Similar Documents at Cook |
|---|
|
LER-1981-010, /03L-0:on 810414,root Isolation Valve for Containment Pressure Transmitter PPP-301 Was Found Closed. Cause Unknown.Valve Opened & Modified So That Valve Movement Will Be More Apparent |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3151981010R03 - NRC Website |
|
text
REGULATOR, NFORHATION DISTRIBUTION TEM (RIDS)
ACCESSION NBR;8105120374 DOC ~ DATE: 81/05/OS NOTARIZED!
NO DOCKET ¹ FACIL:50 3i5 Donald C ~
Cook Nuclear Power Plant~ Unit ir Indiana 8
05000315
'AUTH BYNAME AUTHOR AFFILIATION CAMPBELL"gD~
1ndiana 8 Michigan Electr ic Co.
REC IP ~ NAME RECIPIENT AFFILIATION Region 3iChicagoi Office of the Director
SUBJECT:
LER 81 010/03Lr0:on 810414iroot'solation valve for containment pressure transmitter PPP-301 was found closed.
Cause
unknown,'Valve opened
& modified so that valve movement; will be more apparent'ISTRIBUTION CODE:
A002S COPIES RECEIVED ~ LTR ~ ENCL~
SIZE ~
= ~
TITLE:,Inci dent Reports NOTES:I8E:3 copies all materials 05000315 REC IPIENT ID CODE/NAME ACTION; VAAGA,8 ~
04 INTERNAL'/D COMP&STRU06 A/0 MATL 8 QU08 A/0 PLANT SYS10, A/D SFTY'SSE42'EOD ASLBP/J ~ HARD CHEM ENG BR 16 COAE PERF BR 18 UIAgHUM FAC S21 EFF TR SYS BR23~
GEOSC IKNCKS 26 I &E-05 LIC GUID BR 30 HELH ENG BR 33 OR ASSESS BR 35 R
SS BR39 G FI Oi ROG EVA42'OPIES CTTR ENCL 3
1 1
1 1
1 1
1 3
1 1
1 1
1 1
1 i
1 1
1 1
1 1
1 1
1 1
1 1
1 1
RECIPIENT ID CODE/NAME A/D ENV TECH 07 A/D OP REACT009 A/D RAD PROT 11 ACC EVAL BR 14 AEOD/DMU AUX SYS BR 15 CONT SYS BR i7 DIRg ENGINKERI20 DIRgSYS'NTEG22 EQUIP QUAL SR25 I8,C SYS BR 29 JORDAN'
~/IE MATL ENG BR 32 NRC PDR 02 POWER SYS BR 36 REACT SYS BR 40 REL 8
RISK A 41 STRUCT ENG BR%4 COPIES LTTR ENCL 1
1 i
1 1
3 3
1 1
1 1
1 1
1 1
1 1
1 1i 1
1 1
1 1i 1
i EXTERNALS ACRS NSLC 46 05 16 16 1
1 LPDR 03 TOTAL NUMBER OF COPIES REQUIRED:
LTTR 64 ENCL
t
orlaan
/
laetda INDIANA& MICHIGANELECTRIC COMPANY DONALDC. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 (616) 465-5901 May 5, 1981 Mr. J.G. Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315
Dear Mr. Keppler:
Pursuant to the requirements of the Appendix A Technical Specifications, the following report/s are submitted:
RO 81-010/03L-O.
Sincerely, D.V. Shaller Plant Manager
/bab cc:
J.E.
Dolan R.S. Hunter R.W. Jurgensen R.F. Kroeger R.W. Kilburn E.
Swanson/N.
DuBry RO:III R.C. Callen MPSC G. Charnoff, Esq.
J.M. Hennigan W. Lavallee EPRI PNSRC J.F. Stietzel E.L. Townley Dir., IE (30 copies)
Dir., MIPC (3 copies)
1
~ %~
~
0( l I
,,NRC FORM 366
.'7.77>
LlCENSEE EVENT REPORT J
CONTROL BLOCK:
Qi tPLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)
I 6
~01 N
I 0
0 0 1Q0 0
0 0
0 0
0 0
0 0
0 Q4 1
1 1
1 O~QE 9
LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58
( CON'T 0
1 soURGE LIJOB O
5 O
O O
3 1
5 07O 4
1 4
OS 0
5 0
5 1
QB 7
8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABL.E CONSEQUENCES 010 THE UNIT WAS OPERATING IN MODE ONE ~
THE ROOT ISOLATION VALVE FOR CONTAINMENT PRESSUR
~O3 TRANSMITTER, PPP-301 WAS FOUND CLOSED.
THE VALVE WAS IMMEDIATELYOPENED RESTORING THE LOOP TO OPERABLE STATUS.
PPP-301 PROVIDES INPUT TO PROTECTION SET III OF THE
~OS
~O6
~O7 CONTAINMENT PRESSURE HIGH 2 OF 3 S. I. ACTUATION LOGIC AND THE CONTAINMENT PRESSURE HIGH - HIGH 2 OF 4 CONTAINMENT SPRAY LOGIC.
THIS CONDITION VIOLATES THE REQUIREMENTS OF TECH ~
SPEC ~ 3.3.2. 1 TABLE 3 ~ 3-3.
IT DID NOT PREVENT THE ACTUATION OF EITHER SAFEGUARDS SIGNAL FROM THE REMAINING OPERABLE CHANNELS.
THEREFORE, THE PUBLIC HEALTH
~OS 80 7
8 SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
~OB QTT A
Qn
~XQTE X
X X
X X
X QT4
~ZQ>>
~ZQEE 7
8 9
10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER(RO EVENTYEAR REPORT NO.
CODE TYPE NO.
QTT REPQRT
~01
+
~01 0
Q~
~Ql 3 I1I L=I 0
21 22 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME POMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS'22 SUBMITTED FORM SUB.
SUPPLIER MANUFACTURER
~XQTR ~GQTE
~ZQER
~ZQET 0
0 0
0
~YQEE
~NQEE
~ZQEE Z
9 9
9 Qss 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 p
THE CAUSE FOR THE CLOSED VALVE COULD NOT BE DETERMINED THE SEAL ON THE VALVE WAS FOUND INTACT~
THIS VALVE HAD A CHAIN AND A SEAL.
IT IS A SMALL VALVE AND IT WAS FOUND THAT. THE VALVE POSITION COULD BE CHANGED, DUE TO SLACK IN, THE CHAIN ~
THE CHAINS 3
HAVE BEEN REMOVED FROM THESE SMALL VALVES AND A SEAL ONLY INSTALLED IN SUCH A MANNER THAT ANY MOVEMENT OF THE VALVE WILL BREAK'THE SEAL WHICH WILL BE MORE APPARENT TO 9
11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
Z Q4, NA 9
10 PUBLICITY ISSUED DESCRIPTION~
- LNJQ44, NA 9
10 9
7 8
O 8
7 8
9 FACILITY STATUS
% POWER OTHER STATUS Q s
E Qss ~10 0
Qss NA 7
8 9
10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY [i']
Z Q33 Z
Q34 NA 7
8 9
10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39
~00 0 QMZQEE NA 7
8 9
11 12 13 PERSONNEI. INJURIES 7
8 METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32
~BQ31 OPERATOR OBSERVATION 45 46 LOCATIONOF RELEASE Q NA 45 NRC USE ONLY 80 80 80 80 80 80 NAME OF PREPARER DAVID CAMPBELL 68 69 80 o PH0NE. 616-465-5901 EXT. 1316
s
SUPPLEMENT TO LER 81-010/03L-0 EVENT DESCRIPTION AND PROBABLE CONSE UENCES aiid safety was not affected.
Similar occurrence reported on LER No. 79-018/03L-O.
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS an Operator making routine checks.
lr
~
Q4'
~
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000315/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000316/LER-1981-001-03, /03L-0:on 810103,annunciator Indicated Loss of Control Voltage to West RHR Pump,Making Train of RHR Inoperable.Caused by Loose Fuse Clip on Main Control Fuses. Clip Adjusted & Breaker Cycled.Pump Placed on mini-flow | /03L-0:on 810103,annunciator Indicated Loss of Control Voltage to West RHR Pump,Making Train of RHR Inoperable.Caused by Loose Fuse Clip on Main Control Fuses. Clip Adjusted & Breaker Cycled.Pump Placed on mini-flow | | | 05000315/LER-1981-001-03, /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased | /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased | | | 05000316/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000316/LER-1981-001-04, No Apparent Flow Observed Through Radiation Monitor R-19 from Steam Generator 21. Caused by Bad Diaphragm in roto-meter Flow Regulator.Flow Meters to Radiation Monitor to Be Modified | No Apparent Flow Observed Through Radiation Monitor R-19 from Steam Generator 21. Caused by Bad Diaphragm in roto-meter Flow Regulator.Flow Meters to Radiation Monitor to Be Modified | | | 05000315/LER-1981-001-04, /04L-0:on 810313 & 0224,unplanned & Unsampled Radioactive Gases Found Released.Caused by Excessive Leakage from Reciprocating Charging Pump Stuffing Box & Leaking Isolated Gas Decay Tank Valves | /04L-0:on 810313 & 0224,unplanned & Unsampled Radioactive Gases Found Released.Caused by Excessive Leakage from Reciprocating Charging Pump Stuffing Box & Leaking Isolated Gas Decay Tank Valves | | | 05000315/LER-1981-002, Forwards Updated LER 81-002/03X-1 & LERs 82-031/03L-0, 82-032/03L-0 & 82-033/03L-0 | Forwards Updated LER 81-002/03X-1 & LERs 82-031/03L-0, 82-032/03L-0 & 82-033/03L-0 | | | 05000316/LER-1981-002-03, /03L-0:on 810103,east Motor Auxiliary Feed Pump Inoperable.Caused by Repair of Emergency Leakoff Line Check Valve FW-153.Check Valve Disc Replaced,Seat Lapped & Spool Piece Installed in Place of Strainer | /03L-0:on 810103,east Motor Auxiliary Feed Pump Inoperable.Caused by Repair of Emergency Leakoff Line Check Valve FW-153.Check Valve Disc Replaced,Seat Lapped & Spool Piece Installed in Place of Strainer | | | 05000316/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000316/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000315/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000315/LER-1981-003-03, /03L-0:on 810212,during Normal Operations,Control Room Cable Vault Left Unattended W/No Fire Watch Posted While Access Door Was Sealed for Testing.Caused by Misunderstanding of Tech Spec 3.7.10.Personnel Reinstructed | /03L-0:on 810212,during Normal Operations,Control Room Cable Vault Left Unattended W/No Fire Watch Posted While Access Door Was Sealed for Testing.Caused by Misunderstanding of Tech Spec 3.7.10.Personnel Reinstructed | | | 05000316/LER-1981-003-03, /03L-0:on 810217 & 0301,ESW Pump 2-E Found Inoperable.Caused by Closed Inlet & Outlet Slide Gate Valves to Strainers on Discharge of ESW Pumps Due to Defective Agastat Timer.Timer Replaced & Backwash Sys Cycled | /03L-0:on 810217 & 0301,ESW Pump 2-E Found Inoperable.Caused by Closed Inlet & Outlet Slide Gate Valves to Strainers on Discharge of ESW Pumps Due to Defective Agastat Timer.Timer Replaced & Backwash Sys Cycled | | | 05000316/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000316/LER-1981-004-03, /03L-0:on 810308,ISI Data Review for Ba Transfer Pump 3 Was Not Reviewed within 96-h Time Limit.Caused by Test Data Being Inadvertently Overlooked by Technical Inservice Insp Coordinator.Card File Developed | /03L-0:on 810308,ISI Data Review for Ba Transfer Pump 3 Was Not Reviewed within 96-h Time Limit.Caused by Test Data Being Inadvertently Overlooked by Technical Inservice Insp Coordinator.Card File Developed | | | 05000315/LER-1981-004-03, /03L-0:on 810328,east Motor Driven Auxiliary Feed Pump Found Removed from Svc Twice for Repairs to ESW 4-inch Centerline Supply valve,WMO-754.Caused by Valve Stem Seized in Body & Twisted.Centerline Valve Replaced W/Pratt Va | /03L-0:on 810328,east Motor Driven Auxiliary Feed Pump Found Removed from Svc Twice for Repairs to ESW 4-inch Centerline Supply valve,WMO-754.Caused by Valve Stem Seized in Body & Twisted.Centerline Valve Replaced W/Pratt Valve | | | 05000316/LER-1981-005-01, /01T-0:on 810331,spray Additive Tank Level Found Below Tech Spec Limit During Removal of Magnetrol for 18 Month Surveillance.Caused by Absence of Alarm Due to Contacts Wired Backwards.Tank Refilled | /01T-0:on 810331,spray Additive Tank Level Found Below Tech Spec Limit During Removal of Magnetrol for 18 Month Surveillance.Caused by Absence of Alarm Due to Contacts Wired Backwards.Tank Refilled | | | 05000315/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000315/LER-1981-005-03, /03L-0:on 810314,breakers for Five Specified Motor Operator Valves Mistakenly Opened in Unit 1 Instead of Unit 2.Caused by Personnel Error.Operator Disciplined & Warning Ltr Issued to Operating Shifts | /03L-0:on 810314,breakers for Five Specified Motor Operator Valves Mistakenly Opened in Unit 1 Instead of Unit 2.Caused by Personnel Error.Operator Disciplined & Warning Ltr Issued to Operating Shifts | | | 05000316/LER-1981-005, Describes 810331 Incident Reported in LER 81-005/01T-0 Re Spray Additive Tank Level | Describes 810331 Incident Reported in LER 81-005/01T-0 Re Spray Additive Tank Level | | | 05000316/LER-1981-006-03, /03L-0:on 810316,during Automatic Load Sequence Surveillance Test,Safety Injection Sys Relay Timers Exceeded Tolerance Allowed by Tech Specs.Caused by Instrument Drift. Component Cooling Water Pump 2E Timer Replaced | /03L-0:on 810316,during Automatic Load Sequence Surveillance Test,Safety Injection Sys Relay Timers Exceeded Tolerance Allowed by Tech Specs.Caused by Instrument Drift. Component Cooling Water Pump 2E Timer Replaced | | | 05000315/LER-1981-006, Forwards Updated LER 81-006/03X-1 & LER 81-059/03L-0 | Forwards Updated LER 81-006/03X-1 & LER 81-059/03L-0 | | | 05000315/LER-1981-006-03, /03L-0:on 810317,ground Detected & Traced to Power Cable for Motor Operated Isolation valve,IMO-910,in Flowpath from RWST to Centrifugal Charging Pumps.Caused by Cable Damaged Near Termination at Motor Operator Junction Box | /03L-0:on 810317,ground Detected & Traced to Power Cable for Motor Operated Isolation valve,IMO-910,in Flowpath from RWST to Centrifugal Charging Pumps.Caused by Cable Damaged Near Termination at Motor Operator Junction Box | | | 05000315/LER-1981-007-03, /03L-0:on 810318,loop 2 T-average & delta-T Indicated Low Temps.Caused by Resistance Temp Detector Producing Erroneous Temp Readings.Detector Replaced & Trip Setpoints Verified | /03L-0:on 810318,loop 2 T-average & delta-T Indicated Low Temps.Caused by Resistance Temp Detector Producing Erroneous Temp Readings.Detector Replaced & Trip Setpoints Verified | | | 05000316/LER-1981-007-03, /03L-0:on 810315 During Operation of 2CD Emergency Diesel in Preparation for Surveillance,Hot Starting Air Line Observed.Caused by Valve Damage & Exhaust Expansion Joint Inner Liner Failure.Intake & Exhaust Valves Replaced | /03L-0:on 810315 During Operation of 2CD Emergency Diesel in Preparation for Surveillance,Hot Starting Air Line Observed.Caused by Valve Damage & Exhaust Expansion Joint Inner Liner Failure.Intake & Exhaust Valves Replaced | | | 05000315/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000315/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000316/LER-1981-008-03, /03L-0:on 810407,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Features Vent Charcoal Filter 2-HV-AES-1 & 14 Nozzles for 2-HV-AES-2 Were Found Partially Plugged.Sys Flushed | /03L-0:on 810407,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Features Vent Charcoal Filter 2-HV-AES-1 & 14 Nozzles for 2-HV-AES-2 Were Found Partially Plugged.Sys Flushed | | | 05000315/LER-1981-008-03, /03L-0:on 810317,large Piece of Herculite Found Securely Fastened in Canopy Fashion Over Walkway & Plastic Pail Found in Vicinity of Lower Ice Condenser Access Door. Cause Not Determined.Canopy Disassembled & Bucket Removed | /03L-0:on 810317,large Piece of Herculite Found Securely Fastened in Canopy Fashion Over Walkway & Plastic Pail Found in Vicinity of Lower Ice Condenser Access Door. Cause Not Determined.Canopy Disassembled & Bucket Removed | | | 05000316/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000316/LER-1981-009, Confirms 810710 Verbal Rept to Region 3 Providing Correction to LER 81-09/03L-0.Written Revision to Be Submitted Under Separate Cover | Confirms 810710 Verbal Rept to Region 3 Providing Correction to LER 81-09/03L-0.Written Revision to Be Submitted Under Separate Cover | | | 05000316/LER-1981-009-03, /03L-0:on 810331,after Entering Mode 6 & Floodup of Reactor Cavity,Routine Analysis of RCS Indicated Chloride Concentration of 0.26 Ppm.Cause Is Undetermined. Contamination Was Reduced by Purification | /03L-0:on 810331,after Entering Mode 6 & Floodup of Reactor Cavity,Routine Analysis of RCS Indicated Chloride Concentration of 0.26 Ppm.Cause Is Undetermined. Contamination Was Reduced by Purification | | | 05000315/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000315/LER-1981-009-03, /03L-0:on 810408,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Feature Charcoal Filter 1-HV-AES-1 Were Found Partially Plugged.Caused by Buildup of Debris in Nozzles.Sys Flushed | /03L-0:on 810408,during Fire Protection Spray Sys Surveillance Test,Eight Spray Nozzles for Engineered Safety Feature Charcoal Filter 1-HV-AES-1 Were Found Partially Plugged.Caused by Buildup of Debris in Nozzles.Sys Flushed | | | 05000315/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000315/LER-1981-010-03, /03L-0:on 810414,root Isolation Valve for Containment Pressure Transmitter PPP-301 Was Found Closed. Cause Unknown.Valve Opened & Modified So That Valve Movement Will Be More Apparent | /03L-0:on 810414,root Isolation Valve for Containment Pressure Transmitter PPP-301 Was Found Closed. Cause Unknown.Valve Opened & Modified So That Valve Movement Will Be More Apparent | | | 05000316/LER-1981-010-03, /03L-0:on 810411,snubbers 1 & 29 Were Found Inoperable.Caused by Fluid Leak on 29 Due to Separation of Joint at End Seal O-ring.O-ring Replaced.Snubber 1 Upside Down Due to Loose Extension Rod Locknut.Locknut Tightened | /03L-0:on 810411,snubbers 1 & 29 Were Found Inoperable.Caused by Fluid Leak on 29 Due to Separation of Joint at End Seal O-ring.O-ring Replaced.Snubber 1 Upside Down Due to Loose Extension Rod Locknut.Locknut Tightened | | | 05000315/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000316/LER-1981-011-03, /03L-0:on 810411,steam Line Pressure Transmitter MPP-210 Was Found Exceeding Allowable Value for Differential Pressure Between Steam Lines.Caused by Instrument Drift. Transmitter Recalibr | /03L-0:on 810411,steam Line Pressure Transmitter MPP-210 Was Found Exceeding Allowable Value for Differential Pressure Between Steam Lines.Caused by Instrument Drift. Transmitter Recalibr | | | 05000315/LER-1981-011-03, /03L-0:on 810413,while Examining Test Data from Type B & C Leak Rate Tests,Jul 1980 Test for Unit 1 Found to Have Exceeded Allowable Value of Tech Specs.Caused by Faulty NESW Check Valves.Valves Repaired | /03L-0:on 810413,while Examining Test Data from Type B & C Leak Rate Tests,Jul 1980 Test for Unit 1 Found to Have Exceeded Allowable Value of Tech Specs.Caused by Faulty NESW Check Valves.Valves Repaired | | | 05000316/LER-1981-012-03, /03L-0:on 810413,cracks Found in Divider Barrier Seal.Cause Unknown.Defective Portions Replaced | /03L-0:on 810413,cracks Found in Divider Barrier Seal.Cause Unknown.Defective Portions Replaced | | | 05000315/LER-1981-012-03, L-0:on 810428,Steam Generator 2,Channel 4 Level Indication Found Indicating High.Caused by Leak on Ref Line of Transmitter BLP-120.Leak Suspected Inside Containment & Will Be Corrected on Next Refueling Outage | L-0:on 810428,Steam Generator 2,Channel 4 Level Indication Found Indicating High.Caused by Leak on Ref Line of Transmitter BLP-120.Leak Suspected Inside Containment & Will Be Corrected on Next Refueling Outage | | | 05000315/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000316/LER-1981-013-03, /03L-0:on 810428,all Charging Pumps Were Removed from Svc Contrary to Tech Spec Requirements.Caused by Leak on East Pump Discharge Isolation Valve CS-300E.Valve Repacked.Drain Valve CS-349 Also Repacked | /03L-0:on 810428,all Charging Pumps Were Removed from Svc Contrary to Tech Spec Requirements.Caused by Leak on East Pump Discharge Isolation Valve CS-300E.Valve Repacked.Drain Valve CS-349 Also Repacked | | | 05000316/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000315/LER-1981-013, Forwards Revised LER 81-013/03X-1 & LER 81-023/03L-0 | Forwards Revised LER 81-013/03X-1 & LER 81-023/03L-0 | | | 05000315/LER-1981-013-03, Source Range Ni Channels Declared Inoperable.Caused by Defective Source Range Detector N-32 Possibly Due to Dried Moisture Connectors. Detector Replaced | Source Range Ni Channels Declared Inoperable.Caused by Defective Source Range Detector N-32 Possibly Due to Dried Moisture Connectors. Detector Replaced | | | 05000316/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000315/LER-1981-014-03, /03L-0:on 810606,during Surveillance insp,non- Penetrating Cracks Were Found in Divider Barrier Seal.Cause Unknown.Defective Portions of Seal Replaced | /03L-0:on 810606,during Surveillance insp,non- Penetrating Cracks Were Found in Divider Barrier Seal.Cause Unknown.Defective Portions of Seal Replaced | | | 05000316/LER-1981-014-03, /03L-0:on 810415,steam Generator Level Protection Set 3 Transmitter BLP-142 Was Found Outside Tech Spec.Caused by Instrument Drift.Transmitter Recalibr | /03L-0:on 810415,steam Generator Level Protection Set 3 Transmitter BLP-142 Was Found Outside Tech Spec.Caused by Instrument Drift.Transmitter Recalibr | |
|