05000316/LER-1979-034-03, /03L-0:on 790926,sample Pump for Radiation Monitors R-11 & R-12 Tripped at Frequent Intervals on Two Occasions.Cause Unknown.Pumps Replaced & Tested Satisfactorily.Pumps Scheduled for Periodic Replacement

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/03L-0:on 790926,sample Pump for Radiation Monitors R-11 & R-12 Tripped at Frequent Intervals on Two Occasions.Cause Unknown.Pumps Replaced & Tested Satisfactorily.Pumps Scheduled for Periodic Replacement
ML17326A296
Person / Time
Site: Cook 
Issue date: 10/26/1979
From: Wizner D
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17318A376 List:
References
LER-79-034-03L-01, LER-79-34-3L-1, NUDOCS 7910310407
Download: ML17326A296 (2)


LER-1979-034, /03L-0:on 790926,sample Pump for Radiation Monitors R-11 & R-12 Tripped at Frequent Intervals on Two Occasions.Cause Unknown.Pumps Replaced & Tested Satisfactorily.Pumps Scheduled for Periodic Replacement
Event date:
Report date:
3161979034R03 - NRC Website

text

U. S. NUCLEAR REGULATORYCOMMISSION

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11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION041 EZ LoaoojQ4p NA 7

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10 DISCOVERY DESCRIPTION Q32 80 LOCATION OF RELEASE Q 80 80 80 80 NRC USE ONLY 80 68 69 PHDNE.

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