ML17345A658

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Insp Repts 50-250/89-12 & 50-251/89-12 on 890225-0331. Violation Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Esf Walkdowns,Operational Safety & Plant Events.One Unresolved Item Identified
ML17345A658
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/24/1989
From: Butcher R, Crlenjak R, Mcelhinney T, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17345A655 List:
References
50-250-89-12, 50-251-89-12, NUDOCS 8905100054
Download: ML17345A658 (19)


See also: IR 05000250/1989012

Text

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UNITED STATES

NUCLEAR R EGU LATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-2SO/89-12

and SO-251/89-12

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami,

FL

33.'.02

Docket Nos.:

50-250

and 50-251

Facility Name:

Turkey Point

3 and

4

License Nos.:

DPR-31

and

DPR-41

Inspection

Conducted:

February

25,

1989 through March 31,

1989

Inspectors:

R.

C. Butcher,

Senior

Resi ent Inspector

ate

igned

T.

F. McElhinney, Resident

nspector

Da

e

igned

G. A.

S

ebli, Resid

t In pector

Approved by

R.

V. Crlenja

, Section

C

ef

Division of Reactor Projects

4'.

C

Da

e

S gned

ate

igned

SUMMARY

Scope:

This routine resident

inspector inspection entailed direct inspection

at

the

site

in

the

areas

of monthly surveillance

observations,

monthly

maintenance

observations,

engineered

safety

features

walkdowns, operational

safety

and plant events.

Results:

One violation was identified:

Failure to follow procedures

resulting

in valve 4-201B being

open

and draining

RCS water to the containment

sump.

One

licensee

identified violation

was

identified:

Failure

to

calibrate

a liquid radwaste

effluent line flow transmitter wit1in

ADM-021 frequency.

One unresolved

item" was identified in that Reactor Coolant

Pump

(RCP)

seal

injection throttle valve

4-297A was

open, contrary to GOP-305,

resulting in the inadvertent

increase

in drain

down water level.

"Unresolved

items

are

matters

about

which

more

information is

required

to

determine

whether they are acceptable

or may involve violations or deviations.

N'051OI.IO54

~~.A@42*

PDR

AEIOCK 0. OOOZCO

Q

PDC

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

"T. Abbatiello, guality Assurance

Supervisor

J.

W. Anderson, (}uality Assurance

Supervisor

J. Arias, Senior Technical Advisor to the Plant Manager

L.

W. Bladow, guality Assurance

Superintendent

J.

E. Cross,

Plant Manager-Nuclear

"R. J. Earl, guality Control Supervisor

T. A. Finn, Training Supervisor

S. 'T. Hale,

Engineering Project Supervisor

R. J. Gianfrencesco,

Maintenance

Superintendent

V. A. Kaminskas,

Technical

Department

Supervisor

R.

G.

Mende, Operations

Supervisor

  • J.

S.

Odom, Site Vice President

L.

W. Pearce,

Operations

Superintendent

"F.

H. Southworth, Assistant to Site

VP

J.

C. Strong,

Mechanical

Department

Supervisor

M. Stanton,

Instrument

and Control Department Supervisor

"K. Van Dyne, Acting Regulatory

and Compliance Supervisor

M. B. Wayland, Electrical

Department

Supervisor

"J.

D. Webb, Operations - Maintenance

Coordinator

Other

licensee

employees

contacted

included

construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

"Attended exit interview on March 31,

1989

Note:

An alphabetical

tabulation of acronyms

used in this report is

listed in paragraph

12.

Followup on Items of Noncompliance

(92702)

A review

was

conducted

of the following noncompliances

to assure

that

corrective actions

were adequately

implemented

and resulted

in conformance

with regulatory

requirements.

Verification of corrective

action

was

achieved

through record reviews,

observation

and discussions

with licensee

personnel.

Licensee

correspondence

was

evaluated

to

ensure

that

the

responses

were timely and that corrective actions

were

implemented within

the time periods specified

i.n the reply.

(Closed)

Violation 50-250,251/88-14-01,

concerning

material

for use

in

ICW gauge fittings was not properly controlled.

The licensee

responded

to

this violation

in letter

L-88-364,

dated

August 29,

1988.

The

NRC

considered

the

response

and the actions

taken

to prevent

recurrence

to

be adequate.

This violation is closed.

(Closed) Violation 50-250,251/88-18-01,

concerning

the* failur e to follow

procedure

for rod control

system malfunction.

The licensee

responded

to

this violation in Letter

L-88-433,

dated

September

30,

1988.

The

NRC

considered

their response

and

the actions

taken to prevent recurrence

to

be adequate.

This violation is closed.

Follow-up on Inspector

Followup Items

( IFIs) (92701).

(Closed)

Inspector

Followup

Item

50-250,251/88-11-03,

concerning

the

differences

in documentation

associated

with ICW gauge

assembly material.

This IFI was

subsequently

upgraded

to

a violation (50-250,251/88-14-01)

and therefore this IFI is closed.

Onsite

Followup

and In-Office Review of Written

Reports

of Nonroutine

Events

(92700/90712)

The

Licensee

Event

Reports

( LERs)

discussed

below were

reviewed

and

closed.

The inspectors verified that reporting requirements

had

been

met,

root

cause

analysis

was

performed,

corrective

actions

appeared

appropriate,

and generic applicability had

been considered.

Additionally,

the

inspectors

verified that

the

licensee

had

reviewed

each

event,

corrective actions

were implemented,

responsibility for corrective actions

not fully completed

was clearly

assigned,

safety

questions

had

been

evaluated

and resolved,

and violations of regulations

or

TS conditions

had

been identified.

When applicable,

the criteria of

10 CFR 2,

Appendix

C,

were applied.

(Closed)

LER

50-251/87-19,

concerning

a

turbine

runback

caused

by

a

spurious

spi ke in the

RPI system

due to

a

loose

solder joint in

a cable

connector

for

Rod

E-5.

The

loose

solder joint was

repaired

and

the

connectors

for all remaining

RPIs

were

inspected

and defects

identified.

This

LER is closed.

(Closed)

LER

50-251/87-25,

concerning

a

containment

and

control

room

ventilation isolation

due to high Rubidium in the containment following a

unit shutdown.

The event

was evaluated

to have

been

caused

by the rapid

shutdown of the unit and

subsequent

depressurization

as

a precautionary

measure

against

an approaching

hurricane.

An

RCS

leak rate calculation

was performed

and the results

showed

no unexpected

RCS leakage.

This

LER

is closed.

(Closed)

LER 50-250/88-02,

concerning

a reactor

coolant

system

pressure

decrease

caused

by

a malfunctioning pressurizer

spray valve.

The primary

cause of the event

was

a defective controller for pressurizer

spray valve

PCV-3-455B.

The controller

was

subsequently

replaced.

This

LER is

closed.

(Closed)

LER 50-250/88-04,

concerning

AFW initiation on low SG level due

to inadequate

monitoring of the

SG level

by the operator.

The root cause

of the event

was

the failure of the operator to monitor

SG level

due to

involvement

in other testing.

The operator

was

counseled

and the event

was discussed

with all other operations

personnel.

This

LER is closed.

5.

Monthly Surveillance

Observations

(61726)

The

inspectors

observed

TS required

surveillance

testing

and verified:

that

the test

procedure

conformed

to the

requirements

of the

TS,

that

testing

was

performed

in accordance

with adequate

procedures,

that test

instrumentation

was calibrated,

that limiting conditions

for operation

(LCO) were met, that test results

met acceptance

criteria requirements

and

were reviewed

by personnel

other than

the individual directing the test,

that

deficiencies

were identified,

as

appropriate,

and

were

properly

reviewed

and resolved

by management

personnel

and that

system

restoration

was

adequate.

For completed tests,

the

inspectors

verified that testing

frequencies

were met and tests

were performed

by qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

3-OSP-075.

1

Auxiliary Feedwater

Train

1 Operability

Verification

0-OSP-023.

1

Diesel Generator Operability Test

O-OSP-074.3

Standby

Steam Generator

Feedwater

Pumps

Available Test

O-OSP-074.4

Standby

Steam Generator

Feedwater

Pumps/Cranking

Diesel's Test

On March 6,

1989,

during performance

of 3-OSP-075. 1, Auxiliary Feedwater

(AFW) Train

1 Operability Test, revision

dated

September

20,

1988,

the

A

AFW pump governor oil level

was

found out of sight high.

A Plant

Work

Order

(PWO)

was initiated to drain

some of the oil out of the governor

while the

pump was operating.

The oil was drained to the proper level in

the sightglass

and the test

was completed satisfactorily.

The inspectors

questioned

the

licensee

as to the

adequacy

of the governor oil filling

method

when

ILC department

draws

a

sample.

The vendor

manual

(Woodward

Governor)

recommends

that the oil level

be at the mark on the sightglass

with the

pump operating.

Oil level

should

be visible in the sightglass

under all other conditions.

The vendor further stated that the oil must

never

be

above

the line where

the

case

and

column castings

meet.

Oil

above this level will be churned into foam by the flyweight head.

The

I&C

department periodically drains

an oil sample

from the

AFW pump governors

for oil analysis,

This draining is accomplished

by a

PWO.

The inspectors

reviewed

some

of the instructions

contained

on

these

PWOs

and

found

varying degrees

of instructions listed.

Some instructions

gave

a specific

oil level while others

directed

I&C personnel

to return oil level

to

normal.

The inspectors

believe that non-specific instructions

on the

PWO

could lead to improper oil level

in the

AFW pump governors

such

as

was

found

on the

March 6,

1989,

surveillance

test.

The other

item noted

by

the

inspectors

is that

3-OSP-075. 1,

step

7. 13,

has

the operators

check

governor oil level prior to running the

pump by verifying that the level

is above the line in the sightglass.

This check verifies that the minimum

level is present,

however, it does

not verify if too much oil is present.

Therefore

the

pump could

be

started

with too

high of

a

level

in the

governor.

The

inspectors

will followup

on this

issue

via Inspector

Fol 1owup Item (IFI) 50-250,251/89-12-01.

On

March 27,

1989,

the

licensee

discovered

that

the liquid radwaste

effluent line flow transmitter,

FT-1064,

was

out of calibration.

The

operators

placed

Process

Radiation Monitor (PRM)

R-18 out of service

and

restricted

any

furt'her liquid releases

until

the

flow channel

was

calibrated.

The flow transmitter

was calibrated

and returned

to service

on

March 29,

1989.

The

flow transmitter

was

previously calibrated

on

April 11,

1987.

Technical

Specifications

(TS),

table

4. 1-3,

item 2.a,

specified

the liquid radwaste

effluent line flow rate

monitor channel

calibration frequency

as

each

refueling.

Since this flow transmitter is

common

equipment,

the

licensee

performed

the calibrations

based

on the

Unit 3 refueling

cycles.

However,

Administrative

Procedure

(ADM)-021,

Technical Specification

Implementation

Procedure,

revision dated

March 13,

1989,

table 4.3.6,

requires

that the

channel

calibration for FT-1064

be

performed

at least

once

per

18 months.

Considering

the

25 percent

grace

period from the last performance

date,

the flow transmitter

was required

to

be calibrated

by February

27,

1989.

TS 6.8. 1 requires

that written

procedures

and administrative policies shall

be established,

implemented

and maintained that meet or exceed

the requirements

and

recommendations

of

Appendix

A of USNRC Regulatory

Guide 1.33

and Sections

5. 1 and 5.3 of ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process..

ANSI

section

5. 1

requires

that

procedures

be

followed.

ADM-021, Technical Specification

Implementation

Procedure,

revision dated

March 13,

1989,

requires

that

the

requirements

of the

Interim

TS

be

complied with unless

the requirements

are either

waived in accordance

with

ADM-021, or are less restrictive than the current

TS.

Table 4.3.6 of the

Interim

TS

requires

that

the liquid radwaste

effluent line flow rate

monitor

be calibrated at least

once per

18 months.

Contrary to the above,

FT-1064

was

not calibrated within the specified

frequency,

and

a waiver

was

not

obtained

in

accordance

with

ADM-021.

This's

a violation,

however,

no notice of violation will be issued

since thi s item meets

the

criteria

specified

in

10 CFR 2,

Appendix

C, for

a licensee

identified

violation.

No violations or deviations

were identified in the areas

inspected.

Monthly Maintenance

Observations

(62703)

Station

maintenance

activities

on safety related

systems

and

components

were

observed

and

reviewed

to ascertain

that

they

were

conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and

standards,

and in conformance with TS.

The following items

were considered

during this review,

as appropriate:

LCOs

were

met while

components

or

systems

were

removed

from service;

approvals

were

obtained

prior

to initiating work; activities

were

accomplished

using approved

procedures

and

were

inspected

as applicable;

procedures

used

were

adequate

to control

the activity; troubleshooting

activities

were controlled

and repair

records

accurately

reflected

the

maintenance

performed;

functional

testing

and/or

calibrations

were

performed prior to returning components

or systems

to service;

gC records

were

maintained;

activities

were

accomplished

by qualified personnel;

parts

and materials

used

were properly certified; radiological controls

were properly

implemented;

gC hold points

were established

and

observed

where

required;

fire

prevention

controls

were

implemented;

outside

contractor

force activities

were

controlled

in

accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The

inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Repair of 4A HHSI pump.

Troubleshooting

"A" AFW pump

T&T valve.

Troubleshooting Unit 4

PORV Backup Nitrogen Regulators.

No violations or deviations

were identified in the areas

inspected.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room

operators,

observed

shift

turnovers

and

confirmed operability

of instrumentation.

The inspectors

verified the operability of selected

emergency

systems,

verified that

maintenance

work orders

had

been

submitted

as required

and that followup

and prioritization of work was

accomplished.

The

inspectors

reviewed

tagout

records,

verified compliance with TS

LCOs and verified the return

to service of affected

components.

By observation

and direct interviews,

verification

was

made

that

the

physical security plan was being implemented.

Plant

housekeeping/cleanliness

conditions

and

implementation

of

radiological controls were observed.

Tours of the intake structure

and diesel, auxiliary, control

and turbine

buildings

were

conducted

to observe

plant equipment conditions including

potential fire hazards, fluid leaks

and excessive

vibrations.

The

inspectors

walked

down accessible

portions of the following safety

related

systems to verify operability

and proper valve/switch alignment:

A and

B Emergency Diesel

Generators

Control

Room Vertical Panels

and Safeguards

Racks

Intake Cooling Water Structure

4160 Volt Buses

and

480 Volt Load and Motor .Control Centers

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank Area

Auxiliary Feedwater

Area

Unit 3 and

4 Main Steam Platforms

On

March 29,

1989,

the

licensee

shut

down Unit 3.

At 4:53 p.m.,

power

reduction

was initiated per

GOP-103,

Power Operation

to Hot Standby,

and

the unit

was

taken off line at 8:30 p.m.

Unit

4 was already

in cold

shutdown for

a refueling outage.

Unit 3

was

taken off line while the

licensee

assures

itself

of

the

effectiveness

o'f its

operator

requalification training program.

This action

was

taken

as

a result of

deficiencies

identified during requalification testing the previous week.

A Confirmation

of Action Letter

dated

March 30,

1989,

confirms

the

licensee's

commitment

to

take

Unit

3 off line until the

licensee

can

perform special

evaluations

to demonstrate

that operators

not involved in

the

recent

requalification testing

meet

performance

requi elements.

This

effort is expected

to be completed within one week.

On March 2,

1989, with Unit 4 in

Mode 5. and drained

down to the reactor

vessel

flange,

the Unit 4 Reactor Control Operator

(RCO) noted

an increase

in the

draindown level.

Investigation

by the operators

found that

the

increase

in level

was

due to unisolating

the

"A" Reactor

Coolant

Pump

(RCP)

seal injection isolation valve (4-298G).

The "A" RCP seal injection

throttle valve (4-297A), which is upstream

of 4-298G,

was

found

open

on

its backseat.

Valve 4-297A was required to be tagged closed in accordance

with

General

Operating

Procedure

(GOP)

4-305,

Hot

Standby

to

Cold

Shutdown,

under

a

cold

shutdown

clearance.

The

licensee

was still

investigating

this

incident

at

the

end

of this

inspection

period,

therefore,

this

item will

be

tracked

as

Unresolved

Item

(URI)

50-250,251/89-12-02.

No violations or deviations

were identified in the areas

inspected.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need for further followup action.

Plant

parameters

were

evaluated

during transient

response.

The significance of the event

was

evaluated

along with the

performance

of the

appropriate

safety

systems

and

the

actions

taken

by the

licensee.

The

inspectors

verified that

required

notifications were

made to the

NRC.

Evaluations

were performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were

examined,

as

appropriate:

details

regarding

the

cause

of the event;

event chronology; safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences,

if any;

and proposed corrective actions.

At

8: 15 a.m.

on

March 9,

1989,

the

licensee

declared

and

terminated

simultaneously

an

unusual

event after finding

Unit 4 drain valve

201B

open

and draining reactor

coolant to the containment

sump.

Unit 4 was

in

cold shutdown

and the licensee

was filling and venting the reactor coolant

system

per

4-0P-041.8.

Section

5.2.2. 15

requires

increasing

reactor

pressure

to

125 psig.

Due to the slow response

on pressure

increase,

at

5:45 a.m.,

an N.O.

was instructed to look for leaks or misaligned valves.

At

6: 15 a.m.,

valve

4-201B,

letdown

orifice

downstream

drain,

v:as

discovered

open with

a tygon tube

vent rig installed.

The tygon tubing

was

routed to drain to the containment

sump.

The valve

was

immediately

closed.

The Unit 4 containment

sump

level

instrumentation

was

out of

service

for maintenance.

Health

physics

reported

the

containment

sump

level

was at

67

inches

following this event

which corresponds

to

a

sump

inventory of approximately

9926

gallons.

The leak rate

was originally

estimated

at approximately

39.8

gpm.

Later calculations

indicate the leak

rate

was

probably closer to

11

gpm.

Based

on

an estimated

39

gpm, at

6:58 p.m.

per

the

PSN

log,

emergency

notification

should

have

been

initiated per the licensee's

Emergency

Plan

Implementing

Procedure

(EPIP)

20101.

Paragraph

3.2 of

EPIP

20101,

requires

declaration

of an

unusual

event if reactor coolant

system water inventory indicates

leakage

greater

than

10

gpm.

The licensee's

promptness

on reporting this event will be

discussed

in

Inspection

Report

50-250,251/89-08.

The

licensee

has

initiated

an

Event

Response

Team

(ERT)

to

review

the

circumstances

regarding

this

event

and

determine

the

cause

and

recommend

corrective

actions to prevent recurrence.

Preliminary investigation

has

shown that

a

drain rig was installed

on valve

201B on December

3,

1988, to permit work

on valves

CV-200A and

C.

No documentation

exists

showing this drain rig

was

ever

removed.

On January

13,

1989,

an

LLRT for valves

200A,

B and

C

was conducted

which required valve

201B to

be closed

and/or

capped.

The

clearance

for this test did not address

the

201B valve.

On January

17,

1989, operations verified valve

201B closed with independent verification.

Again

on

March 5,

1989,

operations

verified

valve

201B

closed

with

independent

verification.

On March 8,

1989,

at 3:00 p.m.,

the licensee

initiated fill and vent of the

RCS,

per 4-0P-041.8,

and control

valves

CV-200A,

B and

C were

opened

which would allow

RCS water to fill the

piping which valve

201B drains.

Paragraph

3. 1 of 4-0P-041.8

requires

the Chemical

and Volume Control System

be operable

or in operation.

Calculations

indicate

valve

201B was

open at the time

CV 200A,

B, and

C

were

opened

permitting

RCS water to drain to the containment

sump.

On

March 9,

1989, at 6: 15 a.m.,

valve 201B was found open

as stated earlier.

Operations

had conducted

procedure

OSP-041. 1, Reactor Coolant System

Leak

Rate Calculation,

on March 8,

1989, at 5:30 p.m.,

and

March 9,

1989, at

5:00 a.m.,

and failed to identify that valve

201B was

open

and draining

RCS water.

TS 6.8. 1 requires that written procedures

and administrative

policies

shall

be established,

implemented

and maintained that

meet or

exceed

the

requirements

and

recommendations

of Section

5. 1 of

ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process..

ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

section

5

~ 1.2

specifies

that

procedures

shall

be followed.

Operating

Procedure

4-0P-047,

CVCS-Charging

and

Letdown,

requires

valve

'-201B

to be closed

as its normal position.

Contrary to the above,

valve

201B was found open with no written clearance

to place

the valve in the

open position.

Failure to follow procedures

and maintain valve

201B in

the closed position will be identified

as violation 50-250,251/89-12-03.

Problems

with configuration control

have

been identified in previous

NRC

inspection

reports

and

have resulted

in violations being

issued.

Due to

NRC

concerns

in this

area

and

since

a root

cause

has

not yet

been

identified, this will be cited as

a separate

violations

9.

Installation

and Testing of Modifications (37828)

An

inspection

was

conducted

to

ascertain

the

licensee's

methods

of

assuring that'esign

changes

and modifications

meet the

requirements

of

Technical

Specifications,

10 CFR 50.59,

and

10 CFR 50,

Appendix B,

Criterion III.

Each

of the

PC/M

packages

contained

a written safety

evaluation

which concluded

that

the

change

could, be

implemented without

prior

NRC

approval

under

the

provisions

of

10 CFR 50.59.

Each

modification resulted

in the respective

system,

as described

in the

FSAR,

being

changed

to provide

increased reliability or maintainability.

None

of the

PC/Ms required

change

to the facility Technical

Specifications.

The

inspectors

verified

by direct observation

that the

work was being

performed

by

qualified

workers

and

in

accordance

with

approved

instructions

and drawings contained

in the work package.

The installation

of the

hardware

was verified to

be

in

accordance

with the

as-built

drawings.

Installation, preoperational,

and startup testing

were adequate

to ensure

that the

system/equipment

met the

performance

requirements

of

the design criteria.

The following modification was reviewed during this

inspection

period:

PC/M 87-100,

Turkey Point Unit 4 Reactor Cavity Seal

Replacement

(REA-TPN-86-83).

This

PC/M provided for the

replacement

of the Unit

4 reactor

cavity seal

system

and the install-ation of

a restraint

system

for the reactor cavity seal

ring plate in its storage location.

The

seal

system

was modified to provide redundant

passive

seals

to prevent

leakage

in excess

of 50

GPM, which is well within the

capacity of the two 75

GPM reactor

sump

pumps

and also provides

an acceptable

rate of level decrease

in the reactor cavity/spent

fuel

pool levels (2 inches/hour)

allowing for adequate

operator

response

time.

This modification also

provided

an inflatable

seal

to reduce

primary seal

leakage

to as

low as practical (less

than

1

GPM) for housekeeping

and- ALARA concerns.

The non-safety

related

inflatable

seal

is also

provided with

a

continuous

pressurization

system.

The

package

also

addressed

the

replacement

of twelve reactor cavity seal ring anchor bolts with

grout-in-place

type anchor bolts.

10

In addition to the

PC/M the following procedures

were reviewed to ensure

this

new seal

design

was included:

O-GMM-043.6, Reactor

Vessel

Cavity Seal

Ring Installation

r

4-OP-038. 1, Preparation

for Refueling Activities

4-0P-201,

Filling/Draining the

Refueling

Cavity

and

the

SFP

Transfer Canal.

During the review of this PC/M,

one concern

was identified in that testing

of the

passive

seals

subsequent

to the initial installation test

may not

be adequate.

This item was discussed

in Inspection

Report

88-39

and

was

promptly corrected

by the licensee.

No violations or deviations

were identified in the areas

inspected.

10.

Management

Meeting (94702)

On March 16,

1989,

the bi-monthly NRC/FPL Management

Meeting was conducted

at the site.

This

was

the

tenth

in

a

series

of'eetings

which were

initiated by Enforcement

Action (EA) 87-85

issued

in October

1987.

The

meeting

was attended

by

NRC Regional

and

Headquarters

Management

and

FPL

Site

and

Corporate

Management.

The topics of discussion

included:

Plant

Status;

RHR draindown event of of January

19,

1989; Thimble tube cracks

on

Unit 3 seal table;

procurement of spare

parts for maintenance;

maintenance

improvement efforts;

and

new security initiatives.

11.

Exit Interview (30703)

The

inspection

scope

and

findings

were

summarized

during

management

interviews

held throughout

the reporting

period with the Plant Manager

Nuclear

and selected

members of his staff.

An exit meeting

was

conducted

on

March 31,

1988.

The

areas

requiring

management

attention

were

reviewed.

No proprietary

information

was

provided

to

the

inspectors

during the reporting period.

The inspectors

had the following findings:

50-250,251/89-12-01,

Inspector

Fol 1 owup Item.

Possible

improper

oil level in the

AFW pump governor.

(Paragraph

5)

50-250,251/89-12-02,

Unresolved

Item.

RCP

seal

injection

throttle

valve

4-297A in the

open

position

contrary

to

GOP

4-305,

resulting

in inadvertent

increase

in drain

down water

level.

(Paragraph

7)

50-250,251/89-12"03,

Violation.

Failure

to follow procedures

resulting in valve 201B being

open

and draining

RCS water to the

containment

sump.

(Paragraph

8)

Licensee

Identified Violation.

Failure to calibrate the liquid

radwaste

effluent

line

flow transmitter

at

the

frequency

specified

by ADM-021.

(Paragraph

5)

11

12.

Acronyms

and Abbreviations

ADM

a.m.

ANSI

AP

ASME

CCW

CCTY

CFR

CS

DP

ENS

EPIP

ERT

FPL

FSAR

HHSI

ICW

IEB

IFI

LCO

LER

LIV

LLRT

LOCA

MP

NCR

NO

NPSH

NRC

'ONOP

OOS

OP

OTSC

PA

PC/M

p.m.

PNSC

PSN

PSP

QA

QC

RCO

RCP

RCS

RHR

SRO

TS

TSA

URI

Administrati ve

ante

meridem

American National

Standards

In

Administrative Procedures

American Society of Mechanical

Component

Cooling Water

Closed Circuit Television

Code of Federal

Regulations

Containment

Spray

Differential Pressure

Emergency Notification System

Emergency

Plan

Implementing

Pr

Event

Response

Team

Florida Power

& Light

Final Safety Analysis Report

High Head Safety Injection

Intake Cooling Water

Inspection

and Enforcement

Bul

Inspector

Followup Item

Limiting Condition for Operati

Licensee

Event Report

Licensee Identified Violation

Local

Leak Rate Test

Loss of Coolant Accident

Maintenance

Procedures

Non-conformance

Report

Nuclear

Operator

Net Positive Suction

Head

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of Service

Operating

Procedure

On the Spot

Change

Protected

Area

Plant Change/Modification

post meridiem

Plant Nuclear Safety

Committee

Plant Supervisor

Nuclear

Physical

Security Procedures

Quality Assurance

Quality Control

Reactor Control Operator

Reactor Coolant

Pump

Reactor

Coolant System

Residual

Heat

Removal

Senior Reactor Operator

Technical Specification

Temporary

System Alteration

Unresolved

Item

stitue

Engineers

ocedure

letin

on