ML17342A801

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SALP Repts 50-250/87-19 & 50-251/87-19 for May 1986 - May 1987
ML17342A801
Person / Time
Site: Turkey Point  
Issue date: 07/17/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17342A800 List:
References
50-250-87-19, 50-251-87-19, NUDOCS 8707290208
Download: ML17342A801 (63)


See also: IR 05000250/1987019

Text

JUL I 7 tgof

ENCLOSURE

SALP

BOARD REPORT

U.

S.

NUCLEAR REGULATORY COMiMISSION

RFGION II

SYSTEMATIC ASSESSMiFHT

OF LICEHSEE

PERFORMANCE

IHSPECTION

REPORT

HUMiBER

50-250/87-19

50-251/87-19

FLORIDA PO'i",ER AND LIGHT COMPANY

TURKEY POINT UNITS 3 AND 4

MAY 1,

1986

THROUGH MAY 31,

1987

90~08 670717

PDR

ADOCN 05000250

PDR

I .

Introduc.i on

The

Systemat'.c

Assessment

of Licensee

Performance

(SALP) program is

an

integrated

NRC staff

e fort to collect available observations

and data

on

a periodic basis

and to-evaluate

licensee

performance

based

upon this

informa ion.

The

SALP

program

is

supplemental

to

normal

regulatory

processes

used

to determine

compliance- with

NRC rules

and

regulations.

The

SALP program is intended

to

be sufficiently diagnostic

to provide

a

rational

basis

for allocating

NRC

resources

and

to provide

meaningful

guidance

to licensee

management

to promote quality and

safety of plant

construction

and operation.

An

NRC

SALP Board,

composed

of the staff

members

listed below,

met

on

July 10,

1987, to'eview the collection of performance

observations

and

data

to assess

licensee

performance

in accordance

with guidance

in

NRC

Manual

Ch'apter

0516,

"Systematic

Assessment

of Licensee

Performance."

A

summary of the guidance

and'evaluation criteria is provided in Section II

of this report.

This report is

the

SALP Board's

assessment

of the

licensee's

safety

performance

at Turkey Point Units

3

and

4 for the

period

May 1,

1986,

through

May 31,

1987.

SALP Board for Turkey Point Units

3 and 4:

L. A. Reyes,

(Chairman) Director, Division of Reactor Projects

(DRP), RII

A.

F. Gibson, Director, Division of Reactor Safety

(DRS), RII

J.

P. Stohr, Director, Division of Radiation Safety

and

Safeguards

(DRSS), RII

D.

M. Verrelli, Chief, Reactor Projects

Branch

1,

DRP, RII

L.

S.

Rubenstein,

Director, Project Directorate II-2, Division of

Reactor Projects,

NRR

D.

G. McDonald, Project

Manager,

Project Directorate II-2, Division of

Reactor Projects,

NRR

D.

R. Brewer, Senior Resident

Inspector,

Turkey Point,

DRP, RII

Attendees

at

SALP Board Meeting:

M. L. Ernst,

Deputy Regional Administrator, RII

B. A. Wilson, Chief, Reactor Projects

Section

1C (RP1C),

DRP, RII

K. D. Landis, Chief, Technical

Support Staff (TSS),

DRP, RII

H. 0. Christensen,

Project Engineer,

RP1C,

DRP, RII

M. A. Scott, Project Engineer,

RP1C,

DRP, RII

K.

Van Dyne, Resident

Inspector,

Turkey Point,

DRP, RII

T.

C. MacArthur, Radiation Specialist,

TSS,

DRP, RII

J. Zeiler, Reactor

Engineer,

TSS,

DRP, RII

,

M.

M. Troskoski,

Regional

Coordinator - RII, .EDO

II.

Cl iteria

Licensee

performance

is assessed

in selected

functional areas

depending

on

whether

the facility has

been -in the

construction,

preoperational,

or

operating

phase

during

the

SALP review period.

Each

functional

area

represents

an area which is normally significant to nuclear safety

and the

environment

and

which is

a

normal

programmatic

area.

Some

functional

areas

may

no

be

assessed

because

of li tie or

no licensee

ac ivity or

lack

of meaningful

NRC observations.

Special

areas

may

be

added

to

highlight significant observations.

One or more of the following evaluation criteria was

used to 'assess

each

functional area;

however,

the

SALP Board is not limited to these criteria

.and others

may have

been

used

where appropriate.

C.

D.

F

G.

Management

involvement in assuring quality

Approach

to

the

resolution

of technical

issues

from

a

safety

standpoint

Responsiveness

to

t<RC initiatives

Enforcement history

Operational

and construction

events (including response

to, analysis

of, and corrective actions for)

St=->fing (including management)

Training and qualification effectiveness

Based

upon

the

SALP Board

assessment,

each

functional

area

evaluated

is

'classified

into one of three

performance

categories.

The definitions of

these

performance

categories

are:

Cateoorv

1:

Reduced

NRC attention

may

be

appropriate.

Licensee

management

attention

and

involvement

are

aggressive

and

oriented

toward nuclear

safe y; licensee

resources

are

ample

and effectively

used

such

that

a

high

level

of

performance

with respect

to

operational

safety or construction quality is being achieved.

~Cate or

2:

NRC attention

should

be

maintained

at

normal

levels.

Licensee

management

attention

and

involvement

are evident

and

are

concerned

with nuclear

safety;

licensee

resources

are

adequate

and

are

reasonably

effective

such

that satisfactory

performance

with

respect

to

operational

safety

or construction

quality is

being

achieved.

~Cate

or

3:

Both

NRC

and

licensee

attention

should

be

increased.

Licensee

management

attention

or

involvement

is

acceptable

and

considers

nuclear

safety,

but

weaknesses

are

evident;

licensee

resources

appear

to

be strained

or not effectively used

such that

minimally satisfactory

performance with respect

to operational

safety

or construction quality is being achieved.

The functional

are

being

evaluated

may

have

some a.tributes

that would

place

the

evaluation

in Category

1,

and others

that would place it in

either Catego".y

2 o.

3.

The final rating for each

functional

area

is

a

composite of the attributes

tempered with the judgement of

NRC management

as to the significance of individual items.

The

SALP Board

may also include

an appraisal

of the performance

trend of a

functioral

area.

This performance

trend will only be

used

when both

a

definite trend

os

performance within the evaluation

period is discernible

and

the

Board believes

that continuation of the trend

may result in

a

change

of performance

level.

The trend, if used,

is defined as:

~lm rovin

Licensee

perrormo-nce

was determined

to

be

improving near the

close of the assessment

period.

Da-lininc:

Licans

e performance

was

de:ermined

to

be declining

near

the

close o':he

assessmant

period.

III. Summary'f Results

A.

Overall Facility Evaluation

The licensee

has

made

some

noteworthy

improvements

in the last year

particularly

plant

operations,

maintenance,

and quality

programs

and administrative

controls affecting quality which all

had

been

identified

as

weaknesses

each of the last

two

SALP. periods.

These

improvements

may have

been at the expense

of management

attention

in

other

areas

such

as security,

where

performance

declined;

training

and

qualification

effectiveness

which

remained

a

weakness;

and

engineering

support,

which

was

included

for the first

time

as

a

functional

area

due

to

identified

deficiencies.

Emergency

preparedness

has

cont',nued

as

a major strength

area.

Since

the

licensee's

Performance

Enhancement

Program

(PEP)

was

implemented

by

a Confirmatory Order

in July 1984,

many significant

events

and

enhancements

have

occurred.

A Safety

System

Functional

Inspection

(SSFI)

was

conducted

in

1985 which resulted

in numerous

violations

and

a

substantial

Civil Penalty.

This resulted

in the

original

PEP

being

expanded

and

then

superseded

by

a

Confirmatory

Order

in

August 1986.

The

licensee

has

implemented

numerous

improvement

programs

and

expended

tremendous

resources

in their

commitment to safe

and reliable operation of the Turkey Point units.

The results of many of these

programs

have

been

evident during this

SALP

period.

These

results

have

included

tangible

benefits

in

facilities

such

as

a

new training building,

a

new administration

building,

and

a simulator

and

a maintenance

building that are nearing.

completion.

The

Phase

II Assessment

Program

has

also

provided

positive

results

such

as'hose

described

in Section IV.l,. of this

report.

In

October

1986,

the

licensee

submitted

their

proposed

Technical

Specifications

(TS)

to the,NRC for review

and approval.

These modified standard

TS represent

a significant

improvement

over

JUL I 7

l987

the old custom

TS.

Increased

staffing levels, training and enhanced

procedures

are

all

evidence

of

the

licensee's

commitment,

to

subs.an

ially upgrade

prev ously identified

problem

areas.

There

remains,

however,

some

evidence

of the

need for further management

responsiveness

in certain

areas.

'xamples

of this

include

the

imprudent decision to

s art

up Unit 4 in September

1986 with a

known

leak

on the vessel

head.

This

was

exacerbated

by the decision

to

restart

he unit in October following an inspection of the area which

showed

a substantial

spread of boric acid residues.

In addition,

the

NRC

Augmented

Inspection

Team

(AIT)

in

March

1987 initially

encountered

a management

attitude that appeared

more oriented

toward

a unit restart

rather

than

a comprehensive

analysis of the problem.

It should

be

noted

that

the

licensee's

subsequent

response

was

comprehensive

and

the corrective

actions

were

reviewed prior to the

HRC

concur ring in restart.

The

special

testing

of the

Emergency

Diesel

Generator

(EDG)

load

sequencers

was

another

instance

of

management

involvement

and

support that were initially perceived

to

be lacking but once

the

commitment to resolve

the

issue

was

made,

personnel

performed

in

a

comprehensive

and

technically

competent

manner.

Management

effectiveness

was also

lacking in the level of

awareness

of the

obligatio'ns

associated

with the

containment

and

surveillance

functions of international

safeguards.

The

HRC notes

that

management

attention

to solving the

problems at

Turkey Point is evident in a number of areas

and that this attitude

must continue

to

be successfully

conveyed to the plant personnel

at

all levels.

B.

The performance

categories

for the current

and previous

SALP period

in each functional

area

are

as follows:

Functional

Area

November

1, 1984-

May 1, 1986

7

Plant Operations

Radiological Controls

Maintenance

Surveillance

Fire Protection

Emergency

Preparedness

Security

and Safeguards

Outages

Quality Programs

and Administrative

Controls Affecting Quality

Licensing Activities

Training and Qualification

Effectiveness

Engineering

Support

H/R

Not Rated

"

N/R

2

2

2

2

N/R

1

3

.2

2

2

3

IV.

Performance

Analysis

A.

Plan.

Opera

ions

1.

Analysi s

During -this assessment

period,

inspections

were conducted

by the

residen

and regional

inspec

ion staff.

At the beginning of the

evaluation

period

Unit 3

was

in

commercial

operation

while

Unit 4

remained

shutdown

until

September

1986 while emergency

diesel

generator

loading

modifi'cations

were

being

performed.

Unit 3 continued

operating until early March 1987,

when it was

shutdown

for

refueling

and

maintenance.

Unit 4,

following

restart

in September,

operated

until March

1987 at which time

boric acid deposits

on the reactor

vessel

head

from the leaking

conoseal

were

discovered.

Both units

remained

shutdown

the

remainder of the

SALP period.

Since

the category of Operations

has received

three consecutive

SALP

3 ratings,

additional

HRC attention

was

devoted

to thi s

area.

A special

team inspection

was conducted

in February

1987

to specifically assess

plant operations

in addition to routine

and enhanced

',nspections

by the Resident

Inspector staff.

" Operations

has

been

identified

in

the

past

as

having

programmatic

deficiencies

in

a

number

of areas.

Among these

have

been

inadequate

system configuration control,

failure to

follow procedures,

excessive

on-the-spot

changes

to procedures,

inadequate

control

room

and

plant

labeling,

and

missed

surveillance- testing.

The previous

SALP report specifically singled out the licensee's

tendency

for

the

Operations

Department

to

operate

around

maintenance

problems.

Seven

examples

were cited, four of which

resulted

in violations.

During this

SALP period,

there

was

little indication

of this

tendency

and,

in

fact,

plant

management

has

stressed

ihe

concept

of Operations

as

the

"customer"

for

the

support

groups

such

as

Maintenance,

Engineering,

and the Technical

Departments.

The

outage

caused

by the leaking boric acid

from the conoseal

could be construed

to

be "operating

around

a maintenance

problem",

but

was

more

logically attributed

to Engineering

Support

(See

Section IV.L)

and

imprudent

management

decisions.

These

decisions

involved

the startup

of Unit'

in September

1986 with

a

known Reactor

Coolant

System

(.RCS)

leak

on the reactor

vessel

head

and the

restart of the Unit in October after

a short unrelated

outage.

With

regard

to

the

above

identified deficiencies,

both

the

Residents

and

the

team inspection

found that programmatically,

the

operators

have

been

sensitized

to

follow procedures

carefully.

Although nine of the twelve violations that occurred

in

.he Opera.ions

area

were attributed to failure to follow or

properly implement procedures,

the violations were

due p.imarily

to

either

personnel

error

or

incomplete

under standing

of

procedural

intent.

A comprehensive,

independent

verification

program exists

which

has

helped

reduce

personnel

errors.

The

policy of verbatim compliance with procedural

requirements

is

strongly supported

by the operations staff and plant management.

Improvements

in plant

labeling

are

discUssed

later

in this

section.

. One event that occurred at the end of the

SALP period tended to

refute

the

above

comments

with regard to procedural

adherence

and configuration control.

From May 28 until June

3,

1987, with

both units

in

mode

5, nitrogen intrusion into the Boric Acid

system

through

a failed boric acid transfer

pump seal,

caused

'problems with regard to operators

establishing

and maintaining

a

boric acid, flow path to the vessel

in accordance

with approved

procedures.

A special

inspection

was

conducted

in June

1987

and

although

the results

are

preliminary,

there

are

several

violations which are being considered

for escalated

enforcement.

In general,

management

involvement with operations

activities

has

increased

over the past year.

Shift briefings,

performed

by

a licensed

Senior

Reactor

Operator

(SRO),

are

performed after

each

shift

assumes

their duties.

These

briefings

provide

information relative to goals

and objectives for the

subsequent

shift.

As

a result,

general

awareness

of site activities is

enhanced

and complex evolutions are

more smoothly performed.

In December

1986,

the licensee

placed

a third

SRO on each shift

as

assistant

to

the

Plant

. Supervisor-Nuclear

(PSN).

As

a

result,

tours

of the facility by supervisory

personnel

have

increased.

This

has

resulted

in

more

prompt

deficiency

identification, resolu-ior. of problems,

and

increased

liaison

between

operators

and supervisor s.

The additional shift manning

has further reduced

the administrative

requirements

placed

on

the

PSN

which

was

begun

when administrative

technicians

were

assigned

to each shift during the last

SALP evaluation period.

The staffing of the Operations

Department,

is adequate

to meet

routine

needs.

The staffing level

has

remained

approximately

constant

at

125 persons.

However,

operator

overtime

has

been

excessive,and

was

found to

exceed

administrative

guidelines.

This

resulted

in

the

issuance

of

a

level

IV violation

as

discussed

in

Section

IV.I

of this

report.

The

increased

overtime workload resulted primarily from poor pass

rates

on

NRC

requalification

examinations

and site activities

accompanying

the 'dual unit outage

which occurred

between

March and June

1987.

JUL 17

195

The

licensee

has

since

resumed

five shift operation

with

a

licensed

shift'complement

of the

PSM (SRO). Assistant

PSH (SRO),

Nuclea

L"atch

Engineer

(SRO),

and

three

Reac.or

Con rol

Operators

(RO,

minimum).

Although additional

ROs

and

SROs are

presently

in license preparation

classes,

FPL does

not expect to

realize their design shift complement for another

two years.

The Operations-Maintenance

Coordinator,

a licensed

SRO,

and his

staff

improved

communications

between

the

two departments

and

for the most part, facilitated the operational

readiness

of the

plant.

However,

a proposed violation (e) listed in Section

IV.C

of this report

was partially due to poor communication

between

Operations

and

Maintenance

when

the

core

alterations

were

performed

without

establishing

containment

integrity.

Communications within the Operations

department

was

not evident

during

the

February

1987

team

inspection.

Communications

appeared

casual

and

on

a first name basis,

with operators

rarely

using

any

form of verbal

repeat

feedback.

Operators

indicated

to

HRC

inspectors

that

there

were

concerns

with in-plant

communications

including

radios

and

the

page

system.

Both

communications

systems

are being upgraded.

The violation in the

Emergency

Preparedness

analysis

section

documents

four examples

of disc-.epancies

associated

with the public address

system,

each

of which adversely

affected site communications.

Con rol

room

demeanor

remains

satisfactory

overall

but varies

between shifts.

The relatively small dual unit control

room is

susceptible

to crowding.

During

day shift, the control

room

becomes

busy

and

noisy.

The

requirement

for individuals to

obtain

permission

prior to entering

the control

area

is not

generally enforced.

However, supervisory

personnel

do minimize

visits by nonessential

personnel

during important evolutions

and

during shift turnover.

The clearance

tagging

center

was

moved

outside

the control

room during the latter half of the Unit 3

refueling'utage.

This

change

was

beneficial

in

reducing

personnel

traffic

flow

and

congestion.

The

licensee

is

considering

a permanent

relocation of the tagging center.

Unit 3 was in operation for approximately ten of the

13 months

during

this

SALP

period

and

experienced

eight

manual

or

automatic

unplanned

reactor trips.

Three of the trips were

due

to personnel

error in the conduct of periodic tests,

while three

others

were

due to problems with the turbine

governor control

oil

system.

The trip rate for Unit 3 is approximately

equal

to the industry

average

for older plants.

Unit 4 was only in

operation

for about

six

months

and

sustained

five manual

or

automatic

unplanned trips.

Four trips were caused

by equipment

malfunction, while the fifth was

due to

a procedural

error.

The

rate

of trips

for Unit 4

was

slightly

above

the

industry

average.

JUL

1 7

]987

The quality of plant procedures

continues

to improve as

more are

rewrit en

and

reissued

through

the

Procedures

Upgrade

Program

(PUP}.

The

PUP

has

been especially effective in improving the

con ent

and

form of approximately eight

hundred

procedures

and

has

reduced,

though not eliminated,

the potential for personnel

error

and

misinterpretation.

The

PUP

continues

to

be well

received

by the plant staff

and is widely recognized

for its

con ribution

to

reliable

plant

operations.

During

this

assessment

period

the

PUP

has

completed

130

surveillance

procedures

in

support

of the

Technical

Specification

upgrade

program.

Since

its

inception

the

PUP

has

responded

to

approximately

5,000

requests

for real

time

support

in the

improvement

of

existing

procedures.

The

large

volume

of

on-the-spot-changes

(OTSCs)

which existed

during the previous

SALP

period

has

been

reduced

to

a

manageable

level.

As

procedure quality has

improved there

has

been

less

need for the

operations staff to implement

OTSCs.

Additionally, supervisory

personnel

have

monitored

spot

changes

and

approved

only those

meeting

approved criteria.

An eouipment labeling

and valve tagging

program continues

to be

expanded.

Virtually all safety related

systems

have

had their

alum',num

tags

replaced

with larger,

more legible,

fiberglass,

color coded

tags.

Equipment stenciling effectively identifies

major components,

systems,

rooms

and buildings.

Separation

of

Unit 3 and

4 equipment

is emphasized

by color-coding, with tan

representing

common

equipment.

Control

room

panels

have

been

relabeled

with

clearly

legible

color-coded

power

supply

identification tags.

The labeling

and tagging

program

appears

to have resulted

in tangible benefits

in that licensee

trended

data

shows,

that, except for the

May 2,

1986 Unit 3 Trip,

no

other

personnel

errors

or reactor trips attributed

to

wrong

unit/wrong train events

over this

SALP period.

The

use oi brightly colored

information,

clearance

and

work

order tags allows operators

to more easily assess

the status of

equipment.

Even

minor

deficiencies

in

control

room

instrumentation

receive

work order

deficiency

tags

alerting

operators

to the discrepancy.

'

large

number of the deficiency

tags exist at

any

one time.

The minor deficiencies

may exist

for extended

periods

because

of

more

pressing

maintenance

requirements

on the

Instrument

and Control staff.

Coordinated

efforts between

the Operations

and Maintenance

Departments

have

maintained

the

amount of control

room instrumentation

which is

actually out of service

to acceptable

levels of magnitude

and

duration.

Instrumentation

which is subject to repeated

failures

is discussed

in the maintenance

analysis

section.

Management

has

continued

to

emphasize

the

requirement

for

housekeeping.

Primary

plant

housekeeping

has

continued

the

improving

trend

documented

during

the

previous

assessment

JUL 1P

]987

period.

Cleanliness

remains fully satisfactory

due, primarily,

to partial

cleanup

as

the repair effort progresses,

minimizing

.the

need

for large-scale,

post

maintenance

cleanup.

House-

keeping

prac.ices

are

better

implemented

in

plant

areas

containing safety related

equipment rather than balance

of plant

sys

ems.

As d'.scussed

in the Maintenance

analysis

section,

the

material

condition of the

secondary

systems

is not

as

good

as

prima y systems.

Some

severe

pump and valve leaks

have existed

for

extended

periods

in the

secondary

plant.

Additionally,

unused

hoses,

burned

out lightbulbs,

small

leaks

and

standing

water

are

not

uncommon

secondary

plant

housekeeping

deficiencies.

Activities associated

with the

Performance

Enhancement

Program

(PEP) were closely monitored.

The

PEP,

which was

confirmed

by

an

NRC Order dated July 13,

1984,

is intended

to address

NRC

concerns,

improve regulatory compliance

and 'implement regulatory

corrective action,

and is scheduled

to continue into 1988.

The

PEP

has

resulted

in improvements

in the following areas:

organizational

structure

and personnel,

guality Assurance

(gA)

program,

upgrade of Technical Specifications

(TS), establishment

of safety engineering

groups, allocation of additional

resources

and

upgrade

of facilities,

operation

enhancement,

procedures

upgrade,

improvement of the plant configuration control program,

and

training

and

improvements

in maintenance

management.

A

Program for Improved Operation

(PIO) was added

to the

PEP

by

a

Confirmation

of

Concurrence

letter

on

October

11,

1984,

and

includes

reviewing the Final Safety Analysis

Report

(FSAR) to

assure

plant

operation

within

the

safety

analysis,

identification

and

correction

of

surveillance

program

deficiencies,

and increased

management

awareness

and overview of

operations.

In

9eneral,

the

implementation

of the

PEP/PIO

and

Phase II

Assessment

has

shown

successes

in that

adequate

corporate

attention

and resources

have

been

focused

on identified problem

areas.

Adherence

to

established

schedules

and

regional

briefings

have

been

satisfactory

in

most

areas.

Upper

management's

commitment to excellence

is apparent

not only in

the

Turkey

Point

PEP

but

also

in

other

corporate

quality

improvement

programs.

. Licensee

management

has

continued

to

implement

and to support

PEP'nd

has

expanded

the

program to

include areas

not originally addressed.

The

contribution

of

the

Operations

Group to,overall

plant

operations

has

improved

considerably

within the

past

year.

Initial implementation of the various

upgrade

programs

has

made

noticeable

improvements

to control

room and plant operations

and

the

interface

with other -plant groups,

including Maintenance,

Training,

and Engineering.

10

JUL I V

ISSUE

Twelve violations were identified.

Nine of the twelve were due

to failure

o

follow or properly

implement

procedures

as

discussed

ea. lier.

Violations

e

(example, 1), i,

and

1

are

repetitive violations i ndica .i ng that corrective

action

may not

always

be effective at correcting

the root cause of the problem.

Twelve violations were identified:

c

~

Severity

Level

IV violation for three

examples of failure

to follow procedures

(reactor protection

system 'testing,

emergency diesel

generator

[EDG] valve lineup,

EOG startup

operation).

(86-25)

Severity

Level

IV violation for failure to establish

an

adequate

procedure for the control of several

EDG valves.

(86-25)

Severity

Level

IV violation

(one

example)

in which the

Plant Supervisor

Nuclear misinterpreted

an administrative

procedural

requirement

concerning

plant

work

order

priorities.

(86-25)

Sever i ty

Level

IV vio'. ation

for

not

impl ementing

an

off-normal

procedure

for

a failed

steam

1 ine

pressure

transmitter.

(Unit 3 only, 86-33)

e.

Severity

Level

IV violation for two examples of failure to

follow procedures

(a clearance

procedure

not

implemented,

an

administrative

procedure

not

properly

implemented).

(86-33)

CI

~

Severity

Level

IV violation for two examples of failure to

follow procedures

(steam

generator

level

was

not properly

controlled,

the auxiliary feedwater nitrogen

system

was not

properly aligned).

(86-39)

Severity

Level

IV violation for three

examples of failure

to

follow

procedures

(scaffolding

control,

auxiliary

feedwater

valves

not

aligned,

the

third

example

is

addressed

in the maintenance

section)

and

one

example of a

fai lure

to

establish

a

necessary

auxiliary

feedwater

procedure.

(86-45)

Severity

Level

IV violation for failure to follow secondary

source

handling procedures.

(Unit 3 only, 87-14)

.

Severity

Level IV violation for failure to follow clearance

tag procedures.

(87-22)

SUL I 7

1997

j.

Severity

Level

V violation for failure to follow procedures,

for containment

spray

system

valve lineup

and

independent

ver"ica.ior,.

(Unit 3 only, 86-31)

Severity

Level

V violation for failure

to

comply with

Technical Specification 3.3.3,

in that

on

two occasions

failed containment

isolation valves

were

not isolated

as

required.

(Unit 4 only, 86-45)

1.

Severity

Level

V violation for fai lure to follow clearance

tag procedures.

(Unit 3 only, 87-06)

2.

Conclusion

Category:

2

Trend:

3.

Board Recommendations

Additional plant

management

effort needs

to

be applied to the

areas

of inadequate

staffing

and

excessive

overtime,

secondary

plant

physical

condit o." control

room congestion,

and

plant

communications.

No change

to inspection

program is recommended.

B.

Radiological Controls

1.

Analysi s

During this assessment

resident

and regional

radiological controls,

ments

using the

Region

the plant chemistry.

period,

inspections

were conducted

by the

inspection

staffs.

Inspections

included

radwaste

controls,

confirmatory measure-

II Mobile Laboratory,

and inspections

of

The

licensee's

health

physics

(HP)

staffing

level

compared

favorably with other utilities

having

a facility of similar

size.

An

adequate

number

of

American

Nuclear

Standards

Institute

(ANSI)

qualified

licensee

HP

technicians

were

available

to

support

routine

operations.

During

outage

operations,

additional

contract

HP technicians

were

used

to

supplement

the permanent

HP staff.

One

strength

noted

in

the

health

.physics

program

was

the

stability of the health

physics staff.

The

low turnover

rate

has resulted

in a more experienced

group of individuals and has

provided

the

time necessary

to

implement

a continuing training

program for the staff.

On the other

hand,

the contributors

to

chemistry

program deficiencies

were staff turnover

and lack of

training.

A new Chemistry

Supervisor

was appointed

at the

end

of the evaluation period.

12

During the

SALP period the licensee

began

upgrading their health

physics

procedures

to

add

more formality to

the

conduct

of.

rou.ine operations.

The

improvement of procedures

along with

the experience

of the health physics staff should contribute.to

improved implementation of the health physics

program.

There

was

also

a

lack

of

formality

in

the

posting

of

instructions

to workers in that

hand written memoranda,

signs,

instructions

and documents

were routinely posted

throughout

the

site to provide guidance

to plant personnel.

It was noted that

in

some

cases,

the

posted

guidance

did not reflect

the

most

current practice.

Management

support

and

involvement

in

matters

related

to

radiation protection

was

adequate.

Health

physics

management

was

involved sufficiently early in outage preparation

to permit

adequate

planning.

The health

physics

supervisor

received

the

support of other plant managers

in implementing

the radiation

protection

program.

Resolution of technical

issues

by the health physics staff was

a

weakness

early

in the

period.

Since

the

reassignment

of

a

technical

staff

member

from corporate

headquarte.

s,

technical

evaluations

have

improved.

However, there are,

on

a continuing

basis,

many techn'ical

evaluations

necessary,

at times more

than

the current professional

staff can complete in a timely manner.

Those technical

evaluations

which

have

been

completed

are

good

as demonstrated

by the licensee's

response

to

NRC initiatives in

the conduct of an alpha radiation

survey program.

The licensee

developed this program in response

to

a violation.

The licensee

has continued to improve the alpha

program

as

more data

has

been

gathered.

The radiological effluent program

was conducted

in an acceptable

manner.

Effluent

releases

for

the

past

th~ee

years

are

summarized

in the

Supporting

Data

and

Summaries

Section

V.K.

The

licensee's

calculated

offsite

doses

for

1986

from

radioactive

effluents

were

1.24

E-02

mrem

gamma

to the whole

body and 9. 13 E-02 mrad beta.

These

values

place

the licensee

well within the limi.ts of 40

CFR 190. 10, e.g.,

25 mrem to the

whole

body

over

any

12 consecutive

months.

There

were

no

significant trends during the

SALP review period.

The

licensee

is currently

working with

a

liquid

radwaste

processing

contractor to improve the efficiency of the portable

demineralizer

system to further reduce

the quantity of effluent.

Some progress

has

been

made with informal leak reduction efforts

to reduce

the quantity of liquid waste to be processed.

'13

JUL I P

]g87

One

unplanned

release

resulted

from

contamination

of

the

demineralized

water

sys.em

by spen.

fuel

pool water.

The root

cause

Gf this

contamination

appeared

to

be

a

check

valve

failure, which allowed contaminated

water in

o the demineralized

water system

and which eventually

led to unmonitored releases

to

unrestricted

areas.

After-the-fact analyses

showed

the releases

had

been within limits.

The

licensee

expended

considerable

resources

to .upgrade

components

in

the

secondary

water

cycle affect,ing

chemistry

control.

As

a result, corrosion within the secondary

system

was

reduced.'s

of the

end of the,SALP

review period,

the plant

improvement

program

had not been

extended

to facilities used

by

the

chemistry staff, i.e.,

sampling

panels

and

laboratories,

although

improvements

within these

areas

are

scheduled

to

be

performed within a few years.

Audits performed

by the corporate

staff of the health

physics

program

have

improved during the

SALP period.

The .site internal

audit

organization

conducted

audits

of the

health

physics

program

using

personnel

that

were

experienced

in the

health

physics

area.

Appropriate

corrective

actions

were

taken

and

documen.ed.

During

.the

evaluation

period,

the

licensee's

radiation

work

permit

and

respiratory

protection

programs

were

found to

be

satisfactory.

Control

of

contamination

and

radioactive

materials within the facility was generally

adequate.

At the

beginning of the

assessment

period in 'Nay

1986,

the

licensee

maintained

41;> of the total

area

regarded

as

the

Radiation

Con rol Area

(RCA) under contaminaton controls.

The

RCA did not

include

the

containments.

in April

1987,

the

area

under

contamination controls

had

been

reduced to approximately 38:.'f

the total

RCA.

During

1986,

the

licensee's

cumulative

exposure

was

445

person-rem

per unit as

measured

by thermoluminescent

dosimeter

(TLD).

Tnis

value

is

above

the

national

average

of

397

person-rem

unit observed

at similar

PWR facilities.

However,

the

number

of person-rem

above

the

national

average

is

not

considered

to

be significant.

The licensee

has

established

a

500 person-rem

goal

per unit as

measured

by pocket ion chamber

(PIC) for 1987.

The total exposure

per unit through

June

1987,

as

measured

by

PIC,

was

660 .person-rem.

This total

included

exposure

received

during

extended

outages

necessitated

by

a

boric acid

problem

and

Raychem

splice repair work.

The boric

acid repairs

accounted for approximately

170 person-rem

and the

Raychem

splice

work accounted

for approximately

139 person-rem.

It should

be

noted

that

the

licensee

expended

considerable

resources

to support the installation of temporary shielding in

order to further reduce

the

exposure

of workers

performing the

splice repair work.

14

SUL 1P

Ig87

During

1986,

the

licensee

made

25

solid

radioactive

waste

shipments

totalling

11420

cubic

feet

(fthm)

(5710

fthm

per

reactor)

and

con.ai ning

89 curies

of ac.ivity.

This

is

signi,icantly below

he

1986

na ional average

for

PWR facilities

of 9,400

fthm per reactor.

Through April 31,

1987,

the licensee

made

7 solid radioactive

waste

shipments totalling 1194 fi~ (597

ft

per

reactor)

and

containing

approximately

78 curies

of

activity.

Four violations were identified:

a.

Severity

Level

IV violation for failure

to calibrate

air-line pressure

gauges

on the breathing air distribution

system

as

required

by

10 CFR 20,

Appendix

A,

Footnote

h

(86-36).

b.

Severity

Level

IV violation f'r failure to conduct

an alpha

radiation

survey

program

and evaluate

the

extent

of the

alpha

hazard

present

as

required

by

10 CFR 20.201(b)

(86-36).

c.

Severity Level

IV violation for failure to ensure that each

procedure

and administrative

policy

was

reviewed

by the

Plant Nuclear Safety

Committee

(PNSC) prior to implementa-

tion as required

by Technical Specification 6.8.2 (86-36).

d.

Severity

Level

V violation for failure to post notices of

violation and licensee

responses

to Notices of Violation as

required

by 10 CFR 19. 11 (87-15).

2.

Conclusion

Category:

2

3.

Board Recommendations

No change

in the

NRC's inspection

resources

are

recommended.

C.

Maintenance

l.

Analysis

The major maintenance

deficiencies

noted during the last

SALP

evaluation

included

inadequate

training,

failure

to follow

procedures,

high work order backlog,

and

a tendency to postpone

necessary

maintenance

forcing operations

to "operate

around"

problems.

JUL l 7

1987

Durino the evaluation period,

inspec

ions were performed

by the

residen

and regional

s.affs.

Supervisory

involvement

in the

opera

ion cf the maintenance

program

has significantly improved

and is apparen

during daily work activities.

Foremen

and line

supervisors

have

increased

direct

monitoring of maintenance

-asks

resul:ing

in generally

effective

work order

implemen-

tation.

Maintenance

work packages

have consistently

documented

the root cause

of problems,

alleviating

a significant concern

documented

in

the

previous

assessment

period.

Numerous

NRC

inspections

performed

during

this

assessment-

period

have

verified that work packages

are

complete

and work instructions

are adequate.

Maintenance

procedures

are utilized at the work

location

and are appropriate for the work activity.

In February

1987,

selected

review of the licensee's

Plant Work

Order

(PWO) backlog resulted

in the following concerns:

The required review of the computerized

PWO tracking system

does

not appear

to be thorough,

and was not being performed

on

a timely basis.

The

requested

as~istance,

(i.e.

Request

for Technical

Assistance

(RTAs),

Requ st

for

Engineering

Assist

nce

(REAs), Requisition

and Purchasing

Authorization (RPAs)

and

parts

request)

did not receive

the

same priority as

the

requesting

PWO.

A

new

engineering

work

request

system

was

implemented

in

September

1986 to prevent the loss of REAs.

This should aid in

assuring

more timely responses.

However, the

REAs that were

in

the engineering

review process

prior to the

implementation

of

the

new system did not appear

subject to the

improved con rois.

The licensee

has

a

PWO backlog target criterion of having

no

more

than

50 percent

of the corrective

maintenance

PWOs older

than

three

months

which is

based

on

an

INPO guideline.

In

February

1987,

the

Mechanical

and Electrical

Departments

were

very close

to

the

target

indicator

but

the

IEC

Department

appeared

to be about

10 percent

above

the target.

In

the

past,

the

I8C

PWO

backlog

was fairly large,

with

approximately

900

PWOs.

In response

to an

NRC expressed

concern

with this

backlog,

the

licensee

hired eighteen

temporary

I@C

technicians

to aid the permanent

IKC staff in reducing

the

PWO

backlog.

With their

help the

licensee

reduced

the backlog to

approximately

400

PWOs,

at

which

time

the

temporary

ISC

technicians

were

terminated.

A review of the

backlog

trend

curves for all three

maintenance

departments

indicated that the

16

JUL 2r lgs7

P'l'0 backlog

had been increasing.

In addition to the loss of the

temporary

technicians,

other

apparent

reasons

for

this

increasing

trend are:

The

number

of

PMOs

has

increased

because

the

plant

operating s-aff has experienced

improved response

from the

Maintenance

Department

on correcting identified problems.

As

a result more

PMOs were being generated.

The Maintenance

Department

was

using

improved maintenance

procedures,

which require

more time to perform.

The licensee

has committed to stay within the

INPO guidelines

in

the

number

of outstanding

maintenance

work orders,

and it

appears

that these guidelines

are being met at the present

time.

The total

PYO prioritization

system

as currently

impleme'nted

does

noi

appear

to

adequately

define

appropriate

work

prioritization.

There

appeared

to

be

a conflict between

the

original priorities as assigned

by the author,

the priority as

revised

by the work planners,

and the priority as revised

by the

Operations/Maintenance

Coordinator

and the "hot items list."

The direct, supervision of maintenance

personnel

was noted to be

increased

during this

SALP period

when

compared with the past.

Supervisors

are

now available

to aid in the completion of the

work activity,

and

to

interface

with the

Operations

staff

regarding

work in progress.

Since

there

are

more maintenance

personnel

than

in the past, all overtime is usually

done

on

a

voluntary

basis.

Excessive

overtime

appeared

to

have

contributed

to maintenance

errors

and plant events

in the past.

In general

the philosophy of the Maintenance

Department

appears

to

have

changed greatly over the past

two years.

There is more

attention

paid to the

assembly

of adequate

work packages,

the

specific

needs oi mechanics

arid technicians,

and to maintenance

training.

Management

support

of maintenance.

was readily apparent

in the

areas

of training

and facilities.

Maintenance

training

was

reinstated

in

early

1986

after

accomplishing

the

INPO

accreditation

effort with

a

new

performance

based

Continuing

Maintenance

.Training

Program.

'Providing

on-going

performance-based

training

to

maintenance

personnel

is

a

definite

improvement,

and

should

result

in

a

noticeable

performance

improvement.

The

new maintenance

building, which is

under construction,

should further improve the training

program

by providing mechanical,

I&C, and electrical

laboratories

for

hands-on training.

17

JUL

2 c

>gy

The

licensee's

recently

implemented

Preventive

and Predictive

Mainterance

Program

has aided in .he generation

of approximately

40 percen.

more maintenance

procedures

than there

were

18 months

ago.

This is primarily due to the licensee's

effort to provide

an apploved procedure for every task

and their implementation of

the upgraded

program.

These

upgraded

procedures

appear

adequate

in scope

and in cross-reference

material.

Implementation of the

improved procedures

represents

a significant improvement in the

potential

effectiveness

of

the

licensee's

Preventative

Maintenance

(PN)

Program.

The

licensee

is

additionally,

implementing

an Analytical

Based

Preventive

Maintenance

(ABPN)

Program

to

augment

their

PM program.

ABPN includes "oil

and

vibration analysis for pumps

and motors.

The licensee

intends to expand the

scope of the

ABPN program in-

Aear

future

to

include

pipe

wall thickness

monitoring,

infrared

scanning

of

breakers

and

electrical

connections,

'attery

voltage

monitoring,

and

generator/exciter

load

and

voltage testing.,

The program represents

a definite improvement,

and

should

help the

licensee

in identifying equipment

problems

prior to fai lure as well as

reduce

unscheduled

nutages.

Due to

increases

in the

scope

of the

ABPM program, its projected date-

- for full implementat

on is August 1987,

as

specified

in the

Integrated

Schedule.

The

post

maintenance

testing

program

for all,

maintenance

s'ections

on

balance

of plant

equipment

was

implemented

in

Hovember

1986.

The

electrical

and

instrument

and

control

sections

implemented

the

program,

however,

the

mechanical

maintenance

section

did not.

This deficiency

was identified

during

an

HRC inspection

in

February

1987

and

was

promptly

corrected.

Management's

approach to the resolution of technical

issues

has

improved.

Supervisory

involvement in the identification of the

root

causes

of problems

is evident through the

assignment

of

experienced

personnel

as

Event

Response

Team

(ERT) Leaders.

The

ERT is respon5ible for identifying and resolving the root cause

of a system or component deficiency in

a manner that precludes

recurrence.

On at least

ten previous

events

in 1986,

some of

which were reactor trips,'he

ERT succeeded

in ensuring that

an

acceptable

solution was

implemented without recurrence.

The licensee's

favorable results

achieved

through

use of

ERTs

for events

resulting

in plant outages

have

led to

use of the

team

approach

to resolve

equipment deficiencies

which do not

require

plant

shutdowns.

The

procedural

requirements

and

administrative policies to

be followed during

an

ERT were not

clearly

established

except

when

dealing

with

an

outage

initiating

event.

The

licensee

has

recognized

that

this

18

limitation has,

on occasion,

impacted

the effectiveness

of the

team's

response.

An

ERT administrative

procedure

is currently

under development.

Maintenance

related deficiencies

have resulted

in ten critical

and

one subcritical reactor trips.

The maintenance

deficiencies

associated

with

these

trips

were

not

generally

repetitive.

However,

five Unit

3 reactor trips

were

related

to turbine

generator

problems.

Two of these trips were manually initiated

by Control

Room Operators

when the turbine governor oil control

system

malfunctioned

causing

a

loss

of load.

An additional

reactor trip occurred during post maintenance

testing following

'eplacement

of

a turbine

governor oil impeller

sleeve.

The

replacement

was

necessitated

because

of unstable

governor oil

pressures.

A fourth

reactor trip

occurred

during

turbine

surveillance

testing

when

a technician inadvertently let go of a

trip test

handle.

The likelihood of

a personnel

error of this

sort was increased

because

a failed test valve coupling required

the operator to hold the trip test

handle

in the test position

for an extended

period of time.

The

ERT which addressed

the turbine governor oil problem was not

successful

in precluding recurrence.

A reactor trip occurred in

December

1986.

Significant load swings occurred in January

and

February

and

a reactor t'rip occurred

in March 1987.

The problem

with turbine governor performance

resulted

from poor cleanliness

of the oil- system.

The magnitude of the deficiency was realized

in

March

1987

and

resulted

in Unit 3 entering

a

scheduled

refueling

outage

approximately

one

week early

due to concerns

for turbine reliability.

Turbine control oil, lube oil and seal

oil piping was cleaned

during the outage to correct the problem.

Similar maintenance will be performed

on Unit 4 in a Spring

1988

refueling outage.

Repe itive

maintenance

problems

have

affected

other

safety-

related

systems.

Although

general

system

performance

has

improved,

the Auxiliary Feedwater

(AFW) system

malfunctioned

on

numerous

occasions

resulting

in

seven

Licensee

Event

Reports

(LERs)

and

causing

repetitive

reductions

in

load

or plant

cooldowns.

Numerous

initiatives

have

been

implemented

to

improve

AFW system

performance,

including

improved

nitrogen

supplies,

check

valve

replacements,

restoration

of automatic

system

control,

and

flow transmitter

upgrades.

However,

the

reliability of

system

valves

and

flow transmitters,

as

documented

in six LERs,

needs

to improve.

Intake

Cooling

Water

( ICW)

pumps,

check

valves

and

heat,

exchangers

continue

to require extensive

maintenance

resources.

All six

ICW

check

valves

were

replaced

in

January

1987

subsequent

to the identification of. internal

degradation.

An

19

JUL

1 7

198)

improved

valve

design

was installed

to preclude

recurrence.

Hea. exchanger

fouling due to calcium carbonate

buildup required

repetitive

cleanings

and entrance

into limiting conditions for

opera.ion.

An Amertap

system

has recently

been installed

on the

Unit

3 heat

exchangers

to allow cleaning without removing the

heat

exchanger

from

service.

Cleaning

the

Unit

4

heat

exchangers

wi 11

remain

manpower intensive until

a similar system

is installed

on Uni

4 in the Spring

1988 refueling outage.

The

performance

of

the

charging

pumps

continues

to

be

a

maintenance

problem.

On

two occasions

multiple out-of-service

pumps

required

the

plant

to initiate

a

load

reduction

in

preparation for a reactor

shutdown

because

a limiting condition

for

operation

was

exceeded.

The

efforts

of .a

guality

Improvement

Team have

reduced

but not eliminated

t,he problems.

Excessive vibration and reduced

pump flow capacity

have required

the

pumps to be taken out of service.

A plant modification is

planned

to

reduce

vibration.

The

pumps

have

repeatedly

been

susceptible

to air

binding

which

reduces

flow output

to

unacceptable

levels

and requires

venting to restore operability.

The

pumps

are designed

to maintain

60 aallons

per

minute

(gpm)

flow but frequently provide only 45 gpm.

The operability of the Source

Range Nuclear Instruments

remains

a problem

area

as identified in the last

two assessments.

A

program developed

by the

IKC Department

in late

1985 to enhance

'perability

through physical

and procedural

improvements

has not

resulted

in significantly increased reliability.

Consequently,

the

instruments

are

frequently

out of service

during

power

operation

and

a single train may not be available for use during

unplanned

shutdowns.

As

mentioned

in the

previous

assessment,

the

area

radiation

monitoring

system,and

the process

radiation monitoring

system

continue

to have

numerous

inoperable

channels.

Improvement

in

operability

has

not

been

noted.

Long

term

plans

exist

to

replace

both

systems.

Failures of process

radiation monitors,

particularly

gaseous

and particulate

containment monitors,

have

resulted

in at least

twelve

LERs documenting

the actuation

of

the control

room ventilation isolation

system.

Some of these

actuations

were caused

during maintenance

repairs

on previously

failed

channels.

Inadvertent

system

actuation

during

maintenance

is difficult to avoid due to the design of the power

supplies.

After

numerous

system

actuations,

I&C personnel

developed

a procedure

which greatly reduced

actuations

caused

by

improper maintenance.

Personnel

errors

and procedural

noncompliances

remain

a problem

as indicated in multiple LERs and the repetitive

nature

of the

violations

listed

below.

The

identified

discrepancies

are

20

JUL 1F

198'ymptomatic

of individual rather

than

programmatic

problems.

The

need for individual

a tentiveness

continues

to be stressed

Ly management

and individual technicians

and

foremen

are

held

strictly accountable

for their actions.

A desire to meet plant

expectations

of verbatim compliance

is evident

in the majority

of maintenance

asks.

However,

procedural

noncompliances

have

occurred,

as

indicated

by violations (a)

and (c)

and

proposed

violation (e)

below, during maintenance

evolutions

which were

directly supervised

by experienced

foremen.

This indicates that

verbatim

compliance

is

not yet

ingrained

at all

supervisory

levels

and

represents

a

concern

because

of the

example

that

foremen set for technicians.

Maintenance

liaison with the Operations

Department

has

improved

through the efforts of an Operations/l1aintenance

Coordinator

and

because

frequent

planning

meetings

are

held.

However,

ineffective

communication

has

occasionally

resulted

in

noncompliances.

Violation (a)

documents

an

instance

where

maintenance

personnel

performed calibration procedures

on

steam

break

protection circuitry while the circuit was

not

removed

from service.

Control

Room Operators

were not

aware of which

circuit was

being calibrated.

A reactor trip ensued.

Proposed

violation (e)

documents

multiple

Technical

Specification

violations

which

occurred

because

maintenance

personnel

performed

a core alteration without the

knowledge or consent

of

the

Operations

staff.

This

miscommunication

precluded

the

establishment

of containment integrity when required.

Four violations were identified:

a.

Severity

Level

IV violation for

a maintenance

supervisor

fail'ng to follow procedural

requirements

during

a

steam

generator

protection

channel

periodic test.

(86-30)

b.

Severity

Level

IV violation for

ai lure to establish

an

adequate

maintenance

procedural

precaution

for protection

circuitry calibration resulting in a reactor trip.

(Unit 3

only, 86-33)

Severity

Level IV violation for two examples of failure to

perform required post maintenance

valve testing

(exceeding

Technical Specification 3.3.3

requirements

for containment

isolation valves,

not implementing

an administrative

and

operating

procedure).

(Unit 4 only, 86-41)

d..'everity

Level

V violation for removal

of

a pipe

support

without the authorization of a

PWO.

(86-44)

21

The following viola ion is

under

consideration

for escalated

enfo, cemel t a tlon:

e.

Proposed

violation

for

failure

to

meet

containment

integrity requirements

during

core alterations.

(Unit 4

only, 87-14)

2.

Conclusiion

Category:

2

Trend:

3.

Board Recommendation

The in'itial implementation

of the various

maintenance

upgrade

programs

and the resultant

improvements

in training,

procedural

compliance,

work

planning,

root

cause

identification,

Maintenance-Operations

interface,

and

individual

emphasis

on

quality,

appears

to have

improved the Naintenance

contribution

to plant operations.

Additional

management

effort needs

to

be

applied

to

reduce

the

excessive

PWO backlog,

and

to

ensure

that

proper

priorities

are

assigned

to

maintenance

work

I

activities.

It is apparent

that,

based

on past

performance,

more qualified

maintenance

personnel

are required,

especially

in the

IKC area.

This

would also

require

more field supervisors

to maintain

a

suitable ratio between

craftsmen

and supervisors.

No change

in

the

HRC's inspection

resources

is recommended.

D.

Surveillance

1.

Analysi s

During this assessment

period,

reviews of the operational

and

outage

surveillance

testing

programs

were

performed

by

the

resident

and regional

inspection

staffs.

Activities inspected

included

the

surveillance

testing

and

calibration

control

program

and snubber surveillance

program.

The surveillance

program

was deficient at the beginning of the

assessment

period,

in that

some

Technical

Specification

(TS)

required

survei llances

were not identified by the

program

and

therefore

not

performed.

Licensee

Event

Reports

(LERs)

250/86-20,

250/86-27

(5 examples),

and 250/86-29

were generated

through July 8,

1986,

as

a result of the

missed

surveillance

testing.

LERs

250/86-20

and

250/86-29 identified missed fire

protection

pump and

system

component surveillance testing.

JUL 1F

8w'2

L":R 250/86-27 iden.ified-five examples

of missed calibration

and

channel

functionality surveillance

tests.

The

systems

not

tested

within the

TS required

surveillance

period were:

Data

Acquisition

Module

-1 calibration;

Radioactive

waste

liquid

effluent

line

flow rate

monitor

calibration

and

channel

functional test;

Steam

Generator

(SG)

blowdown effluen.

flow

rate monitor channel

functional test

and;

condenser

air ejector

vent.effluent

sys.em

flow rate

measuring

device calibration.

Violation

(a)

below

was

issued

due

to

the

surveillance

programmatic

weaknesses.

The conduct of the surveillance

program

has

improved

substan-

. tially during

the latter portion of the

assessment

period.

Plant

Management

acknowledged

the programmatic

weaknesses

which

resulted

in multiple missed

TS

survei llances

and

subsequent

issuance

of violation (a)

and undertook

an aggressive effort to

eliminate

the deficiencies.

A single

comprehensive

operating

surveillance

procedure

(0-OSP-200. 1)

was

implemented

which

incorporated

all

surveillance,

schedule,

and

departmental

responsibilities.

The

procedure

delineates

.each

surveillance

test, current

TS and

new standard

TS (see

Licensing Activities)

requirement,

applicable

modes

of operation,

responsible

plant

discipline

and .its

schedule

for completion.

Since

issuance

of violation (a)

and

the

implementation

of

0-OSP-200.

1

the

surveillance

program

has

been

highly effective

and

well

controlled.

One

TS surveillance

was not performed

(LER 25/87-13)

as

a result

of personnel

error in the interpretation

of the

applicable

mode for test performance.

Although the surveillance

period was exceeded,

the

new program identified the discrepancy.

guality records

were well maintained,

accessible

and complete.

guality con.rol

reviews of test

procedures

and witnessing

of

test activities was strongly evident.

Surveillance

procedures

were technically

accurate

and provided

sufficient

instruction

to

assure

proper

performance.

The

Procedure

Upgrade

Program

(PUP)

has increased

the quality of the

format

and

content

o'f

surveillance

procedures,

minimizing

personnel

errors

and promoting quality work.

Procedures

for control of the

snubber

surveillance

program are

well defined

and explicit.

Decision 'making

was

usually at

a

level

that

ensured

adequate

management

review.

Records

were

complete,

well maintained,

legible

and retrievable.

Staffing

and training and qualifications of personnel

was adequate.

Two Unit 3 reactor trips

occurred

as

a result

of personnel

errors

in the

performance

of surveillance

procedures

and

one

Unit 3 reactor trip occurred

as

the result

of

an

inadequate

23

JUL 1V lg87

surveillance

procedure.

The licensee

took prompt action after

each

rip to determine

he roo

cause of each

even

and

o .ake

corrective actions to prevent recurrence.

One violation was identified:

a.

Severity

Level

IV violation

for

inadequate

corrective

action

on

missed

surveillances

(86-39;

second

part

of

violation is discussed

in the gA section of text.).

The following violation is

under

consideration

for escalated

enforcement

action:

b.

Proposed,

violation for inadequate

leak rate

procedures.

(Unit 4 only, 87-16)

Conclusion

Category:

2

Trend:

3.

Board Recommendations

The

PUP

group

must

continue

to review

and

upgrade

existing

procedures

and write new procedures,

when appropriate,

to ensure

that

surveillance

test

periodicities,

applicable

modes

of

operation,

and all required

components

and

systems

are tested

consistent

with the requirements

of the

upgraded

TS prior to

their approval

and implementation.

Fire Pro-ec

ion

1.

Analysi s

Fire

protection

was

not

inspected

by

NRC

Region II office

personnel

during

this

period.

During

routine

tours,

the

resident

inspector identified two violations in this area which

are indicated below.

Two violations were identified:

a.

Severity

Level

IV violation

for

not

having

adequate

procedures

for controlling deluge

system

valve

line-ups

including pressure

switch isolation valves (86-33).

b.

Severity

Level

V violation for six occasions

of propped

open fire doors.

(86-39; first part of violation is

on

inadequate

Plant

Change/Modification

functional

testing

and is discussed

in the outage

section of t'ext).

2.

Conclusion:

The

lack

of inspection

activity in this

area

orecludes

a

meaningful

assessment

of

licensee

performance.

Category:

N/R

3.

Board Recommendations

None

Emergency

Preparedness

l. 'nalysis

During the assessment

period, inspections

were performed

by the

regional

and

resident

inspection

staffs.

These

included

observation

of

an

annual

emergency

preparedness

exercise

and

a

routine inspection.

One revision to the Radiological

Emergency

Plan

was reviewed.

During the exercise,

the licensee

continued

to. demonstrate

the

capability to promptly identify and correctly classify emergency

events

consistent

with the Radiological

Emergency

Preparedness

Plan

and

implementing

procedures.

Corporate

management

demonstrated

a strong

commitment to maintenance

of an effective

emergency

response

program.

Consistent

with this

commitment,

corporate

management

was

directly

involved

in

the

annual

exercise

and critique.

Personnel

assigned

to

the

Emergency

Response

Organization

were cognizant of their responsibilities,

and

were

adequately

trained

in required

areas

of

emergency

response.

The

Emergency

Response

Organization's

management

and resolution

of the

postulated

accident

during

the

exercise

demonstrated

significantly improved

emergency

preparedness

training.

Prompt

activation

and

management

of the

emergency

response

facilities

was particularly notable.

The transfer of emergency

management

from

the

Technical

Support

Center

(TSC)

to

the

Emergency

Operation

Facility

(EOF)

was

prompt,

decisive,

and

comprehensive.

The

licensee

effectively

used

emergency

action

level

(EAL)

matrices

in promptly identifying and declaring

each

emergency

classification.

Inplant and offsite protective action decisions

were

effectively

implemented

throughout

the

exercise.

Protective action

recommendations

were promptly communicated

to

the State.

State

and local

government representatives

assigned

to

the

,EOF

were

consistently

factored

into

the

offsite

protective

action

decision-making

process.

Consistent

and

effective

communications

with offsite agencies

were maintained

25

JUL 1V

1987

throughout

the

exercise..

Significant

improvement

in

he

licensee's

communications

wi

h its field radiological monitoring

teams

was

observed.

The subject

teams

were frequently updated

regarding

plant status

and

changing

meteorological

parameters.

Effective

interaction

between

licensee

and

State

field

monitoring teams

and reported data

was maintained

throughout the

exercise.

The

one area

which detracted

from the exemplary performance

was

the licensee'

failure, during the

annual

exercise,

to notify

the

State

of the

Site

Area

Emergency within the

assigned

15

minu

e constraint.

The

15 minute notification is required

by

Regula"on

and

'he

licensee's

notification

procedures.

The

licensee

did

make

the proper notification within

25 minutes.

This finding

was

also

identified

by the

licensee

during the

con rolle. /evaluator

cr',tique.

The

licensee

continued

to

be

responsive

to

HRC initiatives regarding correction of weaknesses

and program

improvements identified during routine inspections,

drills,

and

exercises.

The

licensee

continues

to

conduct

detailed critiques

following each

exercise,

and

implements

the

corrective actions reouired.

One violation .was '.dentified by the Senior Resident

Inspector:

Severity

Level

IV violation defining four examples of the

public address

system

as failure to meet

the requirements

of

10 CFR 50.54(q)

and 50.47(b) (86-33).

(See

IE Bulletin 79-18).

2.

Conclusion

Ca egory:

1

3.

Board Recommendations

Ho change

in the

NRC's inspection

resources

are

recommended.

G.

Security

and Safeguards

1.

'Analysi s

Inspections

were performed

by the resident

and regional staff.

The previous

SALP's analysis

addressed

the licensee's

program to

repair

and maintain'he

aging

security

system's

components.

This program utilized several

full-time employees

to maintain

the

system

and relied

on compensatory

measures.

Currently, the

licensee

has

reduced

the dedicated

maintenance

personnel

to one,

although other plant resources

can

be called upon.

The licensee

continues

to rely heavily

on

compensatory

measures,

some

of

26

JUL

> p

~>87

which have

been

in place

in excess

of two years,

with no

end

date

planned.

The

security

system

computer

continues

to

be

unreliable

with

frequent

down-time,

requiring

addi .ional

ex ensive

compensa.ory

measures.

The

licensee

is currently

having difficulty procuring

spare parts for the system,

which is

approaching

obsolescence.

The licensee

has

long term plans (in

the Integrated

Schedule)

to replace

the security computer

system

but no vendor selection

has

been

made to date.

The

number

and repetitive

nature

of the violations identified

during this period indicated

.a weakness

in the security

program.

These .violations

were

caused

by

a

combination

of inadequate

procedures,

inadequate

compensatory

measures,

and

lack of

management

oversight.

The licensee

does

not

show initiative in

self-identification of problems.

However,

the

licensee

does

show responsiveness

to

NRC initia ives.

1

The security shift supervisors

exhibit

a knowledge of procedures

but

lack training

in regulatory

requirements

and

are

not

familiar with the

basic

documents

detailing

the

licensee's

commizmenis

to the

NRC.

During an inspection,

late in the

SALP

period, it was noted that none of the security force supervisors

had

seen

or

had

access

to the Physical

Security

Plan.

During

this rating period the licensee relied

upon the line supervisors

to implement

compensatory

measures

and

communicate

problems

to

plant

management.

This

lack

of

management

oversight

is

evidenced

by the

nume'rous

violations demonstrating

a lack of

attention

to

details.

Violations

identified

involve:

unescorted

visitors;

unbadged

personnel

inside

the

protected

area;

isolation

zone

degradations;

inadequate

compensatory

measures

and procedures;

and inadequate

door hardware.

The repetitive

nature

of the

more

serious

violations dealing

with failure to adequately

control

access

to the protected

and

vital

., areas

indicate

that

the

licensee

implements

.violation-specific corrective

actions

and fails to address

the

root

cause.

This is particularly significant in that

three

Enforcemeni

Conferences

were

held

in

the

Region II offices

during this rating period at which time the licensee

stated that

the security program would be improved.

The

licensee

has

shown

a willingness

to

improve vital

area

barriers

and

has requested

a meeting to address

the topic.

The

response

to this request

has

been deferred,

pending

completion

of NRC Headquarters

review of vital area policy and criteria.

The licensee

has

made personnel

changes

in the positions of Site

Security

Manager

and

Chief

of

Uniformed

Security.

The

incumbents

are working to improve the security program;

however,

this change

came too late in the

SALP rating period to

have

an

impact

on the current analysis.

27

JUL 1V

>887

Eleven

viola ions

were identified during this rating

period.

Two

viol a i ons

represen

ed

by

(a)

below

were

categorized

o"e her

as

Sc veri ty

Level III

problems

and

a

Seventy-Five

T lousand

Dol 1ar Civil Penalty

was i ssued.

Two violations (j and

k) are currently under review for escalated

enforcement action.

I

Eleven violations were identified during this evaluation period:

a.

Severity

Level III violation

for

security

problems

involving security officers sleeping

on post

and inadequate

visitor control/escorting

(87-11) .

b.

Severity

Level

IV violation

for failure

to

provide

protected

area barri er (86-32) .

c.

Seve. ity Level

IV violation for having

inadequate

pathway

from the protected

area

into vital areas

(86-38).

d.

Severity

Level

IV violation for having

inadequate

access

control to vital areas

(86-38).

e.

Severity

Level

IV violation for having inadequate

lighting

at :he protected

area

perimeter (86-38).

f.

Severity

Level

IV violation

for

having

inadequate

compensatory

measures

(86-40).

g.

Severity

Level

IV violation

for failure

to

maintain

protected

area isolation

zone (86-47).

h.

Severity

Level

IV violation for failure to wear security

badge/keycard

(86-47).

i.

Severity Level

V violation for having inadequate

procedures

(86-38).

The

following

two violations

are

under

consideration

for

escalated

enforcement action:

j.

Inadequate

vehicle search

(87-25).

k.

Failure

to

control

personnel

and

equipment -access

to

containment

(87-25).

2.

Conclusion

'ategory:3

Trend:

28

JUl.

g 7

1987

3.

Board Recommendation

The

board

recommends

increased

management

attention

and

commitment in order to effect

necessary

improvements

in this

area.

H.

Outages

1.

Ana lysi s

During

this

evaluation

period,

inspections

of

refueling

activities,

outage

management,

major

plant

modifications,

inservice

inspec-.ion

and test

( ISI/IST) and post-outage

startup

testing

were performed

by the regional

and resident

inspection

staffs.

Unit 4

rema i ned

in col d

shutdown

through

the fi r st

week

in

August

1986,

to

complete

electrical

load

modifications

to

preclude

the

potential

for overloading

the

emergency

diesel

generators

(EDG).

To support

the final implementation

of these

modifications

required

both

units

to

be

in

cold

shutdown

simultaneously.

Unit 3

came off line

on July 15,

1986,

to complete elec'trical

modifica~ions required

to resolve

the

EDG overload evaluation.

The

outage

was

scheduled

for eighteen

days

with electrical

system modifications

and

RHR motor

end bell inspections.

The

electrical

system

modifications

were

completed

and

tested

satisfactorily

and the outage

lasted

nineteen

days.

On July 26,

and July 28,

1986,

the licensee

performed engineered

sa eguards

testing

on Units .3

and

4,

respectively.

Licensee

letter

JPES-PTP-86-1099,

dated July 29,

1986,

documented

that

the test

results

were

acceptable

with regard

to

EDG loading

concerns.

The testing

was per'formed in

a manner

which required

the measurement

of EDG loading values

during

a simulated

large

break

LOCA coincident with a loss of offsite power.

These tests

did

not

involve

Units 3

and

4

simultaneously.

Additional

loading

values

were

obtained

assuming

only

a loss of offsite

power.

Correction factors were applied to the data

as necessary

to account for the .increased

power consumption

some

equipment

would require

. under

actual

accident

conditions.

The

maximum

load that could automatically

load

on

a single operable

EDG was

calculated.

As documented

in letter JPES-PTP-86-1099,

the worst

case

load 'values

were found to remain within those predicted

by

licensee

in Safety Evaluation JPE-L-86-074,

Revision

1, "Safety

Evaluation Turkey Point Units

3 and

4 (PTPN)

Emergency

Diesel

Generator

Load", dated July 1986.

The inspectors

conducted

an

29

JUL I'7 lg87

independen.

review of ihe

surveillance

results

and .concluded

that

.he wors.

case

au+o-connected

loading

during single

EDG

operation did not exceed

the 2750 ki iowa+t limit specified in TS 4.8.1.c.8.

in returning

Unit 3 to service

no significant primary system

problems

were

encountered

although

the

secondary

system

experienced

several

problems.

On August 21,

1986,

the unit was

forced to come off the line as

a result of a main condenser

tube

leak apparently

due,

in part, to

a free bolt in the tube bundle.

Also discovered

at this time

was

a hole in the

3B condensate

pump suction piping.

An ongoing

problem exists with

a leaking

condenser

boot seal.

The interim solution

has

been to seal

the

leak with condensate

flow to prevent air

from entering

the

secondary

system.

Unit

4 restart

was

contingent

upon

completion

of electrical

system modifications.

Subsequent

to the

successful

testing of

these

modifications,

simultaneous

unit operation

was concurred

in

by

the

NRC.

Unit 4

encountered

.several

delays

while

a-tempting

unit restart

and/or

while achieving

rated

power.

During rod testing,

multiple control

rod failures resulted

in

the

repair

and/or

replacement

o

control

rod drive mechanism

instrumentation.

On August 2,

1986,

the

4C

AFW

steam

supply

check valve (4-383)

required

replacement

due to excessive

seat

leakage.

Unit operation

was further delayed

as

a result of high

vibration in the exciter.

The exciter

was replaced,

but the

vibration

was

later

determined

to

be

caused

by

a

bowed

turbine-generator

rotor.

Additionally,

the

4A

feedwater

regulating

bypass

valve

(4-FCV-479)

had to

be repaired

due to

difficulty in maintaining

steam

generator

level

at

a

low

feedwa er

flow

ra e.

Throughou'he

startup

period,

he

secondary

system

experienced

chemistry

problems

which required

low power level holds.

On

August 30,

an

RCS

leak

was

identified

coming

from the

conoseal

on the reactor vessel

head.

An engineering

evaluation

was

performed

and

approved

which justified operation with the

existing leak.

Unit 4

was

then

started

up

and

achieved

power

operation

in early

September.

A further

discussion

of the

conoseal

leak

is

contained

in

Section

IV.L.,

Engineering

Support.'iolations

of

NRC

reqUirements

were

identified

during

the

extended

Unit 4

refueling

outage.

On

Augu'st

5,

1986,

a

'ubcritical

reactor

trip

occurred

while

performing

post

modification

acceptance

testing

(86-39);

this

violation is

listed in Section

IV.E.

Of particular.

concern

in reviewing the

reactor trip was that

two departments

were performing separate

30

JUL 17

lgsy

tests

without apparent

knowledge of the unit test status.

On

August 9,

1986,

during Unit

4 hea.

up apparent

operator error

resulted

in the automat'.c

actuation

of the

AFIRE'ystem (85-39);

thi s violation is listed in Section IV.A., Plant Operations.,

On October 23,

1986, Unit 4 was

shutdown to locate

and repair

a

suspected

condenser

tube leak.

All steam generator

conductivity

meters

in

the

control

room

had

pegged

high off scale

and

chemical

analysis

verified excessive

conductivity

and chloride

levels

in the condenser

and the

steam generators,

indicative of

gross

tube

leakage.

Unit 4 was

shutdown while

an investigation

commenced

to determine

the root cause

of the condenser

inleakage.

Based

on the chloride concentration

and conductivity levels in

the

secondary

system

the

licensee

calculated

that

there

was

approximately

600

gallons

of circulating

water

inleakage.

Because

of

the

severity

of

the

chloride

contamination,

an

extensive

clean

up of the

conden,sate

and feedwater

systems

was

initiated.

This was

hampered

by a shortage

of water meeting

the

quality standards

for the secon'dary

system.

The water treatment

plant onsite

which provides

such

water

was

in service

only

intermittently and resin type ion exchangers

were trucked to the

site to provide adequate

water.

Several

leak detection

methods

>>ere

used

in an attempt to locate the leak, including the

use of

a

helium sniffer,

soaping

of the

water

box

tube

sheet,

and

hydrostatic

testing of the hotwell side of the condenser

tubes.

All were

unsuccessful

in determining

the

source

of inleakage.

On October

27,

1986, while Unit 4 was in Mode

3 (hot standby)

in

preparation

for reactor startup,

operating

personnel

discovered

that

the required

post-maintenance

testing for numerous

valves

inside

containment

had

not

been

performed.

The

valves,

primarily

from

the

IST

Program,

included

two

containment

isola.ion

valves,

which

were

subsequently

declared

out

of

service.

The licensee

commenced

an immediate unit cooldown per-

TS 3.3.3

and

made preparations

to test all affected valves.

In

addition

Motor Operated

Valve (MOV)-751, which is in the

RHR

pump

suction

line,

required

plant

depressurization

to

less

than

525 psig

for testing

(violation (c)

of Section IV.C.,

Maintenance).

On

March 6,

1987,

after manually tripping the reactor

due to

turbine control oil system

problems,

Unit 3 was brought to cold

shutdown

to

commence

preparations

for the

refueling

outage,

which was

scheduled

approximately

a week later.

One violation

was identified during the Unit 3 refueling outage.

It involved

the

failure

to control

the lifting/handling of regenerative

Secondary

Sources

in a manner to prevent

damage,

which is listed

as violation (h) in Section IV.A., Plant Operations.

31

On

March 11,

1987,

Unit 4 reactor

was

manually

shutdown

as

required

by Technical

Specifications

due

to

a

leak

in

the

containment

personnel

hatch

inner door.

Unit 4 was maintained

in

Mode 3,

Hot Standby,

until March 13, while

r epair s to the

personnel

hatch

door were in progress.

On March 13,

1987,

The

unit was taken to Mode 5, Cold Shutdown, io assess

a

known leak

from

a port instrumentation

column

assembly

(conoseal)

and the

ex ent

of

he

boric

acid

contamination

and

subsequent

surroundino

corrosion

areas.

Subsequently,

an

NRC

Augmented

Inspec

ion

Team (AIT) was. formed

and dispatched

to

the site.

Section IV.L., Engineering

Support,

contains

the details of the

'conoseal

leak and AIT findings..

A violation

identified

during

the

Unit 4

outage

involved

the

performance

of

core

alterations

prior

to establishing

containment

integrity.

This

was

attribu

ed

to

inadequate

procedures

and

poor

communications

between

Maintenance

and

Operations

(see

proposed violation (e) in Section

IV.C).

In

general,

there

is

management

evidence

of planning

and

assignment

of priorities for maintenance

and modifications of

known tasks.

Schedules

have slipped considerably

from original

estima+es

primarily

as

a result

of the

iden+ifica+ion

of

unforeseen

work activity.

Raychem splice

rework was identified

only after both unit outages

had

commenced.

As

a result of the

Unit 4 conoseal

leak, detailed

inspection

of the Unit 3 vessel

head

identified

CRDM seal

housing

leaks

that

also

required

repair.

Leaks

in the

Post Accident Hydrogen Monitoring System

sample line were identified by local leak rate testing

and have

further delayed restart of Unit 4.

Regional

Inspec ors reviewed

he ISI/IST program,

procedures

and

. observed

work activities.

The

staff

found

that

ISI/IST

activities

were

procedurally

well

delineated

for

ISI/IST

personnel.

Training, qualification and certification of ISI/IST

personnel

has contributed to good, adherence

to procedures

with

only

a modest

number of personnel

errors.

Responsiveness

to

NRC

initiative was usually timely; however,

the deviation indicated

below is

an exception

in this area.

Aside from violation (c),

of Section IV.C., Maintenance,

discussed

previously,

the ISI/IST

corrective

action

system

promptly

and consistently

recognized

and

addressed

non-reportable

concerns.

Records

were complete,

well maintained

and available.

In May 1987,

the licensee

developed

and conducted

a special test

of the "cross-talk" capability of the

EDG load sequencers.

This

test

was

deemed

necessary

following the discovery of

EDG wiring

discrepancies

as discussed

in Section IV.L., Engineering

Support.

Subsequent

to

discussions

with

the

Resident

Inspectors

and

regional

management,

the licensee

elected to conduct these tests

32

JUL

1 p

)gal

to ensure all aspects

of the load sequences

abilities to operate

properly for both units had

been adequately

tested.

These tests

involved simula.ing

a

Loss

of Ofisite

Power

(LOOP)

and

then

manually initiating

a

Safety

Injection

(SI)

on

each

unit.

Previous integrated

safeguards

tests did not involve both units

sim ltaneously

and therefore,

with only two EDG'

the ability of

the sequencers

to properly sequence

the safeguards

loads

on the

SI affec.ed

unit

and

shutdown

loads

on the non-affected

unit

(cross-talk)

had never

been completely tested.

These tests

were

conducted

in late

May 1987

and

resulted

in the initial test

being unsuccessful

due to personnel

errors that occurred

during

a

related

preventive

maintenance

test

conducted

the

previous

week.

The licensee's

troubleshooting efforts were effective

and

the

subsequent.

tests

for

each

unit

were

successful.

NRC

inspectors

had

the following reservations

with regard

to the

licensee's

performance

of these tests:

management

involvement

and support were not always evident

both in the development

and conduct of the test.

The licensee's

initial root cause

analysis

was superficial

but subsequent

efforts were comprehensive.

Personnel

errors

that

resulted

in the first test

being

unsuccessful

were

att,ributed

to

deficiencies

in

the

training

and qualification of the electrical

maintenance

personnel

involved.

One deviation

was identified.

,

2

Deviation for failure to submit inservice inspection relief

request

as committed (86-31).

Conclusion

Category:

2

3.

Board Recommendations

No change

in the

NRC's inspection

resources

are

recommended.

Quality Programs

and Administrative Controls Affecting Quality

1.

Analysi s

During the

assessment

period inspections

were

performed

by the

resident

and regional

inspection staff.

33

JUL 1V 1987

For the purposes

of this assessment,

this area is defined

as the

ability of

the

licensee

to identify and correct

heir

own

problems.

It

encompasses

all

plan+

activi+ies,

all

plant

personnel,

as well

as

those

corporate

functions

and

personnel

that provide services

to the plant.

The plant and corporate

QA

staf=

have

responsibi li y for verifying quality.

The rating in

this area

specifically denotes

results

for various

groups

in

achieving

quality

as

well

as

the

QA staff in verifying that

ouality.

A QA effectiveness

inspection

was conducted of licensee

trending

indicators

as

the

basis

for

a

broad

based

assessment

across

various performance

areas.

The premise of the

QA program is to

ensure

safe

and

reliable

plant

operation

and

the

ultimate

effectiveness

of the licensee's

QA program

can

be

measured

by

examining

various

operational

trending

indica ors.

The

inspection

included

reviewing

licensee

corrective

actions

developed

to address

the indicated

problem areas.

The inspection effort was divided into the following areas:

Operations

and Maintenance

Qual;+y Assurance

Quality Con rol and Licensing

Commitments

Design Control

In

the

area

of operations

and

maintenance,

some

short-term

improvements

were

evident

but

long

term

improvements

were

indeterminant.

An activity which

had

produced

verifiable

short-term

improvements

was

the 'establishment

of

the

Event

Response

Team

(ERT).

The

ERT

was apparently

instrumental

in

decreasing

he

number of repeated

or recurrent ouiages.

Large

scope corrective action

programs

were developed to reduce

personnel

errors,

to develop

and implement

an equipment labeling

program

and to develop

a procedures

upgrade

program.

The

1987

policy statement

for

FPRL states

that

40

percent

of reactor

trips at

Turkey Point

were

caused

by personnel

error.

The

equipment

labeling

program

has

shown its effectiveness

to

some

extent

in that

no

wrong

train/wrong -unit

personnel

errors

occurred

after

Nay

1986.

The

procedure

upgrade

program

is

intended

to

provide

"user

friendly" procedures

for safety-

related

systems.

These

improvement

programs

address

the major

identified causes

of personnel

error

reactor trips

and

should

improve

the

long-term performance

in this area..

The general

conclusion of QA effectiveness

in the operations

area

was that

the licensee

can identify and was correcting

problems.

34

JUL 17

>9S7

The maintenance

department

has initiated several

projects

in an

ef for . 'to'mprove

performance

and

increase

plant reliability.

However,

the

license-" trend indicators (corrective

main.enance

backlog,

unplanned

days off line,

and equipment out of service)

used for measuring

the effectiveness

of maintenance

activities

do

no

reflect

convincing

trend

changes

in this

area.

One

improvement

example

was

in

source

range

instrumentation

reliability.

A Quality Improvement

Team reviewing

.the chronic

failure problem identified two mechanisms

of detector failure.

The

licensee

has

initiated

some

other

improvements

in the

Preventative

Maintenance

(PM)

program,

and

the

Nuclear

Job

Planning

System

(NJPS);

they

also

created

positions

for

engineers

dedicated

to root cause

analysis.

These

corrective

actions

have the potential to improve maintenance

performance.

The quality

assurance

department

appeared

to

be

adequately

accomplishing

its

assigned

function

of

identifying

and

correcting

site

problems

based

on

interviews

with

site

personnel,

reviewing audit findings, reviewing audit schedules,

and reviewing corrective action 'requests.

During l986, the licensing group

has significantly increased its

involvement in the review of reportable

events;

consequently,

a

more effective liaison exists

between

licensing

and operations

personnel.

Quality improvement

teams

have

been established

which consist of

'ersonnel

from different departments

addressing

problem areas.

Approximately 25 teams

have

been established,

about

one half of

which

have

completed

a project

resul

ing in various quality

. improvements.

Problems

were

noted

in the

area

of design control.

FPC L, in

their letter

dated

October

I,

1986,

committed

to

develop

corrective

action

plans

to address

identified deficiencies

in

design

control,

10 CFR 50.59

evaluations,

and

timelines

of

corrective

action

in

i"esponse

to confirmatory action letter.

Considerable

resources

have

been

expended

in the

process

of

meeting

these

'requirements.

However,

a- review of

selected

elements

of

the

corrective

action

plans

identified

that

weaknesses

still

exist.

Relative

'to

corrective

action

timeliness

for

site

QA identified

problems,

administrative

control's for justifications for operations

evaluations

and

high

backlogs

of drawings

needed

to

be

updated.

Other

elements

of

.the

commitments

made

in the letter

appear

to

be

on

schedule

including

the

site

engineering

staffing

level

and

program

procedures,

the Standard

Engineering

Package

for Nuclear Plants,

and

various

aspects

of the

comprehensive

review effort for

selected

systems.

35

SUL ~'7

>s87

The

QA organi=ation

a- Turkey Point has

been

reorganized

into a

Performance

tionitoring

Section

and

a

Regulatory

Compliance

Section.

The

Performance

Monitoring

Sec

ion

provides

,or

a

significan

increase

in

QA/QC

involvement

in monitoring all

plant activities

through. observation

and

walkdowns

of various

systems

and equipmen

.

The

Regulatory

Compliance

Section

is

responsible

for

the

traditional

QA/QC audit function.- Improvements

in this

area

include

increasing

the

audit

frequency

to

quarterly

and

increasing

the time constraints

associated

with Non Conformance

Reports

(NCRs) to assist

in expediting

response

and corrective

action.

However,

this

group

is

not

involved

in

auditing

Requests

for

Engineering

Assistance

(REAs),

Event

Response

Team

(ERT) activites

and investigations,

and the monitoring of

activities

and

equipment

associated

with the secondary,

balance

of plant area.

The quality control

over

the

procurement

and

issuance

of

replacement

parts

has

been

improved

by

the

licensee.

The

licensee

es~ablished

an

onsite

group

called

the

Purcnase

Document

Review

Team

(PORT)

to

address

excessive

delays

in

procurement.

The licensee

has

also

improved the control over safety-related

spare

parts

in

storage

on site.

Personnel

responsible

for

cataloging

these

parts

have

been

moved

from corporate

to the

site.

In addition, the nuclear stores

have

been

segregated

from

the fossil

stores

to help

ensure

that non-qualified parts

and

equipment

are

not utilized in safety-related

or important to

quality applications.

An

inspection

of

the

corrective

action

program

was

also

conducted

as part of a special

performance

assessment

inspection

oi maintenance activities.

Two violations occurred

during the

SALP period

which

document

fai lures

of the

licensee

to take

timely

adequate

corrective

action.

In

violation

(c)

of

Section

IV.L.,

the

licensee

failed to

take

timely corrective

action for two support

hangers

on the Unit 4 charging line.

A

second

example

involved improperly bolted starting air receivers

on the

A and

B Emergency

Diesel

Generator.

Violation (e) of

Section IV.L. involved the failure of the licensee

to identify

and correct

a deficient condition involving an Intake Cooling

Mater check valve, which exhibited

symptoms of internal

key and

keyway damage.

Plant

personnel

indicated

that

the

responsiveness

of plant

management

has

been

improving

in

many

areas

including work

requests

and

NCRs.

There

were

also positive

indications

of

increased

management

involvement

in daily plant operations,

36

~UL ~r

>s87

including frequen

plan.

and control

room tours

and a.tendance

a

he

morning olant status

mee+inqs.

Manaaement

sensi .ivity

.raining

which is

designed

+o "sensitize"

employees

to

the

corporate

and plant goals,

has

been

implemented for all Turkey

Point personnel.

An important aspect

of this training was that senior

members of

managemen

, including the Plant Manager

and Site Yice President,

were available at each

session

to answer questions.

In general,

it appeared

that

management

attention

to plant operations

and

response

to identified problems

has

been

improving.

A review was performed

on all sections

of the

SALP report in an

attempt

to capture

apparent

strengths

and weaknesses

related to

management

controls affecting quality.

The following are

some

pe.ceived

strengths

in management

controls affecting quality:

Plant

management

stressed

the concept of Operations

as the

"customer" for various plant

support

groups,

reducing

the

previous

tendency

for

Operations

to

operate

around

maintenance

problems.

Plant

management's

emphasis

on

procedural

verbatim

compliance

helped to reduce

personnel

errors.

Management

involvement

with

operations

activities

has

increased.

As

a result,

complex

evolutions

are

more

smoothly performed.

Primary plant housekeeping

has continued to improve in the

wake of increased

management

attention in this area.

Management

has

shown

a

commitment

to excellence

in its

support of the

PEP

and other corporate quality improvement

programs.

Management

involvement

in health

physics

was sufficient

earlv in outage preparation

to permit adequate

planning.

Supervisory

involvement

in

the

maintenance

program

has

significantly improved resulting

in effective

work order

implementation.

Management

support of maintenance

was readily apparent

in

the areas

of training and facilities.

Supervisory

involvement in the identification of the root

ca'uses

of problems

has

improved through the assignment

of

experienced

personnel

as Event

Response

Team leaders.

37

JUL 1'7

1987

Plant

management

has

undertaken

an

aggressive

effort to

eliminate

m'.ssed

TS

survei llances,

resulting

in

conside,able

improvement to this program.

Corporate

management

demonstrated

a strong

commitment to

main-enance

of ar. effect,ive emergency

response

program.

There

has

been

increased

management

involvement in plant

operations,

including frequent plant and control

room tours

and attendance

at morning meetings.

Since

the

last

SALP

period,

management

attention

to

licensing initiatives

has

improved

as

demonstrated

by the

reduction of the backlog in licensing actions.

Opera

ional

Experience

Feedback

Training control

has

been

improved

due

to management

attention

to documentation

and

timely disposition

of information.

It was

unsuccessful,

however, with regard to

two events;

the

conoseal

leak

and

the nitrogen intrusion into the boric acid system.

The

following

are

some

perceived

weaknesses

in

management

controls a;fe ting quality:

Secondary

plant

housekeeping

has

been

mediocre

as

management

emphasis

has concentrated

on the primary side.

Plant

management

has

been

previously

unsuccessful

in

assuring

adequate

staffing in the Operations

Department

to

preclude

excessive

overtime.

Specific plans

and

programs

are presently

in place to correct this deficiency.

Management

support

in

the

plant

chemistry

improvement

program

was

not evident with regard

to the timeliness for

upgrading

of

the

chemistry

laboratories

and

sampling

panels.

Management

has

not

been fully successful

in preventing

repetitive maintenance

problems (e.g.

AFW,

ICW and nuclear

instrumentation)

and

in

stemming

an increasing

number of

PWO's.

This increasing

PWO backlog

can also

be viewed as

a

positive

indication

of

maintenance

responsiveness

( see

Section IV.C).

The licensee

has continued to rely heavily

on compensatory

measures

for

the

maintenance

of

the

security

system

computer,

which remains unreliable.

Lack of management

oversight

has contributed

to

numerous

and repetitive violations concerning

the security program.

38

Shor

ages

in the staffing of qualified instructors

has

led

to deficiencies

in the training area.

The

use of contract

instructors

has

had diminished effectiveness

due to their

lack of knowledge of plant specifics.

The existing training

program

and its documentation

has

lacked adequate

management

attention.

Two violations were identified:

a.

Severity

Level

IV violation for failing to have the proper

number of radios

in the Control

Room

as

required

by the

Control

Room Inacessibi lity Off Normal Procedure

(86-37).

b.

Severity

Level

IV violation

for

excessive

Operations

personnel

overtime.

(87-24)

2.

Conclusion

Category:

2

Trend:

3.

Board Recommendations

The

board

recognized

the fact that

licensee

management

has

expended

significant effort to improve performance

in this area.

Licensing Activities

1.

Analysi s

Management

control

and overview in the licensing activity area

continues

to be evident.

The licensee's

management

continues

to

have

freouent

meetings

and discussions

with the

NRC staff to

assure

there is

a

common understanding

of safety

issues

and the

need

for

timely

resolution.

An

example

of

management

involvemen

is demonstrated

by their initiative in proposing

an

amendment

to incorporate

a license

condition for

an integrated

schedule.

The integrated

schedule

concept provides

a methodical

process

to allocate

and balance

resources

between

improvement of

plant performance

and enhancement

of overall plant safety.

There

has

been

an

improvement

in

the

attention

management

provides

to licensing initiatives

and activities

from the last

SALP period

as demonstrated

by the reduction .of the

backlog

in

licensing

actions.,

Although the

level

of attention

given to

licensing

activities

has

improved,

the

resolution

of

some

licensing

issues

is

impacted

due

to the efforts

required

in

other areas

such

as operations,

maintenance

and select

systems

review.

39

JUL 17

)g87

The

icensee

continues

to

increase

the

technical

staff

supporting

the

Turkey

Point

Plant

both

ir.

the

engineering

offices

and

a+

+he plant site.

The projected

and

agreed

upon

schedules

are

generally

met.

In

most

cases

where

schedul.e

changes

are

necessary

adequate justification is provided.

Some

schedules

have

been slightly delayed

due to resource

cons.raints

resulting

from operational

problems.

In general,

the effects of

the licensee's

consolidation

of the majority of their nuclear

engineering

support

staff

has

resulted

in overall

improvement

and efficiency in the licensing process.

The

licensee's

response

to

NRC initiatives continues

to

be

prompt

and

complete.

During this

SALP period

a total of

30

multi-plant

and

Tt1I related

items

have

been

resolved.

The

licensee

has

taken the initiative of proposing

amendments

to the

Turkey Point licenses

to incorporate

an integrated

schedule

and

to upgrade

the plant specific Technical

Specifications

to the

standard

Technical

Specifications

for Mestinghouse

plants.

It

should

also

be noted that the licensee voluntarily initiated an

administrative Limiting Condition of Operation

on the

emergency

diesel

oenerators

as

an inierim measure

until the staff

com-

pletes

their

review of the

proposed

technical

specification

upgrade

in this area.

The overall staffing to support

licensing activities continues

to

be

more

.han

adequate.

The

increased

diversity

in

the

technical

backgrounds

of the

licensing staff is

an

asset

in

resolution of technical

problems."

The overall coordination of

the licensing activities generally results in prompt and timely

responses,

although the extremely

heavy workload of the on-site

staff

continues

to result

in

scheduler

delays

on

occasion.

Increased

interaction

of the

o f-site

and

on-site

licensing

staff has led to overall

improvement.

The

licensee

has

been

responsive

to

Regional

initiatives to

reduce

the

NRC

backlog

of Outstanding

Items

(closeout

of

violations,

unresolved

items,

etc.).

They

have

prepared

and

submitted

packages

to the inspection staff of those

items

deemed

ready for closeout inspection.

The licensee

continues

to, provide specialized

training to the

licensing staff.

As noted previously,

the diverse

backgrounds

of

the

licensing

staff

have

aided

in prompt resolution

of

licensing activities and providing timely information related to

operational

occurrences.

The

licensing staff provided timely

and detailed

information rel,ating to the recent reactor

coolant

system

leak

on Unit 4.

The licensing staff also participates

in industry initiatives

such

as

the

technical

specification

improvement

program.

40

JVL lp8y

During

the

evaluation

period of

Nay 1,

1986

through

May 31,

1987,

several

situa.ions

occurred at Unit 4 which had

a negative

impact

on the implementa.ion

of in.ernational

safeguards

in the

U.S.

-The

implemen.ing

instrument

for International

Atomic

Energy

Agency

( IAEA) safeguards

at the facility level is the Facility

Attachment

(FA) which contains

detailed

information

as to

how

IAEA safeguards will be performed at the facility.

In Nay 1986,

the

NRC sent the licensee

a copy of the draft IAEA FA for review

and,

in

October

1986,

he

was

provided with

a

copy of the

finalized

FA for informational

purposes.

The

FA was formally

imposed

as

a condi

ion of license

by

NRR on April 10,

1987.

.Although licensee

management

did perform the records

and reports

functions

in

an

adequate

manner,

they

did

not

maintain

an

adequate

level of awareness

of the obligations associated

with

the

containment

and

surveillance

functions

of international

safeguards.

On

several

occasions

continuous

illumination for

surveillance

cameras

was not maintained

in the

spent

fuel

bay.

This reouired

two re-verifications of the spent fuel inventory.

Also,

IAEA seals

designated

to maintain the safeguards

integrity

of 'he

reactor

core

were

broken

on

several

occasions

which

require

re-verification

by

the

IAEA.

During

the

period,

however,

the facility was not required

by the license to fulfill

the

requirements

of the

FA

and

there

was

a difference

in

perception

of the

requirements

between

the licensee,

IAEA, and

the

HRC.

No violations were identified during this period.

. Conclusion

Category:

2

Trend:

3.

Board Recommendations

None

K.

Training and gualification Effectiveness

1."

Analysis

During this

SALP reporting period,

several

routine

and reactive

inspections

were conducted

in the area of training at the Turkey

Point facility.

In addition,

replacement

and requalification

examinations

were

conducted

in

September

and

December

1986.

During the last

SALP period,

major deficiencies

identified in

41

the area of training have included

an inadequate

training staff,

a

lack of

con inuing train'.ng

for ma'ntenance

personnel,

an

nsat,sfactory

Licensed

Operator

Requalifica.ion

Program,

General

Employee

Training

(GET)

deficiencies,

programmatic

deficiencies

in the Required

Reading

and Operational

Experience

Feedback

Programs,

and

Emergency

Operating

Procedure

(EOP)

training deficiencies.

In addition,

an

internal

assessment

conducted

by the licensee

in June

1986 identified

165 specific

training deficiencies.

In the previous

SALP report it was

stated

that

an

inadequate

number of instructors

and training staff have

had

a significant

nega-ive

impact

on training, testing,

and documentation.

The

continuing

maintenance

training

was

discontinued

for

over

a

year

to allow the

small

training staff to

support

the

INPO

acc. edita.ion

effort.

Licensed

operator

requalification

was

staffed

by

a

minimal

staff

responsible

for

development,

instruction, testing,

scheduling,

and documentation.

Based

on

their poor performance

on

an

NRC requalification examination

in

February

1986,

the

licensee's

Requalification

Program

was

determined

to

be unsatisfactory.

Numerous

deficiencies

were

also identified in the testing

and documentation

associated

with

GET

'.raining,

and

those

deficiencies

appeared

somewhat

attributable to an inadequate

training staff.

The licensee

has

increased

the

size of the training staff from

35

in April

1986,

to

58

in

February

1987.

Three

program

supervisor positions

have

been established

which report directly

to the Training Superintendent.

The program supervisor positions

for

Operations

and

'thai ntenance

Training were'illed

with

incumbents

from the in-plant organization,

thus

increasing

the

experience

levels within the Training Depar men'anagement.

The

simulator

training staff will consist

of

a

Simulator

Engineer

Coordinator,

who is

a contract individual, four support

specialists,

and two instructors.

The only instructor

assigned

at the time of the February

1987 inspection

was

a supervi sor who

had

been

unsuccessful

on

the

recent

NRC

requalification

examination.

This simulato'r staff does

not appear

adequate

to

supp'ort curriculum development for simulator delivery this year,

or to provide simulator instruction for hot license

and license

requalification training.

While the overall

numbers of training staff have

been

increased,

the licensee

was critically short of qualified instructors for

Licensed

Operator

Requalification Training.

Two of the

three

instructors

assigned

to

requalification

training

were

SRO

licensed,

but

had

recently

failed

NRC

requalification

examinations.

Several

other

instructors

who

had failed

NRC

requalification

programs

were

permanently

reassigned

to other

42

JUL 1'7

1987

du.ies.

The

utilization

of

instructors

who

have

failed

requalification

examinations

to prepare

licensed

operators

for

th

same

type of examination

jeopardizes

the effectiveness

of

the

Upgrade

Requalification

Program

and

undermines

student

confidences

As

an interim solution to the instructor shortage,

the licensee

was utilizing contract instructors

in the

Upgrade/

Accelerated

Licensed

Operator

Requalification

Program.

Contract

instructors,

however,

were found to be lacking in plant specific

knowledge.

Utilizing contract instructors to teach

systems

and

integrated

plant

response

without si e-specific

knowledoe

or

training prevents

them from being able to provide plant specific

information.

During most of 1986i

Turl ey Point

embarked

upon

an accelerated

requali fication

training

program.

All'icensed

operators

were

removed

from licensed

duties until they

passed

an

HRC

administered

requalification

examination.

These

examinations

were administered

in April, September,

and

December

of

1986.

The

overall

oass

rate

was

63;;.

The

NRC's criterion

for

evaluating

a facility's requalification

training

program

as

unsatisfactory

is below

60.'o'.

Contributing factors to this lack of performance

appeared

to be

the shortage

of qualified instructors

and instructors

working

excessive

overtime,. the utilization of upgrade

requalification

participants

for in-plant overtime,

and

an apparent

inadequate

evaluation

and identification of the specific

knowledge

areas

requiring

upgrade

training.

An additional, contributing factor

to this relatively

low

pass

rate

was

that

those

licensed

individuals

associated

wi:h

the facility'

training staff

achieved

only

a

14

pass

rate.

If these

individuals

are

extracted

from the overall results,

then

a

75ro

success

rate,

representing

those individuals in Turkey Point's

operations

and

technical

support staffs, is observed.

This indicates that the

accelerated

program

was marginally effective in correcting

noted

deficiencies

and

improving the overall

knowledge

1 vel for the

licensed

operators

in these positions.

The

Operational

Experience

Feedback

and

Required

Reading

Programs

continue

to experience

problems.

Operating

Experience

Feedba'ck

Training control

has

been

improved

due to management

attention

to

documentation

and

timely

disposition

of

info'rmation.

The program,

however,

was apparently

unsuccessful

in responding

to prior information

on the boric acid/conoseal

leak and the nitrogen intrusion into the boric acid system.

43

JUL l7

1981

The

number

of

procedure

revi sions

being

generated

by

the

Procedure

Upgrade

Program.

including

minor

administrative

changes,

had virtually inunda'ed

the

operators

with

a

large

volume

of

material

to

review

and

seriously

impeded

the

effectiveness

of the

required

reading.

In

response

to

NRC

concerns,

the

Required

Reading

Program

had

been

effectively

revised to provide the operators

with a synopsis of significant

procedural

changes

vice

a

de ai led

review of all

procedure

changes.

As

noted

previously

in this

SALP,

the

licensee

has utilized

non-licensed

ins ructors

who

have

not

attended

a

licensed

opera

or training or received site specific training.

An audit

of the records for the current instructor Certification Program

revealed

disorganized

and

incomplete

records with records

such

as

lesson

plans

and instructor in-plant training time missing.

While the licensee

has conducted

an instructor job tasl

analysis

to be used. in their new four phase,

performance-based

instructor

Developement

and Certification Project,

the existing program

and

its documentation

lacked adequate

management

attention.

Early in the

SALP period,

the licensee

conducted

an internal

assessment

o: the Training

D partment.

Thiis licensee-initiated

review

was

very beneficial

in .uncovering

deficiencies

and

potential

problem

areas.

An

NRC

inspection

conducted

in

November

1986 revealed that although the assessment

was thorough

and

comprehensive,

the

licensee

was

slow in taking corrective

action,

especially for

some of the

more serious

deficiencies.

Several

discussions

and meetings

with regional

representatives

resulted

in

accelerated

closeout

of

the

identified

problem

areas.

A tracking

system

is

in

place

for monitoring

the

close-out

of

ac ion items associated

wi

h identified training

deficiencies.

The completion of this activity is instrumental

'in the

success

of the Training Department's

Quality Improvement

PrografA/

Quality

in

Daily

Work

(QIP/QiDW)

programs.

By

November

15,

1986,

nine

items

which were classified

by the

licensee

as regulatory

in -nature

had

been

closed

out,

and

by

January

15,

1987,

35

additional

items

had

been

closed.

Completion of the training audit action

items

is progressing

ahead of the projected

schedule.

Additional

long-term

programs

were

in the

early

stages

of

implementation,

but

should

provide

a positive

impact

on

the

quality of training at the licensee.

These

programs

include the

following:

(1)

Training Assurance

Program

(TAPS)

(2)

Training Information Management

System

(TRIMS)

(3)

INPO Accreditation Effort

JUL 1'7

1987

The

TAPS

program

is charged

with moving the Nuclear Training

Sys.em

from

a reactive

to

a proactive

mode of operation.

The

TRIMS program

involves

a method to identify tracking

needs

by

the review of change-indicators,

and to track both internal

and

external

change

indicators,

documenting

the

use

of

the

systema.ic

approach

to iraining (SAT) process.

As of January

1987,

1,229

items of instructional

materials

had

been

entered

into

he

system.

This

data

base

allows efficient

use

of

available

data

for training

cour ses,

e.g.,

Licensee

Event

Reports

( LERs), Significant Operating

Event Reports

(SOERs),

and

Operating

Event Reports

(OERs) student

feedback.

Due to the

NRC/INPO Memorandum of Understanding

with regard to

training programs,

no violations were issued during this period.

2.

Conclusion

Category:

3

3.

SALP Board Recommendations

Turkey

Point

has

made

limited

improvements

in the

area

of

training

through

increases

in

management

controls,

implementation

of

performance

based

continuing training for

maintenance

personnel,

and preparation

for

IHPO accreditation.

The

licensee

management

has

not,

however,

provided

adequate

attention

to

and

control

over

the

Licensed

Operator

Requalification

Program.

Continued

NRC and licensee

management

attention

in this area is recommended.

L.

Engineering

Support

1.

Analysis

This functional

area

is

included

in this =SALP report

since

licensee

activities

and

HRC

inspections

showed

significant

contributions to many other areas

of licensee

performance.

This

area

was

evaluated

through

routine

and

specific

resident

inspections,

regional

review of Safety Evaluations

(SEs),

and

a

special

inspection

conducted

by the

regional

gA Section

in

May 1987.

The concerns

in the area of Engi'neering

Support were highlighted

in Enforcement

Action 86-20 dated August 12,

1986.

As

a result

of the

SSFI conducted

in 1985, six violations were cited in this

enforcement

action

with

an

accompanying

Civil

Penalty

of

$300,000.

Two of the violations were directly attributable

to

Engineering

Support:

Design

Control

and

inadequate

SEs,

while

engineering

functions directly contributed

to

several

others.

Previous

enforcement

actions

in

1984

and

1985

also

involved

examples of inadequate

SEs

and failure to control

PC/Ms.

45

JUL l '7

1987

In

a letter dated October

1,

1986,

FPL responded

to

EA 86-20

and

delineated

numerous

correc ive actions,

completed

or planned,

'.",=-: addressed

each

of the six basic

areas

identified in the

No ice of Violation.

With regard

to the

functional

area

of

Engineering

Support these corrective actions included:

1)

Phase II Select

System Safety

Review

2)

Standard

Engineering

Design

Package

for Controlling Plant

Changes

3)

Reoroanization

of the

engineering

function

and

increased

s-.affing

of

both

the

engineering

and

technical

organizations

at, the plant.

'4)

Traininc

o> technical

personnel

and management

attention to

the

new plant modification process.

The majority of the

Phase II Select

System

Review

has

been

completed

for

the

14

systems.

This

extensive

effort

has

included:

reconstitution

of design

bases,

system

walkdowns,

Safety

Engineering

Group

(SEG)

comprehensive

review

and

an

enhanced

configuration

management

program.

The

implementation

of the effort has

been effective

and

has

required significant

resources.

The

review

effort

has

identified

numerous

deficiencies

in

system

design

to

which

the

Engineering

Departments

have

responded

promptly

and

adequately.

Examples

include;

identification of

emergency

diesel

generator

loading

limitations,

the

absence

of containment

spray

flow limiting

orifices,

the

potential

for safety

injection recirculation

valves to fail in a non-conservative

position,

the potential for

electrical

relays

to prevent proper diesel

operation,

potential

ventilation system failures,

and

the

need

to expedite

the post

accident

ECCS

recirculation

initiation.

The

Engineering

Departments,

both site

and corporate,

have

responded

to these

deficiencies with careful

analyses

and

sound short term and long

term corrective action proposals.

Electrical modifications were

completed

in August

1986 to preclude

the potential

for diesel

overload.

Containment

Spray flow orifices were installed in May

1987

to preclude

the possibility of

pump

runout.

Emergency

procedures

were revised

to require

post accident recirculation

initiation without

delay.

Temporary

procedures

.have

been

developed

to

supply inverter ventilation in'he

event

of

a

sustained

loss of offsite power.

Modifications

have

been

made

to the Unit 3 Component

Cooling Water heat

exchangers

to allow

continuous

online

cleaning.

The

Unit 3

safety

injection

recirculation valves

have

been modified so that the flow path is

not

susceptible

to

a

single

failure.

Numerous

additional

improvements

are

being

developed

by the engineering

staff for

future implementation.

46

JUL

1 '7

1987

A significant initiative of the engineering

organizations

was

the

developmen

of

a

Standard

Engineering

Design

Packace

to

control

he

manner

in which plant modifications

a. e developed

and

implemented;

By standardizing

the format,

content,

review

process

and

approval

mechanisms

the

licensee

has

reduced

the

potential

for

changes

to

have

adverse

affects

on

the plant.

Included

in the design

package

are

requirements

for procedure

and drawing reviews to ensure

hat modifications

have

been fully

completed prior to system turnover for operation.

The Standard

Engineering

Design

Package

has

been

recognized

by the Institute

for Nuclear

Power Operations

(INPO) as

a good practice worthy of

consideration

for use

by other industry organizations.

The site engineering

function

was

reorganized

in early

1986 to

create

the position of Site Engineering

Manager

and to increase

site

staffing.

In

addition

to

the

Site

Engineering

organization,

there

is

a

functionally

separate

Technical

Department

that

reports

directly to the

Plant

Yianager.

The

staff allowance for this Technical

Department

was also increased

to provide additional

system

engineers.

This

has

reduced

the

qumber of systems

assigned

to each

engineer

and

increased

the

level

of attention

to

design

control

with respect

to

each

individual

plant

system.

Th se

organizational

and staffing

improvements

enabled

the engineering

organizations

to respond to

requests

for assistance

in

a

more effective manner

and allowed

more complex issues

to be pursued

by site rather

than corporate

personnel.

Enhanced

training

of

technical

personnel

and

increased

management

attention

have also

been evident

and are discussed

in

the training and

gA sections

of this report.

'While

many

engineering

problems

have

been

identified,

compensated

for in the

short

term

and

apparently

corrected

programmatically,

some deficiencies

have

been evident.

In March

1987,

an

NRC Augmented Inspection

Team (AIT) began

a review of

the

consequences

of the licensee's

decision to operate

the Unit

4 reactor with a small instrument

seal

(conoseal)

leak which had

been

identified

in

August

1986.

The

Engineering

Department

issued,

on August 30,

1986,

a safety evaluation

which considered

the

leakage

minor, within Technical

Specification limits,

and

recommended

that

the

leaking

conoseal

be

reinspected

in six

months

and

repaired

during

the

next

available

shutdown

of

sufficient length.

The safety evaluation

was

approved

by the

Plant

Nuclear

Safety

Committee

on

August 31,

1986.

Between

August

1986

and

March

1987,

a

large

amount

of boric

acid

accumulated

on the reactor

vessel

head

and resulted

in c'orrosion

damage

to surrounding

equipment

and

components.

Analysis

and

repair resulted

in an extended Unit 4 outage.

JUL 1'7

1987

The AIT determined

that

the engineering

safety evaluation

used

'.o justify reactor operation

was deficient in that it:

was

not

based

on

a detailed

inspection

of the leaking component;

based

corrosion

calculations

on

a

non-conservative

corrosion

rate;

failed

to

evaluate

the effects

of corrosion

on

surrounding

components

and equipmen

and was performed in

a hurried

manner

without

complete

and

comprehensive

supervisory

review.

In

add',:ion,

the

engineering

inspection

review

of

the

leaking

conoseal,

a month

and

a half after discovery, failed to consider

the

ex ensive

spread

of boric acid residues

on

and

around

the

reactor

vessel

head

area.

Proposed

violation (f) below

was

issued

concerning

this deficient

safety

evaluation.

Also,

a

re iated

violation

(g)

was

proposed

for fai lure

to properly

adhere

to tne drawing accuracy/control

of the conoseal.

The licensee's

program for recovery

from the leakage

even

was

very complehensive.

An hRC review of the licensee's

engineering

analysis of the event,

including safety significance resulted

in

concurrence

in

the

reactor

restart

plan.

However,

some

prompting

as to the level of detail

expected

from the licensee

in its event evaluation

was

necessary

when the AIT arrived

on

site.

Programmatic

improvements

in the area of leak detection,

engineering

analyses,

and corrective actions

have

been developed

and implemented.

Violation (c)

below

documents

two

examples

when

the

safety

significance

of discrepant

conditions

was

not, evaluated

in

a

timely manner.

In each

case,

several

weeks

elapsed

between

the

discovery of the condition

and the initiation of an engineering

review to determine

the

consequences

of the condition.

In the

interim,

the operability of the

equipment

was

not established

because

he

plant

staff

did

not insist

on

an

engineering

assessment

and

the

engineering

staff

was

not

procedurally

required

to

supply operability determination,

either

oral

or

writ~en.

Subsequently,

in early

December

1986,

engineering

procedures

were

approved

and

implemented

which require written

operability

assessments

within three

days of the receipt of

a

nonconformance

report.

This

represented

the first

formal

procedural

guidance

implemented

for

the

Site

Engineering

Department

subsequent

to its establishment

in

February

1986.

Between

February

and December

1986 draft versions of procedures

were circulated but compliance

was left to the discretion of the

individual engineers.

Violation

(e)

below

documents

an

example

where

inadequate

inspection

and analysis

were

performed relative to

an

observed

deficiency

in

a safety related

check valve.

As

a result,

the

discrepant

condition existed for several

months

before it was

determined

to

be

symptomatic

of undesirable

internal

valve

degradation.

Inspection

of similar

valves

revealed

multiple

48

JlJf 17

1987

examples

of internal

degradation

different in type

and origin

than those previously

known to exist.

All valves

were

replaced

wi.h

an

improved

design

which

reduces

the

potential

for

recurrence.

Violation (b)

was

issued

in

1986

but

is

based

on

a

1984

Unr'esolved

Item concerning

a failure to perform

a

10 CFR 50.59

evaluation

on the throttling of an

RHR discharge

valve.

Turkey Point is

considered

by

NRC Region II staff to

have

a

reasonably

effective

program

with

regard

to

environmental

qualification (Eg) aspects.

This

may

be the result of lessons

learned

from

an earlier

inspection

performed

at

FPL's

other

nuclear

site

(St. Lucie).

In

February

1987,

a

special

team

inspection,

lead

by the

IRE Vendor Program

Branch

was performed

Turkey

Point

to

examine

the

licensee's

program

fol

establishing

Eg of electrical

equipment

within the

scope

of

10 CFR 50.49.,

Using enforcement criteria specified

in Generic Letters 85-15

and 86-15 several

potential

Enforcement/Unresolved

Items

and

Open

Items were identified.

An

NRC

Team

inspection

in

February

1987

revealed

that

many

Requests

for

Engineering

Assistance

(REAs)

remained

open

approximately

525 and that these

numbers

were still increasing.

This

was attributable,

in part,

to the increased

confidence

in

Site

Engineering

Office by various

plant

groups,

and

to

the

extensive

plant modifications taking place.

It should

be noted

that

a high percentage

of the

open

REAs were

a year or more old

and

had not been

the object of any action or review.

Several

additional

concerns

with

Engineering

,Support

were

identified

during

tne

SALP

period.

Inspector

review

of

JPE"L-85-38,

"Substantial

Safety

Hazards

Evaluation

for

ICM

System

Design",

identified

a

potential

operability

problem.

This

SE apparently

au'horizes

the operation

of the plant with

the Intake Cooling Mater (ICW) system outside its design

basis.

Due

to

fouling of the

heat

exchangers

and

elevated

Intake

Cooling Mater temperature

there

are

times

when the

ICM system

may

not or

has

not

been

capable

of performing its

intended

safety function during

a design

basis

accident

and

assuming

a

single

active failure.

The

SE

has

been

forwarded to

NRR for

further

evaluation

and

for possible

generic

considerations

concerning fouling of service water systems.

During

an inspection

conducted

in January

1987

in the

area

of

seismic

analysis

for as-built safety-related

piping,

supp'orts,

etc,

the

inspector

had

several

unresolved

items

(URIs).

These

URIs

concerned

the

failure

to

identify

and

to

evaluate

discrepancies

that

could

potentially

have

affected

the

49

JUL I7

1987

operabi

1 i y of

the

Component

Cool ing

'l4ater

(CCl'!)

sys

em.

Although the

URIs

have

not yet

been

closed

out,

corrective

ac ion

by

the

licensee

was

only

.aken

after

prompting

by

regional

management.

The

Res dent Inspectors'eport

for March and April 1987 de.ai ls

two

proposed

violations

concerning

electrical

wiring

discrepancies

in

the

Emergency

Diesel

Generator

(EOG)

load

sequencers

and protective

relays.

The latter

discrepancy

was

identified first during routine

surveillance

testing

and

was

attributed to the generation

of an incorrect connection

diagram

developed

as part of a

PC/M package.

Violation (h) was proposed

in

response

to this

problem.

Additional

inspections

were

conducted

by

the

licensee

to determine if any

other wiring

discrepancies,

existed that were related to work performed

under

this

PC/M.

The inspection

revealed

two problem areas

in the

3B

load sequencer.

The root cause

of one wiring error has not yet

been

found while the other cause

was attributed to an incorrect

Process

Sheet.

Proposed violation (i) addresses

this error.

In

response

to

these

various

concerns

over

the

Engineering

Support function,

a special

announced

inspection

was

conducted

in

May i9S7.

Areas

inspected

included engineering

procedures,

controls

for

engineering

evaluations,

and

a

review

and

assessment

of

engineering

evaluations.

In

the

area

of

engineering

procedures,

the inspectors

found that

the licensee

had

established

adequate

engineering

procedures

for

the

performance

of safety evaluations

associated

with

10 CFR 50.59

requirements

related to plant modifications, justifications for

continued

operations,

and

controlled

plant

work

orders.

However,

requirements

for the

assessment

of the

effects

of

nonconforming

conditions

on safety-related

equipment

function,

performance,

reliability

and

response

time

had

not

been

explicitly defined.

At the conclusion of the

SALP period, the

licensee

was

in

the

process

of

revising

procedures

that

delineate

the

administrative

controls

for

processing

nonconformance

reports.

Based

on

the

sample

reviewed,

the

licensee

appeared

to

be

performing

an

adequate

job of performing

safety

evaluations

associated

with plant change/modifications,

justifications for

continued

operations,

and controlled

plant

work orders

with

regard to the effect of the change or activity on safety-related

equipment

function,

performance reliability, and response

time.

Most,

safety

evaluations

adequately

addressed

critical

engineering

design

requirements, where applicable

such

as single

failure criteria, separation criteria,

and seismic requirements.

In

a

related

area,

improvement

was

apparent

in

the

site

engineering

organizations disposition of nonconformance

reports

50

Jgg gg

1987

with respect

to roo.

and pos.-modification

sta+'.stica'.

sampling

SALP period which did

cause

analysis,

corrective

action plans,

testing.

This conclusion

was

based

on

a

of nonconiormance

reports

covering thi s

not identify any deficiencies.

ive violations were identified:

Severity

Level

IV violation with four

examples

of

incorrect diesel

generator

drawings

due to incomplete

iield veri iication.

(86-25)

Severity

Level

IV violation for failure to evaluate

valve

modi iications for unreviewed

safety

question.

(86-44)

Severity Level IV viola.ion for failure .o assure

that

conditions adverse

to quality were promptly corrected;

two examples - support

hangers

not properly

assembled

and

emergency

diesel

generator

air receivers

not

properly bolted to the floor.

(86-45)

Severity

Level

V violation for incorrect

steam

break

protection logic drawings.

(86=33)

Severity

Level

V violation ior failure to take prompt

corrective action to identify and correct

damaged

ICM

check valves.

(Unit 4 only, 87-06)

The following four violations are

under consideration

for

escalated

enforcement

actions:

Proposed violation for inadequate

safety evaluation

on

conoseal

boric acid leak.

(Unit 4 only, 87-16)

9.

Proposed

violation

for

insufficient

iniormation

regarding

conoseal

shims

in

procedure

for

the

installation

of

reactor

vessel

head

conoseals.

(Unit 4 only, 87-16)

Proposed

violation for failure to

have

and accurate

connection

.diagram

for safety

related

EDG wiring.

(87-14)

Proposed

violation for failure to maintain

adequate

control of design

changes

affecting the

3B

EOG load

sequencer

.

(87-14)

2.

Conclusion

Category:

51

JUL 17

1S87

3.

Board Recommendation

The

Board

',s

concern

d

hat although

the engineering

support

programs

have

been substantially

improved, there exists

a large

number

of request

for engineering

assistance

over

a year

old

that

remain

open with no action or review.

In addition several

significant examples

of engineering

evaluation

or modifications

have

resulted

in the operation

of the facility with degraded

sa:ety

related

equipment.

Additional

NRC

and

licensee

management

attention

in this area is recommended.

V.

SUPPORTING

DATA AiND SUMMARIES

A.

Licensee Activities

During

he

assessment

period,

Unit 3 was in routine commercial

operations with a refueling

outage

from March ll, 1987,

to the

end of the

SALP period.

Other outages

included those

discussed

under

Item J

Reactor

trips

and

an

outage

to

perform

modifications

required

for

Emergency

Diesel

. Generator

load

considerations

from July 15,

1986

to

August 5,

1987.

The

present

refueling

outage

began

one

week early

due to problems

w'.th the turbine-generator

hydraulic .oil

system

and

has

been

extended

about

two months

due to the

Raychem

splice

issue

and

the cracks

found in the Post Accident Hydrogen Monitoring sample

line:

Unit 4 remained

in

a refueling

outage

at the beginning of the

assessment

period

due

to

EDG

overload

concerns

and

modifications.

Commercial

operation

was

conducted

from

September

1986 until March 10,

1987,

when it was

shutdown

due to

a failure of the

personnel

hatch

to meet

con ainment integrity,

and

has

remained

down through the remainder of the

SALP period,

due to discovery of excess

boric acid buildup

on the reactor

vessel

from a conoseal

leak.

Replacement

of Raychem splices

has

also extended this outage.

B.

Inspection Activities

The routine inspection

program

was performed during this period, with

special

inspections, conducted to augment

the program

as follows:

1.

April 28 -

May 2,

1986,

in

the

area

of the

control

and

distribution of electrical

loads

which are

connected

to the

emergency

diesel

generators

in the

event

of

a

design

basis

accident.

2.

June

10

and

August 18,

1986,

involving

physical

security

concerns

observed

by

the

Resident

Inspector

relative

to

protected

are barriers,

gates

and compensatory

measures.

'52

JUl. rV >S87

July 22-26,

1986,

in the

areas

of modifications

in elect. ical

loads

for emergency

diesel

generators

(EDGs)

and

integrated

safeguards

testing

associated

with modifications

and

EOG load

evaluation.

4

5.

September

28-29,

1986,

involved

a review of scaffolding which

provided

a pathway from the protected

area into

a vital area.

november

17-21,

1986,

in the area of training.

'I

January

20-21,

1987,

a review of the circumstances

of a licensee

reported incident of failure to,provide positive access

control

to

a vi al, area

as

a result of a posted security officer being

asleep

on post.-

March 2-6,

1987,

in the area of equipment qualifications.

February

16-21,

1987,

to assess

plant operations

in four major

assessment

areas

which include

maintenance,

operations,

plant

management

controls

and training.

March

19 - May 5,

1987,

an Augmented Inspection

was conducted to

monitor the lic nsee's

response

and to review the circumstances

associated

with

a

problem

identified

by

the

licensee

with

corrosion

caused

by deposits

of crystalline boric acid

on the

reactor vessel

head

and surrounding

areas.

10.

April 28 - May 1,

1987, in the area of followup on worker health

physics

concerns.

May 11-15,

1987,

in the

area

of Engineering

Support

and Safety

Evaluations.

12.

May 18-.29,

1987,

in

the

area

of performance

of

a

loss

of

off-site

power testing

on

both units with

a loss of coolant

accident

on one unit.

C.'icensing

Ac ivities

The

basis

for this

appraisal

was

the

licensee's

performance

in

support

of licensing

actions

that

were either

completed

or

had

a

significant

level

.of activity during

the

rating

period.

These

actions

consisted

of

amendment

requests,

exemption

requests,

responses

to generic

letters,

TMI items,

and

other

actions.

The

numbers of closed licensing actions

can

be

summarized

as follows:

Active actions at beginning of period (6/1/86)

Actions added during. period

Total actions

Completed actions during period

Active actions at end of period (6/31/87)

76

28

104

64

40

53

JUL 1.7

1987

The

64 actions

completed during this

SALP period

can

be divided into

three major cateoories.

The

number of actions

which were

completed

for each category

are:

Plant specific actions

Multi-plant actions

TMI actions

34 completed

16 completed,

14 completed

1.

Licensing Actions Completed

During This

SALP Period

ASME Code

Case

N-416

Generic Letter (GL) 83-28,

Item 4. 1 Reactor Trip System

(RTS) Reliability

GL 83-28,

Item 4.5. 1 -

RTS

NUREG-0737,

Item III.A.1.2,

Emergency

Response

Facility

(ERFs)

NUREG-0737,

Item III.A.2.2, Meteorological

Upgrade

TMI Order Modification (July 15,

1985 Order)

GL 85-15,

Environmental qualification (Eg) - Clarification

Code

Case

N-411

Use at Turkey Point

NUREG-0737,

Item II.K.3.31, Small Break

LOCA

Emergency Diesel Generator

Load Evaluation

NUREG-0737,

Item I.D. I, Control

Room Design

Review

Emergency

Diesel Generator Reliability

Containment

Purge/Vent

GL 83-28

Items

3. 1. 1

and

3. 1.2,

Post

Maintenance

Testing

(RTS Components)

GL 83-28

Items 3.2. 1

and 3.2.2,

Post

Maintenance

Testing

(All Other Safety-Related

Components)

Component Cooling Mater Flow Balance

PTS Rule (10 CFR 50.61)

,54

JUL

1 7

1987

2.

HRR-Licensina Yieetin

s

%ubga~t

USI A-44 Station Blackout,

Bethesda

Physical Security,

Bethesda

. Technical Specification

Upgrade,

Bethesda

Integrated

Schedules,

Atlanta

3.

HRR Si

e Visits

Subject

Performance

Enhancement

Program

50.59

Review

R Licensing Activities

Boric Acid Leak Evaluation

SPDS Implementation Audit

4.

Commission Briefin

Hone

Date

9/3/86

9/12/86

11/18/86

2/19/87

Date

5/28-30/86

12/8-10/86

3/20-22/87

3/23-26/87

Subject

Boric Acid Leak Event

6.

Schedular

Extensions

Granted

Subject

50.48 Schedular.

Exemption

Appendix

R

Surveillance

Report

Schedular

Exemption

7.

Reliefs Granted

IST Relief - Spent

Fuel

Pool Cooling

Pumps

IST Relief

Snubbers

ISI Relief - Safe

End Welds

Date

4/10/87

Date

6/9/86

8/25/86

9/18/86

10/9/86

2/13/87

55

JUL 1'7

1987

8.

Exemptions

Granted

one

9

~

License

Amendment

Issued

Amendment

Nos.

Subject

Date

116/110

117/111

118/112

Snubber Technical Specifications

5/6/86

Per

GL 84-13

Use of Burnable

Poisons

7/14/86

LCO and Survei1 lance

Non Safety

8/13/86

Standby

Feedwater

System

119/113

120/114

ISI Program - Second

10 Year

Diesel

Generator

Inspections

(Exigent Amend)

10/27/86

11/10/86

121/115

122

Cont~ol

Room Habitability

2/2/87

Extend Surveillance

- Containment

2/12/87

Filter System

(Emergency

Amend)

123/116

Reporting

Requirements

10 CFR 50.72

and 50.73

3/6/87

117

IAEA Safeguards

License Condition

4/10/87

D.

Investigation

and Allega.ion Review

No major investigations

were

conducted

at Turkey Point during this

appraisal

period.

E.

Escalated

Enforcement Actions

1.

Civil Penalties

Six Notices of Violations (Severity

Level III, Supplement

I) and Proposed

Imposition of Civil Penalty

(EA-86-20) for

a total of $ 300,000

was issued

on August 12,

1986, for the

following:

1) significant

weaknesses

identified in the

design

control

program;

2)

Failure

to

satisfy

the

requirements

of 10 CFR 50.59;

3) significant violation of

Technical

Specification

(TS)

Limit,ing

Conditions

for

Operations

(LCOs);

4) identified weaknesses

in procedural

control

program;

5) fai lure

to

conduct

adequate

load

capacity

testing

and

monthly

surveillance

tests

of

safety-related

batter ies and;

6) failure to take prompt and

comprehensive

actions

once deficiencies

were identified.

This violation,

although

issued

during

the current

SALP

peri.od,

was addressed

in the previous 'SALP analysis.

A Notice of Violation (Severity

Level III, Supplement

I)

and

Proposed

Imposition of Civil Penalty

(EA-86-28) for

$50,000,was

issued

June

25,

1986, for inadequate

testing

and

failing

to

satisfy

an

NRC

order

regarding

the

operability of

a neutron flux detector

system

on Unit 3.

This violation,

although

issued

during

the current

SALP

period.

was addressed

in the previous

SALP analysis.

A Notice of Violation (Severity

Level III, Supplement

IV)

,and

Proposed

Imposition of Civil Penalty

(EA-86-38) for

$ 50,000

was

issued

on

April 28,

1986,

for

radiation

exposure

control

problems

associated

with

maintenance

activities

on the Unit 3 traversing

incore probe

system

on

January

8,

1986.

The licensee's

request

for mitigation of

the Severity

Level

and Civil Penalty resulted

in the Civil

Penalty being mitigated

on October

14,

1986 to $25,000

and

the

Severity

Level

remained

unchanged.

This violation,

although

issued

during

the

current

SALP

period,

was

addressed

in the previous

SALP analysis.

C

A No ice of Violation (Severity Level III, Supplement III)

and

Proposed

Imposition of Civil Penalty

(EA-87-40) for

$75,000

was

i ssued

April 21,

1987, for physi cal

securi ty

i ssues.

e.

T.

A proposed

violation with an associated

Civil Penalty for

inadequate

Safety

Evaluation

concerning

a

boric

acid

conoseal

leak

on Unit 4.

A proposed

violation with an associated

Civil Penalty for

failure to maintain access control'f a vital area.

Orders

An order

imposing

a civil monetary

penalty

was

issued

on

October

14,

1986;

as discussed

in paragraph

E. l.c above.

An order updating

the

Performance

Enhancement

Program

was

issued

on August 12,

1986, this is in relation to paragraph

E. l.a above.

57

JUg ] g

1S87

F.

Licensee

Conferences

Held During Appraisal

Period

1.

May 9,

1985,

Enforcemen.

Conference

to discuss

Turkey Point

issues

related

to

Component

Cooling Mater

and Intake Cooling

Vater issues.

2.

May 20,

1986,

Management

meeting

to discuss

emergency

diesel

generator

loading.

3.

May 29,

1986,

Management

meeting to discuss

PEP progress.

4.

August 18,

1986,

Enforcement

Conference

to discuss

protected

area

boundary control.

5.

September

11,

1986,

Management

meeting

to discuss

SALP

Board

Assessment

and

PEP progress.

6.

September

23,

1986,

Management

meeting

to

discuss

the

construction of the

NRC and

FPL administered

operator

licensing

examinations.

7.

October

1,

1986,

Enforcement

Co'nference

to discuss

vital area

boundary control.

8.

October 29,

1986,

Management

meeting

to discuss

the integrated

,schedule,

general

employee

training

examinations

grading

and

resolution of items

on Region II's outstanding

items list.

9.

December

16,

1986,

Management

meeting

to discuss

corrective

action for training deficiencies.

10.

February

19,

1987,

Management

meeting

to discuss

the

Proposed

License

Amendment

on Integrated

Schedule.

11.

February

23,

1987,

Enforcement

Conference

to discuss

security

issues.

12.

May 14,

1987,

Management

meeting

to discuss

Operator

License

Training.

G.

Confirmation of Action Letters

(CALs)

NONE

58

Jgg

] y

1987

H.

Licensee

Even. Report Analysi s

During the assessmeht

~e.'.od

57

LERs for Units

3 & 4 were analyzed.

The distribution of these

events

by cause,

as determined

by the

NRC

staff,

was

as follows:

Cause

Component Failure

Design

Construction,

Fabrica ion, or

Installation

Personnel:

-,Operating Activity

- Maintenance Activity

- Test/Calibration Activity

- Other

Out of Calibration

Other

Unit 3

Unit 4

Total

5

14

19

5

1

3

6

11

2

TOTAL

31

26

57

I.

Enforcement Activity

UNIT SUMMARY

FUNCTIONAL

NO.

OF DEVIATIONS AND VIOLATIONS IN EACH

AREA

SEVERITY LEVEL

D

V'V

III

II

I

UNIT NO.

-

3/4

3/4

3/4

3/4

3/4

3/4

Plant Operations

Radiological Controls

Maintenance

Surveillance

.Fire Protection

Emergency

Preparedness

Security

Outages

equality

Programs

and

Administrative Controls

Affecting (}uality

Licensing Activities

Training

Engineering

Support

TOTAL

2/1

9/7

1/1

3/3

1/1

2/2

1/1"

1/1

1/1

1/1

1/1

7/7

2/2

1/2

3/3

I/I+

59

><< >q le~!

FACILITY SUMMARY

FUNCTIONAL

AREA

HO.

OF DEVIATIONS AND VIOLATIOHS IH EACH

SEVERITY LEVEL

D

V.

IV

III

II

.

I

Plant Operations

Radiological Controls

Maintenance

Surveillance

Fire Protection

Emergency

Preparedness

Security

Outages

Quality Programs

and

Administrative Controls

Affecting Quality

Licensing Activities

Training

Engineering

Support

TO:A'

9

1

3

1

3

1

1

1

1

7

2

3

(")An additional

apparent

violations

(one

in Maintenance,

four in

Engineering

Support,

one

in Surveillance,

and

one

in Security

and

Safeguards)

was issued after the

end of the

SALP period

as discussed

in the text of this report.

Reactor Trips

Eigh- unplanned

reactor

rips and

one manual

shutdown occurred during

this evaluation

period for Unit 3.

Unit 4 sustained

five unplanned

trips

and three

manual

shutdowns.

The unplanned trips and

shutdown

are listed below.

1.

Unit 3

a.

May 2,

1986,

the reactor tripped from 100 percent

power due

to operator error while performing the

Reactor

Protection

Periodic Test.

b.

June

27,

1986;

the reactor tripped from'00 percent

and

a

Safety Injection actuation

occurred

due to Instrumentation

and Control personnel

while performing the

Steam

Generator

Protection

Channels

Periodic Test.

August 3,

1986,

the unit was

shutdown

from

1 percent

power

due to train

2 of Auxiliary Feedwater

(AFM) being declared

out of service

on the failure of a ARl flow control valve.

60

gag ] y

1981

August 13,

1986,

the reactor tripped from 53 percent

power

due to spurious

actua.ion

of the Pressur'.zer

Low Pressure

Chanrel

logic.

The actuation

was apparently

caused

by

a

lighting strike.

September

21,

1986,

the reactor

tripped

from

100 percent

power

due to personnel

error while performing

a Secondary

Plant Periodic test.

December

27,

1986,

the reactor

was manually tripped due to

a

loss

of turbine

governor oil

system

pressure

and

a

subsequent

rapid electrical

load decrease.

January

12,

1987,

the reactor tripped during

a rapid load

reduction

due to low pressurizer

pressure.

February

15,

1987,

the reactor tripped from 7 percent

power

due to personnel

error while performing adjustments

on the

turbine governor control oil system.

March 6,

1987,

the

reactor

was manually tripped

from 95

percent

power due to malfunctioning turbine governor.

2.

Unit

August 5,

1986, the reactor tripped from subcritical

power

.

levels

due to

a procedure error while personnel

performed

a

temporary

procedure

to

functionally

test

a

plant

modification

on

the

Turbine

Runback

arid

Power

Mismatch

systems.

August 21,

1986,

the- reactor

was

shutdown

to repair

an

Auxiliary Feedwater

Steam

Supply Valve.

August 23,

1986,

the reactor

was manually tripped from zero

percent

power but critical due to dropped

rods caused

by a

24 volt DC power

supply failure.

September

.6,

1986,

the

reactor

tripped

from

38 percent

power

due

to

a

short

in the light socket

for

the

4C

feedwater

isolation circuit.

September

16,

1986,

the unit conducted

a shutdown

due to

a

malfunction in the rod position indication system.

October 27,

1986,

the unit conducted

a

shutdown

due

to

missed

Post-Maintenance

testing

of containment

isolation

valves.

61

gUg ] p

1987

o.

November

10,

1986,

the

reactor

tripped

from

100

percent

power due to

a feedwater

flow control valve failing closed.

h.

January

6,

1987, reactor tripped from 100 percent

power,due

to one

channel

of over-power

delta

temperature

and

over

x,emperav.ure

del

a temperature

reactor trip channels

being

tripped

and receiving

a spike in another

channel.

i.

February 7,

1987,

the unit conducted

a

shutdown

to hot

s andby to meet Technical Specification

requirements

due to

a failure of an Intake Cooling Water

Pump shaft coupling.

h,.

Efiluen-

Summary for Turkey Point

1984

1985

1986

Gaseous

Effluents*

Fission

and Activation Gases

Iodine and Particulates

Tritium

1. 16E+3

3. 11E-2

'.

27E-1

1. 10E+3

8. 66E+3

4. 19E-3

4. 12E-2

3.85E-2

1.92E-2-

Tritium

Whole Body Oose

8. 90E+2

Liquid Effluents

Fission

and Activation Products

1.07E+2

9. OOE-1

4. 2E-1

8. 69E+2

5. 17E+2

1. 24E-2

mrem

In curies