skills of maintenance

technicians

as

a substitute for detailed procedures

to be

unjustified in view of the limited training provided to

maintenance

technicians

and the high turnover rate

among

maintenance

personnel.

(See Maintenance

Observations

10 and 11.)

.

9.

A backlog of approximately

900

PWOs existed in the I5C section.

Included in this backlog of PWOs were

a number affecting control

room instruments.

The team considers that any degraded

condition of these

instruments

could hamper the

operators'bility

to diagnose

and respond to abnormal plant conditions.

Examples of instruments that fit into this category were:

Unit 3 Steam Jet Air Ejector

(SJAE) Process

Monitor had

been out-of-service

(OOS) since

February

13,

1985,

and the

Unit 4 SJAE Process

Monitor Cabinet

had been pulled from

the control

room for maintenance for approximately

6

months.

The SJAE Process

Mo'nitors are used to monitor

radioactivity in the steam exhausted

to the main condenser

and are

an important diagnostic tool for identifying a

primary-to-secondary

leak.

At the time of the inspection,

the

SJAE exhaust

gas radioactivity was being recorded

by a

backup

(SPING) system that

had

no control

room indications

or alarms.

The readout of the

SPING system

was checked

by

the chemistry department

every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

The Unit 4 Containment

Sump High Level Annunciator

had been

OOS since

December 6, 1984.

The cause

was determined

to be

an inoperable

level switch, LS-1538.

The containment

sump

pump handswitches

(labelled

"Off-Auto-Run") were in the "Off" position for both units.

This was

done

because

the

pumps would not cut off auto-

matically when

sump level

was

pumped

down if the switches

were left in "Auto" as designed.

-9-

Two of the four accident monitors for Unit 4 containment

sump level indication, which are used to determine the

level during a Loss-of-Coolant Accident (LOCA), had been

OOS since February 7, 1985.

The Hi/Low Pressure

Annunciator and Hi/Low Level

Annunciator for one of three Unit 3 Safety Injection

Accumulators were in an alarmed condition.

Area Radiation Monitors on both units

had many

PWO tags

which had been in place for extended

periods.

Some of

these monitors were in degraded

conditions for greater

than

6 months.

This reduced

the operators'bility to diagnose

abnormal plant conditions

and also increased

the

possibility of personnel

exposure.

The

AFW nitrogen supply station

number

2 low pressure

annunciators

were alarmed

on both units.

These annunci-

.,

ators

were used to indicate

low nitrogen supply to the

AFW

differential pressure

transmitters,

which had been

disconnected

since January

1985.

Further,

these

annunciators

were located beside

the

AFW nitrogen system

station I and station

4 low pressure

annunciators,

and

therefore

could potentially degrade

the control

room

operators'bility to distinguish

a valid low nitrogen

supply pressure

condition (see Operations

and Surveillance

Observation l.a and I.b for further discussion).

10.

Interviews with maintenance

supervisors

and training personnel

indicated that formal classroom training sessions

for

maintenance

technicians

had been discontinued

in August 1984.

Licensee

management

stated that maintenance

training had been

discontinued to dedicate training resources

to developing

training materials

required to support Institute of Nuclear

Power Operations

(INPO) accreditation. of the maintenance

training program.

The licensee

stated that this decision

was

necessary

in order to meet the

INPO accreditation Self

Evaluation Report submittal date of February

1986.

Additionally, a review of maintenance

training records

indicated

that

a very limited amount of on-the-job

(OJT) training and

vendor supplied training had been conducted

since the decision

to discontinue

classroom training.

The team concluded that maintenance

training being conducted did

not appear

adequate

to maintain staff proficiency and to train

new personnel,

particularly in view of the high turnover rates

experienced

by the maintenance staff (see Maintenance

Observation

11 of this section).

11.

Review of training records

and interviews with training and

maintenance

supervisors

raised

the following concerns:

Over half of the

ISC technicians

that conduct surveillance

tests

( 15 of 27 at the time of the inspection)

had

an

- 10-

average of less

than 6.5 months of experience

at Turkey

Point.

The electrical

and mechanical

maintenance

groups

had also recently experienced

high turnover rates

among

their technicians,

but not to the degree of the

18C group,

The licensee's

management

controls for safety-related

maintenance

work assignments

were considered

weak.

Maintenance

supervisors

relied on their knowledge of each

technician's abilities and experience for work assignments.

OJT records or other forms of qualification documentation

were not used to assure that only properly qualified

personnel

were assigned safety-related

maintenance

activities ~

B.

0 erations

and Surveillance

1.

The procedures for normal

and emergency operation of the

auxiliary feedwater

system were evaluated

as weak, with numerous

instances

of incorrect information that could result in degraded

AFW system operation.

For example:

a ~

b.

Procedure

0208.11,

"Off-Normal Operating Procedure,"

stated

that in the event of a low hitrogen pressure

annunciator

alarm the standby nitrogen bottle should

be valved in.

However, in the case of the train

1 nitrogen system,

the

procedure states

that if all three available nitrogen

bottles are valved in, the operators

were to ignore the

alarm.

To ignore the annunciator

alarm in that instance

could quickly lead to a loss of sufficient nitrogen

pressure

to operate

the train

1

AFW flow.

The licensee

informed the team that this procedural

inadequacy

would be

corrected

on a priority basis.

This item will remain

an

inspector

followup item pending confirmation of the

licensee's

corrective actions

(50-250/8532-4;

50-251/-

8532-4).

Additionally, this procedure

did not alert the

operator to the fact that very limited time might be

available to take corrective action, nor did the procedure

advise the operators

to conserve

nitrogen pressure

by

shifting AFW flow control valve operation

from automatic to

manual.

The team determined that confusing

and incorrect

information was available to control

room operators

regarding the capacity of the

AFW nitrogen backup system.

'Procedure

7300.2.

"AFW System

Flow Control Valves

Instrument Air/Nitrogen Backup System Operation," states

the operators

have

15 minutes to valve in standby nitrogen

bottles after the low nitrogen pressure

annunciator

alarms.

However, licensed operators

were trained in their ongoing

requalification training program that they have

20 minutes

to take action (reference:

Training Brief f9, dated

March

1, 1984).

The

AFW system description

and design basis

states

that only 10 minutes

are avai'table for the operators

to take action.

At the request of the

NRC, the licensee

performed

a functional test of the nitrogen backup

system

- 11-

c ~

d.

during this inspection period.

The test results indicated

that, in fact, operators

had as little as six minutes (with

the flow control valves in auto) to take action to avoid

the loss of AFW due to a loss of nitrogen pressure.

Because of the inadequate

operator training and incorrect

procedural

information available,

the team lacked assurance

that appropriate

operator action would be taken

1n the

event of a low nitrogen pressure

annunciator

alarm

following a loss of instrument air.

Emergency operating

procedures

did not provide adequate

guidance to control

room operators

to assure

that adequate

AFW flow (286 gpm) would be provided to each unit within 3

minutes,

as required

by the

AFW design basis,

in the event

of a two-unit trip with only one

AFW pump available.

EOP

20004,

"Loss of Offsite Power," and

EOP 20007, "Total Loss

of AC," made

no mention of the need for timely operator

action to balance flow between

the units in this instance.

EOP 20003 (E-3), "Steam Generator

Tube Rupture," dated

December 20,

1984, provided incorrect information to the

control

room operators

regarding

how to isolate the steam

supply to the

AFW turbines from the affected

steam

generator.

Specifically,

EOP 20003 directed the control

room operators

to isolate the steam supply from the

affected

steam generator

by shutting the associated

motor-operated

isolation valve using the handswitch in the

control

room.

However, the inspection

team determined that

these

AFW isolation valves could not be remotely shut from

the control

room if there

was

an

AFW actuation signal

present

(see

Design

Changes

and Modifications Observation

5.c for further details).

The licensee

had not recognized

this design feature

and therefore

had not provided operator

training or procedures

to ensure that alternate

methods

were available to isolate the

AFW steam supply from the

affected steam generator

in the event of a tube rupture.

The licensee

stated that the affected

EOPs would be

corrected

on a priority basis.

Further, the licensee

provided training to all on-coming control

room operators

regarding this matter.

This item will remain

an inspector

followup item (50-250/8532-5;

50-251/8532-5).

2.

During a system walkdown of the auxiliary feedwater

supply and

the auxiliary feedwater

steam

systems,

as described

in piping

and instrument drawings 5610-T-E-4062,

Rev. 33, and

5610-T-E-4061,

Rev. 6, the following observations

were noted:

turbine casing

and exhaust silencer drain valves 328, 329,

331 and 332 were missing their associated

handwheels;

local pressure

instruments

(PI) 1416,

1417,

and

1418 had an

additional isolation valve not shown

on the drawing;

- 12-

feed flow transmitter

3-1401B was marked 4-1401B and

one

isolation valve, 3-002,

was not tagged;

feed flow

transmitter 3-1457B had an isolation valve, 3-003, not

tagged;

the following valves

had

no identification tags:

3-012,

RV-6401A, AFWU-010)70-102,

AFWU-011,70-103)

AFWU-012,70-104,

and isolation valves

on PI-1430, PI-1431;

a flexible hose

was supplied from the backup service water

system through Aeroquip quick disconnect fittings to supply

backup

AFW pump cooling water.

Debris

was noted in the

hose for the "A" pump.

There

was

no control for either the

male or female fittings;

all the valves for nitrogen station

No. 4 were mislabelled

as station

No. I valves;

three nitrogen bottles in each nitrogen station

(No. I and

No. 4) had "empty" tags

on them.

When questioned

by the

inspector,

the licensee

determined that the bottles were,

in fact, full;

the licensee

had not established

contingency measures

to

ensure that replacement

nitrogen bottles could be made

available

on backshifts.

This issue

was significant

because

only about

3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of nitrogen is available at the

nitrogen stations,

so several

replacement

nitrogen bottles

would be required to operate

the

AFW system long enough to

cool

down the units to allow for residual

heat

removal

operation.

The

AFW system walkdown revealed that replace-

ment nitrogen bottles were not readily available.

3.

A review of "Auxiliary Feedwater Train I Operability Verifica-

tion," Procedure

3-OSP-075. I, dated August 7, 1985, identified

that it did not adequately verify the operability of AFW steam

supply

HOVs 3-1404

and 3-1405.

Limit switches

located in these

valves are used to control associated

flow control valves in the

feedwater lines.

When either of the

MOVs opens, all flow

control valves in trains I and

2 open to assure

a feedwater flow

path.

However, procedure

3-0SP-075.1

required opening both of

these

steam supply valves together.

Therefore,

each of the

NOVs

was not independently verified capable of opening all the flow

control valves

as designed.

4.

The team considers

local control of train 2 AFW valves to be

virtually impossible.

Off-Normal Operating Procedure

0208.17,

"Control

Room Inaccessibility," dated

Nay 24,

1985, would be

used to take local feedwater

control in the event of a control

room evacuation.

This procedure

has

no guidance for local con-

trol of train 2 AFW valves.

Additionally, it appeared

that

operation of this train would be difficult because

the valves

are located under the feedwater platforms

and all indications

for train

2 are located

on the platform area.

- 13-

The team's

concern

regarding the ability of the licensee

to

safely shut

down the plant in the event of control

room inac-

cessibility was reinforced

by the observation that the licensed

operator requalification program did not include drills or plant

walkthroughs to simulate local control of essential

safety

systems.

This is considered

a weakness

at Turkey Point for two

reasons.

First, Turkey Point does not have

a safe

shutdown

panel outside the control

room that would provide

a central

location for essential

instrumentation

and control.

Second,

less

than

a quarter of the licensed control

room operators

had

previously been

a watchstander

outside the control

room; there-

foree,

the majority were not as familiar with local equipment

operation.

5.

The team noted the following concerns with the condition of the

auxiliary feed

pump turbines

and their associated

steam supply

system.

a.

During a system walkdown, the drain lines on the turbine

casings

and the exhaust silencers

were noted to be hot.

Water

was flowing from the drains

on the A and

C turbines.

The steam supply isolation valves for the

A and

C turbines

were leaking and allowing steam to reach the turbines

even

though the valves were closed

(MOV-3-1404, NOV-3-1405).

A

review of the valves'aintenance

history revealed that

these

valves

had been

reworked several

times.

However, it

did not appear that the problem had been resolved.

The

associated

steam supply valves

on Unit 4 also appeared

to

be leaking.

It should

be noted that the

B turbine did not

appear to have any leakage

from its steam supply valves

(NOV-3-1403 and HOV-4-1403).

During this inspection

period,

no current

PWOs were noted

on the leaking steam

supply valves.

b.

The steam supply vent system did not appear to be

functioning properly in that the vent valves were open but

only a small amount of steam

was being vented.

Further,

a

substantial

amount of steam

appeared

to be reaching

the

AFW

turbines

based

on the condensate

flow from the casing

and

silencer drains

and the elevated

temperature of the exhaust

stack.

The team identified that one of the vent valves

on

Unit 3 was failed shut

on September

11,

1985.

The licensee

promptly corrected this problem.

6.

It was noted during walkdowns of the auxiliary feedwater

system

that the seismic qualification of portions of the system

was not

being proper ly maintained;

The following observations

were

noted: control air lines going to CV-3-2816 were attached

to

their tubing tray but the tray was not attached to the floor for

several feet; nitrogen instrument lines were noted to go

underground to transit from one location to another;

and

nitrogen bottles stored at nitrogen station

No. I were not

adequately

restrained.

- 14-

It was noted also that temporary scaffolding was in place above

all four instrument racks for Unit 3 and

4 auxiliary feedwater

flow transmitters.

In addition,

a leg of one of these scaffolds

was installed adjacent to the Unit 3 train 2 auxiliary feedwater

instrument rack right between

two of the flow transmitters.

The

failure of non-seismic

components

(scaffolding) could cause

the

failure of safety-related

AFW components

with the resultant

common

mode failure of all auxiliary feedwater flow to both

units.

This item will remain unresolved

pending .followup by the Region

II Office (50-250/8532-6;

50-251/8532-6).

7.

Procedure

4-0SP-075.3,

"AFW Nitrogen Backup System Operability

Verification," was reviewed by the team.

This procedure

did not

appear

adequate

to functionally test the nitrogen backup system

as it only tested

the operability of the system during static

conditions.

The test did not demonstrate

that the nitrogen

backup system would function properly in its design basis

mode

of supplying the

AFW flow control valves with the valves in

automatic.

8.

The differential pressure

transmitters

on the discharge of each

AFW pump were disconnected

in January

1985 in accordance

with

Procedure

0103.3,

"Control and

Use of Temporary System

Alterations."

This procedure

required that

a

10 CFR 50.59

safety evaluation

be written and the alteration

be reviewed

and

approved

by the Plant Nuclear Safety Committee

(PNSC).

The

Temporary System Alteration for disconnecting

these differential

pressure

transmitters

included neither

a

10. CFR 50.59 safety

evaluation

nor

PNSC approval.

This item will remain unresolved

pending followup by the Region II Office (50-250/8532-7;

50-251/8532-7).

C.

Oesi

n Chan

es

and Modifications

1.

Plant Change/Modification

(PC/M) 80-77 was reviewed by the team.

This modification package installed redundant

instrument strin9s

to provide safety related

condensate

storage

tank level

indication and .an alarm 20 minutes prior to needing another

source of water for the auxiliary feedwater

pumps.

The team

determined that the implementation of this design

change failed

to ensure that it met the single failure criteria.

Specifically,

an operator error to close

one manual isolation

valve (isolation valve 428) could have

caused

an undetected

'ommon mode failure of safety-related

condensate

storage

tank

level indication and alarm functions.

The level transmitters

for redundant

level indication are connected

to a

common

instrument tap from the condensate

storage

tank.

The

common

instrument tap has

a normally open isolation valve which could

be mistakenly closed

by an operator causing

co@non

mode failure

of the level instruments.

No valve position indication was

provided to alert the operator of incorrect valve position and

- 15-

no administrative controls

(such

as locking the valve open) were

applied to ensure that the valve remained

open.

As a result of the inspection concern,

the licensee

checked

open

isolation valve 428 and installed

a locking device.

Revision of

appropriate

valve lineup sheets

and plant drawings will also

be

required.

This item will remain

an inspector followup item

(50-250/8532-8)

50-251/8532-8).

2.

PC/8 80-117

was reviewed.

This modification added

redundant

steam supplies

to the auxiliary feedwater turbines.

The modi-

fication also replaced

the auxiliary feedwater flow control

valves.

Upon auxiliary feedwater initiation, six pneumatic flow

control valves per unit are automatically opened

and controlled

to supply

125

gpm through each valve.

The three auxiliary

feedwater

pumps are aligned in a two train arrangement

with

turbine

pumps

A and

C assigned

to train

1 and turbine

pump

B to

train 2.

Three flow control valves are assigned

to each train

to provide auxiliary feedwater

flow to each of three

steam

generators.

Flow transmitters

immediately downstream of the

flow control valves monitor feedwater flow and provide feedback

to I/P converters

to alter control air pressure

to flow control

valve positioners.

Upon loss of instrument air these

valves are

designed to fail shut.

To prevent this from occurring the flow

control valves are provided with a safety-related

source of

bottled nitrogen to restore

the sources of motive and control

power for the flow control valves.

PC/Yi 80-117 also added six new flow control valves (three valves

per unit) and replaced

the actuators

on the six installed valves

(three actuators

per unit).

To accommodate

redundancy

in the

nitrogen system,

the existing nitrogen cylinders (five cylinders

per unit) were divided into two trains per unit.

This division

resulted in assigning

three nitrogen cylinders to train

1 and

two cylinders to train 2.

In each train, only one cylinder was

valved on-line.

During the team's

review of PC/N 80-117, the

design of the nitrogen system

was examined.

The following

observations

were made during the review of the modification

package.

a.

The implementation of the design control process for this

modification did not produce

a documented

analysis

substantiating

the design

adequacy of the nitrogen system.

The team found that

a design analysis

was not performed

by

Bechtel to confirm that the design

change

was acceptable.

The team was informed that Bechtel

reviewed the original

design analysis

and confirmed that the

new design

was

bounded

by that calculation in lieu of a new design

analysis.

No evidence existed

documenting this engineering

judgment.

The team was informed that the existing calcula-

tion was considered

bounding

because

the

new components

had

a lower nitrogen consumption rate.

The original design

analysis

was performed in 1972 and

had consumption

rates

for components

which existed in the original control

scheme

and which were subsequently

replaced with new components

by

-16-

PC/M 80-117.

The calculation

had

no indication of a check

or verification.

Likewise, the sources

and nature of the

consumption

rates

were not identified.

During the inspec-

tion, Bechtel could not determine if the values in the

1972

calculation represented

steady-state

conditions or consump-

tion rates reflecting

some assumption for valve modulation

and component

leakages.

Bechtel cited information from a

vendor technical

manual

which indicated that the-new valve

actuators

have

a lower steady-state

air usage

value of 0.26

scfm per valve, rather than the 1.0 scfm per valve used in

the existing calculation.

The valve actuators

are

diaphragm actuators

with a balance positioner constantly

exhausting air through

a detecting nozzle.

Bechtel pointed

out that only three actuators

are being supplied

by the one

nitrogen cylinder on line instead of six per the original

design.

Thus, Bechtel

concluded that the original design

analysis

bounded the

new design.

By inspection,

the team

could not arrive at the

same conclusion for the

following'easons:

The team determined that the steady-state

air usage

value of 0.26 scfm was based

upon

a vendor test of a

similar, but not identical valve positioner.

The

vendor test

was conducted with an air supply pressure

of 60 psi instead of the minimum nitrogen supply

pressure of 80 psi furnished by the installed nitrogen

system regulators at Turkey Point.

As a consequence,

the steady-state

air usage

value can

be expected to

increase.

During the inspection,

Bechtel indicated

that

a linear extrapolation

was

a reasonable

assumption.

Therefore,

the steady-state

consumption

rate approaches

0.36 scfm (i.e., increased

by a factor

of 80 psi/60 psi).

The assumption of instantaneous

steady-state

operations

does not appear

to be consistent with the

as-designed

valve response (i.e., upon actuation

the

valve cycles full open

and then closes

towards the

125

gpm flow setpoint).

The vendor's technical literature

indicates that high operating

speed is achieved with

virtually no overshoot

when approaching

the final plug

position.

Although a designer might choose to assume

a leak tight system with periodic testing to confirm

this assumption, it appears

unreasonable

to conclude

that no valve modulation is required

and that

a

steady-state

condition is reached

imnediately.

The

team

was informed that the operators typically take

the flow control valves out of automatic control

and

place

them in remote

manual control immediately after

an auxiliary feedwater flow to maintain steam

generator level.

The team was informed that this

operator action results in elimination of control

valve modulation except for the initial valve cycle.

However, the team determined that the operators

were

not required

by procedure

to take remote

manual

- 17-

control nor were the operators

directed to do so by

existing management

guidelines or training.

Consequently,

the team concluded that the licensee's

assumption that operators

would immediately take

remote manual control of the flow control valves

(and

thereby reduce

the valves'ir usage rate)

was

unjustified.

In addition, the team found no periodic

testing performed

on the nitrogen system to confirm

its leak tightness

and instead

observed

a system with

significant leakage rates.

The minimum available

volume of nitrogen is higher in

the original design analysis

than prescribed

in the

system design description.

Specifically, the original

design calculation

uses

a minimum volume based

upon

1005 psig in the cylinder, and the system description

indicates

a minimum volume based

upon 500 psig.

This

reduction can, in part,

be explained

by the reduction

in the assumed

time the operator

has available to

valve in a new nitrogen cylinder.

The original

analysis

was performed with a design basis of operator

action within 15 minutes of receiving

a low nitrogen

pressure

alarm, whereas,

the current system

description specifies

10 minutes.

This time reduction

does not appear to be based

on a documented

analysis

of the actions required of the operator to recognize

the alarm, analyze the appropriate

response,

send

another plant operator to the nitrogen cylinder and

valve in a second nitrogen cylindet

.

(See Operations

and Surveillance Observation I for further

discussion.)

The original nitrogen system design

bases

included

a

requirement that the stored

volume of nitrogen

be able

to permit system operation for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> assuming that

all five nitrogen cylinders were full.

A similar

requirement for the current system

does not appear to

be addressed.

This does not appear to be consistent

with the licensee's

comnitment to have at least

one

AFM system

pump and its associated

flow path

and

essential

instrumentation

capable of being operated

independent of any AC power source for at least

two

hours

(SER related to Amendment

No.

75 to operating

license

No.

DPR-31 and Amendment

No.

69 to facility

operating license

No. DPR-41).

b.

The team found that

a design analysis

did not exist to

document

the setpoint selection for pressure

switches

used

to alert the operator via control

room annunciation that

ten minutes of nitrogen remained before loss of motive and

control power to the

AFW flow control valves.

Instead

the

team was informed that the setpoint reduction from 1005

psig to 500 psig for the pressure

switches

was established

by testing performed under Temporary Procedure

085 on Parch

I, 1984.

This test appeared

to have

been

performed prior

- 18-

0

to the splitting of nitrogen system into two redundant

trains but after addition of the

new flow control valves

and actuators.

The test was performed with one nitrogen

control cylinder supplying all six flow control valves with

the valves in a full open position'.

Placing the valves in

a full open position causes

the air usage to be in a

steady-state

condition.

Because

the nitrogen pressure

decayed

the last 500 psig in 15 minutes, the low-pressure

alarm was set at 500 psig.

This setpoint

was selected

based

upon

a steady-state

test without consideration

of

instrument error and without compensation for that pressure

at which the flow control valve can

no longer modulate

(approximately

30 psig per manufacturer information).

The

issue is safety significant because

incorrect setpoint

selection could result in the premature

loss of nitrogen

pressure

and closure of all auxiliary flow control valves.

c.

The design verification process failed to ensure that

appropriate quality assurance

requirements

were specified

for nitrogen system

components.

Electrical

and

I5C

equipment associated

with the nitrogen system were not

identified as safety-related

in FP8L's g-List.

As a

consequence,

the pressure

switches

used to alert the

control

room operator of low nitrogen pressure

and the need

for immediate operator action were not being treated

as

safety-related

by the 'site

IEC group.

The AFM system design description identifies the

AFW system

as

an emergency

safeguards

system to prevent core

damage

in

the event of transients

such

as

a loss of normal feedwater

or a main steam line break.

The nitrogen system is

essential

to operation of the auxiliary feedwater flow

control valves and,

as such,

the nitrogen system serves

a

safety-related

function.

FPEL (}uality Instruction

JPE-g1-2.3A,

"Classification. Of Structures,

Systems

and

Components,"

indicated that the mechanical

equipment but

not the electrical

and instrumentation

and control

equipment associated

with the nitrogen system were

safety-related.

The team was informed that

a more detailed

component level g-List was being developed

and that this

list indicated the pressure

switches

were safety-related;

however, this list had not been

issued

from engineering at

the time of the inspection,

and the

IAC group was

unaware

that the safety classification for the pressure

switches

had changed.

It appears

that, contrary to the requirements

of ANSI

N45.2. 11Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2. 11" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. Section 6.3, the design verification process for

the g-List and the design modification did not ensure that

equipment performing

a safety-related

function were

designed,

specified,

and maintained

commensurate

with that

function.

This item wi'll remain unresolved

pending

followup by the Region II Office (50-250/8532-9;

50'-251/8532-9).

-19-

0

d.

Implementation of the design

change

process for this

modification did not produce

a design analyses

to confirm

that non-safety

components of a system

do not adversely

affect the safety function of the system.

Although not

identified in the system design description

and design

bases

document for the auxiliary system,

steam vent valves

were provided to vent steam

when the system is not

operating.

The valves are signaled to close

on increasing

steam pressure

(increasing

steam pressure

indicates that

auxiliary feedwater

system

has initiated) and to open

upon

decreasing

pressure

to vent the steam lines between

the

steam admission

valves

and the auxiliary feedwater

pump

turbines.

The steam vent valves are outside of the seismic

boundary

and are treated

as non-safety-related.

In

reviewing

PC/M 80-117 this design feature

was examined

and

the following observations

were made.

Design analysis

does not exist to document the

consequence

of a failure of the vent valves to shut "

and the ability of the auxiliary feedwater

pump to

supply sufficient feedwater flow at reduced

steam

generator

pressures

to reach the point of Residual

Heat

Removal

System operation.

Design analysis

does not exist to document the

setpoint selection for pressure

switches

and the error

band used to control the operation of solenoid-

operated

steam vent valves.

The setpoint

was verified

to be at 150 psig which would permit the valve to open

automatically before the cooldown has

been transferred

to the Residual

Heat Removal

System.

The lack of a design analysis

in the cases

cited above in

subparagraphs

a, b, and

c appears

to be contrary to the

requirements

of ANSI N45.2. 11 Sections

4. 1 and 4.2 which

requires that design analyses

be performed in a planned,

controlled and correct manner

and that there exist

traceability from design input through to design output.

This item will remain unresolved

pending followup by the

Region II Office (50-250/8532-10;

50-251/8532-10).

3.

During the review of PC/N 80-117, the team observed

nitrogen

system tubing which did not appear to be seismically supported

and instances of broken supports.

This tubing was routed from

the nitrogen cylinder racks to the flow control valves

and

included original tubing as well as

new tubing.

The team was

informed that this lack of adequate

seismic supports

was

known

by the licensee

as

documented

in REA No.

TPN 85-30.

In a March

7,

1985 letter, the licensee directed Bechtel to walk down the

system in the field and determine if the tubing was actually

supported

in accordance

with Bechtel's

design specification for

seismic

Class

I tubing supports or in accordance

with the

original seismic design specification.

On July 19,

1985, in

response

to this request,

Bechtel reported that most of the

3/8-inch tubing was installed in accordance

with Bechtel

- 20-

specifications

but with two tube spans

greater

than that

allowed.

These deviations

were evaluated

and found to be

acceptable

as installed.

Mith respect to the old tubing in the

rest of the system,

Bechtel identified that the configuration

was different than originally accepted

by Project Engineering.

Bechtel evaluated

the configuration using the functionality

criteria developed to justify continued operation in response

to

IE Bulletin 79-014.

The Bechtel analysis

determined that the

tubing must be supported at 27 inch maximum intervals-to meet

final design requirements for long term operation.

The licensee

informed the team that correction of this. nonconforming

condition will be performed during the next refueling outage.

This item will remain

an inspector followup item (50-250/8532-11;

50-251/8532-11).

4.

The team found that design calculations

were not being updated

by FPSL to reflect current modifications.

The team was informed

that design inputs were maintained

so that, if required,

the

calculations

could be recreated.

The team found that design

criteria documents

did not exist and that design

bases

were, in

many instances, difficult to retrieve.

This condition was

further complicated

by the controls Bechtel maintains over

calculations

performed

by Bechtel.

The team found that Bechtel

had

a set of original project design calculations

which were

used for reference

purposes

but not updated.

For current design

activities, Bechtel maintained

design calculations

and updated

those calculations

as plant modifications were assigned

to their

design responsibility by FPhL.

As

a consequence, it was

difficult for a Bechtel or FPhL engineer to know where

applicable

design analyses

were to be found.

Further,

the team

observed

a lack of attention to documenting

assumptions,

.justification for their use,

and confirmation that the

assumptions

were accurate after the design

had proceeded.

Likewise, the team found that the source of input data

was not

consistently

design

documents

but,the

FSAR or uncontrolled Plant

Data Books.

During the inspection the

team observed errors in design

documents (e.g., calculations,

drawing and specifications)

which

do not represent,

in themselves,

inadequate

designs

but reflect

a need for more attention to design traceability.

For example:

a.

Bechtel calculation

(M-08-093-02, Auxiliary Feedwater

System Control Valve Sizing, Rev.

1, July 31,

1981) did not

identify the source of assumptions

and input data

such

as

main steam safety valve setpoints, relief valve

accumulation, auxiliary feedwater

pump flow, and

pump

discharge

pressure.

The calculation

made

a general

reference

to FPSL's Turkey Point Unit 3 and

4 Plant Data

Book, Volume 1.

Although this document is not

a design

document, it appears

that it was used

as

a source

document

for design input.

b.

Bechtel

drawing 5610-P-151,

Piping Isometric Auxiliary

Feedwater

System

Pump Discharge,

Rev. 0, November I, 1981,

-21-

had incorrect valve weights

shown for AFW valves CV-3-2818,

CV-3-2816,

and CV-2-2817.

The team confirmed that the

valve weights identified on the vendor valve drawing were

on Bechtel. Drawing 5177-162-P-325,

Rev. 1, dated

May 16,

1983,

and that these weights were used in the piping stress

analysis.

During the inspection,

FP&L initiated an

External

Request for As-Built Verification and Document

Review to correct the identified discrepancies

in the

Bechtel isometric drawings.

c.

Bechtel calculation M-08-093-03, Auxiliary Feedwater

Flow

At Minimum Steam Conditions,

Rev. 0, May 4,

1982,

references

FP&L Plant Data Book, Sections

5.6 and 5.7, for

pump performance ratings.

As stated

above

(subparagraph

a), the Plant Data

Book is an uncontrolled

document

and is

not considered

a suitable

source for design input.

d.

FP&L Calculation,

Low Level Alarm on Condensate

Storage

Tank,

November 15,

1979,

does not identify all of the

assumptions

and design inputs used to perform the

calculation.

The calculation

was performed to establish

the alarm setpoint a'lerting the operator in the control

room of the need to provide makeup water or transfer to an

alternate

water supply in order to prevent

a low pump

suction pressure

condition from occurring.

The team found

no evidence in the calculation that the preparer

considered

the

NPSH required to maintain

AFW pump operation.

Instead,

the preparer

appeared

to have

assumed that the minimUm NPSH

would be below the instrument tap,

because

the analysis

calculated

the height above the instrument tap which

corresponds

to 20 minutes of water at a usage rate of 600

gpm with a

105 factor for conservatism.

The team

independently

confirmed that the

NPSH is well below the

instrument tap and the design is not deficient.

However,

the calculation did not document

assumptions

nor identified

those assumptions

that required verification as the design

proceeded.

The calculation did not define the design

bases

and their sources.

FP&L procedures

in place at the time

this calculation

was performed required

a design analysis

to contain this information (guality Instruction

EPP-gI-3.1,

"Control of EPP Design,"

Rev. 2, October 9,

1979).

e.

Bechtel

Drawing 5610-M-339 Sheet I of 1, Rev.

15,

incorrectly shows that the nitrogen system pressure

control

valves

PC-3-1706,

PC-3-1708,

PC-4-1705,

and PC-4-1709

were

set to provide

55 psig.

These

pressure

control valves were

set for 80 psig.

f.

The

AFW System Description and Design

Bases

document dated

January 31,

1985 had the following errors.

The system description stated that an air signal is

supplied

by a differential pressure

controller which

is set to maintain

a minimum pump discharge

pressure

22

approximately

125 psi higher than the steam supply

pressure.

As observed during the inspection, this

design feature

had been disconnected

(see Operations

and Surveillance Observation 8).

The system description incorrectly stated that when

instrument air pressure

drops

below 55 psig (nitrogen

regulator valve outlet pressure),

check valves

open to

automatically supply backup nitrogen.

As stated

previously, the pressure

control valves were set at 80

psig.

The system description incorrectly stated that the low

pressure

nitrogen alarm will allow about

10 minutes

for the operator to get to the station,

close off the

first bottle and cut in bottles 2, 3, and 4, which

will each provide about

a 30 minute supply to the flow

control valves.

This description

appeared

to refer to

the intended operation of the nitrogen station before

the station

was divided into two trains with three

bottles in train I and two bottles in train 2.

The

described action would violate the single failure

criterion.

5.

PC/N Numbers 80-78 and 80-79 were reviewed.

These

PC/Ms

addressed

the diversity of the power supplies to the steam

admission

valves of the auxiliary feedwater

system.

The steam

supply for the auxiliary feedwater

pump turbines is developed in

, the steam generators

and fed to the station

common auxiliary

feedwater turbine

pumps through six steam lines associated

with

the six steam generators

(three

steam generators

per unit).

'Each

steam generator is isolated from the steam

header with a

normally closed motor-operated

gate valve.

These valves are

powered from a safety-related

power supply (two motor-operators

per unit are

DC powered

and

one is AC powered)

and will auto-

matically open

upon

an auxiliary feedwater initiation signal.

Downstream of these

steam admission valves,

steam vents are

provided to vent off steam that may leak past the isolation

valves.

The following observations

were

made during the review

of the modification package:

a.

The modification of the motor-operators

on the steam supply

valves involved the purchase

of new

DC motor starters.

These motor starters

were specified

and purchased

by

material requisition No. 5177-B6-E-818-4.

These starters

were to be supplied complete with motor overload heaters

compatible with Limitorque operators.

The team reviewed

the motor starter vendor's

drawings to determine

the

overload heater size supplied

and to verify that the type

of overload heater installed agreed with the drawing.

In response

to a team request for criteria and the

calculation

used to determine

the size of the motor

overload heater

needed

to protect the steam supply valve

motors, the licensee

produced

a preliminary calculation,

23

R

~

No. 5177-462-E-02,

prepared

on September

6,

1985 (i.e.,

prepared

during the inspection), to demonstrate

that the

as-installed

motor overload protection would not trip the

valve motor for continuous currents

below 9.19 amperes.

From inspection of the motor nameplate

data,

the team

determined. that these

DC motors are

5 minute duty rated

motors

and the full load current is 6.5 amperes.

This

results in a trip point 140 percent of full load-current.

The team independently

determined that the setting of the

overload devices

provided inadequate

ovet load or stall

protection for the motor-operators.

The team also

confirmed this conclusion with the motor-operator vendor's

engineering

department.

The team's

concern

was that the. motor insulation could be

damaged

during normal plant operations

or periodic testing

because of inadequate

overload protection.

This could

result in the inability of the

DC motor-operated

valves to

perform their safety function during

a design basis event.

In an attempt to determine the generic implications of this

issue,

the team requested, the Bechtel criteria used to

determine

the overload protection for the existing

AC

motor-operated

valve on the third steam supply line.

No

basis for selection of the overload protection

on these

motor-operated

valves at Turkey Point was provided during

the inspection.

The failure of the design organization to verify the

adequacy of the overload protection specified for the

DC

motor-operated

valves is contrary to ANSI N45.2. 11-1974

Section 6.3 which requires that specified parts

and

equipment

be suitable for the required application.

This

item will remain unresolved

pending following by the Region

II Office (50-250/8532-12

50-251/8532-12).

b.

Implementation of the design

change

process failed to

verify that the design

change

did not violate the original

design function.

The proposed

cable routing for motor cable 400128( from

motor starter

3N1403 to steam valve MOV-3-1403, as

shown in

the cable

and raceway schedule,

was

78 feet of 5 conductor

AWG No.

12 wire. The team requested

the sizing criteria and

supporting calculations that would indicate that the

conductor size

was sufficient.

During the second

week of

the inspection the licensee

produced

a calculation,

dated

September

10, 1985, With no calculation

number or file

identification.

The calculation

was prepared

during the

inspection

and appears

to have

been

performed in response

to the team's

concerns

about the adequacy of the wire size.

No earlier calculation could be located at Bechtel's

offices either

on site or in Gaithersburg,

Maryland.

The

calculation

used as-installed

cable lengths obtained

from

Bechtel's

5177-E-45C Electrical Circuit Schedule

and motor

- 24-

data

from the Limitorque data sheet.

Although this motor

data did not agree with the motor nameplate full load

current, fts application in this calculation

was judged to

be conservative

by the team.

The calculation demonstrated

that the cable's

ampacity and short circuit withstand

capability were adequate.

However, the calculation stated

that the cable resistance

was sufficiently low so that the

voltage drop was not a concern

because

voltage at the worst

case valve (MOV-4-1403) would remain above

96 volts

DC.

The team questioned this conclusion

because

Bechtel

had

failed to consider starting current.

The team contacted

the actuator manufacturer directly and

confirmed that starting current

and the resulting voltage

drop to the motor must be considered

because

the valve was

tested with only 90 volts

DC as the minimum starting

voltage.

To assess

the effect of starting current, the

team substituted

the published

53 amperes

locked rotor

current obtained

from the Limitorque data sheet for the

8

Amperes full load current used in the Bechtel calculation.

The team determined that the voltage would be less

than the

required

minimum starting voltage of 90 volts for

NOY-4-1403.

F

The team is concerned that during a loss of offsite power

and the resulting

DC system voltage drop, inadequate

voltage would be available at the motor terminals resulting

in a stall condition and

a failure of the

DC motor-operated

valves to perform their safety function.

The failure to adequately

understand

the requirements of

the original design

and to confirm that those

requirements

were met with the new design, is contrary to ANSI N45.2.11

Section 6.3 and 8.2.

This item will remain unresolved

pending followup by the Region II Office (50-250/8532-13;

50-251/8532-13).

c.

The control circuit schematic for the

DC and

AC motor-oper-

ated

steam isolation valves

shows that the control switch

used in the circuit is

a momentary open/closed

return to

normal control switch.

As a consequence,

this switch will

not stop the valve from automatically reopening following

an operator's

attempt to shut the valve as long as

an auxi-

liary feedwater initiation signal is present.

The licensee

had not recognized this design feature

(see Operations

and

Surveillance Observation

1.d for further discussion).

d.

PC/Vi 80-117 added

a second

steam vent valve between

the

steam admission valves

and the auxiliary feedwater

pump

turbines.

The original header

design contained

an

air-operated,

DC solenoid controlled steam vent valve whose

purpose

was to vent steam that may leak by the normally

closed

steam admission valves.

The vent valve is normally

open

and closes

when the

DC solenoid is energized

through

a

pressure

interlock.

When the steam supply header

was

- 25-

separated

into two headers,

an additional vent valve was

added.

The solenoid for this new valve must be energized

to close the valve; however, the valve was powered from an

.

AC source.

The team is concerned that on

a loss of AC

power the open vent on the train 2 steam

header will result

in a path for steam loss.

6.

The design of the nitrogen system failed to provide the required

separation

in the low nitrogen pressure

alarm circuit. Alarms

are provided on the redundant nitrogen system to warn the

operator that he must take action to maintain the nitrogen

system's ability to position the auxiliary feedwater flow

control valves.

The team determined that the low pressure

signals

from pressure

switches

PS-3-2322

(nitrogen train No. I)

and PS-3-2323

(nitrogen train No. 2) feed adjacent control

room

annunciator

windows.

Associated

pressure

switch contacts

must

close to alarm.

The team determined that the two signals

share

a

common field wire (cable 3R38/3C05-TB3414/I is a

3 conductor

cable with wire AN38 common to both alarm circuits).

The team is concerned that

a single failure, such

as

a loose or

disconnected

wire could result in the co+non

mode failure of all

low pressure

alarms for the redundant nitrogen system.

Further,

this design

appears

to be contrary to the redundancy

and

separation

requirements

of ANSI N45.2.11, Section 3.2.

This

item will remain unresolved

pending followup by the Region II

Office (50-250/8532-14;

50-251/8532-14).

7.

The team reviewed

PC/M 83-05 concerning

replacement of the

safety-related

station batteries.

The auxiliary feedwater

system

uses direct current motor-operated

valves

and control

'systems

whose

power is derived from the station batteries.

Turkey Point Units 3 and 4 share safety-related

batteries

such

that the

DC power for some of the .Unit 3 auxiliary feedwater

components

is derived from the Unit 4 batteries.

The converse

is true for Unit 4 auxiliary feedwater

components.

The

following observations

were

made during the review of this

modification package.

a,

The safety-related

battery system which existed before

PC/M

83-05 consisted of four batteries,

two per unit.

Unit 3

had

one

C&D battery rated at

1885 ampere-hours

and an

EXIDE

battery rated at 648 ampere-hours,

Unit 4 had one

C&D

battery rated at 2175 ampere-hours

and

an

EXIDE battery

rated at 648 ampere

hours,

With PC/M 83-05, the

1885

ampere-hour

and 2175 ampere-hour

C&D batteries

were

replaced with smaller Gould-GNB 1800 ampere-hour cells.

The 648 ampere-hour

EXIDE batteries

were replaced with

larger Gould-GNB 1200 ampere-hour cells.

These

new

batteries

were purchased

using Bechtel specification

5177-272-E-850.1,

Rev. 0, dated January

18,

1983.

This

document contained

a one-hour battery load profile and

required corrections for

a minimum electrolyte temperature

of 55'

and

an 80 percent end-of-life compensation

in

accordance

with IEEE Standard

485. This specified load

-26-

profile did not agree with that given in FSAR Table 8.2.4.

The team noted that the

DC loads listed in this table did

not include the auxiliary feedwater

DC motor-operated

valves.

In an attempt to determine if all

DC loads

were

accounted for in the sizing of the

new replacement

batteries,

the team requested

the battery sizing

calculations.

The licensee

was unable to produce

an analysis

oP calcu-

lation which was used to develop the load profile used in

the procurement specification.

However, the licensee

did

exhibit a

DC 'system capability study, calculation

5177-399-E-01,

which was performed

by Bechtel during the

first half of 1985.

The purpose of this study was to.

determine

the capability of the

DC system to respond to the

unavailability of selected batteries

under different

operating conditions.

In case I of this study,

each

battery was checked with its own emergency

loads.

This

calculation did include loads for the auxiliary

feedwater'C

motor-operated

valves;

however, it assumed

data

based

upon

a preliminary 1980 calculation

and not on manu-

facturer's

data or the equipment

nameplate

data.

This

calculation included inappropriate

assumptions

for the

steady-state

load by basing this load on battery charger

readings

under normal operating plant conditions.

The

calculation did not identify these

as assumptions

requiring

verification.

This calculation also did not include design

margin correction factors for temperature

or inadequate

maintenance

as required

by IEEE Standard

485.

b.

The design modification process failed to include adequate

acceptance

criteria and verification testing for the

new

batteries.

The purchasing

documents specified required

testing

by the battery manufacturer.

Gould-GNB performed

a

standard eight hour capacity test which showed that the

batteries

would deliver at least their eight hour rated

capacity.

This test stopped short of determining

any

margin above rating (Inspection Report 83779 dated

May 5,

1983).

The manufacturer

also performed

a load duty cycle

test

on selected cells in accordance

with the specified

load profile but failed to correct the discharge

rates for

the specified

minimum temperature

condition.

The post-mod-

ification testing performed

on the Unit 3

B battery (Plant

Mork Order 358353) tested

the

new battery using the

FSAR

half hour profile, not the one hour duty cycle of the

specification.

Again, no temperature

correction

was

made

to the discharge

rate

as indicated

on the July 12,

1985

data sheets.

Because of the lack of an acceptable

load analysis

combined

with inadequate

testing,

the team was unable to determine

the degree of margin existing in the

new batteries.

c.

The plant operating

procedures for the

DC System failed to

reference

the specific periodic testing requirements

for

- 27-

the

new Gould-GNB batteries.

Plant Operating

Procedure

96041.1,

dated

June

19, 1985, specified the requirements

for the monthly equalizing charge.

However, the

new

Gould-GNB batteries

are

composed of lead calcium cells,

and

this type of battery cell should not be given monthly

equalizing charges.

Instead,

they should only be given an

equalizing charge

when required in accordance

with the

manufacturer's

recommendation.

Further, this operating

procedure

references

the instruction manuals for the old

batteries

and does not reference

the new Gould-GNB in-

struction manuals.

Also this procedure calls for different

float and equalizing voltages for the two new Unit 3 bat-

teries.

These batteries

are both made

up of Gould-GNB

NCX

type cells and should have the

same charging voltages.

Plant operating

Procedures

9654.1

and 9654.2,

dated

November 8, 1984, describe

the load test procedures for all

four safety-related

batteries.

Again, these

procedures

only refer to the

CSD Batteries Instruction Manual

(even

though batteries

3B and

4A were originally EXIDE batteries)

and do not reference

the new Gould-GNB instructions.

Additionally, the description of the battery load test

profile used in these

procedures

use the 30 minute

FSAR

profile also without compensation for minimum electrolyte

temperature

requirements.

The team could not find plant operating

procedures

describing

a battery performance test to determine actual

battery capacity

compared to rated capacity

(as

recommended

by IEEE Standard

450).

The apparent failure to establish

and implement technically

adequate

procedures for the

new station batteries will

remain unresolved

pending followup by the Region II Office

(50-250/8532-15;

50-251/8532-15).

'he

team had

a significant concern that excessive

reliance

was

placed

on operator action instead of design features

to ensure

the proper functioning of the auxiliary feedwater

system.

Specifically, the team was concerned that immediate operator

action

may be required

upon initiation of the auxiliary feed-

watet

system following a loss of main feedwater

and reactor trip

with a concomitant loss of the non-safety-related

instrument air

supply.

Although the auxiliary feedwater

system is designed

to

automatically initiate, design calculations

do not exist which

demonstrate

that the system will continue to run for a period of

time without immediate operator action.

This concern is, in

part,

based

upon the lack of design analyses

to support nitrogen

system design details

and the need for immediate operator action

inherent in the design of the nitrogen system.

This concern is

based

upon the following observations:

Lack of design analysis

based

upon the as-installed

system

to document the setpoint selection for pressure

switches

used to alert the operator that ten minutes of nitrogen

-28-

remain before loss of motive and control pressure (i.e.,

closure of flow control valves

and loss of all feedwater).

Lack of design criterion to define

how long the auxiliary

feedwater,

system

has to operate without operation action.

Consequently,

no guidance

was provided to establish operat-

ing limits on available nitrogen supply before reaching the

low level setpoint.

Lack of engineering direction with respect to post-modifi-

cation testing requirements

to confirm the adequacy of the

installation to design

bases.

II. ~ll l

A review of the corporate

and site quality assurance

auditing

activities revealed that these audits,

as implemented,

neither

had

identified nor were capable of identifying quality concerns of a

technical

and operational

nature similar to those

concerns identified

during this

NRC inspection.

Both the corporate

vendor audit and the

plant audit programs

were designed

to assure that gA programs

met

NRC

requirements

and licensee

commitments

from a programmatic basis only.

The following are examples of audits

conducted

by corporate

and site

gA staffs that failed to identify any of the significant weaknesses

identified during this inspection.

Audit Numbers

Activit Audited

08. 01. DTLMD.84. 1

OAS-EPP-83-1

gAS-JPE-84-1

gAO-PTP-84-549

gAO-PTN-85-657

gAO-PTP-82-10-421

0AO-PTP-84-584

gA program including

design control

(BPCO)

Power Plant Engineering

Training

Plant Change-Modification

The lack of an implemented corporate

and site audit program providing

for technical

and operational

reviews of vendor and plant activities

meant that

FPSL management

was not receiving important feedback

on

the quality of activities affecting the safe operation of the plant.

The team noted that recent Performance

Enhancement

Program

initiatives were being implemented

and guality Improvement

Program

efforts were underway to address

some aspects

of these

gA weaknesses.

The progress of this effort will be tracked

by the

NRC Region II

Office as part of their routine followup to the licensee's

Perform-

ance

Enhancement

Program.

IV.

MANAGEMENT EXIT MEETINGS

An exit meeting

was conducted

on September

13,

1985, at the Turkey Point

plant.

The licensee's

representatives

are identified in the Appendix.

- 29-

The scope of the inspection

was discussed,

and the licensee

was informed

that the inspection would continue with further in-office data review and

analysis

by team members.

The licensee

was informed that

some of the ob-

servations

could become potential enforcement findings.

The team members

presented their observations for each area

inspected

and responded

to

questions

from licensee's

representatives.

-30-

Persons

Contacted

APPENDIX

The following lists the persons

who attended

the exit interview.

persons

were contacted

during this inspection

and other technica

strative personnel

were also contacted.

C. 0.

Woody, Vice President,

Nuclear Operations

J.

W, Dickey, Assistant to the Vice President,

Nuclear Operation

C.

M. Wethy, Vice President,

Turkey Point

C. J. Baker, Plant Manager,

Nuclear

H. T. Young, Site Project Manager

and Acting Plant Manager

D. D. Grandage,

Operations

Superintendent

T. A. Finn, Operations

Supervisor

J.

E. Price,

Corporate

Engineer

R. J. Acosta, guality Assurance

Superintendent

L.

W. Bladow, gualfty Assurance

Supervisor

T. P. Coste, Project guality 'Assurance

Engineer

J.

W. Kappes,

Maintenance

Superintendent

W. C. Miller, Training Supervisor

E. F. Hayes.

I&C Department Supervisor

S.

G. Brain, Turkey Point Project Engineer

K. L. Jones,

Technical

Department Supervisor

J. Arias, Jr., Regulatory

and Compliance Supervisor

'.

E. Boger,

ANI Inspector

J.

K. Hayes,

Manager, Licensing and guality Assurance

E.

H. O'Neal,

Systems

Engineer,

AFWS

J.

M. Donfs, Site Resident

Engineering Supervisor

H. E. Hartman, In-Service Inspection Supervisor

R. Gouldy, Corporate,

Licensing

D.

W. Haase,

Safety Engineering,

Group Chairman

M. J. Crisler, gualfty Control Supervisor

G.

M. Vaux, Safety Engineer

J. Rosenfeker,

Corporate

Engineer

F.

H. Southworth, Corporate

Engineer

R. A. Longtemps, Assistant Superintendent,

Maintenance

Some of these

1 and admini-

Enclosure

2

Su

ested Addition

The following insert would update the draft report.

This insert could

be placed after the first full paragraph

on page 35:

The NRC's Office for Analysis and Evaluation of Operational

Data

collects,

assesses,

and distributes

data,

including statisical

measures

of licensee

performance.

Recent activities in this regard

include:

o

The Licensee

Event Report System

was modified through adoption

of a new rule, 50.73, which was effective January I, 1984.

The

new LER rule, for the first time, places

uniform reporting

requirements

on all nuclear

power plants

and assures

that events

of interest,

such

as actuations of all engineered

safety features,

will be reported to the

NRC.

Thus data,

which was not previously

readily available,

now exists to track the operational

experience

of each plant on

a defined

and consistent

base.

o

AEOD analyzes

the trends

and patterns of individual plant perfor-

mance

as well as that of the industry.

Included in this activity

are performance

indicators

based

upon operational

data.

Two major

studies

in this regard

have

been

produced;

one study covers the

scram history of all plants during 1984,

and the other study covers

the actuation of Engineered

Safety Features

(ESF) equipment for the

first six months of 1984.

These studies

have

been distributed to

the staff and are intended for use

as input into the

SALP Program.

hase studies

are the first in a series of reports

on scrams

and

ESF

actuations.

Subsequent

reports will also consider the trends in these

measures

of licensee

performance.

AEOD also

has in progress

studies

which will provide statistical

measures

associated

with safety system

availability and technical specification violations.

o

As another specific measure of plant performance,

AEOD is implementing

a quantitative

program to assess

the quality of Licensee

Event Reports

prepared

by licensees.

This program provides

a summary of the strengths

and.weaknesses

of LERs from individual plants

and then provides

a summary

of all plants.

This data is also being routinely provided to each

region

as input to SALP determinations.