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LER-1981-001, No Apparent Flow Observed Through Radiation Monitor R-19 from Steam Generator 21. Caused by Bad Diaphragm in roto-meter Flow Regulator.Flow Meters to Radiation Monitor to Be Modified |
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RESULATORN',NFORMATION DISTRIBUTION +TEN (RIDS)
~'0 419 ACCESSION NBR:8103100369 DOC ~ DATE: 81/03/M NOTARIZED:
NO DOCKETt ¹ FACIL:50 316 Donald C ~
Cook Nuclear Power PlantE Unit 2R Indiana 8
05000316'UTH BYNAME AUTHOR AFFILIATION RISCHLINGiR ~ L, Indiana 8 Michigan Electr ic Co ~
RECIP ~ NAME RECIPIENT AFFILIATION Region ?i Atlanta< Office of the Director SUBJECT'pdated LER 81 001/04X 1 $ on 810112) there was no appar ent flow through radiation monitor R
19 from -steam generator 21 ~
'aused by bad diaphragm in roto meter flow regulator
~ Flow meter s to r adiation moni'tor to be modified.
DISTRIBUTION CODE:
A002S COPIES RECEIVED:LTR ~ ENCL SIZE:
TITLE: Incident'eports NOTES:Send 3 copies of all material to I8E, 05000316'XTERNAL:
ACRS NSIC 46 05 RECIPIENT ID CODE/NAME ACT'ION!
VARGAiS ~
04 INTERNAL~
A/D COMPLSTRU06 A/D MATL 8 QU08 A/D PLANT SYS10, A/D SFTY ASSE12 AEOD AUX SYS BR 15 CONT SYS BR 17 DIR p ENGINEER I20 DIR,SYS INTEG22" EQUIP QUAL BR25.
I8,C SYS BR 29 JORDANgE ~ /IE MATL ENG BR 32'PA OP EX EVAL BR34 POHER SYS BR 36 REACT SYS BR 40 REL 8
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1 RECIPIENT ID CODE/NAME A/D ENV TECH 07 A/D OP REACT009 A/D RAD PROT 11 ACC EVAL BR 14 ASLBP/J',HARD CHEM ENG BR 16 CORE PERF BR 18 DIRr HUM FAC S21-EFF TR SYS BR23 GEOSCIENCES
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,t Iootr4o INDIANA& MICHIGANEIECTRIC COMPANIY DONALDC. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 (616) 465-5901 March 3, 1981 Mr. J.G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 woa 09 ~9Si 9
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Operating License DPR-74 Docket No. 50-316
Dear Mr. Keppler:
Pursuant to the requirements of the Appendix A Technical Specifications, the following report/s are submitted:
RO 81-001/04X-1.
Sincerely,
/or D.V. Shaller Plant Manager
/bab cc:
J.E.
Dolan R.S. Hunter R.W. Jurgensen R.F. Kroeger R.W. Kilburn E.
Swanson/N.
DuBry RO:III R.C. Callen MPSC G. Charnoff, Esq.
J.M. Hennigan W. Lavallee EPRI PNSRC J.F. Stietzel E.L. Townley Dir., IE (20 copies)
Dir., MIPC (2 copies)
Directorate of Licensing o>
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QB03O4S i'4 75 REPORT DATE 80
~03 SECONDARY SYSTEM CHEMICAL CONTAMINATION FROM CONDENSER IN LEAKAGE.
4 DETERMINED THAT ON JAN 12 AT APPROXIMATELY 2200 THERE HAD BEE NRC FORM 366 UPDATE REPORT - PREVIOUS REPORT DATE 02rO>rm'"'"""""""""""
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60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10
~02 DURING NORMAL OPERATION THE S
~06 MONITOR R-19 FROM NUMBER 21 S.G.
THIS IS NON-CONSERVATIVE IN RESPECT TO APPE DI
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13 AT 0318 AND AT 0334 BLOWDOWN WAS AG
~OB THE NORMAL BLOWDOWN TANK WHERE ADDITIONAL EFFLUENT RADIATIO 7
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CODE TYPE Q17 REPoRT
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21 22 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.
TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.
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THE ATTACHED IN DETAIL.
OTHER STATUS QBO N A METHOD OF DISCOVERY
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10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ 6
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10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3 7
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11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 s
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11 12 LOSS OF OR DAMAGETO FACILITY 43 TYPE
DESCRIPTION
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10 DISCOVERY DESCRIPTION Q32 LOCATIONOF RELEASE Q NRC USF. ONLY 68 69
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ATTACHMENT TO LER II81-001/04X-1 SUPPLEMENTAL TO CAUSE DESCRIPTION This incident was reported to Mr. E.
Swanson of the NRC on January 22, 1981.
On January 22, 1981, it was determined that on January 12, at approximately
- 2200, there was no apparent flow through radiation monitor R-19 from number 21 steam generator.
During normal operation, the blowdown effluent would also pass through the steam generator blowdown treatment demineralizers where radiation monitor R-24 is located between the second and thiid demineralizers.
However, while investiga-ting the flow meter problem, the steam generator startup blowdown flash tank was in service, thus making R-19 the only radiation monitor,'hat was monitoring the blowdown effluent.
The startup blowdown flash tank was in service to reduce secondary system chemical contamination from condenser inleakage.
As Unit 2 has been experiencing a primary to secondary leak, routine daily samples are taken for leak rate determination and effluent release quanti-fication.
The activity of the blowdown from the steam generator number 21 was known prior to the incident and the activity levels were lower then had been determined the previous several months.
The startup blowdown flash tank was in service for 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> and 18 minutes, during which time the blow--
down from only number 21 steam generator was unmonitored prior to release to the environment.
Flow from the other three steam generators continued to be monitored during this time period.
Releases were calculated based on data taken on January 12,
- 1981, and the following results obtained:
Parameter Gross beta gamma
~Activit (u Ci/cc)
- - 5 1.94 x 10 Release Total Release (m Ci)
Concentration (u Ci/cc)
- - 9 2.04 x 10 1.75 Tritium Iodine-131
- - 6 5.62 x 10
- - 7 4.82 x 10
- - 10 6.07 x 10-ll 5.20 x 10 0.506 0.043
These results are considered conservative as the use of the startup blowdown flash tank has a dilution effect on all parameters by discharging larger blow-down volumes and replacing it via a high makeup flow.
This is evident by data taken at 0115 hours0.00133 days <br />0.0319 hours <br />1.901455e-4 weeks <br />4.37575e-5 months <br /> on January 13, 1981, during the release, which shows all activities had decreased.
These samples were part of the plants routine daily analysis program.
The results are listed below:
Parameter Gross beta-gamma Tritium Iodine - 131
~Activit (u Ci/cc)
- - 5 1.94 x 10
- - 6 5.62 x 10
- - 7 4.82 x 10 1-12-81
~Activit (u Ci/cc) 1/13/81
- - 5 1.33 x 10
- - 6 5.37 x 10
- - 7 3.13 x 10 During the release, no other alarms or indications of increased primary to secondary leakage were noted.
Radiation monitors R-15, steam jet air ejector, and R-33 gland seal
- exhaust, gave no indication of increased activity.
Estimates or releases were made assuming a constant 500 gallons per day primary to secondary leak rate with coincident lX failed fuel in the core and using the worst case meteorological data.
It was also assumed that.all activity remains in solution until reaching the startup blowdown flash tank.
Under these hypo-thetical worst case conditions, the following exposure rates would exist at the site boundary:
- - 7 8.0 x 10 R/hr whole body from noble gases
- - 7 3.0 x 10 R/hr from iodines with a thyroid dose rate
- - 4 of 2.5 x 10 R/hr.
These estimates would yeild an integrated whole body dose of 0.0047 mR and an integrated thyroid dose of 1 mR.
The estimated release under these hypothetical conditions would be 0.023K of technical specifications or noble gases and 135 of technical specifications for radioiodines.
The summation of all radioiodines in the liquid release would be 46.5X of technical specifications.
In an effort to prevent reoccurrence of this problem, a design change (RFC No.
12-1825) was initiated to modify the flow meters to the radiation monitor, R-19 to include a loss of flow alarm.
In addition, a departmental standing order, TS0-021, was written to provide accurate responses if the condition were to exist again prior to completion of the design change.
This information has been distributed to all plant departments.
Although the incident allowed unmonitored effluent to be released to the environment, sufficient data is available to indicate thatduring the release the levels of radioactivity were low enough not to pose a threat to the health of safety of the public.
The sole purpose in revising this LER is to correct a typographical error for the value stated as the whole body-dose rate -from iodines under hypothetical worst case conditions.
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| 05000315/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000316/LER-1981-001-03, /03L-0:on 810103,annunciator Indicated Loss of Control Voltage to West RHR Pump,Making Train of RHR Inoperable.Caused by Loose Fuse Clip on Main Control Fuses. Clip Adjusted & Breaker Cycled.Pump Placed on mini-flow | /03L-0:on 810103,annunciator Indicated Loss of Control Voltage to West RHR Pump,Making Train of RHR Inoperable.Caused by Loose Fuse Clip on Main Control Fuses. Clip Adjusted & Breaker Cycled.Pump Placed on mini-flow | | | 05000315/LER-1981-001-03, /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased | /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased | | | 05000316/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000316/LER-1981-001-04, No Apparent Flow Observed Through Radiation Monitor R-19 from Steam Generator 21. Caused by Bad Diaphragm in roto-meter Flow Regulator.Flow Meters to Radiation Monitor to Be Modified | No Apparent Flow Observed Through Radiation Monitor R-19 from Steam Generator 21. Caused by Bad Diaphragm in roto-meter Flow Regulator.Flow Meters to Radiation Monitor to Be Modified | | | 05000315/LER-1981-001-04, /04L-0:on 810313 & 0224,unplanned & Unsampled Radioactive Gases Found Released.Caused by Excessive Leakage from Reciprocating Charging Pump Stuffing Box & Leaking Isolated Gas Decay Tank Valves | /04L-0:on 810313 & 0224,unplanned & Unsampled Radioactive Gases Found Released.Caused by Excessive Leakage from Reciprocating Charging Pump Stuffing Box & Leaking Isolated Gas Decay Tank Valves | | | 05000315/LER-1981-002, Forwards Updated LER 81-002/03X-1 & LERs 82-031/03L-0, 82-032/03L-0 & 82-033/03L-0 | Forwards Updated LER 81-002/03X-1 & LERs 82-031/03L-0, 82-032/03L-0 & 82-033/03L-0 | | | 05000316/LER-1981-002-03, /03L-0:on 810103,east Motor Auxiliary Feed Pump Inoperable.Caused by Repair of Emergency Leakoff Line Check Valve FW-153.Check Valve Disc Replaced,Seat Lapped & Spool Piece Installed in Place of Strainer | /03L-0:on 810103,east Motor Auxiliary Feed Pump Inoperable.Caused by Repair of Emergency Leakoff Line Check Valve FW-153.Check Valve Disc Replaced,Seat Lapped & Spool Piece Installed in Place of Strainer | | | 05000316/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000316/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000315/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000315/LER-1981-003-03, /03L-0:on 810212,during Normal Operations,Control Room Cable Vault Left Unattended W/No Fire Watch Posted While Access Door Was Sealed for Testing.Caused by Misunderstanding of Tech Spec 3.7.10.Personnel Reinstructed | /03L-0:on 810212,during Normal Operations,Control Room Cable Vault Left Unattended W/No Fire Watch Posted While Access Door Was Sealed for Testing.Caused by Misunderstanding of Tech Spec 3.7.10.Personnel Reinstructed | | | 05000316/LER-1981-003-03, /03L-0:on 810217 & 0301,ESW Pump 2-E Found Inoperable.Caused by Closed Inlet & Outlet Slide Gate Valves to Strainers on Discharge of ESW Pumps Due to Defective Agastat Timer.Timer Replaced & Backwash Sys Cycled | /03L-0:on 810217 & 0301,ESW Pump 2-E Found Inoperable.Caused by Closed Inlet & Outlet Slide Gate Valves to Strainers on Discharge of ESW Pumps Due to Defective Agastat Timer.Timer Replaced & Backwash Sys Cycled | | | 05000316/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000316/LER-1981-004-03, /03L-0:on 810308,ISI Data Review for Ba Transfer Pump 3 Was Not Reviewed within 96-h Time Limit.Caused by Test Data Being Inadvertently Overlooked by Technical Inservice Insp Coordinator.Card File Developed | /03L-0:on 810308,ISI Data Review for Ba Transfer Pump 3 Was Not Reviewed within 96-h Time Limit.Caused by Test Data Being Inadvertently Overlooked by Technical Inservice Insp Coordinator.Card File Developed | | | 05000315/LER-1981-004-03, /03L-0:on 810328,east Motor Driven Auxiliary Feed Pump Found Removed from Svc Twice for Repairs to ESW 4-inch Centerline Supply valve,WMO-754.Caused by Valve Stem Seized in Body & Twisted.Centerline Valve Replaced W/Pratt Va | /03L-0:on 810328,east Motor Driven Auxiliary Feed Pump Found Removed from Svc Twice for Repairs to ESW 4-inch Centerline Supply valve,WMO-754.Caused by Valve Stem Seized in Body & Twisted.Centerline Valve Replaced W/Pratt Valve | | | 05000316/LER-1981-005-01, /01T-0:on 810331,spray Additive Tank Level Found Below Tech Spec Limit During Removal of Magnetrol for 18 Month Surveillance.Caused by Absence of Alarm Due to Contacts Wired Backwards.Tank Refilled | /01T-0:on 810331,spray Additive Tank Level Found Below Tech Spec Limit During Removal of Magnetrol for 18 Month Surveillance.Caused by Absence of Alarm Due to Contacts Wired Backwards.Tank Refilled | | | 05000315/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000315/LER-1981-005-03, /03L-0:on 810314,breakers for Five Specified Motor Operator Valves Mistakenly Opened in Unit 1 Instead of Unit 2.Caused by Personnel Error.Operator Disciplined & Warning Ltr Issued to Operating Shifts | /03L-0:on 810314,breakers for Five Specified Motor Operator Valves Mistakenly Opened in Unit 1 Instead of Unit 2.Caused by Personnel Error.Operator Disciplined & Warning Ltr Issued to Operating Shifts | | | 05000316/LER-1981-005, Describes 810331 Incident Reported in LER 81-005/01T-0 Re Spray Additive Tank Level | Describes 810331 Incident Reported in LER 81-005/01T-0 Re Spray Additive Tank Level | | | 05000316/LER-1981-006-03, /03L-0:on 810316,during Automatic Load Sequence Surveillance Test,Safety Injection Sys Relay Timers Exceeded Tolerance Allowed by Tech Specs.Caused by Instrument Drift. Component Cooling Water Pump 2E Timer Replaced | /03L-0:on 810316,during Automatic Load Sequence Surveillance Test,Safety Injection Sys Relay Timers Exceeded Tolerance Allowed by Tech Specs.Caused by Instrument Drift. Component Cooling Water Pump 2E Timer Replaced | | | 05000315/LER-1981-006, Forwards Updated LER 81-006/03X-1 & LER 81-059/03L-0 | Forwards Updated LER 81-006/03X-1 & LER 81-059/03L-0 | | | 05000315/LER-1981-006-03, /03L-0:on 810317,ground Detected & Traced to Power Cable for Motor Operated Isolation valve,IMO-910,in Flowpath from RWST to Centrifugal Charging Pumps.Caused by Cable Damaged Near Termination at Motor Operator Junction Box | /03L-0:on 810317,ground Detected & Traced to Power Cable for Motor Operated Isolation valve,IMO-910,in Flowpath from RWST to Centrifugal Charging Pumps.Caused by Cable Damaged Near Termination at Motor Operator Junction Box | | | 05000315/LER-1981-007-03, /03L-0:on 810318,loop 2 T-average & delta-T Indicated Low Temps.Caused by Resistance Temp Detector Producing Erroneous Temp Readings.Detector Replaced & Trip Setpoints Verified | /03L-0:on 810318,loop 2 T-average & delta-T Indicated Low Temps.Caused by Resistance Temp Detector Producing Erroneous Temp Readings.Detector Replaced & Trip Setpoints Verified | | | 05000316/LER-1981-007-03, /03L-0:on 810315 During Operation of 2CD Emergency Diesel in Preparation for Surveillance,Hot Starting Air Line Observed.Caused by Valve Damage & Exhaust Expansion Joint Inner Liner Failure.Intake & Exhaust Valves Replaced | /03L-0:on 810315 During Operation of 2CD Emergency Diesel in Preparation for Surveillance,Hot Starting Air Line Observed.Caused by Valve Damage & Exhaust Expansion Joint Inner Liner Failure.Intake & Exhaust Valves Replaced | | | 05000315/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000315/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000316/LER-1981-008-03, /03L-0:on 810407,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Features Vent Charcoal Filter 2-HV-AES-1 & 14 Nozzles for 2-HV-AES-2 Were Found Partially Plugged.Sys Flushed | /03L-0:on 810407,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Features Vent Charcoal Filter 2-HV-AES-1 & 14 Nozzles for 2-HV-AES-2 Were Found Partially Plugged.Sys Flushed | | | 05000315/LER-1981-008-03, /03L-0:on 810317,large Piece of Herculite Found Securely Fastened in Canopy Fashion Over Walkway & Plastic Pail Found in Vicinity of Lower Ice Condenser Access Door. Cause Not Determined.Canopy Disassembled & Bucket Removed | /03L-0:on 810317,large Piece of Herculite Found Securely Fastened in Canopy Fashion Over Walkway & Plastic Pail Found in Vicinity of Lower Ice Condenser Access Door. Cause Not Determined.Canopy Disassembled & Bucket Removed | | | 05000316/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000316/LER-1981-009, Confirms 810710 Verbal Rept to Region 3 Providing Correction to LER 81-09/03L-0.Written Revision to Be Submitted Under Separate Cover | Confirms 810710 Verbal Rept to Region 3 Providing Correction to LER 81-09/03L-0.Written Revision to Be Submitted Under Separate Cover | | | 05000316/LER-1981-009-03, /03L-0:on 810331,after Entering Mode 6 & Floodup of Reactor Cavity,Routine Analysis of RCS Indicated Chloride Concentration of 0.26 Ppm.Cause Is Undetermined. Contamination Was Reduced by Purification | /03L-0:on 810331,after Entering Mode 6 & Floodup of Reactor Cavity,Routine Analysis of RCS Indicated Chloride Concentration of 0.26 Ppm.Cause Is Undetermined. Contamination Was Reduced by Purification | | | 05000315/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000315/LER-1981-009-03, /03L-0:on 810408,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Feature Charcoal Filter 1-HV-AES-1 Were Found Partially Plugged.Caused by Buildup of Debris in Nozzles.Sys Flushed | /03L-0:on 810408,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Feature Charcoal Filter 1-HV-AES-1 Were Found Partially Plugged.Caused by Buildup of Debris in Nozzles.Sys Flushed | | | 05000315/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000315/LER-1981-010-03, /03L-0:on 810414,root Isolation Valve for Containment Pressure Transmitter PPP-301 Was Found Closed. Cause Unknown.Valve Opened & Modified So That Valve Movement Will Be More Apparent | /03L-0:on 810414,root Isolation Valve for Containment Pressure Transmitter PPP-301 Was Found Closed. Cause Unknown.Valve Opened & Modified So That Valve Movement Will Be More Apparent | | | 05000316/LER-1981-010-03, /03L-0:on 810411,snubbers 1 & 29 Were Found Inoperable.Caused by Fluid Leak on 29 Due to Separation of Joint at End Seal O-ring.O-ring Replaced.Snubber 1 Upside Down Due to Loose Extension Rod Locknut.Locknut Tightened | /03L-0:on 810411,snubbers 1 & 29 Were Found Inoperable.Caused by Fluid Leak on 29 Due to Separation of Joint at End Seal O-ring.O-ring Replaced.Snubber 1 Upside Down Due to Loose Extension Rod Locknut.Locknut Tightened | | | 05000315/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000316/LER-1981-011-03, /03L-0:on 810411,steam Line Pressure Transmitter MPP-210 Was Found Exceeding Allowable Value for Differential Pressure Between Steam Lines.Caused by Instrument Drift. Transmitter Recalibr | /03L-0:on 810411,steam Line Pressure Transmitter MPP-210 Was Found Exceeding Allowable Value for Differential Pressure Between Steam Lines.Caused by Instrument Drift. Transmitter Recalibr | | | 05000315/LER-1981-011-03, /03L-0:on 810413,while Examining Test Data from Type B & C Leak Rate Tests,Jul 1980 Test for Unit 1 Found to Have Exceeded Allowable Value of Tech Specs.Caused by Faulty NESW Check Valves.Valves Repaired | /03L-0:on 810413,while Examining Test Data from Type B & C Leak Rate Tests,Jul 1980 Test for Unit 1 Found to Have Exceeded Allowable Value of Tech Specs.Caused by Faulty NESW Check Valves.Valves Repaired | | | 05000316/LER-1981-012-03, /03L-0:on 810413,cracks Found in Divider Barrier Seal.Cause Unknown.Defective Portions Replaced | /03L-0:on 810413,cracks Found in Divider Barrier Seal.Cause Unknown.Defective Portions Replaced | | | 05000315/LER-1981-012-03, L-0:on 810428,Steam Generator 2,Channel 4 Level Indication Found Indicating High.Caused by Leak on Ref Line of Transmitter BLP-120.Leak Suspected Inside Containment & Will Be Corrected on Next Refueling Outage | L-0:on 810428,Steam Generator 2,Channel 4 Level Indication Found Indicating High.Caused by Leak on Ref Line of Transmitter BLP-120.Leak Suspected Inside Containment & Will Be Corrected on Next Refueling Outage | | | 05000315/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000316/LER-1981-013-03, /03L-0:on 810428,all Charging Pumps Were Removed from Svc Contrary to Tech Spec Requirements.Caused by Leak on East Pump Discharge Isolation Valve CS-300E.Valve Repacked.Drain Valve CS-349 Also Repacked | /03L-0:on 810428,all Charging Pumps Were Removed from Svc Contrary to Tech Spec Requirements.Caused by Leak on East Pump Discharge Isolation Valve CS-300E.Valve Repacked.Drain Valve CS-349 Also Repacked | | | 05000316/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000315/LER-1981-013, Forwards Revised LER 81-013/03X-1 & LER 81-023/03L-0 | Forwards Revised LER 81-013/03X-1 & LER 81-023/03L-0 | | | 05000315/LER-1981-013-03, Source Range Ni Channels Declared Inoperable.Caused by Defective Source Range Detector N-32 Possibly Due to Dried Moisture Connectors. Detector Replaced | Source Range Ni Channels Declared Inoperable.Caused by Defective Source Range Detector N-32 Possibly Due to Dried Moisture Connectors. Detector Replaced | | | 05000316/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000315/LER-1981-014-03, /03L-0:on 810606,during Surveillance insp,non- Penetrating Cracks Were Found in Divider Barrier Seal.Cause Unknown.Defective Portions of Seal Replaced | /03L-0:on 810606,during Surveillance insp,non- Penetrating Cracks Were Found in Divider Barrier Seal.Cause Unknown.Defective Portions of Seal Replaced | | | 05000316/LER-1981-014-03, /03L-0:on 810415,steam Generator Level Protection Set 3 Transmitter BLP-142 Was Found Outside Tech Spec.Caused by Instrument Drift.Transmitter Recalibr | /03L-0:on 810415,steam Generator Level Protection Set 3 Transmitter BLP-142 Was Found Outside Tech Spec.Caused by Instrument Drift.Transmitter Recalibr | |
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