LER-1979-001, /03L-0 on 790118:valve V-14-35 Failed to Open Completely During Routine Isolation Condenser Valve Operability Test.Caused by Dirty Torque Limit Switch Contacts,Which Were Subsequently Cleaned & Burnished |
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When the test initiating signal was applied, the valve opened approximately 104 and then stopped.
Valve V-14-35 is D.C.
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The cause of this occurrence was dirty torque limit switch contacts 1
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The contacts were cleaned and burnished and the valve test was successfully completed.
The use of an 'ohm meter to check the torque limit switch contacts will be incorporated into the P.H.
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ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY 3
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Jersey Central Power & Ught Company Madison Avenue at Punch Bowl Road Morristown, New Jersey 07960 (201) 455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/79-1/3L"0 Report Date February 15, 1979 Occurrence Date January 18, 1979 Identification of Occurrence Violation of the Technical Specifications, paragraph 3.8:A when valve V-14-35 failed to operate as required during a routine valve operability test.
This event is considered.to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b.2.
Condit'ions Prior. to Occurrence The plant was in a shutdown condition for maintenance.
Plant parameters at the time of the occurrence were:
Reactor pressure 145 psig Recirculation flow - 3.1 x 104 gpm Stack Gas
- - 90 ttCi/sec Description of Occurrence On Thursday, January 18, 1979, at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, while performing the isolation condenser valve operability test, valve V-14-35 failed to open completely.
Upon an initiation signal, valve V-14-35 opened approximately
- 100, and then stopped.
Apparent Cause of Occurrence Component failure was the cause of this event.
Valve V-14-35 is D.C. motor operated and is fitted with a double torque limit switch.
Jersey Central Power Light Company is a Memper of the General Pu inc Utilities System
Reportable Occurrence No. 50-219/79"1/3L-0 February 15, 1979 Page 2
During approximately the first lOR of travel in the opening
- mode, the torque limit switch is bypassed by the use of a shorting switch because of the high torque required to unseat the valve.
After 10'f travel, the torque limit switch controls valve travel.
Upon failure of valve V-14-35, investigation revealed that the contacts on the torque limit switch were dirty; thus creating an opening in the motor circuit after approximately 10'f valve travel.
Anal sis of Occurrence The safety significance of this event is considered to be minimal since during this period the "A" isolation condenser was available for operation.
If one isolation condenser is found to be inoperable, there is no immediate threat to the heat removal capability for the reactor and reactor operation.
The purpose of the isolation condenser is to depressurize the reactor and to remove reactor decay heat in the event that the main condenser is unavailable as a heat sink and heat removal systems which required AC power for operation are not available.
Corrective Action
The torque limit switch contacts were cleaned with a suitable solvent type cleaner and burnishi'ng, tool.
The use of an ohm meter to check the torque limit 'switch contacts will be incorporated into the preventative maintenance program.
Valve V-14-35 was then cycled three times successfully, meeting all the requirements of the isolation condenser valve operability test.
Failure Data Manufacturer:
Limitorque Corporation Part No.
SMB-00 Type SMB-2
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| 05000219/LER-1979-001-03, /03L-0 on 790118:valve V-14-35 Failed to Open Completely During Routine Isolation Condenser Valve Operability Test.Caused by Dirty Torque Limit Switch Contacts,Which Were Subsequently Cleaned & Burnished | /03L-0 on 790118:valve V-14-35 Failed to Open Completely During Routine Isolation Condenser Valve Operability Test.Caused by Dirty Torque Limit Switch Contacts,Which Were Subsequently Cleaned & Burnished | | | 05000219/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000219/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000219/LER-1979-002-03, /03L-0 on 790206:while Performing Isolation Condenser Automatic Actuation Test & calibr,RE-15B Trip Point Was Less Conservative than Tech Spec Std.Caused by RE-15B Switch Not Set at 1068 Psig valve.RE-15B Reset | /03L-0 on 790206:while Performing Isolation Condenser Automatic Actuation Test & calibr,RE-15B Trip Point Was Less Conservative than Tech Spec Std.Caused by RE-15B Switch Not Set at 1068 Psig valve.RE-15B Reset | | | 05000219/LER-1979-010-03, /03L-0 on 790417:leak of Isotopic Concentration Noticed Near Inside Penetration within Pipe Tunnel.Caused by Component Failure.Drywell Equipment Drain Tank Line Rerouted to Prevent Further Leakage | /03L-0 on 790417:leak of Isotopic Concentration Noticed Near Inside Penetration within Pipe Tunnel.Caused by Component Failure.Drywell Equipment Drain Tank Line Rerouted to Prevent Further Leakage | | | 05000219/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000219/LER-1979-011-03, /03L-0 on 790419:core Spray Pump NZO1A in Sys 1 Failed to Start Upon Initiation Signal.Caused by Fuse Failure.Fuse Replaced & Pump Test Successfully Completed | /03L-0 on 790419:core Spray Pump NZO1A in Sys 1 Failed to Start Upon Initiation Signal.Caused by Fuse Failure.Fuse Replaced & Pump Test Successfully Completed | | | 05000219/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000219/LER-1979-012-03, /03L-0 on 790419:oxygen Level in Suppression Chamber Atmosphere Was Greater than 5%.Caused by Sensitivity of Sampling Sys & Position of Sample Flow Control Valve. Oxygen Analyzer Recalibr;Level Now Below 5% | /03L-0 on 790419:oxygen Level in Suppression Chamber Atmosphere Was Greater than 5%.Caused by Sensitivity of Sampling Sys & Position of Sample Flow Control Valve. Oxygen Analyzer Recalibr;Level Now Below 5% | | | 05000219/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000219/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000219/LER-1979-016-03, /03L-0 on 790506:during Surveillance Test, Isolator Condenser Isolation Sensor Setpoint a Measured Two Inches of Excess Water.Caused by Instrument Drift in Excess of Design Accuracy.Switch Was Recalibr & Put Back in Svc | /03L-0 on 790506:during Surveillance Test, Isolator Condenser Isolation Sensor Setpoint a Measured Two Inches of Excess Water.Caused by Instrument Drift in Excess of Design Accuracy.Switch Was Recalibr & Put Back in Svc | | | 05000219/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000219/LER-1979-017-03, /03L-0 on 790517:during Routine Surveillance of Core Spray Sys Ii,Parallel Isolation Valve V-20-21 Failed to Operate.Caused by Circuit Breaker Contacts Making Poor Contact in B Phase,Creating Overcurrent.Part Replaced | /03L-0 on 790517:during Routine Surveillance of Core Spray Sys Ii,Parallel Isolation Valve V-20-21 Failed to Operate.Caused by Circuit Breaker Contacts Making Poor Contact in B Phase,Creating Overcurrent.Part Replaced | | | 05000219/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000219/LER-1979-018-03, /03L-0 on 790517:snubber 51/21,core Spray Sys II, Had Signs of Grease on Alemite Fitting on Accumulator.Cause Unknown But Appears Related to Rigorous Svc Conditions. Snubber Replaced | /03L-0 on 790517:snubber 51/21,core Spray Sys II, Had Signs of Grease on Alemite Fitting on Accumulator.Cause Unknown But Appears Related to Rigorous Svc Conditions. Snubber Replaced | | | 05000219/LER-1979-019-03, /03L-0 on 790526:reactor High Pressure Isolation Condenser Initiation Switch RE-15A Tripped at 3 Psig Greater than Specified.Caused by Instrument repeatability.RE-158 Reset to Trip at 1,068 Psig | /03L-0 on 790526:reactor High Pressure Isolation Condenser Initiation Switch RE-15A Tripped at 3 Psig Greater than Specified.Caused by Instrument repeatability.RE-158 Reset to Trip at 1,068 Psig | | | 05000219/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000219/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000219/LER-1979-020-01, /01T-0 on 790613:secondary Containment Integrity Breached When Reactor Bldg Airlock Doors Were Opened Simultaneously.Caused by Failure of Procedure to State Correct Method for Securing Airlock Doors.Procedure Revised | /01T-0 on 790613:secondary Containment Integrity Breached When Reactor Bldg Airlock Doors Were Opened Simultaneously.Caused by Failure of Procedure to State Correct Method for Securing Airlock Doors.Procedure Revised | | | 05000219/LER-1979-021-03, /03L-0 on 790620:during Surveillance Testing Activities,Instrument 1P15A Was Found to Trip at Valve Higher than Allowed by Tech Specs.Instrument Found to Be within Expected Accuracy Attainable | /03L-0 on 790620:during Surveillance Testing Activities,Instrument 1P15A Was Found to Trip at Valve Higher than Allowed by Tech Specs.Instrument Found to Be within Expected Accuracy Attainable | | | 05000219/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000219/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000219/LER-1979-022-03, /03L-0 on 790627:leak Detected on Emergency Svc Water Side of Containment Spray Heat Exchanger 1-2.Caused by Leaking Nipple Connection Between Water Box & Piping to Valve V-3-83,due to Corrosion.Nipple Replaced | /03L-0 on 790627:leak Detected on Emergency Svc Water Side of Containment Spray Heat Exchanger 1-2.Caused by Leaking Nipple Connection Between Water Box & Piping to Valve V-3-83,due to Corrosion.Nipple Replaced | | | 05000219/LER-1979-023-01, /01T-0 on 790719:reactor Power Was Reduced Above Value for Removal of a Feedwater String.Caused by Removal of Recirculating Pump Reactor for Maint.Inboard & Outboard Collector Rings Resurfaced & Pump Returned to Svc | /01T-0 on 790719:reactor Power Was Reduced Above Value for Removal of a Feedwater String.Caused by Removal of Recirculating Pump Reactor for Maint.Inboard & Outboard Collector Rings Resurfaced & Pump Returned to Svc | | | 05000219/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000219/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000219/LER-1979-024-03, /03L-0:on 790730,control Rod Drive Pump a Discovered Spraying Water Through Seal.Caused by Failure of Mechanical Seal.Inboard Mechanical Seal & Inboard Bearing Replaced | /03L-0:on 790730,control Rod Drive Pump a Discovered Spraying Water Through Seal.Caused by Failure of Mechanical Seal.Inboard Mechanical Seal & Inboard Bearing Replaced | | | 05000219/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000219/LER-1979-025-03, /03L-0:on 790806,10,000 Gallons of Torus Water Drained & Ability of Primary Containment Degraded.Caused by Isolation Valve Left Open After Water Samplings.Change to Sampling Procedure Submitted on Use of Valve | /03L-0:on 790806,10,000 Gallons of Torus Water Drained & Ability of Primary Containment Degraded.Caused by Isolation Valve Left Open After Water Samplings.Change to Sampling Procedure Submitted on Use of Valve | | | 05000219/LER-1979-026-03, /03L-0:on 790807,while Excavating to Repair Equipment Drain Tank Line,Leak in Laundry Tank Discharge Pipe Discovered.Caused by Levels of Mn-54 & Co-60.Line Temporarily Rerouted Until Repairs Made | /03L-0:on 790807,while Excavating to Repair Equipment Drain Tank Line,Leak in Laundry Tank Discharge Pipe Discovered.Caused by Levels of Mn-54 & Co-60.Line Temporarily Rerouted Until Repairs Made | | | 05000219/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000219/LER-1979-027, Forwards LER 79-027/01T-0 | Forwards LER 79-027/01T-0 | | | 05000219/LER-1979-027-01, /01T-0 on 790807:four Seismic restraints,NZ-2-R5 NZ-2R7,NZ-2-R8 & NZ-2-R9,in Positions Other than Required by Original Design.Caused by Improper Installation & Damage Due to Unrestrained Pipe Movement | /01T-0 on 790807:four Seismic restraints,NZ-2-R5 NZ-2R7,NZ-2-R8 & NZ-2-R9,in Positions Other than Required by Original Design.Caused by Improper Installation & Damage Due to Unrestrained Pipe Movement | | | 05000219/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000219/LER-1979-028-03, /03L-0:on 790807,during Routine Surveillance of Core Spray Sys 1,parallel Isolation Valve V-20-15 Became Inoperable in Open Position.Caused by High Motor Current Drawn When Close Signal Inadvertently Initiated | /03L-0:on 790807,during Routine Surveillance of Core Spray Sys 1,parallel Isolation Valve V-20-15 Became Inoperable in Open Position.Caused by High Motor Current Drawn When Close Signal Inadvertently Initiated | | | 05000219/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000219/LER-1979-029-03, /03L-0:on 790822,rod Block Trip Setting Was Below 100 Counts Per Second 26 Times During QA Audit.Caused by Calibr Procedure Setting Rod Trip at Tech Spec Limit.Rod Withdrawal Block Setpoint Increased | /03L-0:on 790822,rod Block Trip Setting Was Below 100 Counts Per Second 26 Times During QA Audit.Caused by Calibr Procedure Setting Rod Trip at Tech Spec Limit.Rod Withdrawal Block Setpoint Increased | | | 05000219/LER-1979-030, Revised Attachment to LER 79-030/03L-0:on 790812,control Rod Drive Pump a Removed from Svc for Repair of Pump Vent Piping.Piping Cracked at Bushing at Entry to Pump Casing. Caused by Operator Carelessness.Bushing Replaced | Revised Attachment to LER 79-030/03L-0:on 790812,control Rod Drive Pump a Removed from Svc for Repair of Pump Vent Piping.Piping Cracked at Bushing at Entry to Pump Casing. Caused by Operator Carelessness.Bushing Replaced | | | 05000219/LER-1979-030-03, /03L-0:on 790812,control Rod Drive Pump Removed from Svc Due to Excessive Leakage from Pump Vent Piping. Piping Was Cracked at Bushing.Caused by Use of Vent Line as Operator Foot Support.Bushing & Pipe Nipple Replaced | /03L-0:on 790812,control Rod Drive Pump Removed from Svc Due to Excessive Leakage from Pump Vent Piping. Piping Was Cracked at Bushing.Caused by Use of Vent Line as Operator Foot Support.Bushing & Pipe Nipple Replaced | | | 05000219/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000219/LER-1979-031-03, /03L-0:on 790829,seal Water Piping Found Cracked on Short Pipe Nipple Section Where Threaded Into Seal Cartridge.Caused by Operator Using half-inch Piping as Foot Support.Pipe Nipple Replaced | /03L-0:on 790829,seal Water Piping Found Cracked on Short Pipe Nipple Section Where Threaded Into Seal Cartridge.Caused by Operator Using half-inch Piping as Foot Support.Pipe Nipple Replaced | | | 05000219/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000219/LER-1979-032-03, /03L-0:on 790914,leaks Discovered in Both Containment Spray Sys.Caused by Corrosion Accelerated by Galvanic Action.Matl Change in Nipple Recommended | /03L-0:on 790914,leaks Discovered in Both Containment Spray Sys.Caused by Corrosion Accelerated by Galvanic Action.Matl Change in Nipple Recommended | | | 05000219/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000219/LER-1979-033-03, /03L-0:on 790917,electromatic Relief Valve Pressure Switch 1A83A Tripped at Pressure in Excess of Limit.Caused by Defective High Pressure Microswitch. Replacement Switch Installed | /03L-0:on 790917,electromatic Relief Valve Pressure Switch 1A83A Tripped at Pressure in Excess of Limit.Caused by Defective High Pressure Microswitch. Replacement Switch Installed | | | 05000219/LER-1979-034, Forwards LER 79-034/01T-0 | Forwards LER 79-034/01T-0 | | | 05000219/LER-1979-034-01, /01T-0:on 791008,both Personnel Access Air Lock 15ors of Reactor Bldg Were Simultaneoulsy Open.Caused by Contractor Personnel Disconnecting Automatic Closing Device on One Door.Device Reconnected | /01T-0:on 791008,both Personnel Access Air Lock 15ors of Reactor Bldg Were Simultaneoulsy Open.Caused by Contractor Personnel Disconnecting Automatic Closing Device on One Door.Device Reconnected | | | 05000219/LER-1979-035, Forwards LER 79-035/03L-0 | Forwards LER 79-035/03L-0 | | | 05000219/LER-1979-035-03, /03L-0:on 790926,during Normal Operation,Reading on Main Steam Line Radiation Monitor Lower than Other Three Monitors.Caused by Drift of Zero Setpoint of Amplifier in Monitor.Setpoint Reset to Zero | /03L-0:on 790926,during Normal Operation,Reading on Main Steam Line Radiation Monitor Lower than Other Three Monitors.Caused by Drift of Zero Setpoint of Amplifier in Monitor.Setpoint Reset to Zero | |
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