ML17333A460

From kanterella
Jump to navigation Jump to search
Insp Repts 50-315/96-04 & 50-316/96-04 on 960227-0408. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering,Preparation for Refueling,Plant Support & Review of UFSAR Commitments Performed
ML17333A460
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 05/17/1996
From: Kropp W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17333A459 List:
References
50-315-96-04, 50-315-96-4, 50-316-96-04, 50-316-96-4, NUDOCS 9605290182
Download: ML17333A460 (40)


See also: IR 05000315/1996004

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

REPORT

NO.

50-315 96004'0-316

96004

FACILITY

Donald

C.

Cook Nuclear Generating

Plant

LICENSEE

Indiana Michigan Power

Company

Donald

C.

Cook Nuclear Generating

Plant

1 Riverside .Plaza

Columbus,

OH 43216

DATES

February

27,

1996 through April 8,

1996

INSPECTORS

B.

L. Bartlett, Senior Resident

Inspector

D. J. Hartland,

Resident

Inspector

C.

N. Orsini, Resident

Inspector

G. Osterholtz,

Operating

License

Examiner

J.

Belanger,

Senior Physical

Security Inspector

J.

Foster,

Senior

Emergency

Preparedness

Analyst

R. Paul,

Senior Radiation Specialist

S. Orth, Radiation Specialist

R.-Glinski, Radiation Specialist

,

APPROVED

BY

~l )

W. J.

Kropgj Chief

Reactor Projects

Branch

3

Date

AREAS

INSPECTED

A routine,

unannounced

inspection of operations,

maintenance,

engineering,

preparation for refueling, plant support,

and review of UFSAR commitments

was

performed.

Safety

assessment

and quality verification activities were

routinely evaluated.

Fol'low-up'inspection

was also performed for non-routine

events.

9605290182

9605i6

PDR

AOQCK 050003'

6

PDH

Executive

Summar

OPERATIONS

The inspectors

continue to identify problems with the control

and

use of

procedures

and instructions.

Two of the following examples identified during

this inspection period pertained

to non-routine plant evolutions:

~

Operators

verbatim complied to

a procedure for a non-routine plant

evolution,

even though there

was

a known operator workaround that

resulted

in immediately deviating from the procedure

(Section 1.2).

Procedures

for a reactor

shutdown

and technical specification

surveillance

were revised utilizing the temporary

change

process,

even

though the revisions

changed

the intent of the approved

procedures

(Section 1.3.1).,

~

An approved

process

allowed written guidance to be provided to the

operators

that was outside of plant procedures.

The process

did not

ensure that the additional

guidance

was evaluated for the introduction

of an unreviewed safety question

(Section 1.3.2).

The following operator workarounds

were not identified by the licensee:

During the non-routine evolution of removing the Unit 2 normal

chemical

and volume control

system

(CVCS) letdown flow path from service,

the

operators

had to quickly reopen

the letdown containment isolation

valves to prevent lifting of a safety relief valve,

due to known leakby

of upstream

valves

(Section 1.2).

The automatic design feature of the condensate

booster pumps'inimum

control flow valves is procedurally defeated

during plant operations

due

to the discharge line of the

CBPs being 20" in diameter

and the minimum

flow line being

10" line (Section 3.3).

NAINTENANCE

FHE controls around the fuel handling areas,

general

containment cleanliness,

and housekeeping

were excellent.

Licensee

management

made regular tours of

containment

and the fuel handling areas

and prompt action

was taken to correct

any identified discrepancies

(Section 1.4.2).

There were missed opportunities to ensure that the installation of a

containment jig crane while the unit was at power was properly performed.

The

missed opportunities

consisted of: I) Workers not being attentive for possible

interferences

during initial rotational

checks of the jig crane

and

2) the jig

crane

was not thoroughly inspected

following inadvertent

damage to the crane

(Section 2.2).

ENGINEERING

A review of the technical specification

(TS) surveillances

for the ice

condenser identified the following concerns

(Section 3. 1):

~

The system engineer believed that the allowable ice condenser

bypass

was

50 ft', rather than the allowable

5 ft'Section 3. 1).

~

No tracking mechanism existed to ensure

the

5 ft'esign limit was not

exceeded

(Section 3.2).

PLANT SUPPORT

Radiolo ical Controls (Section 4. 1)

~

Implementation of radiological controls during the Unit 2 refueling

outage

were characterized

by good

RP controls

and careful radiological

work practices.

~

Source term exposure efforts continued to be successful

in reducing

radiation exposure.

~

Concerns

were raised

about workers loitering in the upper containment

during ongoing outage activities.

A tour of the 'auxiliary and turbine buildings

showed

good radiological

housekeeping

and worker

RP awareness.

Control

and Review of Water Chemistr

(Section 4. 1.3)

I

Contaminants

in plant water systems

were generally controlled at or

below the licensee's

aggressive. goals.

4

Periodically elevated

chemistry contaminants

were attributable to oxygen

inleakage into the condensate

system

and the limited capacity of the

RO

~

system.

4

Some weaknesses

in chemistry technician

(CT) performance

were observed,

which was inconsistent with management's

expectations.

ost Accident

Sam lin

S stem

PASS

(Section 4. 1.5)

Based

on the

IPAP inspection,

a violation was issued for failure to perform

PASS

gC activities in accordance

with procedures.

During this inspection,

the

inspectors identified that

a

CT had difficulty in operating the

PASS in

accordance

with chemistry procedures.

0

4

Chemistr

Labo ator

u lit Control

C

(Section 4. 1.6)

~

Problems

were identified with procedural

adherence

and supervisory

review of gC data.

~

Inconsistencies

were identified concerning

the application of the

gC

program,

which may decrease

the overall effectiveness

of the program.

Emer enc

Pre

ar edness

EP

Pro

ram (Section 4.2)

~

To enhance

the effectiveness

of the

EP program,

a new offsite EOF/ASPIC

facility has

been

purchased

and will be remodeled

(Section 4.2.3).

~

Procedures/drills

for offsite communication of Protective Action

Recommendations

(PARs) were weak in that

a key

EP director had never

had

the opportunity to exercise

his responsibility for this function

(Section 4.2.5).

~

Although identified in previous actions, training was not updated with

information on

NRC and

DOE response

practices

and operational

concepts

for key incident response

personnel.

Additionally, confusion over

initial PARs has not been resolved

(Section 5.0).

~Secnrit

(Section 4.3)

e

~

The security testing

and maintenance

program was well implemented.

The

licensee's'implementation

of a hand geometry

access

control

system

was

considered

good (Section 4.3.2).

SAFETY ASSESSMENT

AND EQUALITY VERIFICATION

Corrective actions for the damaged

fuel grids were thorough

(Section

1.4.1).

The licensee's

control, identification,

and removal of foreign material

in the areas

around the fuel handling operations

was excellent,

and

much

improved over previous inspection findings (Section 1.4.2).

The chemistry self assessments

and quality assurance

audits

were

sufficient in depth

and identified concerns with procedural

guidance,

data review,

and instruments.

Corrective actions to address

the

observations

were developed

and

implemented

(Section 4. 1.7).

Summary of Open

Items

Violations: identified in Sections

1.3. 1, 4. 1.5

and 4. 1.6.

Unresolved

Items:

non identified

Ins ector Follow-u

Items: identified in Sections'4.2.5

and 6.0.

Non-cited Violations: identified in Section

1.2

and 1.4.3.

k

!

4

I

INSPECTION DETAILS

1. 0

OPERATIONS

NRC Inspection

Procedure

71707 was

used in ongoing inspection of plant

operations.

1. 1

Reactor Tri

Due To A Controller Failure

Unit

1

On March 17,

1996, Unit

1 automatically tripped

on low feed flow coincident

with low steam generator level.

All safety

systems

responded

as designed.

The cause

was the failure of the differential pressure

(d/p) controller for

the main feed

pumps.

The licensee initiated

an investigation to determine

the cause of the d/p

controller failure and recent

problems with other controllers.

Other problems

observed,

which have not impacted. the actual

function of controllers,

were

intermittent loss of face plate display

and .loss of the audible

beep

associated

with manual input., Preliminarily, the licensee

believed that the

root cause of some of the problems

was electrostatic

discharge.

As an

immediate action,

the licensed

operators

were instructed to ground themselves

prior to operating the controllers.

The licensee

was also evaluating long-

term actions to eliminate the problem.

The

10 CFR 50.72 report stated

the control

room operators

manually started

the

motor driven auxiliary feedwater

pumps

and that

a "secondary safety" lifted

(implying a steam generator

code safety).

The

NRC identified that the trip

report filled out by the balance of plant operator

indicated that the

pumps

automatically actuated.

Also, the

NRC determined that the valve which

actuated

was

a feedwater/heater

system relief valve, not

a steam generator

code safety.

The licensee

investigated

the discrepancy

and concluded that the

motor driven auxiliary feed

pumps automatically actuated,

and that the shift

technical

advisor misunderstood

the operators'ommunication.

The inspectors

.will further review this event during the review of the associated

licensee

event report

(LER).

1

1.2

Procedural

Adherence

Issue

Unit 2

On March 5,

1996,

the inspectors

witnessed

the.non-routine

evolution of

removing the Unit 2 normal

chemical

and volume control

system "(CVCS) letdown

flow path from service to support repair of 2-QRV-500, the deborating

demineralizer divert valve.

The inspectors

determined that the operators

did

not follow procedure,

02-OHP 4021.003.001,

"Removing Letdown,

Charging

and

Seal

Water

From Service,"

when removing the normal letdown from service.

Procedure,

02-OHP 4021.003.001,

paragraph

2.2. 1, required closing the normal

letdown isolation valves,

the orifice isolation valves,

and the letdown

containment isolation valves

(2-QCR-300

and 2-QCR-301).

After closing these

valves,

the operators

quickly reopened

2-QRC-300

and

2-QRC-301 to prevent the

0

l

1

I

f

lifting of a safety relief valve due to known leakby of the normal letdown

isolation valves

and the orifice isolation valves.

The safety relief valve

was installed

on

a portion of the piping that

was isolated

when letdown

containment isolation valves

were closed.

During discussions

with the inspectors,

the operators

stated that since the

procedure

was not identified as

an "in-hand" procedure,

verbatim compliance

was not required.

The inspectors

determined

the licensee's

administrative

requirements for procedural

adherence

required that procedures

not designated

as "in hand" must also

be followed.

Since the leakby of the letdown

and

orifice isolation valves

was

a known problem and

was anticipated

by the

operators,

the procedure

should

have

been

changed prior to being performed.

Operations

management initially did not consider this to be

a procedural

compliance

issue

because

operators

needed

to have the flexibilityto deviate

from procedures

for the purpose of placing the plant in a safer configuration.

Since the leakby of the isolation valves

was

known by the operators,

the

inspectors

did not consider this

a valid reason to deviate

from the procedure.

Upon additional

review, the licensee initiated

a condition report to

investigate

the issue of procedure

adherence

and to document that

a

maintenance

action request

had not been initiated for the leaking orifice

isolation valves.

The inspectors

also identified that action requests

were

initiated in Hay 1995 for the leaking letdown isolation valves,

but the job

orders

(which maintenance

workers utilize to perform work on equipment)

had

not yet been written due to the relatively low priority.

The failure to adhere to plant procedures

as required

by 10 CFR 50, Appendix

B, Criterion V, constituted

a violation of minor significance

and is being

treated

as

a Non-cited Violation, consistent with Section

IV of the

NRC

Enforcement Policy. (50-316/96004-03)

The operators'esire

to quickly reopen

the letdown containment isolation

valves to prevent lifting of a safety relief valve,

due to known leakby of

upstream valves

was

a known operator workaround that was not recognized

as

an

operator workaround

by the l,icensee.

1.3

Hanual

Reactor Tri

From 20 Percent

Unit 2

Harch 23,

1996, while shutting

down the plant for a refueling outage,

the

licensee

manually tripped the reactor

from 20 percent

power.

The licensee

originally planned

the manual trip in anticipation that this would be required

in

a soon to be issued

NRC generic communication.

However,

when issued,

NRC

Bulletin 96-01,

"Rod Insertion Problems,"

dated

Harch 8,

1996, did not require

a manual trip, but rather rod drop testing following a reactor

shutdown.

The

licensee,

however,

decided to still manually trip the reactor

from 20 percent

power to collect true as-found rod drop data.

The licensee

also intended to

use the manual reactor trip to meet the

18 month technical specification

(TS)

surveillance

requirement

(4.8. 1. 1. 1) to verify operability of the auto-

transfer of power from the normal auxiliary source to the preferred

reserve

source.

0

1.3. 1 Procedure

Revision Concerns

Prior to the trip, the inspectors

reviewed the procedural

revisions

issued for

performing this non-routine reactor

shutdown for compliance with regulatory

requirements.

The following procedure revisions

were reviewed:

~

Change

Sheet

3 to procedure

02-OHP 4021.001.003,

"Power Reduction,"

revised

the method of a planned reactor

shutdown

from an orderly reactor

shutdown from power to

a manually reactor trip from a power level that

would result in the automatic starting of engineered

safety feature

equipment

(ESF).

~

Change

Sheet

1 to surveillance

procedure

02-0HP4030.STP.026,

"Auxiliary

Power Transfer Test Surveillance

Procedure,"

revised

when to perform the

TS surveillance.

Instead of performing the surveillance

when the

reactor

was

shutdown

(Mode

5 or 6), the revision allowed the

surveillance to be performed at power

(Mode 1) using

an actual

ESF

actuation

(reactor trip).

TS 6.5.3. I.a requires that procedures

which affect plant nuclear safety,

and

changes

thereto,

shall

be prepared,

reviewed,

and approved.

TS 6.5.3. l.e also

requires that

a procedural

change

be reviewed to determine if an unreviewed

safety question exist.

To facilitate implementing

changes

to procedures

that

do not change

the intent of the approved

procedure,

TS 6.5.3. l.a describes

the

use of a temporary

change

process.

These

temporary

changes

deviate

from the

normal review and approval

process

by allowing these

changes

to be approved

by

two members of the pl'ant staff, with at least

one individual holding

a senior

reactor operator license

and allows the safety review, to determine if an

unreviewed safety question exist, to be conducted until

14 days after

implementation of the change.

The inspectors

considered

the above

changes

to

procedures

02-OHP 4021.001.003

and 02-0HP4030.STP.026

as

changes

to the intent

of the procedure

and the temporary

change

process

should not have

been

used.

The

NRC discussed

these

concerns with licensee

management

on March 22,

1996.

In response,

the licensee

revised the procedure

02-OHP 4021.001.00

using the

normal procedural

process,

including the appropriate

safety reviews, prior to

tripping the unit on the following day.

The licensee

canceled

the performance

of surveillance

02-0HP4030.STP.026

due to the time constraint

involved with

the reviews for the proposed

procedural

change.

The use of the temporary

change

process

to issue

Change

Sheet

3 to procedure

02-OHP 4021.001.003,

"Power Reduction"

and

Change

Sheet

1 to surveillance

procedure

02-0HP4030.STP.026,

"Auxiliary Power Transfer Test Surveillance

Procedure"

is

a violation of TS 6.5.3. l.a and

e (50-316/96004-01(DRP)).

1.3.2 Concern with the Process

for Written Guidance to 0 e ators

Plant Managers

Instruction

(PMI) 4090, "Criteria For Conducting Infrequently

Performed Tests Evolutions,"

defines

the controls to allow the use of written

guidance to the operators

which is outside of an approved plant procedure.

PMI 4090 did not ensure that the additional

guidance

was evaluated

for an

unreviewed safety question.

During the planning for the reactor trip from 20

percent

power, the licensee

used the PHI-4090 process

to identify the option

of a manual start of the motor-driven auxiliary feedwater

pumps prior to the

trip.

PHI-4090 required

a screening

in order to provide additional written

information to operators

during certain evolutions.

The inspectors

were

concerned that PHI-4090 did not require that

a safety evaluation

be performed

to ensure that additional

guidance to operators

during infrequent tests

evolutions did not constitute

an unreviewed safety question.

1.4

PREPARATION FOR REFUELING - Unit 2

NRC Inspection'rocedure

60705

was

used to perform

an inspection of the

licensee's

preparation for the planned Unit 2 refueling outage.

This

inspection primarily focused

on the controls

and implementation of core

unloading activities.

1.4. I Dama

e to Fuel Grid Stra

s - Unit 2

On April 3,

1996, while performing

100 percent

in-mast sipping

and visual

examinations

during the removal of the fuel, refueling personnel

identified

that three grid straps

on the fuel assembly

in core location P-'ll were

damaged.

Two of three non-structural

grid straps

had

one entire face removed

and one of the seven structural grid straps

had

a narrow section

(about the

width of two fuel pins)

removed.

No significant damage to the fuel cladding

occurred.

Prior to resuming fuel movement the licensee:

~

Performed

an assessment

of this event.

4

Performed

an examination of the fuel

and searching for the grid straps

that were missing.

P

e

Removed the grid strap piece that was sticking out of the fuel cell that

was in the upender.

Based

on inspection of the damaged

fuel assembly

and interviews of refueling

personnel,

the licensee

determined that the grid damage to the fuel assembly

in core location

P-11 occurred during the removal of the fuel assembly

at core

location R-ll.

Core location R-ll was in the first row of assemblies

removed,

and therefore

was restricted

on three sides during removal.

Two sides

were

adjacent to the core baffle,

and one side

was adjacent to the assembly in

location P-ll.

To ensure that stress

was reduced

on the remaining assemblies

to be removed,

the licensee

revised the unloading pattern.

The

new unloading

pattern would be incorporated

into future outages.

As Unit 2 fuel was thinner

than Unit I fuel, the problems with Unit 2 fuel bowing was more acute.

The

new unloading pattern

was only applicable to Unit 2.

The licensee

did not plan on reusing the once burned

assembly that was the

most damaged.

The other assembly

received minor damaged,

but had already

been

used for three cycles

and was not schedule'd

to be re-used.

The licensee

accounted for all pieces of the grid strap prior to initiating a re-load of

the reactor vessel.

The

NRC observations

of fuel handling activities both before

and after

identification of the

damaged

assembly did not identify any significant

problems.

The licensee's

corrective actions for the damaged grid straps

was

considered

to be excellent.

1.4.2 Forei

n Material Exclusion

FME

Durin

Fuel Handlin

0 erations

The licensee's

control, identification,

and removal of foreign material

in the

'reas

around the fuel handling operations

was excellent,

and

much improved

over previous inspection findings (IR 315/316-95010(DRP).

During

a previous inspection

(IR 315/316-95010(DRP),

the inspectors

had

identified numerous

examples of poor

FHE control around the fuel handling

areas

(e.g.

spent fuel pool, reactor vessel,

refueling cavity, etc).

Based

on

these

examples

the licensee initiated improvements

but,

had not completed all

the corrective actions.

During this inspection period,

the inspectors

observed excellent

FHE control in the containment.

Tight control

was being

maintained over the introduction of materials within the

FHE control

zones

and

regular inspections

and cleanups

were being performed.

In addition to the

FHE controls

around fuel handling areas,

general

containment cleanliness

and housekeeping

were also excellent.

Licensee

management

made regular tours of containment

and the fuel handling areas

and

prompt action

was taken to correct

any identified discrepancies.

Marked

improvement

has

been

noted plant wide in

FHE controls.

1.4.3

S ent Fuel

Pool Radiation Monitors

During a tour of the spent fuel pool

(SFP)

area

and the containment during

fuel handling operations

the

NRC determined

the licensee

had portable

radiation monitors inside containment

but did not have

an operable portable

monitor in the

SFP area.,

The licensee

normally had

a portable radiation

monitor in the

SFP area,

but due to maintenance

the monitor was removed to

replace

the one inside containment.

UFSAR section

14.2. 1. 1 states,

in part, during fuel handling operations:

"In

addition to the area radiation monitor located

on the bridge over the spent

fuel pit, portable radiation monitors capable of emitting audible alarms

are

located in the area during fuel handling operations."

UFSAR section

14.2. 1.2

states,

in part:

"In addition to the area radiation monitors located in the

upper

and lower containment

volumes,

portable monitors capable of sounding

audible alarms

are located in the fuel handling area."

The licensee

did not have

any procedural

requirements

to place portable

radiation monitors inside of containment

and around the

SFP during fuel

handling operations.

This was apparently

due to

a lack of knowledge of the

UFSAR commitment.

Due to good radiological practices

the licensee

made it a

practice of having portable radiation monitors inside containment

but it was

not proceduralized

or occurring in reference

to this commitment.

I'

An additional contributor to the licensee's

failure to identify this

commitment

was the failure to have the commitment in other

UFSAR sections.

For example the commitment

was not contained

in section 9.4,

spent fuel pool,

section 9.7 refueling, nor chapter ll radiation monitoring.

The licensee

committed to revise the procedures

to include the requirement

to have portable

radiation monitors in place prior to fuel movement.

The licensee failed to implement

a commitment in the

UFSAR.

However,

since

other monitors were in the area

and operable this failure constitutes

a

violation of minor significance

and is being treated

as

a Non-Cited violation,

consistent

with Section

IV of the

NRC Enforcement Policy 50-316/96004-05.

Following NRC inspector questioning,

the licensee

began

an assessment

of the

UFSAR requirements

and the area radiation monitors.

The licensee

believed

that the existing radiation monitor on the North wall of the

SFP combined with

the portable monitor located

on the

SFP bridge were adequate

to meet'he

UFSAR

commitment.

However, the licensee

performed

a safety evaluation

and

UFSAR

change

request to use only the portable monitor on the bridge during refueling

operations.

This was completed prior to beginning core re-loading.

1.4.4 Dual Train Outa

e

During a routine review of control

room paperwork,

the

NRC determined

the

licensee

was planning

on performing

a dual train essential

service water

(ESW)

and component cooling water

(CCW) water outage during the Unit 2 refueling

outage.

Due to TS considerations

the licensee's

only work window would occur

while the core

was entirely off-loaded to the

SFP.

However, since

one train

of SFP cooling depended,

upon Unit 2 for power and cooling water, this would

result in only one train of cooling being available to cool the

SFP.

On January

3,

1996,- the licensee

had determined that the practice of having

dual train

ESW and

CCW outages

during

a full core off-load exceeded

the

licensing basis

and that the

UFSAR contained errors which needed

to be

corrected.

Condition report 96-0002

was written as required

by procedure

and

immediate follow-up begun.

The licensee

determined that

as the design basis

would not be exceeded,

the

dual train

ESW/CCW outage

planned for the Unit 2 refueling outage could be

performed provided it was properly approved

through the

10 CFR 50.59 process.

A safety review, engineering

assessment,

and calculation were performed to

verify no unreviewed safety question existed during the plann'ed

dual train

outage.

Subsequently,

due to a change

in the scope of the

ESW outage,

the dual train

ESW outage did not occur.

The licensee

also

was able to isolate the

CCW

system for maintenance

work in a manner which resulted

in the need to perform

a dual train

CCW outage to be eliminated.

Unfortunately due to

a

communications error there

was still about

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in which neither train of

CCW was available to cool Unit 2's

SFP cooling train.

A separate

CR was

written to address

the communications failure.

10

The licensee

planned to update

the

UFSAR during the next annual

update

(June,

1996) to resolve the discrepancies

identified in January

1996.

1.5

Closure of LERs - Both Units

Closed

LER 50-315 95003: - Reactor trip due to turbine trip on loss of

vacuum.

This event

was discussed

in Inspection

Report 50-315;316/95009

and

a

violation was issued

(95009-01).

No new issues

were revealed

by the

LER.

Closed

LERs 50-315

95004

50-315

95005

and 50-316

94009: - Loss of 4-loop

injection,

unexpected auxiliary feedwater

pump start,

and engineered

safety

feature ventilation inoperability during surveillance.

These

events

were

reported

based

on discussion

in Inspection

Report 50-315;316/95009

and the

issuance

of a violation (95009-02).

No new issues

were revealed

by the

LERs.

Closed

L

R 50-315 95011: - West centrifugal charging

pump inoperable for six

months

due to personnel

error during relay calibration.

This event

was

discussed

in Inspection

Report 50-315/95014

and escalated

enforcement

action

taken

(95014-Ola).

No new issues

were revealed

by the

LER.

Closed

LER 50-315 96001:

New fuel vault criticality monitor.

This event

was discussed

in Inspection

Report 50-315;316/96002

and

a violation was issued

(96002-01).

No new issues

were revealed

by the

LER.

Closed

LER 50-316

94008

95004: - Reactor trip caused

by turbine trip on hi

moisture separator

reheater level.

These

events

were discussed

in Inspection

Report 50-315;316/95010.

No new issues

were revealed

by the

LER.

Closed

LER 50-316 95005:

Reactor trip from trip of both control rod drive

motor generator

sets

due to mis-adjusted

voltage regulators.

This event

was

discussed

in Inspection

Report 50-315;316/95010

and

a non-cited violation was

issued.

No new issues

were revealed

by the

LER.

Closed

LER 50-316 95006:

Reactor trip on manual

actuation of trip breaker

control switch.

This event

was discussed

in Inspection

Report 50-

315;316/95010

and

a non-cited violation was issued.

No new issues

were

revealed

by the

LER.

2.0

NAINTENANCE AND SURVEILLANCE

NRC Inspection

Procedures

62703,

61726,

and

92902 were used to perform

an

inspection of maintenance

and testing activities.

2. 1

Maintenance

and Surveillance Testin

Activities

The

NRC observed

routine preventive

and corrective maintenance

and

surveillance activities to ascertain

that these

were conducted

in accordance

with approved

procedures,

regulatory guides,

industry codes or standards,

and

in conformance with Technical Specifications

(TS).

The specific maintenance

activities observed/reviewed

are, listed below:

11

002619501

4

004073607

+

001358105

+

004142907

4

003969203

Repack

RHR valve 2-RH-121W

Lift and inspect Unit 2 upper internals

Perform test

on Unit 2 AB Battery

Repair ice 'condenser

bed

Disassemble

and repair pressurizer

power

operated relief valve 2-NRV-163

+

02-OHP 4021.001.003

02-EHP.4030.STP.211

1-0HP.4030.STP.027AB

The specific surveillance activities observed/reviewed

are listed below:

+

02-EHP.4030.STP.211

Ice Condenser

Surveillance

+

1-0HP.4030.STP.027AB

Diesel

Generator

Slow Start

+

02-0HP4030.STP.026

Auxiliary Power Transfer Test Surveillance

Procedure

Power Reduction

Ice Condenser

Surveillance

Diesel

Generator

Slow Start

2.2

H draulic Fluid

S ill Inside Containment

While On Line - Unit 2

On March 8,

1996, during an initial check out of the

new containment jib

crane,

the crane

was inadvertently rotated into an obstruction

and caused

a

suction

hose to the hydraulic

pump to fail.

Approximately 10 gallons of

hydraulic fluid were spilled in containment while Unit 2 was operating.

The

spilled fluid was immediately cleaned

up and

an operability assessment

was

performed

and determined that the operability of the

ECCS recirculation

system

was not compromised.

The licensee

repaired

the failed hydraulic hose,

corrected

the interference

and resumed

the check out of the jib crane.

On March 21,

1996,

another spill occurred

when the casing of the hydraulic

pump cracked

and about

8 gallons of fluid leaked into containment.

The

spilled fluid was cleaned

up and the licensee

had the

same operability

concluhions.

The cause of the cracked casing

was stresses

introduced during

the initial failure of the hose.

The

pump was replaced

and the operability

checks of the jib crane continued.

While neither spill caused

equipment to

become

inoperable,

there were missed opportunities to improve performance

in

the installation of equipment while the unit was at power.

The missed

opportunities

consisted of:

Workers paying more attention to possible

interferences

during initial

rotational

checks of new equipment.

The need to perform thorough checkouts of equipment following events

where equipment is inadvertently

damaged.

While the licensee's

immediate actions of cleaning the spilled fluid were

sufficient for the short term, the long term assessment

failed to address

the

RCS chemistry effects.

The initial cleanup consisted

only of wiping the oil

up with rags

and

no chemical

cleaning

was performed.

Subsequently,

while

flooding the reactor cavity for refueling activities personnel

reported

a

small oil sheen

on the water.

On April 16,

1996, with the unit de-fueled

licensee

personnel

initiated

a

CR to document that the initial evaluation did

12

not consider the effect of the oil mixing with the reactor cavity water

and

thus mixing with the nuclear fuel.

The licensee

made the evaluation

a

restraint for entry into Mode 5.

3,0

ENGINEERING

NRC Inspection

Procedures

37550

and

37551 were used. to perform

an onsite

inspection of the engineering

functions.

3. 1

Trackin

of Ice Condenser

8

ass

Paths-

Both Units

The inspectors

had previously identified small instrumentation

openings

in

Unit 1,

between

the upper

and lower containment.

The licensee

stated

since

the openings

were small

and few in number,

the design basis for ice condenser

bypass

was still met.

During a recent tour of upper

and lower containment,

the inspectors

had

more questions

regarding ice condenser

bypass for some

penetrations

between

upper

and lower containment.

The inspectors

were

informed by the system engineer that the ice condenser

bypass

design basis

was

a 50 ft'.

The inspectors

determined that the design basis

was only 5

ft'ased

on the present

bypass

paths identified between

upper

and lower

containment,

approximately

44 percent of the allowable

5 ft2 ice condenser

bypass

was being used.

The inspector

were concerned

that there

was

no

tracking mechanism to ensure that the design basis for ice condenser

bypass

was met

and that the system engineer did not know the allowable design basis

for ice condenser

bypass.

3.2

Secondar

Side Transients

Unit

1

The air operated

condensate

booster

pump

(CBP) minimum control flow valve

(emergency leak off or

ELO valve)

was designed

to automatically

open

on low

flow to protect the

pump and to close automatically

on higher flow.

The

discharge line of the

CBPs

was 20" in diameter with the

ELO line being

a 10"

line.

When the

ELO valve opens,

the diverted flow goes to the main condenser.

The use of a 10"

ELO line with a 20"

pump discharge line results

in large

system pressure

and flow perturbations

when the

ELO valves

open or close.

In

an effort to reduce the perturbations,

the operators

modified the procedure to

place the

ELO valves in the open position,

the designed

position during

a

reactor star tup,

and then removing control

power

so the

ELO valve remains

open

during power operations.

This reduced

the number of unexpected

opening

and

closing of the

ELO valve and system perturbations

during plant operations.

On March 19,

1996, with Unit

1 at 30 percent

power in preparation to close the

ELO valve, the breaker for the control

power was closed to the south

CBP

ELO

valve in accordance

with the startup

procedure.

However,

when power was

restored

there

was dual position indication for the

ELO valve. Shortly

afterwards

excessive

vibration was felt in the control

room and various

condensate

heater,

and condenser

level alarms flashed in and out due to high

and low indicated level.

Control

power was immediately removed

from the

valve.

Local inspection revealed that the air supply line to the valve had

partially broken off causing

the

ELO valve to rapidly oscillate

and

subsequently

resulted in the air supply completely failing.

Apparently, the

air line had

been loose

and

when power was restored

to the valve the slight

13

opening motion caused

the line to fail.

The piping around the south

CBP was

inspected for damage

and

a condition report was initiated.

One week later on March 27,

1996, with Unit

1 at full power,

another

CBP

ELO

valve transient

occurred.

A fitting on the air supply to the middle

CBP

ELO

valve developed

a large leak resulting in the valve going from the closed

position to 50 percent

open.

The manual isolation valve was shut, air was

isolated to the

ELO valve and the valve was failed closed.

When the

ELO valve

went

50 percent

open

some flow from the condensate

system

was diverted to the

condenser

and resulted in:

~

An automatic start of the South

CBP

~

An automatic start of the East Turbine Auxiliary Cooling Water

Pump

~

A drop in the main feed

pump differential pressure

low

e

High and low level alarms in the three hotwells

1

The operator workaround concerning

the

ELO was not recognized

by the licensee

as

an operator workaround.

This was similar to the licensee's

failure to

recognize the operator workaround discussed

in paragraph

1.2 above.

4.0

PLANT SUPPORT.

NRC Inspection

Procedures

82701, TI 2515/131,

83750,

84750,

82701 were used to

perform an inspection of Plant Support activities.

Announced inspections of

the Emergency

Preparedness,

Radiological Protection,

Chemistry

and Security

were performed

by region based specialists.

4. 1

Radiolo ical Protection

and Chemistr

RP&C

Controls

4. 1. 1 Refuelin

Outa

e Radiolo ical Controls

Unit 2

and

As Low As Reasonabl

Achievable

ALARA

Pro ram

IP83750

The inspectors

reviewed work activities

and planning to ascertain

the

effectiveness

of the

ALARA program for this outage.

Included in this

assessment

was

a review of selected

work packages,

ALARA reviews, pre-job

briefings, planning

and scheduling,

and the following jobs in progress:

refueling activities

scaffolding installation

shielding installation

The inspectors

also conducted

tours of the containment,

auxiliary and turbine

buildings

and

had discussions

with workers to determine their understanding

of

job requirements

and dose rates.

e

The Unit 2 outage

dose

goal

was set at about

140 person-rem

(1.4 sievert

(Sv)).

Through day

29 of the outage,

the station

dose

was approximately

135

person-rem

(1.35 Sv) which was about

30 rem (0.30 Sv)

above the projected

dose

14

for that period.

Contributing to the higher dose

was about

10 person-rem

(0. 10 Sv) expended

on additional

work scope

(work not originally scheduled).

An additional

10 person-rem

(0. 10 Sv)

was due to work performed

on valves

and

components with dose rates that were higher than those

found during the

previous Unit 2 outage,

and which were used to make the initial dose

projections.

The licensee

was evaluating the cause of the unexpected

higher

dose rates on'hese

components.

Host of the remaining dose

was attributable

to problems with planning and/or preparation for work, such

as the reactor

vessel

internals lift.

The early boration initiative removed

about

600 curies of cobalt-58 from the

system

and appeared

effective in reducing containment

area

dose rates.

General

area

dose rates

were only slightly higher

than those

found during the

previous Unit 2 outage.

ALARA initiatives included continued

improvement in

scaffolding planning

and scheduling

(a factor of two dose reduction over three

years),

mock up training,

improved tool controls,

and considerable

use of

shielding.

The projected

non-outage

dose for 1996

(32 rem (0.32 Sv)

was twice that

received

in 1995 due in part to scheduled

on-line maintenance

and

modifications.

Although some minor problems

were noted with work planning, radiological

controls in the Unit 2 refueling outage

were generally well implemented

and

there

appeared

to be good radiological

work practices.

Source

term reduction

and shielding efforts continued to be successful

in reducing radiation

exposure,

and

ALARA planning for the large exposure

jobs was generally

thorough.

The dose

expended

to date,

although higher than estimated,

was

reasonable

considering

the added

work scope

and higher than expected

dose

rates.

4. 1.2 Tour of Unit 2 Containment

and Station Auxiliar Buildin

The inspectors

toured various work areas

in the plant

and observed

work in

progress.

Interviews of workers

and radiation protection technicians

were

conducted to determine if the workers were knowledgeable of the radiological

conditions in the work area.

During a tour of the Unit 2 upper containment

the inspectors

and the station

Radiation Protection

Hanager

(RPH) identified one person lying down in a low

dose

area,

other workers leaning

on

a hand rail in an area

posted

" Do Not

Linger," and several

other workers

who appeared

to be loitering.

Dose rates

in these

areas

ranged

from about I to 3 mrem/hr and the

RPH instructed

those

workers

who were not currently performing

a task to move to

a lower dose

area.

During

a tour of the refuel floor, the inspectors

noted that

a portable

ventilation hose taking suction from the hot maintenance

shop

was routed with

about

a

180 degree

bend,

thus creating the potential for reducing the design

air flow.

This matter

was discussed

with the

RPH who had the situation

15

l

0

corrected.

A worker was also identified sitting on

a potentially contaminated

lathe in the hot shop.

After discussing this with the floor RP technician,

the worker was requested

to move.

The tours of the radiologically controlled areas

generally demonstrated

good

radiological

housekeeping

and worker

RP practices,

but raised

a question

concerning

about how'ell persons

who appeared

to be loitering in the upper

containment

were challenged

by

RP and first line supervisors.

The inspectors

observations

were discussed

with the

RPH and plant manager

who indicated these

observations

would be addressed.

4.1.3 Control

and Review of Water Chemistr

IP 84750

The inspectors

reviewed the licensee's

plant water chemistry over the last

12

months,

including the sample collection

and the evaluation/trending

of

chemical

impurities in plant water systems.

Overall, primary and secondary

water quality were well maintained.

The

licensee

implemented

aggressive

goals

(contained

in chemistry procedures)

for

steam generator

(SG)

and condensate

chemistry impurities.

With the exception

of condensate

oxygen concentrations,

secondary

water chemistry

was maintained

within the licensee's

goals.

Oxygen inleakage resulted

in several

periods of

operation at condensate

oxygen concentrations

of 5-7 ppb, which is above the

licensee's

goal of 2-5 ppb.

The licensee

was

aware of this problem and

indicated corrective actions

were being taken to address this problem.

The inspectors

observed that the concentrations

of chloride

and sulfate

increased

at times

when the opposite unit was undergoing startup

and shutdown.

During startup evolutions,

the chemistry staff indicated that the reverse

osmosis

(RO) makeup water purification system

had

a output capacity that could

not adequately

meet

demands for both units.

The licensee

plans to upgrade

the

RO system to increase

capacity in 1996.

Although chemistry technician

(CT) knowledge

was found to be very good,

the

inspectors

noted

some weaknesses

in the

CTs knowledge of chemistry action

levels

and in the ability to identify data exceeding

those limits.

Prior to

a

chemistry supervisory review, the inspectors

noted that

a CT,

preparing

a

chemistry data

sheet for April 1,

1996, failed to properly indicate

an out of

specification Unit

1 Steam Generator

(SG) 'll chloride level.

The inspectors

discussed

this with a different

CT who was not familiar with the meaning of

the licensee's

different limits (i.e. goals, limit, and action levels).

Subsequently,

the licensee

corrected

the data sheet

and obtained

an additional

sample.

The licensee

indicated that this performance did not meet management

expectations

and that these

weaknesses

would be addressed.

Contaminants

in plant water systems

were generally controlled at or, below the

licensee's

aggressive

goals.

The periodically elevated

chemistry contaminants

were attributable to oxygen inleakage

into the condensate

system

and the

limited capacity of the

RO system,

Some weaknesses

in CT performance, were

observed,

which was inconsistent with management's

expectations.

16

4. 1.4

Im lementation

o

the Radiolo ical Environmental Honitorin

Pro

ram

REHP

IP 84750

On April 3,

an inspector

accompanied

a licensee

representative

during

REHP air

and drinking water sample collection.

The inspectors

also interviewed the

REHP staff regarding other sampling activities

and reviewed the

REHP data for

1994

and

1995.

The

REHP sample collection

and analyses

were conducted

in accordance

with the

ODCH.

All omissions

were noted in the reports.

The inspector reviewed recent

data for groundwater tritium originating from the Absorption

Pond,

and

no

adverse

trends

were evident.

Other than groundwater tritium, the

REHP data

for 1994

and

1995 indicated

no radiological

impact to the environment

from

plant operations.

All air samplers

were operational

and within calibration.

The observed

sampling activities were good.

However,

the inspector

noted that the

collector had

some difficulty removing the air filter from the sample

head,

and also that the air sample collection procedure

did not provide any guidance

for the removal of the air particulate filter.

Improper air filter removal

can

have

an effect

on sample integrity.

The licensee

indicated that both the

procedure

and practice

would be reviewed to ensure 'that air filter removal

wa's

proper

and consistent

among the collection staff.

Overall, the

REHP was effectively implemented.

4.1.5 Post Accident

Sam lin

S stem

PASS

During this inspection,

inspectors

reviewed weaknesses

in PASS activities that

were identified during the integrated

performance

assessment

(IPAP) documented

in NRC Inspection

Report Nos. 50-315/316-96003,

Section 5.2.

This review,

using procedure

12 THP 6020 PAS.016,

"Post Accident Sampling guality

Assurance,"

revision 2, included assessing

the operability and quality control

(gC) program for PASS.

The inspectors

also observed

a chemistry technician

(CT) obtaining

a

PASS sample.

The inspectors

had identified, during the

IPAP, that the below listed

comparisons

between

the

PASS analyses

and routine analyses

did not satisfy the

licensee's criteria and were not performed at the frequency required

by

procedure

12 THP 6020 PAS.016.

Based

on the inspectors

findings during the

IPAP, the licensee

had issued conditioh reports

(CRs) for. these discrepancies.

~

On August 22,

1995, monthly .boron comparisons

did not meet the

licensee's

acceptance criteria.

Honthly pH, oxygen,

and gas

chromatograph

(GC) samples

were not completed in August 1995.

On

September

5,

1995, the system log book noted that samples

were not

obtained

as the system

was out of service, yet returned to service the

same day.

~

On September

28-29,

1995,

monthly comparisons

for the

GC,

pH,

and

nuclide activity did not meet the licensee's

acceptance

criteria.

A

17

monthly boron comparison

was not completed

in September

1995.

The

system log book indicated that resampling

was not completed

because

of

lack of time.

~

On October 2, '1995,

the monthly comparison for pH did not meet the

licensee's

acceptance criteria.

Honthly comparisons

for the

GC, boron,

and nuclide activity were not performed in October

1995.

PASS boron

samples

for November

and December

1995 monthly comparisons

were discarded prior to analysis.

No resampling

was performed.

Technical Specification (TS) 6.8 requires

a program for post accident

sampling

be implemented

which includes

procedures

to ensure

the capability to analyze

reactor coolant samples.

Procedure

12

THP 6020 PAS.016,

which ensures

proper

PASS system

and instrument functioning for analyzing reactor coolant

samples,

required monthly comparisons

between routine grab samples

and the

PASS system

for the

PASS

pH monitor,

oxygen monitor,

GC,

and boron.

The failure to

perform monthly comparisons

as described

above is

an example of a violation of

TS 6.8 (Violation Nos. 50-315/316-96004-02a).

The failure to take corrective

actions for comparisons

outside of the acceptance

criteria,

as required

by

procedure

12

THP 6020 PAS.016, is another

example of a violation of TS 6.8

(Violation Nos. 50-315/316-96004-02b).

Once identified by the inspectors

during the

IPAP, the licensee

performed

some

immediate corrective actions including the counseling of the chemistry

supervisor responsible for the program.

The acting chemistry superintendent

informed the inspectors that the supervisor

was

unaware of the procedural

requirements

and relied

on the experience of the

CT performing the analyses.

The licensee

had also performed several

isotopic comparisons

to calculate

the

system dilution factor, which had not been

performed since October

1,

1993.

The results of those

analyses

indicated

a dilution of about

800 versus

the

1000 the licensee

had

been using.

Additionally, the inspector reviewed the

licensee's

February

1996 comparisons,

which were complete with followup action

taken for analyses

not meeting

acceptance

criteria.

On April 3 and 4, the inspectors

observed

a

CT calibrating the online

pH meter

and collecting of a diluted liquid sample,

respectively.

A tritium analysis

of the diluted liquid sample was.in

good agreement

with a routine grab sample.

Although the

CT had the applicable

procedures

in hand,

the

CT encountered

a

number of problems.

During the liquid sampling,

an inspector identified to

him that

he had inadvertently started

the sample drain

pump instead of

actuating

a system valve.

Additionally, he performed

some steps

out of

sequence

and

had to return to various parts of the procedure

to complete the

process.

As identified in the

IPAP,

weaknesses

were observed

in licensee

oversight of

the

PASS program that resulted

in two examples of a violation concerning

adherence

to procedure

12 THP 6020 PAS.016.

Additionally, the inspectors

identified

a

CT that

had difficulty operating

the

PASS in accordance

with

chemistry procedures.

18

0

4. 1.6 Chemistr

Laborator

ualit

Control

C

The inspectors

observed

laboratory activities,

reviewed pertinent

gC records,

and interviewed laboratory

and guality Assurance

(gA) personnel

regarding

laboratory

gC.

The analytical

areas

reviewed included radiochemistry,

non-

radiochemistry,

and on-line instrumentation.

The implementation of the radiochemistry

gC was good.

The

gC records for

Lower Limit of Detection

(LLD) indicated that the

gamma isotopic analysis

system

was capable of achieving satisfactory

LLDs.

In addition,

the

laboratory demonstrated

excellent radioanalytical capabilities

as evidenced

by

100 percent

agreement

with the vendor cross-check

program in 1995.

However,

the

1996 control charts for all the counting instruments

indicated the

existence of minor trends

and biases,

as defined in Procedure

12

THP 6020

ADM.001, "guality Control," Rev.

0.

The implementation of the non-radiochemistry

gC was adequate.

The inspectors

noted that the laboratory

was well equipped

and the licensee

had established

a

computer-based

system

(CDMS) to track the

gC performance of the instruments.

However, the lab staff recording of gC data into the

CDMS was inconsistent.

Another

gC data inconsistency

pertained to the use of performance

check data

from analyses

that were considered

non-regulatory.

In these

instances,

the

performance

check data

was

used only if the data point indicated

a problem

with the instrument,

but not if the data point was acceptable.

Therefore,

the

inclusion of these

data points in the

gC program was not uniform.

The inspectors

reviewed

gC data for the past six months for chloride

and

sulphate

analysis

on the ion chromatographs

and noted

a number of biases

and

trends

which were not evaluated

and recorded

as required

by Sections

6.2.4

through 6.2.7 of 12

THM 6020 ADM.001, "guality Control,

Rev.

0.

~

Chloride performance

checks

on instrument

I04 indicated

two biases

and

one trend from October

1995 to April 1996.

~

Chloride performance

checks

on instrument

I06 indicated

two biases

and

one trend from October

1995 to April 1996.

~

Sulphate

performance

checks

on instruments

I04 and

I06 indicated

one

and

two biases,

respectively,

from October

1995 to April 1996.

The lack of procedural

adherence

in the evaluation

and documentation of this

gC information is

an example of a violation of TS 6.8, which requires,

in

part, that procedures

be implemented

as

recommended

in Regulatory

Guide 1.33,

Appendix A (Violation Nos. 50-315/316-96004-02c).

The

gC for online instrumentation

was good.

The licensee

conducted

performance

checks 'in accordance

with gC procedures.

However, there

was

an

inconsistency

in the procedural definition of acceptance

criteria for the

gC

data.

Attachment

3 of Procedure

12 THP 6020 ADM.003, "Online Instrument

guality Control,"

Rev 1, indicates that the acceptance

criteria for hydrazine

is +/- 15 percent for "As Found"

and +/- 10 percent for "As Left."

The

19

inspectors

noted that hydrazine

gC data

on January

26,

1996 exceeded

these

criteria,

and there

was

no indication of corrective action,

as stated

in

Section 6.3.4.

The licensee

indicated that the procedure

required corrective

action only for regulatory parameters

and that this procedure

would be

reviewed to clarify the use of acceptance

criteria for non-regulatory

parameter

analyses.

Laboratory

gC was good, with the exception of procedural

adherence

and

supervisory review of gC data.

An example of a procedural

adherence

violation

was identified regarding the review of control charts.

In addition,

inconsistencies

were identified concerning

the application of the

gC program,

which may decrease

the overall effectiveness

of the program.

4. 1.7* Review of Chemistr

Self Assessments

and

ualit

Assurance

Audits

During the inspection,

the inspectors

reviewed chemistry guality Assurance

(gA) activities.

The chemistry staff, with assistance

from a gA auditor,

performed self-assessments

of selected

chemistry program elements

during the

past six months.

For the elements

reviewed,

the self-assessments

had

sufficient depth

and contained

several

good observations

concerning procedural

guidance

problems,

data review deficiencies,

and instrument issues.

Corrective actions to address

the observations

were developed

and implemented.

However,

as discussed

in the

IPAP inspection,

the self-assessments

were not

effective in ensuring the

1993

and

1994 self-identified problems with

chemistry sampling

and

gC were resolved.

4.2

0 erational

Status of the

Emer enc

Pre aredness

EP

Pro

ram

IP 82701

4.2.1 Actual

E er enc

Plan Activations

An Unusual

Event was declared

at 11: 15 a.m.

on Nay 5,

1995 when

a review of

past inservice inspection

examinations

determined that the ultrasonic

examination

procedure

used to inspect Reactor Coolant

System branch connection

welds was inadequate

to meet welding code requirements.

As such,

the

requirements

of Technical Specification (TS) 4.0.5

had not been

met for

emergency

core cooling systems,

and

a reactor

shutdown

was required per TS 3.0.3.

The Unusual

Event was terminated

at 1: 10 p.m. the

same date

when

an

operability determination

indicated the reactor

shutdown

was overly

conservative

and other means

were available to resolve the nonconformance.

An Unusual

Event was declared

at 1:00 a.m.

on August 20,

1995,

due to an

explosion in the phase

2 main transformer output bushing.

The transformer

was energized

but not providing power when the explosion occurred.

The

Unusual

Event was terminated

at 1:50 a.m.

on the

same date.

An Unusual

Event was declared

and terminated

at 11:55 a.m.

on August 22,

1995,

due to

a fire on the auxiliary building roof.

The fire, caused

by

roofing

repairs,

was extinguished within eight minutes.

The Unusual

Event was

terminated at the

same time as it was declared,

as the fire was extinguished

by that time.

20

Records

reviewed indicated that classification

and notifications had

been

made

properly and in

a timely manner.

Documentation for the events

were complete,

and technically correct.

A formalized procedure did not exist for

standardized

review, critique,

and tracking of corrective actions related to

actual

emergency

plan activations.

4.2.2

mer

e

c

P

a

nd

Im lementi

rocedures

The licensee

had submitted

a revision to the

Emergency Action Level

(EAL)

scheme

devised

by the Nuclear Management

and Resources

Council

(NUHARC).

This

submittal

was under review by the

NRC at the time of this inspection.

When

approved,

procedure

and training changes will be needed

to implement the

new

EALs.

The inspector reviewed

a representative

sample of Emergency

Plan

Implementing

Procedures.

No problems

were identified.

4.2.3

Emer enc

Res

onse Facilities

E ui ment

Instrumentation

and

Su

lies

Tours were conducted

through the Technical

Support Center

(TSC), Operations

Support Area

(OSA),

and

Emergency Operations Facility (EOF).

Each facility

was well maintained

and in an excellent operational

state of readiness.

Current copies of the Emergency

Plan,

Emergency

Plan

Implementing Procedures

and appropriate

forms were present

in each facility.

The field monitoring

team van was inspected,

as well

as field monitoring kits intended to be

utilized for field teams.

All inspected

items were in good material

condition.

A building has

been

purchased

in the town of Buchanon,

Michigan, to house

the

EOF and Joint Public Information Center (JPIC),

as well as individuals from

the Columbus,

Ohio, corporate office.

Inspection of the building indicated it

has

adequate

room for both functions.

Layout of both facilities was yet to

be determined.

Documents

reviewed indicated that emergency

equipment inventories

and

maintenance

were very good, with timely corrective actions

taken where

deficiencies

were identified.

No problems or concerns

were identified.

4.2.4 Or anization

and

Mana ement Control

The overall organization

and management

control of the

EP function was largely

unchanged

from the last inspection,

except that the

EP staff now reported to

the Site Vice President.

The possibility was discussed

that one of the corporate staff would join the

plant

EP staff.

This would consolidate

EP functions in one location

and aid

with the current

EP workload (relocation of the

EOF,

NUMARC EAL procedure

revisions

and training, routine program maintenance, drills, exercises,

Severe

Accident Management

implementation).

21

4.2.6 ~Trainin

Records indicated that drills and exercises

were formally critiqued, training

had

been provided

on formal critiques,

and significant critique items were

appropriately selected for corrective action.

Printouts

from the training tracking systems

were compared with

"Emergency

Call List," with no problems identified.

The

EP staff had proactively

recognized that

some personnel

with emergency

response

positions would be

leaving the organization,

identified their positions

on a'imely basis,

and

were in the process of selecting

and training replacements.

The results of interviews with two key emergency

response

persons

were

generally good.

Very good knowledge of emergency responsibilities

and

activities were generally evident during these

interviews.

The inspectors

interviewed

an individual assigned

as Technical

Support Center

Director (TSCD) that

had initial training and participated

in three drills.

During the training the

TSCD had not been required to perform offsite

communication related to classification

changes

and Protective Action

Recommendations

(PARs) during

TSC drills.

The inclusion of objectives in

periodic

TSC drills to develop

and perform offsite communications relating to

PARs will be tracked

as

an Inspection

Followup Item 315/316/96003-04.

Review of EP training records

and documentation

revealed that excellent

training appeared

to be provided to emergency

response

personnel.

A sample of

lesson

plans

was reviewed.

No concerns

were identified.

4.2.6 audits

The inspector

reviewed Nuclear Safety

and Design Review Committee Audit No.

220,

"Emergency Plan," dated April 6,

1995.

The audit resulted

in four

Condition Reports,

ten recommendations

and four Points of Information.

The

audit concluded that the

"Cook Plant

Emergency

Plan is being effectively

carried out," and noted

many positive program qualities.

Also reviewed

was Plant Performance

Assurance Audit No. (A-96-02,

"Emergency

Planning

and Preparedness

(PHI-2080)," dated

Harch 20,

1996 performed during

January

15 - Harch 7, 1996.

This audit was performed

by five individuals and

concluded that adequate

controls were established

to effectively implement the

program.

Two recommendations

and three points of information were associated

with the audit.

The audit was complete

and well detailed.

The

1996 audit was weak in the area of assessment

of the interface with

offsite authorities,

(the

1995 audit was very detailed

in this area)

but noted

that

a subsequent

surveillance

would be conducted

in this area.

The

1995

and

1996 audits of the

EP program satisfied the requirements

of 10 CFR 50.54(t) with respect

to scope.

Records

also indicated that the

EP staff

fulfilled the requirement

to make relevant

1995 audit results available to

State

and county officials in 1995.

22

4.2. 7

Commun cati o s

2515

131

The Emergency

Plan,

section

12.3.7

"Emergency Communications,"

section

12.3.7.2," Off-Site Communications,"

described

the various communications

systems

available for offsite communications.

These

included:

1. microwave system

2. V.H.F. radio system

3. telephone lines

The following telephone

systems

were discussed

with licensee

personnel:

1. Fiber optic line to Benton"Harbor via microwave link

2. Fiber optic line to Fort Wayne

3. Fiber optic line to the training center

4. Fiber optic line to Columbus

5. Fiber optic line to

GTE

Fiber optic lines were described

as buried in some areas,

but came to the

surface

and shared

a

common manhole

system.

All lines

came into

a

common

room

located

on the second floor of the lakeside office building,

an inside

room

without windows.

A router was available which would switch calls to operable

lines in case of individual line failures.

Battery backups for fiber optic

lines

had

an

assumed

capacity for 4-5 hour operation.

Three chargers

maintained

the battery system.

A low-frequency radio transmitter with an 8-hour uninterruptable

power system

(UPS) (including diesel

backup)

was utilized by Security personnel.

Equipment

for this system

was located at the

595 foot elevation,

in the underground

security equipment

room.

System

antennas

were

on the turbine building roof

'nd

a

UHF radio was

used to communicate with the Berrien County Sheriff,

utilizing the

same

UPS.

Control point consoles for this system include the

Central

Alarm Station,

Secondary

Alarm Station,

and Control

Room.

An offsite repeater

system

was present

at the microwave tower,

equipped with

propane

powered generator

backup power.

Control points for this system were

located at the

OSA and

EOF.

The

EOF microwave link could control the repeater

and function like a mobile unit.

Seven

company cellular telephones

were

available,

assigned

to management

and on-call personnel.

Discussion

indicated that there

was

no formalized procedure for actions to

take in the event of a major communications failure.

However,

a comprehensive

package of information, "E-Plan Communications,"

had

been developed to aid in

evaluating/restoring

communications

in case of major damage to the microwave

tower or

PBX room.

Line drawings of the various

systems

were included in the

package.

This documentation

package,

prepared

due to findings in a previous

drill or exercise,

described

which systems

would remain after various failures

(microwave tower or

PBX switchroom).

Procedure

PHP 2081

EPP.207,

"Barring of PBX," provides for actions to modify

the plant Private Automated

Branch

Exchange

(PBX) to eliminate direct

communications

between

selected

plant and all offsite telephones.

The

TSC

23

Administrative Coordinator is responsible for implementing this procedure,

which directs telecommunications

personnel

or the Security Director to bar the

PBX.

Barred telephones

cannot initiate outgoing calls, limiting

communications

to those

needed

in an emergency.

The overall status of the emergency

preparedness

(EP) program was very good.

Response facilities were in an excellent state of operational

readiness.

The

1995

and

1996 Audits of the

EP program were very good,

and satisfied the

requirements

of 10 CFR 50.54(t).

The

1996 evaluation of the interface with

offsite authorities

was pending surveillance

completion.

A concern

was

identified relative to Technical

Support Center drill objectives.

Emergency

communications capability was reviewed.

No UFSAR deviations

were identified.

4.3

~Secerit

NRC Inspection

Procedure

81700

was

used to perform an inspection of plant

support activities.

The licensee's

testing,

maintenance,

and compensatory

measures

programs

were well conducted,

ensuring

the reliability of physical

protected related

equipment

and security related devices.

4.3. 1 General

Overview

The licensee

employed

compensatory

measures

in accordance

with approved

security plan commitments

when equipment failed or its performance

was

impaired.

Those licensee

personnel

responsible for maintaining security

systems

demonstrated

pride and ownership.

Significant decreases

in the number

of security equipment

and personnel

error

safeguards

loggable events

were

noted during the first quarter of 1996.

The licensee

properly installed

and

effectively implemented

a hand geometry protected

area

access

control

system.

Improvement

was noted in the efforts to reduce the number of vital area

tailgating incidents.

The licensee

declared

operable

the physical

installation of the vehicle bar rier system

upgrades

required

by 10 CFR 73.55

(C)(7) for protection against malevolent

use of vehicles at nuclear

power

plants

on February

23,

1996

4.3.2 Biometrics

Hand Geometr

S stem

On December

18,

1995,

the licensee

implemented

a biometrics

hand geometry

access

control

system at the entrance

to the protected

area.

By letter dated

December

15,

1995, the

NRC granted

the licensee

an exemption to

10 CFR 73.55

badging requirements

relating to the issuance,

storage

and retrieval of

picture badges for individuals who have

been granted

unescorted

access

to the

protected

area;

Specifically, the exemption allowed individuals to keep their

picture badge in their possession

when departing the site.

The

NRC observed

that the

new system functioned well.

5.0

Follow-u

on Previousl

0 ened

Items

A review of the following previously opened

inspection

items

was performed

using Inspection

Procedure

92901.

0

l

4

I

V

'l

'll

0 en

Ins ection Followu

Item No.

315 94019-02: Training modules for key

incident response

personnel

did not contain information relative to the

NRC

Incident Response

Program nor that of the Department of Energy.

A training

session

had

been

conducted

on this information, but the training module

had

not had this material

included.

This item will remain open.

Closed

Ins ection Followu

Item No. 50-315 94019-01:

Procedure

12

THP 6010

RPP.009

(Rev.8),"Emergency

Equipment Inventory" provided for monthly

inventories

but specific numbers of supplies or other equipment

were not

provided for inventory purposes.

Minimum quantities of supplies or equipment

had

been

added to the inventories.

This item is closed.

0 en

Ins ection Followu

Item Nos.

50-315 95007-02

50-316 95007-02:

During

the

1995 Exercise there

was confusion over the initial protective action

recommendation

(PAR).

Verbal communication erroneously

referenced

a

PAR of

sheltering.

The

EOF manager called the State

and clarified the issue,

but

confusion over the

PAR continued for some time.

verbal

communication of

Protective Action Recommendations

to the State of Michigan.

This also

occurred during

a drill.

A consultant

was commissioned

to review the

PAR

communication

process

and

recommend corrective actions

as necessary.

This

item will remain

open.

Closed

Ins ection Followu

Item Nos.

50-315 95007-01

50-315 95007-01:

During the

1995 Exercise,

there

was

no organized or structured debriefing

process for returning inplant response

teams.

A simple form (exhibit

H to

procedure

PMP 2081

EPP.203)

had

been developed

to guide the debriefing

process.

The form had

been utilized in several drills with good results.

This item is closed.

Closed

VIO 50-315 316-95011-01

DRS:

Review licensee corrective actions

addressing

an event in which an access

control clerk incorrectly identified

a

contract

employee

as having been tested

and reported

as negative for chemical

substances.

The clerk failed to properly use information provided to prevent

misidentification.

As

a result of this failure, the contract

employee

worked

with unescorted

access

status

in the plant protected/vital

area

from August

19

through August 22,

1995.

The

NRC verified that the corrective actions listed in the licensee's

dated

November

15,

1995 to the apparent violation.

These actions

appear to be

effective and here

was

no recurrence

of these

events.

This item is closed.

0 en

IFI 50-315 316-95012-03

DRS

Review licensee

actions

addressing

inspector concerns

about

an adverse

trend in the number of tailgating

incidents during the second

and third quarters of 1995.,

Heightened

employee

awareness

of the functioning of the

new security card

reader

system

and continued senior

management

attention to this issue

indicated

improvement in this area.

There were three tailgating incidents

recorded during the first quarter of 1996.

Two of the incidents

were related

to ignorance of the functioning of the system

by employees

with infrequent

site access.

The third was related to an employee

who believed that

he had

received authorization into an area.

25

The licensee

thought that similar incidents with the old card reader

system

occurred,

but that the old system

was incapable of identifying such

occurrences.

6.0

Rev'iew of UFSAR Commitments

A recent discovery of a licensee

operating

a facility in a manner contrary to

the Updated Final Safety Analysis Report

(UFSAR) description highlighted the

'need for a special

focused review that compared plant practices,

procedures

and/or parameters

to the

UFSAR description.

While performing the inspections

discussed

in this report,

the

NRC reviewed the applicable portions of the

UFSAR that related to the areas

inspected.

The following inconsistencies

were

noted

between

the wording of the

UFSAR and the plant practices,

procedures,

and/or parameters

observed

by the

NRC.

~

During a tour of the spent fuel pool

(SFP)

and containment

areas,

the

NRC determined

the licensee

had portable radiation monitors inside

containment

but did not have

an operable portable monitor in the

SFP

area.

(Section 1.4.2)

(50-315/96004-05)

The licensee

had determined that the practice of having dual trai'n

ESW

and

CCW outages

during

a full core off-load exceeded

the licensing basis

and that the

UFSAR contained errors which needed

to be corrected.

(Section 1.4.4)

(50-315/96004-06)

7.0

Heetin

s and Other Activities

The

NRC contacted

various licensee

operations,

maintenance,

engineering,

and

plant support personnel

throughout the inspection period.

Senior personnel

are listed below.

At the conclusion of the inspection

on April 16,

1996, the

NRC met with

licensee

representatives

(denoted

by *) and summarized

the scope

and findings

of the inspection activities.

During this inspection de-briefings

were held

periodically with licensee

management.

Some of the persons listed below were

present for only some of the'e-briefings.

The licensee

did not identify any

of the documents

or processes

reviewed

by the

NRC as proprietary.

  • A. Blind, Site Vice President
  • J. Sampson,

Plant Manager

  • K. Baker, Assistant Plant Manager
  • D. Noble, Radiation Protection Superintendent
  • T. Postlewait,

Site Engineering

Support Manager

  • J. Wiebe, Superintendent,

Plant

Performance

Assurance

  • W. Hodge,

Plant Protection Supervisor

  • J. Allard, Maintenance

Superintendent

  • P. Schoepf,

Plant Engineering

Superintendent

  • T. Beilman, Scheduling

Superintendent

  • H. Hierau,

STA Supervisor

26

t

'L

0

  • D. Londot,

ICS Supervisor

  • M. Ackerman,

Licensing Supervisor

  • J. St.

Amand, Plant Engineering Supervisor

  • R. West, Licensing Coordinator
  • R. Ptacek,

Licensing Coordinator

  • D. Hafer,

NED Engineering Supervisor

  • R. Krieger,

Emergency

Preparedness

Coordinator

  • E. Fitzpatrick, Senior Vice-President

Nuclear

27

4l

0