ML17329A329

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Monthly Operating Rept for Nov 1991 for DC Cook Unit 2.W/
ML17329A329
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 11/30/1991
From: Blind A, Gillett W
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9112170005
Download: ML17329A329 (8)


Text

ACCELERATED DIS IBUTION DEMONS ION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9112170005 DOC.DATE:

NOTARIZED: NO DOCKET FACIL:50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

05000316 AUTH.NAME AUTHOR AFFILIATION GILLETT,W.T.

Indiana Michigan Power Co. (formerly Indiana

& Michigan Ele BLIND,A.A.

Indiana Michigan Power Co.

(formerly Indiana 6 Michigan Ele RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

h-operating rept for Nov 1991 for DC Cook Unit 2.W/

911205 ltr.

DISTRIBUTION CODE:

IE24D COPIES RECEIVED:LTR I

ENCL Q SIZE:

TITLE: Monthly Operating Report (per Tech Specs)

NOTES:

D RECIPIENT ID'CODE/NAME PD3-1 LA COLBURN,T.

INTERNAL: AEOD/DOA NRR J3L MPEB10 EXTERNAL EGGG BRYCE g J ~ H NSIC COPIES LTTR ENCL 3

3 1

1 1

1 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME PD3-1 PD AEOD/DSP/TPAB NRR/DOEA/OEAB RGN3 NRC PDR COPIES LTTR ENCL 1

1 1,

1 1

1 1

1 1

1 D

D R

D NOTE TO ALL"RIDS" RECIPIENTS:

D D

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 14 ENCL 14

Indiana Michigan Power Company Cook Nuclear Plant One Cook Place Bridgman, Ml 49106 616 465 5901 December 5,

1991 U.S. Nuclear Regulatory Commission ATTN:

Document Control Desk Washington, D.C.

20555 Gentlemen:

Pursuant to the recpxirements of Donald C.

Cook Nuclear Plant Unit 2 Technical Specification 6.9.1.10, the attached Monthly Operating Report for the month of November 1991 is submitted.

Respectfully, A.A. Blind Plant Manager Attachment co NRC Region III D.R.

Hahn R.C. Callen S.

Hamming J.G.

Keppler INPO Records Center ANI Nuclear Engineering Department D.H. Williams, Jr.

E.E. Fitzpatrick R.L.

Simms J.J.

Markowsky D.A. Timberlake D.W. Paul T.O., Argenta S.H. Steinhart J.L. Leichner J.A. Isom W.T. Gillett E.A. Smarrella J.C. Krieger B.A. Svensson D.F. Krause E.C.

Schimmel 9112170005 911130 PDR ADOCK 05000316 POR

N.R.C.

OPERATING DATA REPORT DOCKET NO.

50-316 DATE 02-Dec-91 COMPLETED BY WT GILLETT TELEPHONE 616-465-5901 OPERATING STATUS"

1. Unit Name D.

C.

Cook Unit 2

2. Reporting Period NOV.91
3. Licensed Thermal Power (MWt) 3411 4.

Name Plate Rating (Gross MWe) 1133

5. Design Electrical Rating (Net MWe) 1090 6.

Maximum Dependable Capacity (GROSS MWe) 1100 7.

Maximum Dependable Capacity (Net MWe) 1090 notes

8. If Changes Occur in Capacity Ratings (Items no.

3 through 7) Since Last Report Give Reasons 9.

Power Level To Which Restricted. If Any (Net MWe) 10.

Reasons For Restrictions. If Any:

This Mo.

Yr. to Date

11. Hours in Reporting Period 720.0 8016.0 12.

No. of Hrs. Reactor Was Critical 607.4 7309 '

13. Reactor Reserve Shutdown Hours 0.0 0.0
14. Hours Generator on Line 590.4 7270.2
15. Unit Reserve Shutdown Hours 0.0 0.0
16. Gross Therm.

Energy Gen.

(MWH) 1912720 24053298

17. Gross Elect.

Energy Gen.

(MWH) 611250 7684420

18. Net Elect.

Energy Gen.

(MWH) 589533 7415525

19. Unit Service Factor 82.0 90.7
20. Unit Availability Factor 82.0 90.7
21. Unit Capacity Factor (MDC Net)
75. 1 84.9
22. Unit Capacity Factor (DER Net) 75.1 84.3
23. Unit Forced Outage Rate 18.0 9.3 24.

Shutdowns Scheduled over Next Six Months (Type, Date,and Refueling outage to begin 920209 for an estimated duration of 90 Cumm.

121968

~ 0 82444.1 0.0 80856.1 0.0 250220351 81471260 78474492 67.6 67.6 61.9 60.2 13 '

Duration):

days.

25. If Shut Down At End of Report Period, Estimated Date of Startup:
26. Units in Test Status (Prior to Commercial Operation):

Forcast INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION Achieved

AVERAGE DAILY POWER LEVEL (MWe-Net)

DOCKET NO.

50-316 UNIT TWO DATE 02-Dec-91 COMPLETED BY WT GILLETT TELEPHONE 616-465-5901 DAY 1

2 3

4 5

6 7

8 9

10 11 12 13 14 15 16 MONTH AVERAGE DAILY POWER LEVEL 1057 1058 1056 1055 1051 1056 1050 1044 1040 1051 1055 1053 1052 1058 491 0

NOV.91 DAY 17 18 19 20 21 22 23 24 25 26 27 28 29 30 AVERAGE DAILY POWER LEVEL 0

0 0

19 466 602 771 1072 1069 1068 1073 1071 1060 1067

UNIT SIKTKGRNS AND HNZR REIXJCZIONS REEQRP MOTH:

November 1991 DOQKZ NO UNIT NAME:

DATE:

CCMPIZTED BY:

TEXZXSONE 50-316 D.C.

COOK UNIT 2 December 5, 1991 E.C. Schhmel (616) 465-5901 MEIHOD OF SHUITING IZCECSEE IXJRATION DONN EVEPZ SYSZEH CMXRKÃZ CAUSE AND CORRECTIVE ACZION TO NO.

DATE TYPE HOURS REASON2 REACIOR3 REPACK NO.

CODE4 mDE PREVENT REQJRRENCE 220 911115 F

129. 6 91W09 A reactor/turbine trip occurred at 1113 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.234965e-4 months <br /> on 911115 when a turbine contzol fluid pressure sensing line was breached to install a test pressure transducer for monitoring purposes.

%he pressure indicator isolation valve leaked through allowing control fluid to escape causing the turbine cantzol valves to go fully closed.

%he resulting rapid increase in steam generator pressure caused the steam generator water levels to shrink.

Ghe reactor tripped on lo-lo steam generator levels causirg the turbine trip.

The turbine contzol system and other ecpipment problems were reImzeed during the outage anal the unit was returned to service at 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> an 911120.

Reactor power reached 10(S RZP on 911123.

1 2

F:

Porced Reason:

S:

Scheduled A:

Equips~~ Failure (Explain)

C:

Refueling D:

Regulatory Restriction E:

Operator Training and License Examination F:

Actministrative G:

Operational Error (Explain)

H:

Other (Explain) 3 Method' Manual 2:

Manual Scram 3:

Automatic Scram 4:

Other (Explain) 4 5

Exhibit G Instnmtions Exhibit I:

Same Source.

for preparation of data entzy sheets for Licensee Event Report (LER) File (NIIREG 0161)

DOCKET NO:

50-316 UNIT NAME:

D.C.

Cook Unit 2 COMPLETED BY: E.C.

Schimmel TELEPHONE'616) 465-5901 DATE:

December 5,

1991 PAGE 1 of 2 MONTHLY OPERATING ACTIVITIES >> November 1991 HIGHLIGHTS The unit entered the reporting period at 100% RTP.

A reactor/turbine trip occurred at 1113 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.234965e-4 months <br /> on 911115 when a

'urbine control fluid pressure indicator sensing line was breached to install a test pressure transducer for monitoring purposes.

The pressure indicator isolation valve leaked through allowing control fluid to escape causing the turbine control valves to go fully closed.

The resulting rapid increase in steam generator pressure caused the steam generator water levels to shrink.

The reactor tripped on lo-lo steam generator levels causing the turbine trip.

The turbine control system and other equipment problems were repaired during the outage and the unit was returned to service at 2050 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.80025e-4 months <br /> on 911120.

Reactor power reached 100% on 911123.

The unit exited the reporting period at 100% RTP.

There were no challenges to the pressurizer safety valves or power operated relief valves.

Gross electrical generation for the month of November was 611250 MWH.

DETAILS 11/15/91 1113 11/20/91 0222 0347 1732 Reactor/turbine trip caused by lo-lo steam generator water levels.

Commenced reactor startup.

The reactor is critical.

The reactor is in Mode l.

2050 The main generator is paralleled to the system power grid.

Commencing unit power increase to 29% RTP.

2335 2351 11/2 1/9 1 042 1 0730 1007 Holding unit power at 29% for chemistry hold.

Commenced unit power increase to 48%.

Hol'ding unit power at 48% RTP to perform quadrant power tilt ratio verification.

Commenced unit. power increase to 58% RTP.

Holding unit power at 58% RTP due to feedwater heater 6B flow imbalance.

DOCKET NO:

50-316 UNIT NAME:

D.C.

Cook Unit 2 COMPLETED BY: E. C. Schimmel TELEPHONE:

(616) 465-5901 DATE:

December 5,

1991 PAGE:

2 of 2 MONTHLY OPERATING ACTIVITIES - NOVEMBER 1991 11/22/91 0324 0440 11/23/91 0810 1130 1705 2329 Commenced unit power increase to 64% RTP.

Holding power at 64% RTP due to condensate flow limit through a single set of feedwater heaters.

Commenced unit power increase to 80% RTP.

Holding power at 80% RTP for main turbine control valve testing.

Commenced unit power increase to 100% RTP.

The unit is at 100% RTP.

DOCKET NO:

50-316 UNIT NAME:

D.C.

Cook Unit 2 COMPLETED BY: E.C.

Schimmel TELEPHONE:

(616) 465-5901 DATE:

December 6,

1991 PAGE0 1 of 1 MAZOR SAFETY-RELATED MAINTENANCE - November 1991 There were no major safety-related maintenance items during the month of November.