05000250/LER-1979-024-03, /03L-0:on 790802,driver Found in Need of Major Overhaul During Preventive Maint on West Fire Pump.Cause Not Stated.West Pump Tested & Returned to Svc

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/03L-0:on 790802,driver Found in Need of Major Overhaul During Preventive Maint on West Fire Pump.Cause Not Stated.West Pump Tested & Returned to Svc
ML17338B105
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 08/31/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17338B103 List:
References
LER-79-024-03L-01, LER-79-24-3L-1, NUDOCS 7909260293
Download: ML17338B105 (2)


LER-1979-024, /03L-0:on 790802,driver Found in Need of Major Overhaul During Preventive Maint on West Fire Pump.Cause Not Stated.West Pump Tested & Returned to Svc
Event date:
Report date:
2501979024R03 - NRC Website

text

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