ML17326A289

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LER 79-048/03L-0:on 790917,sample Pump for Radiation Monitor Was Inoperable Due to Failed motor-to-pump Coupling Insert. Caused by Failure of Rubber Spider in Coupling.Coupling Was Replaced & Air Sampler Tested
ML17326A289
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 10/17/1979
From: Wizner D
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17318A338 List:
References
LER-79-048-03L, LER-79-48-3L, NUDOCS 7910220260
Download: ML17326A289 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7@7)

ENSEE EVENT REPORT

{PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

CONTROL BLOCK:

,Q M I D C C 14 Q 15 LICENSE NUMBER 25 Q4 26 1 1 1 LICENSE TYPE 30 1 Q4~Qo57 CAT 58 7 8 9 LICENSEE CODE CON'T 1' 1 7 7 9 Q9 7 8 soURcE LJLQ6 60 61,0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 5 0 0 0 DOCKET NUMBER 3

Q10 68 Q7 69 EVENT DATE 74 QB 75 REPORT DATE 80 INVESTIGATION OF A LOW FLOW ALARM FOUND THE SAMPLE P P R-11 R-12 TO BE INOPERABLE DUE TO A FAILED MOTOR TO PUMP COUPLING INSERT.

~03 AND 4 THE ACTION RE(UIREMENTS OF T. S. 3.4.6.1 WERE MET. PUBLIC HEALTH AND SAFETY

~OS WERE NOT JEOPARDIZED. A SIMILAR EVENT WAS REPORTED AS R/0 79-012/03L-O.

~OB

~O7

~OB 80 7 8 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~O9 ~BB10 Q>> B Q>> UBQ'~ P N P 18 Q4 UHQ'o 19 ljJ 20 Q'o

'L 7 8 9 11 12 13 SEQUENTIAL OCCURRENCE REPORT REVISION U MiM EVENT YEAR REPORT NO. CODE TYPE LER(RP Q>v RE~oov L7y~l 21 22 23 24 26 K~I 27 LU~29 28 30 31 Uo ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER UAGsL~JQm 33 34 L>JQoo 35

[lJQ>>

36 37 40 lpga 41 Qoo h42 IQo4 UA 43 Qoo 44 0

47 Qoo CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o FAILURE WAS DUE TO FAILURE OF THE RUBBER SPIDER IN THE LOVEJOY L-100 COUPLING. THE COMPLETE COUPLING WAS REPLACED AND THE AIR SAMPLER TESTED.

NO FURTHER ACTIONS ARE PLANNED.

3

~O 7 8 9 80 FACILITY STATUS  % POWER OTHER STATUS Q METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 CO 7

1 5 8

UO 9

E 26 1 10 0 0 12 29 13 NA 44

~A 45 Q31 46 OPERATOR OBSERVATION 80 ACTIVITY RELEASED OF RELEASE CONTENT AMOUNT OF ACTIVITY NA Q NA LOCATION OF RELEASE Q 6 Z Q33 Z Q34 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 v ~00 0 Qoz UZQ38 NA 80 12 77/0gg ogg p 80 7 8 9 11 LOSS OF OR DAMAGE.TO FACILITY TYPE DESCRIPTION Q43 Z Q42 NA 8 9 10 80 NRC USE ONLY o

ISSUED

~NQ44 P U 8 L I CITY DESCRIPTION Q NA O

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e 7 8 9 10 68, 69 80 o D~ G. WIZNER PHDNE(616)465-5901,'EXT 398 F PREPARER

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