ML17331B344
| ML17331B344 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 04/01/1994 |
| From: | Kropp W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML17331B342 | List: |
| References | |
| 50-315-94-04, 50-315-94-4, NUDOCS 9404140029 | |
| Download: ML17331B344 (25) | |
See also: IR 05000315/1994004
Text
U.S.
NUCLEAR REGULATORY COHHISSION
REGION III
Report
No. 50-315/94004(DRP)
Docket'o.
50-315
Licensee:
Indiana Hichigan Power
Company
1 Riverside
Plaza
Columbus-,
OH
43216
License
Nos.
Facility Name:
Donald
C.
Cook Nuclear
Power Plant, Unit
1
Inspection At:
Donald, C.
Cook Site,
Bridgman,
HI
Inspection
Conducted:
February
16,
1994 through Harch 21,
1994
Inspectors:
R. J.
Leemon
J.
A.
Isom
Approved By:
ropp,
C ie
Reactor Projects
Section
2A
ate
Ins ection
Summar
Ins ection from februar
16
1994
Harch
21
1994
Re ort No. 50-315
94004
Areas
Ins ected:
Special
safety inspection in response
to the reactor level
perturbations
between
February
17 and
18,
1994, during the draining of the
system
(RCS)
from normal operati'ng level
down to th'e reactor
vessel
Results:
Based
on the results of this inspection,
there
were three violations
identified that pertained
to procedures
(paragraph
5.a); correct'ive actions
to
a previous event (5.c);
and equipment status
(S.d).
There were three
unresolved
items identified that pertained
to pre job briefings (5.a),
training of operators for infrequently performed plant evolutions (S.b),
and
work scheduling
and planning 5.e).
One inspection followup item was
identified that pertained
to lack of level indication between
the bottom of
, the pressurizer
and the reactor vessel
flange (5.d).
The following is
a
summary of the licensee's
performance
during the draining of the
on
February
16 through
18,
1994:
0 erations
The performance
of the operations
department
during the February
16 through
18,
1994, draining of the
RCS was considered
poor.
The
NRC staff is concerned
with the failure of the control
room operators
to properly control
a
significant plant evolution such
as the draining of the
RCS.
The staff is
also concerned
with the failure of the contr'ol. room. operators
to understand
9400140029
94040i
ADOCK 050003i5
6
the importance of maintaining identical pressure
throughout the
RCS when
draining,
and also the effects
on
RCS level during rapid depressurization.
Maintenance
Overall, the work planning
and scheduling
performed for the draining of the
RCS was poor.
An outage
schedule
allowed
an air eductor to be installed
on
the reactor vessel
head vent with inappropriate plant conditions.
This
contributed to the perturbations
in the
RCS level during the draining of the
on February
17,
1994.
There were other concerns
noted with work planning
and scheduling that did not
contribute to the event,
but were indicative of poor work planning
and
scheduling.
Both trains of reactor vessel
level indication system
(RVLIS)
were taken out of service with the
RCS level at 620 feet
and
5 psig pressure,
in preparation
to remove the reactor vessel
head.
Other examples
include:
There
was several
hours of delay in venting sight glass
NGG-100
and
'evel
instrument NLI-112'due to ALARA concerns,
because
the containment
purge
system
was not in service
and workers did not obtain
enough
portable tubing.
There
was
a delay in test'ing the eductor after installation because
the
solenoid valve needed for the operation of the eductor
was installed in
a new'ocation.
This was not considered
during the preparation of the
work package.
,
Persons
Contacted
Details
Consumer
Com an
- E.
E.
A. A.
K. R.
L. S.
-~ J.
E.
B. A.
T.
P.
P.
F.
- D
L
L. J.
T. K.
S. A.
P.
G.
- J.
S.
- L. H.
- G. A.
D.
C.
H. L.
Fitzpatrick, Senior Vice President-Nuclear
Generation
Blind, Plant Manager
Baker, Assistant Plant Manager-Production
Gibson, Assistant Plant Manager-Projects
Rutkowski, Assistant Plant Manager-Technical
Support
Svensson,
Executive Staff Assistant
Beilman, Haintenance
Superintendent
Carteaux,
Training Superintendent
Noble, Radiation Protection Superintendent
Matthias, Administrative Superintendent
Postlewait,
Design
Changes
Superintendent
Richardson,
Operations
Superintendent
Schoepf,
Project Engineering Superintendent
Wiebe, Safety
8. Assessment
Superintendent
Vanginhoven, Site Design Superintendent
Weber,
Plant Engineering Superintendent
Loope, Chemistry Superintendent
Horvath, guality Assurance
Supervisor
2.
- Denotes
those attending the exit interview conducted
on Harch 21,
1994.
The. inspectors
also
had discussions
with other licensee
employees,
including members of the technical
and engineering staffs, reactor
and
auxiliary operators,
shift engineers
and foremen,
and electrical,
mechanical
and instrument maintenance
personnel,
and contract security
personnel.
Descri tion of Event
On February
12,
1994, Unit
1 was shut
down to begin
a scheduled
refueling outage.
On February
17,
1994, preparations
were
made to vent
and drain the reactor coolant
system to approximately two feet below the
reactor vessel
flange to remove the reactor vessel
head in preparation
for core offload.
The licensee
also planned to install
an air eductor
on the reactor vessel
vent line to facilitate the 'removal of conoseals.
Due to inadequacies
in the drain down procedure
and ineffective planning
and control
by operations
personnel,
the reactor coolant system level
was off sacle for approximately
a five hour period.
The inspector concluded that the draindown of the
RCS was not adequately
performed since there
was
a period of five hours
when
RCS level
instrumentation
was off scale.
Fortuitously, there
was
no safety
significance to this event since,
at all times,
adequate
decay heat
removal for the reactor core remained available.
However, considering
corrective action needs to be in place to prevent recurrence
of these
events.
3.
Initial Conditions
Prior to the event,
the residual
heat
removal
(RHR) system
was in
service,
maintaining desired
RCS temperature.
Two pressurizer
power
operated relief valves
(PORV) were open to connect the pressurizer
with
the pressurizer relief tank and the
RCS to maintain the entire
system at
5 psig.
The initial conditions prior to commencing the draining of the
RCS was
as follows:
4.
~
RVLIS train
A was out of service
(OOS).
~
RVLIS train
B wide range indication was in service.
Pressurizer'cold
calibration level
was at 85 percent.
~
RCS was pressurized
to
5 psig.
Se
uence of Events
The sequence
of events
was determined
by interviews with licensee
personnel
on shift at the time of the event,
the review of logs,
and the
review of instrumentation strip chart recorders.
The times noted in the
following sequence
of events
labeled with an "(A)" were approximate
times
based
mostly on personnel
interviews.
Wednesda
Februar
16
1993
Shift supervisor for the
1830 to 0630 shift calculates
volume of water
to be drained,
including steam generator
(SG) U-tubes.
However, the
calculation
was not logged or communicated
to subsequent
shifts.
Thursda
Februar
17
1993
0413
Shift supervisor
authorized
the start of the draindown of
the
RCS to the reactor water storage
tank
(RWST) from
82 percent pressurizer
level with only the wide range of
RVLIS in service.
0615
0615
The
RCS drained to 8 percent
and stabilized.
Shift change
in progress.
0900
(A)
Opened bullseye flow indicator on reactor
head vent line.
0930
(A)
Sight glass
NGG-100 vented
and in service.
0936
1100
(A)
1120
(A)
1402
1830
(A)
Started
draindown from 8 percent at
5 to
10 gallons per
minute
(gpm).
Pressurizer
level at
0 percent.
For approximately
20 minutes with no
RCS level instrument available,
draining
was cautiously performed at
5 to 10 gpm..
4
RVLIS upper plenum on scale at
100 to 99 percent
and
tracking.
Stabilized
RCS level at 620 feet (two feet below reactor
vessel
and
5 psig.
Bullseye
was isolated which resulted in the reactor vessel
head
no longer in communication with the pressurizer
and
pressurizer relief tank (PRT).
1830
(A)
Started to isolate
RVLIS for head removal.
1830
1830
(A)
Shift change
(1830 to 0630) in progress.
Started installation of air eductor.
The decision to
isolate
RVLIS and install eductor
was the step in the
sequence
that led to the
RCS level perturbations.
1900
(A)
Air eductor installed.
1900
(A)
1900
2030
2045
(A)
RVLIS taken out of service.
End of shift change with RCS level at the 620 feet elevation
and
5 psig.
When the air eductor
was tested,
a two foot decrease
in
level
was indicated
on NLI-112.
By testing the eductor,
the
reactor vessel
pressure
was inadvertently vented to 0 psig
with the
PRT, pressurizer,
and level instrumentation
being
maintained
at
5 psig.
Also,
some draining of the
SG U-tubes
occurred.
Air eductor tested
again;
a one foot decrease
in level
was
indicated
on NLI-112.
2100
2100
2230
(A)
Rapidly opened
PRT vent valve RC-148 to vent
RCS from 5 psig
to 0 psig.
This caused
the Steam Generator
(SG) U-tubes to
drain,
and level
on sight glass
NGG-100
and NLI-112 rapidly
increased
to off-scale high.
Draining of RCS continues.
2000 gallons drained
from RCS based
on
a 0.5 percent
increase
in RWST.
Draining was stopped
since
NGG-100 was
still not back on-scale.
5
2230
(A)
Shift personnel
caucused
and calculated that approximately
13,000 gallons of water
had drained from the
SG U-tubes.
This ca'iculation
was
based
on
an 'assumption
that. 11.5 feet
of 'water from the
SG U-tubes
was drained
due to the venting
of the
RCS from 5 to 0 psig at 2030.
The decision
was
made
to slowly drain
(40 to 60 gpm) until level
was back on-scale
on NGG-100.
Februar
18
1994
0030
(A)
0200
(A)
Recommenced
draining of the
RCS to obtain
an
on scale
reading for sight glass
NGG-100.
Approximately
5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after going off-scale,
level
indication was back on scale
on NLI-112 and sight glass
NGG-100;
0330
(A)
RCS level
was stable
at 620 feet
and
0 psig with the
SG U-tubes-vented.
0455,
Placed air eductor in service to remove conoseals.
Ins ection Results
The inspector's
review of the activities for the draining of the
RCS on
February
16 through
18,
1994, identified the following concerns
in the
areas of procedures,
training, corrective actions to
a previous event,
equipment status,
and work scheduling
and planning.
a.
Procedures
The inspector identified the following concerns with procedures
01-OHP 4021.002.005,
"RCS Drain to One to Two Feet
Below Reactor
Vessel
Flange with Fuel in Core";
PHI-4090, "Criteria for
Conducting Infrequently Performed Tests or 'Evolutions";
and OHI-
221
"Maintenance of Operations
Department Logs,":
1)
Procedure
01-OHP 4021..002.005
"RCS Drain to One to Two Feet
Below Reactor
Vessel
Flan
e with Fuel in Core"
The inspector
reviewed procedure
01-OHP 4021.002.005
to
determine if the procedure
was adequate
to control the
draining of the
RCS.
This review identified the following
concerns:
The draindown procedure
allowed the shift supervisors
to drain the
RCS without having the
RVLIS in service.
RVLIS, if available,
provided
a mechanism for trending
-
RCS level
between the top the reactor vessel
and the
vessel
Shift supervisors
invoked this option
twice while draining the
RCS.
The first time,
when
commencing the draindown, train
(A) of narrow level
RVLIS was out of service for the modification to
convert the reactor protection
system from analog to
digital,
and train (B) of RVLIS was out of service for
breaker maintenance.
The wide range indication for
train (A) of RVLIS was available.
Also, all of RVLIS
was taken out of service with the
RCS level at
620 feet
and
5 psig pressure,
in preparation
to remove
the reactor
vessel
head.
This premature
removal of
both trains of RVLIS resulted
in operators
having
no
RCS level indication for a 5-hour period when the
was depressurized
shortly after installing the
eductor.
e
The procedure
did not provide the volume of RCS to be
drained or the volume of water expected
from the steam
generator
(SG) U-tubes
when the
RCS was vented from
5 psig to 0 psig.
Therefore,
when the
RCS was vented,
resulting in an off scale indication
on sight glass
NGG-100, the operators
did not know the volume of
.
water to be drained
from the
RCS to restore
RCS level
indication without performing calculations.
The procedure
did not contain
adequate
instructions to
slowly vent the reactor coolant
system
from 5 psig to
0 psig in a controlled manner.
This resulted
in the
rapid depressurization
of the
and subsequent
lost
of level indication.
The procedure
did not contain
any references
between
plant elevations
and the various level instruments.
Therefore,= operating
crews
used personal
not'es
from
previous
draindowns to determine
RCS level
based
on
wide range
The procedure
did not clearly define the plant
conditions required
(RCS at
0 psig) to isolate the
bullseye
and install the air eductor.
2)
Lo
Kee in
and Shift Turnovers
Procedure
OHI-221 "Maintenance of Operations
Department
Logs," Revision
15, step 3.2. I.b for the control
room log
and step 3.3. I.b for the shift supervisor log book, requires
that all significant shift activities
and events,
and all
pertinent information that would assist
in the
reconstruction of a plant event'e
recorded.
The logs were
inadequate
in that the following key plant evolutions were
not properly logged:
~
The calculated
amount of water that was needed
to be
drained
from the
PRT to achieve
a
5 percent level, the
volume of water actually drained,
and the flow path
used to the Reactor Coolant Drain Tank.
The time when
RCS level
was
no longer available
from
pressurizer
level indication.
The time when
RCS level returned
on scale
on wide
range
The time that
RCS level went off scale
high on sight
glass
NGG-100
and the time
RCS level returned
on
scale.
Additionally, calculations for volume changes
were performed
on scratch
paper
and not passed
from one crew to another
during shift turnover.
These calculations
were not kept
which resulted
in some operators
not knowing the quantity of
coolant to be drained.
For example,
the evening shift on
February
16,
1994, did calculations for the quantity of
water needed
to be drained
from the
RCS to reach the reactor
vessel
including the water that would drain when
from the
SG U-tubes.
During the event,
when
RCS level
was
off scale
high on sight glass
NG-100, the shift calculated
that 13,000 gallons of water was
needed to be drained to
obtain
an
on scale reading
on NGG-100.
This calculation
was
written on scratch
paper,
and then selected
information was
entered
into the log.
Also, during this draindown,
there
were several
late entries
in the log relating to important
information.
Based
on the'bove,
the failure to have
an appropriate
procedure
to control the draining of the
RCS,
and the failure to record in
the control
room log or shift supervisor
log book significant
shift activities
and events with other pertinent information that
would assist
in the reconstruction of the reactor coolant
system
draindown event is considered
a violation of Title 10 of the
Code
of Federal
Regulations,
Part 50, Appendix B, Criterion V.
(50-
315/94004-01(DRP) )
During the'eview of the event,
the inspectors
determined that
a
pre-job briefing for draining the
RCS had not been
performed
by
the licensee's
management.
Discussion with licensee's
management
determined that procedure,
PNI-4090 "Criteria for Conducting
Infrequently Performed Tests or Evolutions," did not require
a
pre-job briefing with plant management
in attendance
for each
shift involved in the draining of the
RCS.
The procedure
does
allow management
discretion to conduct
a pre-job briefing for
plant evolutions,
but this discretion
was not invoked for the
,draining of the
on February
16 through
18,
1994.
The
inspectors
were concern that
a pre job briefing was not conducted,
and this matter is considered
an unresolved
item pending further
NRC review (50-315/94004-02).
8
T~rainin
The inspector reviewed the circumstances
that led to the
installation of the air eductor with RCS pressure
at
5 psig.
Through discussions
with licensee
personnel,
the inspectors
determined that the installation of the, air eductor
was placed
on
the schedule without adequate
consideration of the plant status
by
the control
room.
The control room's decision to allow the
installation of the air eductor
was
based
on the refueling outage
schedule,
which identified the necessary
plant condition to
install the eductor
as
RCS level at 620 feet (approximately I foot
below 'the flange).
There was
no consideration
in the schedule for
RCS pressure
during the installation of the eductor.
When the
eductor
was tested,
the reactor vessel
head
was vented,
which
resulted
in the reactor
vessel
being at
a different pressure
(0 psig) than the pressurizer,
PRT,
and the level instrumentation
{5 psig).
This resulted
in an
RCS level indication lower than
actual level.
Also, shortly after testing the eductor,
the control
room directed
operators
in the containment to vent the
RCS through
a connection
to the
PRT.
With the reactor vessel
head at
0 psig; the rapid
venting of the
PRT and pressurizer
resulted
in an
RCS level
change
due to the large volume of coolant drained
from the
SG U-tubes
into the reactor vessel.
The draining of the
SG U-tubes to the
reactor vessel
resulted
in
RCS level going off scale
on sight
glass
NGG-100 for approximately
a 5-hour period with no other
level indication available.
The operators
were not aware of the
effects of rapidly depressurizing
the
RCS.
This was evident
because
of the operators'ubsequent
action to drain
2000 gallons
from the
RCS in an attempt to restore
RCS level indication.
The
operators
proceeded
in the face of uncertainty
by not assessing
the loss of level indication prior to draining the
2000 gallons.
Based
on the above,
the inspectors
had
a concern with the training
of operators
for infrequently performed plant evolutions.
This
matter is unresolved
item pending further review by the licensee
and the
NRC {50-315/94004-03{DRP)).
The licensee
has
agreed
to
respond to this item by August I, 1994.
Previous
Problems with the Drainin
of the
During the draining of the
RCS from the bottom of the pressurizer
to the top of the reactor
vessel
head
on February
17, I994,
no
flow through the bullseye
was observed
by an operator
and verified
by
a second operator.
The bullseye
was installed
on the reactor
vessel
head vent to monitor the status of the
RCS level
between
the bottom of the pressurizer
and the top of the reactor vessel
head during draining.
If flow existed through the bullseye,
the
operators
knew that the
RCS level
was between
the bottom of the
pressurizer
and the top of the reactor
v'essel
head.
head during draining.
If flow existed through the bullseye,
the
operators
knew that the
RCS level
was between the bottom of the
pressurizer
and the top of the reactor vessel
head.
The failure to see flow through the bullseye also occurred during
the draindown of the
RCS on August 5,
1993,
when the reactor
coolant system
was being drained to repair
a reactor
head
conoseal.
As a result,
the reactor
was drained to a lower level
than anticipated prior to valving in sight glass
NGG-100.
The
shift's explanation
in August,
1993,
was that when the bullseye
was monitored for flow, the level
had.- already
been, drained
below
the bullseye connection
on the reactor vessel
vent line.
A condition report
(CR 93-1267)
was issued for the August 5,
1993,
draindown event.
The corrective action consisted of a revision to
procedure,
01-OHP 4021.002.005,
"RCS Drain to One to Two Feet
Below Reactor Vessel
Flange'with
Fuel in Core."
The revision
required that sight glass
NGG-100 be placed in service at
a level
of 5 percent in the pressurizer.
The corrective action was narrow
in scope
and did not adequately
resolve the problem,
since
two
operators
did not observe flow thr ough the bullseye during the
February
16 through
18,
1994, draining of- the
RCS.
The failure to
provide adequate
corrective action to preclude the inability to
use the bullseye during the draining of the
RCS is considered
a
violation of 10 CFR Part 50, Appendix B, Criterion XVI (50-
315/94004-04(DRP)).
E ui ment Status
The inspectors identified that the currently installed
RCS level
instrumentation did not cover the full span
from the top of the
pressurizer
down to the reactor vessel
There
was
approximately
a three foot area
below the pressurizer
and
above
the top of the reactor vessel
where there
was
no installed level
instrumentation.
In addition, the licensee
used
instrumentation, if available,
as
a trending device to monitor
RCS level
between the top of the reactor vessel
and the vessel
At the vessel
flange, the level fell within the scale of
the
NGG-100 gauge glass.
The inspector noted that
01-OHP
4021.002.005
did not require that
RVLIS be available during the
draindown evolution.
The matter regarding full span level
coverage is considered
an Inspection
Followup Item pending further
NRC review (50-315/94004-04(DRP)).
Also, the inspectors
were concerned with the operators'se
of
pressurizer relief tank
(PRT) level instrument indicator,
1-NLA-
351, that
had
a "defective" tag which had
been placed
on the
instrument
on November
18,
1992.
This
PRT level indication was
required to be used during the drain down because
the drain down
procedure,
Ol-OHP 4021.002.005,
required
PRT level to be less
than
5 percent prior to commencing
the draining of the
RCS.
The
operating
crew drained the
PRT to the reactor coolant drain tank
10
appeared
to track, the use of an instrument that was
known to have
accuracy outside of necessary
limits to monitor level in the
PRT,
is considered
a violation of 10 CFR Part 50, Appendix B,
Criterion XII(50-315-94004-05(ORP)).
e)
Schedule
and Plannin
Poor work scheduling
and planning contributed to the perturbations
.
in the
RCS level during the draining of the
on February
17 and
18,
1994.
The following were examples of poor work scheduling
and
planning:
I'oth
trains of RVLIS were taken out of service with the
level at 620 feet
and
5 psig pressure
in preparation
to
remove the reactor vessel
head.
The air eductor
was installed
when plant conditions were not
appropriate for the activ'ity.
The schedule identified that
the eductor
was to be installed
when the
RCS level
was at
620 feet elevation,
without requiring the
RCS to be
depressurized
to 0 psig.
As
a result,
when the
RCS level
was at 620 feet,
maintenance
workers were staged
in
'ontainment
to install the air eductor.
Expediters
repeatedly
telephoned
the control
room requesting
authorization to install the air eductor.
This external
pressure
was
a contributing factor in the
operators'ecision
to install the air eductor with the wrong plant
conditions.
There
was several
hours of delay in venting sight glass
NGG-
100
and level instrument
NLI-112 due to ALARA concerns,
because
the containment
purge
system
was not in service
and
workers did not obtain
enough portable tubing.
The total
delay in putting these
instruments
into service
was
approximately five hours.
However, this delay did not
impact the draining of the
RCS,
since level
was still in the
pressurizer
during this time.
There
was
a delay in testing the eductor after installation,
because
the solenoid valve needed for the operation of the
eductor
was installed in a new location.
This new location
resulted
in maintenance
workers not having enough air line
to test the eductor.
This change
in location of the
solenoid
was not considered
during the preparation of the
work package.
The licensee
issued
Condition Report 94-290
to evaluate this inadequate
work planning
.
Based
on the above,
concerns with work scheduling
and planning are
considered
an Unresolved
)tern pending further review by the
NRC
(50-315/94004-06(DRP)).
11
l'
Root Cause
Anal sis
The inspectors
determined that the major casual
factors for the
level perturbation
event that resulted
in the loss of level indication
for five hours
on February, 17,
1994 were:
~
A draindown procedure that did not provide adequate
instructions
.
to vent the reactor coolant
system from 5 psig to 0 psig in a
controlled manner.
This resulted
in the rapid depressurization
of
the
and subsequent
lost of level indication.
The air eductor
was installed
when plant conditions
were not
appropriate for the activity.
The schedule identified that the
eductor
was to be installed
when the. RCS was at the 620 feet
elevation, without requiring the
RCS to be depressurized
to
0 psig.
/
~
The operating
crew did not maintain adequate
control
when
expediters
repeatedly
telephoned
the control
room requesting
authorization to install the air eductor
Licensee
Immediate Corrective Actions
The licensee
performed
an excellent
sequence
of events root cause
analysis for this event.
The inspector
performed
an independent
sequence
of events
and root cause
assessment
of this event,
then
discussed
the licensee's
sequence
of events
and root cause
assessment
which is still ongoing.
The licensee's
root cause
assessment
agreed
with the inspector's
conclusions.
The immediate
concerns
were
identified and the licensee initiated immediate corrective. actions that
included:
Operating
procedures
01(02)-OHP 4021.002.001,
"Filling and Venting
, the Reactor Coolant System" will be revised to incorporate
lessons
learned
from this event.
The procedure revisions will also
incorporate all applicable
standards
that apply to operation
under
"reduced inventory" conditions.
These
procedure
enhancements
will
be completed prior to replacing the Unit
1 reactor vessel
head
on
the vessel
with fuel in the core
and, for Unit 2, prior to the
next procedure
usage.
Operating
procedures
01(02)-OHP 4021.002.005,
"RCS Draining", will
be revised to incorporate
lessons
learned
from this event.
-The
procedure
revisions will also incorporate all applicable
standards
that currently applied to operation
under "reduced inventory"
conditions.
These
procedure
enhancements
will be completed for
Unit
1 prior to any draindown of the
RCS after the system is
filled and vented following core reload.
These
same
enhancements
will be in,place for Unit 2 prior to the next procedure
usage.
Administrative controls for reactor coolant
system operation at
"reduced inventory" will be reviewed against
lessons
learned
from
12
this event
and will be continuously reviewed against
industry
operating
experience
information.
Enhancements will be made to
reduced
inventory standards,
as appropriate,
prior to operation
at
reduced
inventory levels with fuel in the core (applies to both
Units).
Both units will be provided full-range temporary
RCS level
instrumentation prior to the next draindown of the reactor coolant
system with fuel in the core.
The instrumentation will meet the
Generic Letter 88-17 criteria,
as committed.
An engineering
program will be established
to evaluate
the
feasibility and usefulness
of the RVLIS.system
as
a reactor
coolant
system level indicator during draindown evolutions.
Data
will be gathered
as
a part of this program during the post-
refueling outage
vessel
floodup on Unit 1.
A study will be performed to identify and evaluate full-range
reactor coolant system level indication system,
considering
the
criteria specified in Generic Letter 88-17.
The study will be
completed
by the end of 1994,
and
a document will be available to
the
NRC that describes
the results
and conclusions of the study.
A review of management
effectiveness will be performed.
The
review will be completed
by July 15,
1994, which is prior to the
scheduled-Unit
2 outage.
A document will be available to the
NRC
that describes
the results
and conclusions of this revie~.
Ins
system draindown evolutions will be evaluated
against
the requirements
specified in PHI-4090, "Criteria for
Conducting Infrequently Performed Tests or Evolutions".
The site management staff, production facilitation teams,
and
operating
crew management
have received
an initial briefing on the
February
16 through
18 reactor coolant system level perturbation
event,
including generic implications.
Plant
Management
has historically emphasized
that safety (nuclear,
radiation,
and personnel
safety)
was the "number one" priority
during outage periods,
as well as during normal plant operation.
Management will continue to stress this commitment to safety
during management
meetings
and at other opportunities.
ection Followu
Items
Inspection followup items are matters
which have
been discussed
with the
licensee,
which will be reviewed
by the inspector
and,which involve some
action
on the part of the
NRC or licensee
or both.
An Inspection
Followup Open
Item disclosed
during the inspection is discussed
in
Paragraph
5.d.
13
9.
Unresolved
Items
Unresolved
items are matters
about which more information is required in
order to ascertain
whether they are acceptable
items, violations, or
deviations.
Unresolved
items disclosed
during the inspection
are
discussed
in paragraphs
S..a,
S.b,
and S.e.
10.
Exit Interview (30703)
The inspectors
met with the licensee
representatives
denoted
in
paragraph
1 during the inspection period
and at the conclusion of the
inspection
on March 21,
1994.
The inspectors
summarized
the scope
and
results of the inspection
and discussed
the likely content of this
inspection report.
The licensee
acknowledged
the information and did
not indicate that
any of the information disclosed
during the inspection
could
be considered
proprietary in nature.