ML17342A155

From kanterella
Jump to navigation Jump to search
Insp Repts 50-250/85-13 & 50-251/85-13 on 850408-0520. Violations Noted:Failure to Implement & Establish Procedures Per Tech Spec 6.8.1 & Failure to Implement Requirements of Criteria Xii,Xv & VII of App B to 10CFR50
ML17342A155
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 07/05/1985
From: Brewer D, Elrod S, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17342A153 List:
References
50-250-85-13, 50-251-85-13, IEB-79-18, NUDOCS 8508010782
Download: ML17342A155 (31)


See also: IR 05000250/1985013

Text

gp,8 RECgg

+

0

Cy

  • 0O

e ':.~

+n 0p*~+

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/85-13

and 50-251/85-13

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33101

Docket Nos.:

50-250

and 50-251

Facility Name:

Turkey Point

3 and

4

License Nos.:

DPR-31

and

DPR-41

Inspection

Conducted:

April 8 - May 20

1985

Inspectors:

T. A.

Pee

s

enior

Re ident Inspe

6r

D.

R. Br

esi ent Inspector

Approved by:

p)

n A. Elrod, Section Chief

Divi ion of Reactor Projects

D

S gned

Da

S>gned

D

e

igned

SUMMARY

Scope:

This routine,

unannounced

inspection entailed

361 direct inspection

hours

at the site, including 91 hours0.00105 days <br />0.0253 hours <br />1.50463e-4 weeks <br />3.46255e-5 months <br />

on backshift,

in the areas

of licensee

action

on

previous inspection findings, Inspection

and Enforcement Bulletin ( IEB) followup,

annual

and

monthly surveillance,

maintenance

observations

and reviews,

opera-

tional safety verification, engineered

safety

features

walkdown, plant events,

preparation for refueling and independent

inspection.

Results:

Violations

Failure to implement

procedures

as required

by Technical Specification (TS) 6.8. 1; failure to implement the requirements

of

10 CFR 50,

Appendix B, Criterion XII; failure to implement

the requirements

of

10 CFR 50,

Appendix B, Criterion

XV; failure to implement the

requirements

of

10 CFR 50,

Appendix B, Criterions VII; failure to establish

procedures

as

required

by

TS 6.8. 1;

and faiure to perform adequate

surveillance

per

10 CFR 50.55a

~ (g).

t

.PDR

8> 850710

9 -,< " OCR 05OOOPgo

pap

,

1

F

REPORT DETAILS

1.

Licensee

Employees

Contacted

C.

AC

J.

  • D

T.

  • K

B.

"H.

D.

E.

D.

J.

"R.

"R.

J.

W.

F.

R.

E.

M. Wethy, Vice President - Turkey Point

J.

Baker, Plant Manager - Nuclear

P. Mendieta,

Services

Manager

Nuclear

D. Grandage,

Operations

Superintendent

Nuclear

A. Finn, Operations

Supervisor

L. Jones,

Technical

Department

Supervisor

A. Abrishami, Inservice Testing

( IST) Supervisor

E. Hartman,

Inservice Inspection (ISI) Supervisor

Tomaszewski,

Plant Engineering

Supervisor

A. Suarez,

Technical

Department

Engineer

A. Chancy,

Corporate

Licensing

Arias, Regulation

and Compliance Supervisor

L. Teuteberg,

Regulation

and Compliance

Engineer

Hart, Regulation

and Compliance

Engineer

W. Kappes,

Maintenance

Superintendent

Nuclear

R. Williams, Assistant Superintendent,

Electrical Maint

H. Southworth, Electrical

Department

Engineer

A. Longtemps, Assistant

Superintendent,

Mechanical

Main

F. Hayes, Assistant Superintendent,

Instrument

and

Control (I&C) Maintenance

enance

tenance

V. A. Kaminskas,

Reactor Engineering Supervisor

R.

G.

Mende,

Reactor

Engineer

R.

E. Garrett,

Plant Security Supervisor

  • P.

W. Hughes,

Health Physics

(HP) Supervisor

and Acting Operations

Superintendent

R.

W.

RP

J.

J.

L.

H.

AM

R.

8W

J.

AD

AG

T.

p.

B.

M. Brown, Assi stant

HP Supervi sor

C.

Mi1 1er, Training Supervi sor

J.

Baum, Assistant Training Supervisor

M. Donis, Site Engineering Supervisor

M. Mobray, Site Mechanical

Engineer

C. Huenniger,

Start-up Superintendent

T. Young, Project Site Manager

J. Crisler, Quality Control

(QC) Supervisor

H. Reinhardt,

QC Inspector

Bladow, Quality Assurance

(QA) Inspector

E.

Moaba,

Performance

Enhancement

Program

(PEP)

Manager

W. Hasse,

Safety Engineering

Group Chairman

M. Vaux, Safety Engineering

Group

C. Grozan,

Licensing Engineer

Pace,

Licensing Engineer

C. LaPira, Fire Protection Supervisor

~Attended exit interview

Other

licensee

employees

contacted

included

construction

craftsmen,

engineers,

technicians,

operators,

mechanics,

electricians

and

security

force members.

2.

Exit Interview

The

inspection

scope

and

findings

were

summarized

during

management

interviews

held

throughout

the

reporting

period with the

Plant

Manager-

Nuclear

and selected

members of his staff.

The exit meeting

was

held

on

May 10,

1985,

with the

persons

noted

in

paragraph

1.

The areas

requiring management

attention

were

reviewed'he

six items identified as potential violations were:

Failure to meet the requirements

of TS 6.8. 1, with several

examples

as

follows: failure to implement

procedures

in the

area

of contaminant

exclusion

(paragraph

7), radiation work permit requirements

(paragraphs

9 and ll) and housekeeping

(paragraph

7), (250, 251/85-13-01).

Failure to meet

the

requirements

of

10 CFR 50,

Appendix

B, Criterion

XIII, Handling,

Storage

and

Shi pping

(paragr aphs

7

and

11),

(250,

251/85-13-02).

Failure to meet

the requirements

of

10 CFR 50,

Appendix

B, Criterion

XV,

Control

of

Nonconforming

Materials

(paragraph

ll),

(250,

251/85-13-03).

Failure to meet

the requirements

of

10 CFR 50,

Appendix

B, Criterion

VII, Packaging,

Shipping,

Receiving,

Storage

and Handling (paragraph

11), (250, 251/85-13"04).

Failure to implement maintenance

scheduling

and planning in accordance

with

ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

section

5. 1.6.3,

as

required

by

TS 6.8.1

(paragraph

7), (250, 251/85-13-05).

Failure to implement the requirements

of

10 CFR 50.55a.(g),

Inservice

Inspection

requirements

for Intake Cooling Water system (paragraph

6),

(250, 251/85-13-06).

Two unresolved

items

(URI) were identified:

adequacy

of actions

taken

as

required

by

IEB 79-18 (paragraph

5), this

was

presented

at the exit as

a

deviation but further inspection

was determined

to

be

necessary

(URI 250,

251/85-13-07);

and the validity of testing auxiliary feedwater

(AFW) check

valves

in

only

the

forward

flow direction

(paragraph

12),

(URI

250,

251/85-13-08).

One

inspector

followup

item (IFI) was identified:

followup corrective

actions for residual

heat

removal

(RHR) area

discrepancies

(paragraph

9),

(IFI 250, 251/85-13-10).

The licensee

acknowledged

the findings.

The licensee

did not identify as

proprietary any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Another exit was held with the Plant Manager-Nuclear

on

May 17,

1985,

and

several

items

were discussed

dealing with the operation

of spent

fuel pit

systems differently than

the safety analysis

reports

(SAR).

The facility

license requires that operation of systems different than

the analysis

and

assumptions

of the

safety

analysis

be

reviewed prior to operation

for

unreviewed

safety questions

per

10 CFR 50 '9.

Operation

of the

systems

without

the

review is

an

unresolved

item,

(paragraph

11).

This

was

presented

as

a violation at the exit but was changed

to

an Unresolved

Item

(URI 250, 251/85-13-09)

pending the completion of special

Inspection

Report

(250, 251/85-23).

The

licensee

acknowledged

the finding.

The licensee

did not identify as

proprietary

any of the materials

provided to or reviewed by the inspectors

during this inspection.

Licensee Action on Previous

Inspection

Findings (92702)

a.

Monthly update of Performance

Enhancement

Program

(PEP)

The

PEP

was

reviewed

to determine if commitments

were

being

met.

Status

was discussed

with the

PEP

Manager

and with other

members

of

management.

The facility upgrade

project

has

continued

pouring concrete

support

columns for the

new administration building .

The schedule for comple-

tion of the building including the third floor is the

end of December

1985,

but occupancy

is scheduled

for March 1986.

The

new

HP building

is progressing

toward its

May

1985 completion,

with move-in

scheduled

for July 1985.

The schedule

for the

PEP continues

to be met within acceptable

limits,

and all modifications

have

been cleared

by the Region.

b.

Previous

Inspection

Findings

(Closed) Violation 250, 251/84-11-01

(Closed) Violation 250/84-14-05

The inspectors

verified, through visual

observation,

that Administra-

tive

Procedure

(AP)

103.4,

In-Plant

Equipment

Clearance

Orders,

was

being properly and consistently

implemented.

The

use of caution

tags

has

been

implemented;

consequently,

personnel

no longer

use

"danger"

clearance

tags for unintended

purposes.

Indelible ink is used

on tags

exposed to the environment.

e'

(Closed)

IFI 250/84-18-05.

Fire pre-plans

have

been

implemented

and

are available in the control

room for use.

The pre-plans

are, routinely

utilized during fire drills by the shift supervisor (Plant Supervisor-

Nuclear [PSN]).

(Closed)

IFI 250,

251/83-05-01.

The

QC Inspector checklist for plant

work order

review has

been

substantially

incorporated into AP 190. 19,

Control of Maintenance

on Nuclear Safety

Related

and Fire Protection

Systems.

Those checklist

items

not included in the

procedure

are of

concern

to the

QC

Department

as

a

review organization

and

do

not

specifically concern

other plant personnel.

(Closed)

IFI

250,

251/83-24-02.

Administrative controls

have

been

placed

on the

use of lead

seals

in accordance

with AP 103.5,

section

8.4.5, Administrative Control of Locks, Valves and Switches.

The lead

seals

are

only applied

by

a Senior

Reactor

Operator

(SRO) qualified

individual

who

has

been

designated

by the

PSN,

since

a

SRO qualified

individual is

required

to verify proper

valve

position

prior to

attaching

the seal.

The

seal

crimping tool can

be issued only by the

PSN.

The proper

method of positioning the

AFM valves prior to seal

installation is specified

in the procedure.

Independent

verification

is required.

(Open) Violation 250/84-18-07.

On May 15,

1985,

the inspector

reviewed

the

estimated

critical conditions

(ECC) calculations

performed for

Unit 3 reactor

startup

No. 296.

The

ECC calculation

was

based

on

an

average

temperature

of 525 degrees

F;

however,

the actual

temperature

was

535

degr ees

F.

This discrepancy

introduced

an

unnecessary

error

into the

ECC calculation of approximately

100 per cent

millirho (pcm).

Further review revealed that the licensee

had developed

no criteria by

which to determine if the difference

between calculated

temperature

and

actual

temperature

could adversely

affect

the

ECC

accuracy.

As

a

corrective

action,

the

licensee

plans

to

incorporate

a

maximum

differential

temperature

limit of five degrees

F.

An

additional

discrepancy

was identified in that the

ECC calculation

sheet

did not

record the date

and time of the shutdown.

This omission

increases

the

possibility that

improper

shutdown

times

could

be

used

in

making

required calculations.

The

licensee

has

developed

and

implemented

a

computer

program that

prints

a reactivity poison report at the time of a reactor trip.

Data

is available for xenon,

samarium,

iodine and promethi um.

This informa-

tion will improve the

accuracy

of the

ECC calculations.

However, the

licensee

has yet to develop

a

mechanism

to alert

personnel

to the

possible

inaccuracies

in the computer

generated

poison reports that can

result

when the Digital Data Processing

System

(DDPS) computer

has

gone

off-line.

Personnel

are

aware that the computer generated

data

can

be

erroneous

after

a computer malfunction.

They

have

not

been

provided

with guidance

as

to

how

long the

poison

reports

remain

erroneous

following the event.

It is

up to individual discretion

as to whether

the computer

generated

data will be used.

This is unacceptable

because

it introduces

varying errors of unknown magnitude into the

ECC calcula-

tion process.

4.

Unresolved

Items

Unresolved

items

are matters

about

which more information is required to

determine

whether they are acceptable

or whether they may involve violations

or deviations.

Three unresolved

items were identified and are discussed

in

paragraphs

5,

11 and

12.

5

~

IE Bulletin (IEB) Followup (92703)

(Open)

IEB 79-18.

The

inspector

reviewed

the requirements

of IEB 79-18,

Audibility Problems

Encountered

on Evacuation

of Personnel

From High-Noise

Areas,

which was issued

on August 7,

1979.

The results of a previous review

of this bulletin were

documented

in Inspection

Reports

250,

251/84-11

of

March 1984.

In that report the inspector

expressed

concern that

some alarms

and

announcements

were

not

audible

in certain

high

noise

areas.

The

licensee

agreed

to supply additional

information concerning

Plant

Change/

Modification (PC/M) 80-01 which was installed in January

1980 specifically

to address

the

IEB requirements.

The potential failure to fully implement

IEB 79-18 is

an

Unresolved

Item

(250, 251/85-13-07).

6.

Monthly and Annual Surveillance

Observation

(61726/61700)

The inspectors

observed

TS required surveillance

testing

and verified:

that

the test procedure

conformed to the requirements

of the TS; that testing

was

performed

in accordance

with adequate

procedures;

that test instrumentation

was calibrated; that limiting conditions for operation

(LCO) were met; that

test

results

met

acceptance

criteria

requirements

and

were

reviewed

by

personnel

other

than

the individual directing the test;

that deficiencies

were identified,

as appropriate,

and that any deficiencies identified during

the testing

were properly reviewed

and resolved

by management

personnel;

and

that

system

restoration

was

adequate.

For completed tests,

the inspector

veri.fied that testing

frequencies

were

met

and tests

were

performed

by

qualified individuals.

The inspectors

witnessed/reviewed

portions of the following test activities:

Daily Operability Verification of the

Power

Range Nuclear

Instrument

System

Emergency Diesel Generator

(EDG) Operability. Test

High Head Safety Injection

Pump Monthly Operability Test

Component

Cooling Water System Test

Rod Position Indication and Axial Flux Alarm Calibration

g

1

On

May 6,

1985,

a portion of the Unit 3 intake cooling water (ICW) system

piping

was disassembled

for inspection.

The concrete

lining was

in fair

condition with only the joints in need of repair.

The bolts

on the Unit 3

piping

were

being

replaced

due

to

age

and

cor rosion.

During this

inspection,

the

licensee

noted that

the

concrete

thrust

braces

for the

circulating water

pumps,

located in the

same area,

were

damaged

and began

an

inspection

and repair program.

The inspector

observed

that the bolting

on

the Unit 4

ICW piping was

more deteriorated

than Unit 3's

and notified the

licensee.

This

degraded

condition

was

not

licensee

identified

because

during

the ten year hydrostatic test

in

May 1984,

the section

of piping

which runs through the circulating water intake wells was considered

"buried

piping"; therefore,

no inspection for structural

distress

or corrosion

had

been

conducted

as required.

This is

a Violation (250,

251/85-13-06)

as

stated

below.

10 CFR 50.55a.(g)

requires

ASME Code testing for Class

3 components.

ASME

Code,

Section

XI (1974 Edition), article

IWD-1000 applies

the

requirements

of Section

IWD to Class

3 pressure-retaining

components.

IWD-2000 requires

inspection

of the

components

each inspection'nterval.

IWD-2600 requires

the visual examination to be conducted of the components

during system tests

for evidence of structural distress

or corrosion.

Contrary to the

above,

during the system inservice testing for the Class

3

ICW system

on Unit 3 in December

1983

and

on Unit 4 in

May 1984,

visual

inspections

for structural

di stress

or corrosion

were

not

conducted

for

piping

and

bolted

connections

which were

located

between

the

ICW

pump

discharge

check valve and the header isolation valves.

Maintenance

Observation

(62703

and 62700)

Station maintenance activities of safety-related

systems

and components

were

observed/reviewed

to ascertain

that they were

conducted

in accordance

with

approved

procedures,

regulatory guides,

industry codes

and standards

and in

conformance with TS.

The following items

were

considered

during this

review,

as appropriate:

LCOs

were

met while

components

or

systems

were

removed

from service;

approvals

were

obtained

prior to initiating the

work; activities

were

accomplished

using

approved

procedures

and

were

inspected

as

applicable;

procedures

used

were

adequate

to control

the activity; troubleshooting

activities were controlled,

and the repair record accurately reflected

what

actually took place;

functional testing

and/or calibrations

were performed

prior to returning

components

or systems

to service; quality'control records

were maintained; activities were

accompl.,i shed

by qualified personnel;

parts

and materials

used

were

properly certified;

radiological

controls

were

implemented;

gC

holdpoints

were

established

where

required

and

were

observed;

fire prevention

controls

were

implemented;

outside

contractor

force activities were controlled in accordance

with the approved

gA program;

and housekeeping

was actively pursued.

The following maintenance activities were observed

and/or reviewed:

RHR pump repair

Reactor vessel

head

stud removal

Hydrostatic testing of

RHR motor operated

(MOV) suction valves,

MOV-750 and

MOV-751

Reactor

upper internals split pin replacement

ICW flange bolt replacement

EDG preventive

maintenance

Unit 3 4160 volt bus breaker

maintenance

The inspectors

observed

the detensioning

of the reactor vessel

head closure

studs

in accordance

with Maintenance

Procedure

(MP) 1407.7.

The procedure

requires that tape

be placed

over the holes in the studs to preclude foreign

material

from entering.

The

work site for the

removal

of the

3A

RHR

pump

was

inspected.

Open

flanges in the safety related

component

cooling water

(CCW) supply to the

pump were

not protected

from foreign material

contaminants,

as required

by

section

8. 1. 1.5 of AP 0190. 10

when work was

not in progress

at the

work

site.

The failure to protect safety-related

'systems

and

components

from foreign

material

contamination

discussed

in

the

previous

two

paragraphs

is

a

Violation

(250,

251/85-13-01,

item a).

This violation is

a

repeat

of

previous violations as noted:

Violation 3.c of Inspection

Reports

250/84-34

and

251/84-35;

and

Violation 2.b

of Inspection

Reports

250/84-22

and

251/84-23.

Maintenance

work areas

were routinely observed

in the Units

3 and

4 cask

wash areas

and

on May 8, the Unit 3 new fuel storage

area.

In each location

an accumulation of waste

and debris

was not removed at the end of the work

shift

and

equipment

was

not properly

stored

as

requi red

by

AP 103. 11,

Housekeeping.

The failure to maintain housekeeping

standards

is

a Violation

(2SO,

251/85-13-01,

item c).

This violation is

a

repeat

of

a

previous

violation:

Violation 2.c of Inspection

Reports

2SO/84-22

and 251/84-23.

On

May 9,

1985,

during repair of the Unit 3

CCW system,

a frayed sling was

used

to hoist

a section of piping into position.

Quality Procedure

(QP)

13. 1,

section

5.4.2,

which

implements

Topical

Quality

Report

13.0

and

Criterion XIII of 10 CFR 50, Appendix B, specifies that frayed slings shall

not be used.

This

QP was not further implemented

on site.

The failure to

implement

Criterion XIII of

10 CFR'0,

Appendix

B

is

Violation

(250,

251/85-13-02,

item c) .

An additional

example of thi s violation is discussed

in paragraph

11.

On April 25,

1985, the

A emergency diesel

generator

was

removed

from service

at

a time when it was required

under

TS 3.7.2.b.

The resulting violation is

discussed

in paragraph

12.

8.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room operators

(CRO),

observed

shift

tur novers

and

confirmed operability of instrumentation.

The

inspectors

verified the operability of selected

emergency

systems,

reviewed

tagout

records,

verified compliance with TS limiting conditions of operation

and

verified the return to service of affected

components.

The

inspectors,

by observation

and direct

interviews verified that

the

physical security plan was being implemented

in accordance

with the station

security plan.

The inspectors

verified that maintenance

work orders

had been

submitted

as

required

and that followup and prioritization of work was accomplished.

The

inspectors

observed

plant

housekeeping/cleanliness

conditions

and

verified implementation of radiation protection control.

Tour s of the intake str ucture

and emergency diesel, auxiliary, control

and

turbine buildings

were

conducted

to observe

plant

equipment

conditions

including potential fire hazards,

fluid leaks

and excessive

vibrations.

The

inspectors

walked

down accessible

portions of the following safety-

related

systems

on Unit 3

and Unit 4 to verify operability

and

proper

valve/switch alignment:

Refueling Water Storage

Residual

Heat

Removal

Emergency Diesel

Generators

Auxiliary Feedwater

Pumps

Intake Cooling Water

4160 volt and

480 volt switchgear

Rod Position Indication Cabinets

Control

Room Vertical Panels

Nuclear Instrumentation

Drawers

High Head Safety Injection

Spent

Fuel Pit Cooling

On Nay 14,

1985, during

a tour of the Unit 3 charging

pump room,

an operator

was observed

to not meet the anti-contamination

clothing requirements

of

RWP

85-014.

For general

area

entry,

the

RWP required

that

shoe

covers

and

gloves

be worn.

The operator

entered

the

room without wearing

any gloves.

Health

Physics

Administrative

(HPA)

Procedure

0-HPA 002

requires

that

personnel

read

and

comply with all instructions,

requirements

and

remarks

listed

on an applicable

RWP.

Failure to comply with posted

RWP requi rements

is Violation (250, 251/85-13-01,

item b.(2)).

An additional

example of this

violation is discussed

in paragraph

11.

9.

Engineered

Safety Features

Walkdown (71710)

The inspector s verified the operability of the Units 3 and

4

RHR systems

by

performing

a complete

walkdown of the accessible

portions of the

systems.

The following items

were specifically reviewed

and/or

observed

as

appro-

priate:

a.

that the licensee's

system lineup procedures

matched plant drawings

and

the as-built configuration;

b.

that the

equipment

conditions

were satisfactory

and

items that might

degrade

performance

were identified and evaluated,

e.g.,

hangers

and

supports

were operable,

housekeeping

was adequate;

c.

that instrumentation

was properly

valved in and functioning

and that

calibration dates

were not exceeded;

d.

that

valves

were

in proper position,

breaker

alignment

was correct,

power was available,

and valves were locked/lockwired

as required;

e.

local

and

remote position indication

was

compared,

and remote instru-

mentation

was functional;

and

f.

breakers

and

instrumentation

cabinets

were

inspected

to verify that

they were free of damage

and interference.

The following discrepancies

were identified and initial licensee corrective

actions

have

been

taken:

RHR valve 4-758 air line was crushed;

RHR

sumps

with extra plastic

hoses;

4B

RHR

pump

mechanical

snubber

had

a missing

cotter pin; Unit 4

RHR heat

exchanger

support

had

one

loose bolt;

wooden

wedges

were found between

CCW headers;

and solidified mortar was found in a

sump.

Close

out of these

items will occur at

a later walkdown (IFI 250,

251/85-13-10).

Within this area,

no violations or deviations

were iden'tified.

10.

Plant Events

(93702)

An independent

review was conducted of the following events.

On April 11,

1985,

at

3:45 a.m.

a Unit 4 pressurizer

steam

sample

containment isolation valve did not close

on

command,

and

a report of

loss of containment integrity was prepared

since the

TS have

no action-

time allowed.

A leak at

a swagelok connection outside the containment

between

the

containment

and

the

outside

automatic

isolation

valve

caused

the attempt to close the inside automatic valve from the control

room;

however,

dual

indication indicating 'intermediate

position

was

received.

A containment

entry

was

made

and

the

inside

valve

was

verified to close

when the fuses

were pulled.

The inside manual

valve

was also closed

and the leak stopped at 4:30 a.m.

The leaking fitting

was replaced

and the inside valve will remain closed.

10

On April 25,

1985,

at

1:00 a.m.

the

A

EDG was

removed

from service

which placed Unit 4 in a

TS action

statement

which was

not recognized

prior to entering the condition.

Further discussion

is in paragraph

12

on Independent

Inspection.

The action statement

was cleared within the

time allowed.

On April 29,

1985,

at

2:45 p.m.

the

Unit 3

A bus

was

de-energized

during replacement

of a cover

on the Unit 3 main generator

relay panel.

Control

room lighting

was lost

as

was annunciator

power-with annun-

ciator

power restored

in

20

seconds

and full lighting within

10

minutes.

A lockout of the

main

transformer

occurred

and", with the

unit's start-up transformer

and

3B bus undergoing

maintenance,

the only

source

of power to Unit 3

was the

A EDG which

had auto-started.

The

reactor

core

had

been

off-loaded,

and

the

SFP

temperature

was

137

degrees

F with an increase

of five degrees

F per hour predicted without

cooling.

The

SFP cooling

pump did not start since it is not connected

to the safety bus.

At 4:50 p.m.

an Unusual

Event (UE) was declared

due

to the length of time required to repower

Unit 3 from normal

sources.

The

SFP cooling

pump was started after the non-safety

bus was loaded

on

the

EDG around 5:00 p.m.

At 8:20 p.m.

power to the

3A bus

was fed from

the Unit 4 start-up transformer

through

a maintenance

feed connection.

At 2:35 a.m.

power from the Unit 3 start-up transformer

was restored to

the

3A and

3B buses

and the

UE terminated.

On May 1, the inspector verified that:

the Unit 3

SFP cooling

pump was

aligned via the

lower suction path which allows about

900 gallons

per

minute (gpm) instead of the 2200

gpm when aligned via the upper suction

path;

the

SFP

temperature

of 134 degrees

F was representative

of all

surface points;

CCW flow was being verified to be less

than

2250 gpm-

being

2100

gpm

instead

of the

2800

gpm

design

flow;

SFP

surface

radiation

readings

were

120 mi llirem per

hour

(mrem/hr.)

and at five

feet

above

the

SFP,

without fuel

movement

on

the

bridge

crane,

the

readings

were

10 to

15 mrem/hr.;

and

make-up

to the

SFP

was

2400 to

3000 gallons per day.

On

May 2,

1985,

at

12: 19 a.m.

the Unit 3

CRO was

removing the

3A bus

from service

and the

A EDG auto-started.

The procedure

which was in

use

had

an

error

as it called for the

disabling

of the

3B

EDG

sequencer.

The A EDG was stopped,

and the

3A bus properly removed

from

service.

The

SFP temperature

reached

-153 degrees

F in four hours while

the

SFP cooling was not in service.

On

May 15,

1985,

at 1:07 p.m.

a construction

worker

bumped

a relay in

the Unit 4 safeguards

relay rack while working one to two inches

away

preparing

to pull

a cable.

This relay actuation initiated

a turbine

trip on "hi-hi steam

generator

level" in the

C steam

generator

(SG)

which secured

both

main feedwater

(MFW)

pumps

and isolated

the

C SG.

All

systems

responded

normally.

Pressurizer

pressure

reduced

to

1990 psig.

The unit returned to operation that evening.

On

May 17,

1985,

an

UE was decl ar ed at 12: 10 p.m.

when Unit 4 tripped

due to

a loss of off-site power.

The

B

MFM pump tripped

when

the

switchyard

de-energized

due

to

a fire, North of Miami, affecting

a

500

kV transmission

line.

The

C

SG low level coincident with feedwater

flow less

than

steam

flow tripped

the

reactor

which tripped

the

turbine.

Pressurizer

pressure

reached

2325 psig.

Both

EDGs

auto-

started

and

natural

circulation

was

established;

the

6B feedwater

safety valve lifted, and the

main

steam isolation valves

closed.

All

other

systems

responded

normally.

At 2:07 p.m.

the

UE terminated

as

off-site

power

was

restored

and

forced

reactor

circulation

was

initiated for Unit 4.

The Unit 3

UE terminated at 2:23 p.m.

No violations or deviations

were identified in this section.

11.

Preparation

For/And Refueling (60705/60710)

a,

On April 29,

1985,

the inspector

observed

the receipt

inspection of

hafnium

burnable

poison

inserts

in the

Unit 3

new fuel

room.

The

receipt inspection

was performed in accordance

with Operating

Procedure

(OP)

16009. 11,

On-Site

Unpacking,

Inspection

and

Manual

Loading of

Hafnium

Vessel

Flux

Depression

Assemblies.

The

licensee's

Quality

Assurance

Topical

Report

incorporates

the

requirements

of

ANSI

N45.2.2-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.2-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

Packaging,

Shipping; Receiving,

Storage

and Handling of

Items

for Nuclear

Power

Plants.

QP 7. 1

which

implements

Topical

Quality

Requirements

and

10 CFR 50,

Appendix B,

Criterion VII,

specifies that receipt inspections

of nuclear fuel will be performed in

accordance

with site specific procedures.

The licensee

considers

fuel

inserts

and rod control cluster

(RCC) assemblies

to also

be covered

by

specific

receipt

inspections

and

has

developed

the

following

procedures:

OP 16009.1

OP 16009.6

OP 16009. 10

OP 16009.11

Receipt

and Handling of New Fuel Containers

On-Site Unpacking,

Inspection

and Manual

Loading

of Burnable

Poison

Rod Assemblies

On-Site Unpacking,

Inspection

and Manual

Loading

of Rod Control Cluster Assemblies

On-Site Unpacking,

Inspection

and Manual

Loading

of Hafnium Vessel

Flux Depression

Assemblies

A review of OP 16009. 11 revealed that it inadequate

implemented

TQR 7.0

and

QP

7. 1

requirements

which

inappropriate

ANSI

N45.2.2-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.2-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

requirements

in that:

( 1)

The receipt inspection did not verify that the purchased

material

conformed

to the

procurement

documents.

The purchase

documents

available

during

the receipt

inspection

did not specify

which

quality standards

were required to

be

met

by the vendor.

A QA

product certification supplied

by the vendor could not be verified

to conform with prearranged

mutually acceptable

purchase criteria

(ANSI N45.2.2-1972,

section

5 '.2.2).

12

(2)

Specific

guidance

was

not

available

with which

the

receipt

inspector

could

determine

that

damage

had

not occurred

to the

inserts

and

that

the

inserts

were

sufficiently clean

(ANSI

N45.2.2-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.2-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

sections

5.2.2.7

and 5.2.2.8).

(3)

A preliminary visual inspection of the shipping containers

was not

required.

Criteria for determining that

damage

had not occurred

due to fire, exposure,

rough handling

and tie

down failure were

not procedurally

incorporated.

The preliminary inspection prior

to

unpacking

was

not

documented

(ANSI

N45.2.2-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.2-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

section

5.2.1).

10 CFR 50, Appendix B, Criterion VII, as

implemented

by the

FPL Topical

Quality Assurance

Report,

Revision 6,

TQR 7.0,

Control of Purchased

Items

and

Services,

requires

that

measures

shall

be

established

to

assure

that

purchased

material

conforms

to

the

requirements

of

applicable

procurement

documents.

The

Quality

Assurance

Program

incorporates

the

requirements

of ANSI N45.2.2-1972.

The failure to

meet

the

requirements

of

ANSI

N45.2.2-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.2-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.

is

a

Violation

(250,

251/85-13-04).

During the receipt

inspection

a

QC Inspector

observed

a

condit,ion

adverse

to quality,

and

he did not ensure that corrective actions were

implemented

in

accordance

with

approved

procedures.

One

burnable

poison

insert

was

inadvertently

contaminated

with

grease

from

an

overhead hoist and consequently

was not initially acceptable

for use in

the reactor core.

The nonconformance

was not documented

as required

by

AP 190. 13, Corrective Action for Conditions

Adverse to Quality.

Any

subsequent

measures

used to clean the insert or subsequent

reinspection

of the insert

were

not documented.

The receipt

inspection

documen-

tation did not mention the discrepancy.

The insert

was

placed

in the

spent fuel pool without evaluation.

The failure to implement corrective actions for conditions

adverse

to

quality in

accordance

with approved

procedures

is

a violation of

10 CFR 50,

Appendix B,

Criterion XV,

as

implemented

by

FPL Topical

Quality

Assurance

Report,

Revision 6,

TQR 15.0,

Nonconforming

Materials,

Parts

or

Components,

QP 15.2

and

AP 190. 13

(250,

, 251/85-13"03).

During

poison

insert

handling

the

inspector

observed

the

use, of

handling

equipment

which did not meet the requirements

of 10 CFR 50,

Appendix B,

Criterion XIII, as

implemented

by

FPL

Topical

Quality

Assurance

Report,

Revision 6,

TQR 13.0, Handling, Storage

and Shipping;

QP 13. 1,

and ANSI N45.2.2-1972,

Packaging,

Shipping,

Receiving,

Storage

and

Handling of Items for Nuclear

Power

Plants.

QP 13. 1,

section

5.4.2,

Inspection of Equipment,

requires

that, prior to use,

handling

equipment

be

inspected

for acceptability.

ANSI N45.2.2 requires that

equipment

not be used if it fails to meet manufacturer s specifications,

if it is frayed or deteriorated,

or if it contains

contaminants

that

would be detrimental

to the material

being handled.

'P(

13

On April 29,

1985,

a nylon rope was knotted

and fashioned into a sling

and

used to hoist hafnium burnable

poison assemblies.

The knotted rope

did not meet

any manufacturer's

specifications.

Factory manufactured

slings were available for use

and were not used.

On April 29,

1985,

an electric hoist in the Unit 3

new fuel

storage

room

was

used

to lift hafnium burnable

poison

assemblies.

The hoist

contained

contaminants

in the form of grease

which dripped

on

a poison

assembly.

Failure to meet

equipment

handling

requirements

is

a Violation (250,

251/85-13-02,

items

a and b).

An additional

instance of this violation

is discussed

in paragraph

8.

On April 30,

1985,

the inspector

observed

the change

out of

RCC in the

Unit 3

SFP.

Personnel

were

required

to

comply with the clothing

protection criteria of

RWP 85-500 which specified that

persons

using

telephone

headsets

wear

a full hood.

The full hood provides better

anti-contamination

protection

than the more frequently

used

cap because

it covers the entire

back of the neck.

This is the location where the

telephone

headset

cord tends to rub.

The

HP Department

was

supplying

continuous

coverage

and assistance

for the

RCC

change

out evolution.

The inspector

observed

one person wearing

a telephone

headset

who was

not wearing

a full hood.

The

HP technician

on the

scene,

like the

telephone talker, did not realize that the

RWP required

a full hood.

HPA

procedure

O-HPA-002,

Requirements

for Entry

and

Work in

RCA,

requires

in section 5.2. 15 that all personnel

working in an area

where

a

RWP

is

required

shall

read

and

comply with all

instructions,

requirements

and remarks listed

on the

RWP.

Failure

to

comply

with

RWP

requirements

is

a

Violation

(250,

251/85-13-01,

item b.(1)).

An additional

example of this violation is

discussed

in paragraph

9.

In Inspection

Reports

250, 251/84-18

and 250/84-35

and 251/84-36,

which

covered the

May and

November

1984 periods,

respectively,

the inspectors

addressed

several

aspects

of the operation of SFP

systems that did not

correspond

to that, described

in the

SAR.

The modification of these

systems

had

not received

a

review for

unreviewed

safety

question

determinat'ion

prior to

the

modification

of the

system

from that

described

in the

SAR.

The facility operating

licenses

permit

the

modification of systems

only after

a

review

has

been

conducted

in

accordance

with

10 CFR 50.59.

As

several

of

these

reviews

for

unreviewed safety question determination

have yet to be

made

and as the

systems

are

being

operated differently than

as described

in the

SAR,

these

items constitute

an Unresolved

Item (250, 251/85-13-09).

A

%I

I

1

Independent

Inspection

(92706)

During the report

period the inspectors

routinely attended

meetings with

licensee

management

and monitored shift turnovers

between

PSN, shift foreman

(Nuclear Match Engineers

[NME]), and

CROs.

These

meetings

provided

a daily

status of plant operating

and testing activities in progress

as well

as

a

discussion

of significant

problems

or incidents.

Based

on these

discus-

sions,

the

inspectors

reviewed

potential

problem

areas

to

independently

assess:

their importance to safety;

the proposed

solutions;

improvement

and

progress;

and

adequacy

of corrective actions.

The inspector's

reviews of

these

matters

were

not restricted

to

the

defined

inspection

program.

Independent

inspection efforts were conducted

in the following areas:

Estimated Critical Conditions Calculations

Fire Drills

Auxiliary Feedwater

Check Valve Testing

Reactor

Vessel

Head Stud Reference

Transition Temperature

Residual

Heat

Removal

Suction Valve Testing

On April 25,

1985, at approximately

1:00 a.m.

the licensee

placed the

A EDG

out of service to perform routine preventive

maintenance.

Unit 4 was oper-

ating at

100 percent

power.

Unit 3 was in refueling shutdown with all fuel

removed

from the vessel.

The

3B 4160 volt electrical

bus

was de-energized

to facilitate routine

breaker

inspections;

consequently,

the

3B safety

injection

pump was inoperable.

The

licensee

determined

that

three

of four safety

injection

pumps

were

operable

as

allowed

by

TS 3.4. l.b.2.

The

PSN's

log contained

an

entry

stating that

two safety injection

pumps would remain operable

in the event

of a blackout.

This entry was incorrect.

On

a loss of offsite power with

the

A EDG out of service,

the

B

EDG would be the sole

source of emergency

power.

The

B

EDG would normally supply power to the Unit 3 and Unit 4 4160

volt B buses.

However, with the

3B 4160 volt bus de-energized,

only the

4B

4160 volt bus

would receive

emergency

power.

Consequently

only the

4B

safety

injection

pump would

be available.

The

3A and

4A pumps

would be

unavailable

due to loss

of offsite

power in conjunction with the

A EDG

clearance.

The

3B pump would be unavailable

due to the de-energized

bus.

At approximately 4:30 a.m. the licensee

determined that

a potential

problem

existed concerning

removal of the

A EDG from service with the

3B 4160 volt

bus de-energized.

A decision

was

made to restore

the

A EDG to service

as

soon

as

possible.

The

EDG

was

declared

in service

at

7:30 a.m.

after

successfully

completing

an operability run.

The licensee

was concerned that

the

3A and

4A safety injection pumps might not be considered

operable

under

TS 3.0.2.

While this

TS specifies

that

components

need

not

be considered

inoperable

due to the inoperability of their emergency

power supplies, it

also requires

that

redundant

components

be operable

with their

normal

or

emergency

power supplies

available.

The

concern

was that

the

3B safety

injection

pump was redundant

to the other

pumps

and its normal

and emergency

15

power supplies

were not available.

Afte~ restoring

the

A EDG to service,

the licensee

referred

the matter to the licensing department

for clarifi-

cation.

TS 3.7.2.b

states

that

power operation

may continue if one

EOG is out of

service

provided that the

remaining

EDG is tested daily and its associated

engineered

safety features

are operable.

If one

EDG is inoperable

and the

other

EOG's engineered

safety features

are not fully operable

then

TS 3.0. 1

applies

and the affected reactor

must

be shut

down within seven

hours.

The

licensee

did not initially realize

that

TS 3.7.2.b

applied

to the

EDG/safety

injection

pump

problem

of April 25.

However,

the

licensee

restored

the

A EDG to operation

before

exceeding

the

seven

hour

shutdown

limit imposed

by

TS 3.0. 1

through

TS 3.7.2.b;

consequently,

neither

TS 3.7.2.b nor TS 3.0. 1 were violated.

The

PSN

was

implementing

a preplanned

maintenance

department activity when

he authorized

the removal of the

A EDG from service.

The clearance

tags

had

been

prepared well in advance

by other

CROs.

Maintenance

personnel

had

been

. selected

for the task

and were waiting to begin their work.

The

B

EDG was

tested

to verify that it was

operable

subsequent

to receiving

routine

maintenance

of the type planned for the

A EDG.

Shortly after the

B

EDG was

declared

operable,

the

A EDG

was

removed

from service.

Apparently,

the

ability to

remove

the

B

EOG from service without creating

a

TS limiting

condition of operation resulted

in an inadequate

analysis

of the effect of

removing the

A EDG from service.

TS 6.8. 1 requires

that written procedures

and administrative policies

be

established,

implemented

and maintained that meet or exceed 'the requirements

and recommendations

of sections

5. 1 and 5.3 of ANSI 18.7-1972

and Appendix A

of USNRC Regulatory Guide 1.33.

ANSI N18.7-1972,

section

5. 1.6.3,

Scheduling

of Maintenance,

requires that

maintenance

be

scheduled

and

planned

so

as not to jeopardize

the safety of

the reactor.

Planning

shall

consider

the possible

safety

consequences

of

concurrent

or

sequential

maintenance,

testing

or operating

activities.

Equipment required to be operable for the

mode in which the reactor exists

shall

be available,

and

maintenance

shall

be performed in manner

such that

the license limits are not violated.

The failure to preplan

a maintenance

activity so

as

not to jeopardize

a

safety

system

is

contrary

to

the

requirements

of

ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.,

section

5. 1 and fails to meet the requirements

of TS 6.8. 1; hence, this is

a

Violation (250, 251/85-13-05).

An inspection

was conducted of actions

taken

by the licensee

to address

the

significant safety concern

noted in Inspection

and

Enforcement

Information Notice 84-06, which discussed

a problem of steam binding of the

AFW pumps at

the

H.

B. Robinson Plant.

Other more detailed notification of this problem

16

was received

by the licensee

from the Institute of Nuclear

Power Operations

(INPO).

The inspector

noted that

no

immediate

problem existed

as neither

the suction

nor discharge

piping of any of the three

AFW pumps

was hot to

the

touch during

several

walkdowns

during

the

inspection

period.

The

licensee

has trained the operators

on this problem and procedural

guidelines

are to be provided by June

1,

1985.

The monitoring of pipe temperatures

by

touch will begin

on June

1,

on

a once per shift basis.

It is noted that the

three

AFW pumps for the

two units

are

self-venting

due

to

a

continuous

recirculation

path

from the

pump discharge

through the

lube oil cooler to

the

condensate

storage

tank.

The outlet

valves

downstream

of the

check

valves are normally-closed

globe valves.

The testing of the check valves

as

part of the

ASME Code,

Section XI; program is to assure

that the

pump

can

put out full flow through

the

check

valves.

The

adequacy

of this test

method to support

that

the

check

valve will perform its

intended

check

function (restriction

of backflow) is

an

Unresolved

Item pending further

discussions

with the Region

and

NRR (URI 250, 251/85-13-08).

No violations or deviations

were identified.