ML17319A753

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IE Insp Repts 50-315/80-20 & 50-316/80-16 on 801117-21 & 810113.Noncompliance Noted:Inadequate Pump Run Time During Surveillance & Failure to Establish Ref Valve for Pump Inlet Pressures for Inservice Insp Program
ML17319A753
Person / Time
Site: Cook  
Issue date: 01/22/1981
From: Baker K, Connaughton K, Holzmer M, Peschel J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17319A751 List:
References
50-315-80-20, 50-316-80-16, NUDOCS 8103130119
Download: ML17319A753 (17)


See also: IR 05000315/1980020

Text

U.S.

NUCLEAR REGULATORY COMMISSION

OFFICE

OF INSPECTION AND ENFORCEMENT

REGION III

Reports

No. 50-315/80-20;

50-316/80-16

'ocket Nos. 50-315;

50-316

Licenses

No. DPR-58;

DPR-74

Licensee:

American Electric Power Service Corporation

Indiana

and Michigan Power

Company

2 Broadway

New York, NY

10004

Facility Name:

D.

C.

Cook Nuclear Plant Units

1 6 2

Inspection At:

D.

C.

Cook Site,

Bridgman,

MI

Inspection Conducted:

November 17-21,

1980 and January

13,

1981

Inspectors:

.

M. Peschel

K. R. Baker

A.

Con aughton

I

l>l<A ~h /x.~

M. M.&6lzmer

( Z2. Ri

Approved By: .. Baker, Chief,

Nuclear Support Section

2

Ins ection

Summar

Ins ection on November

17-21

1980 and Januar

13

1981

(Re orts No. 50-315/80-20

No. 50-316/80-16)

Areas Ins ected:

Maintenance

procedures;

maintenance activities; surveillance

procedures;

surveillance activities;

ISI procedures

and activities for pumps

and valves;

licensee

event reports followup and plant tours.

The inspection

involved

a total of 151 inspector-hours

onsite by four NRC inspectors

including

zero inspector-hours offshifts.

Results:

Of the seven areas

inspected,

two apparent

items of noncompliance

were

identified; Inadequate

pump run time during

a surveillance

(Paragraph

3B); and

failure to establish

reference

values for pump inlet pressures

for the ISI

program

(Paragraph

3C).

sl osis 9 Ill"

ill

DETAILS

1.

Personnel

Contacted

>D. Shaller, Plant Manager

"-R. Keith, Operations

Superintendent

R. Dudding, Maintenance

Superintendent

"'E. Smarella,

Technical Superintendent

"J. Stietzel,

QA Supervisor

D. Campbell,

Production Supervisor

>H. Bolinger, ISI Supervisor

W. Golden,

Performance

Engineer

R. Wagner,

Performance

Engineer

E. Kant, Performance

Engineering Supervisor

D. Duncan,

CSI Supervisor

-B. Svensson,

Assistant Plant Manager

T. Beilman, Senior

gA Auditor

The inspectors

also contacted several'ther

licensee

employees,

including operators,

plant engineering

and administrative personnel.

"Denotes

those attending

the exit interview.

2.

Maintenance

a

~

Maintenance Activities

Maintenance activities of safety related

systems

and components

listed below were observed/reviewed

to ascertain

that they were

conducted in accordance

with approved procedures,

regulatory

guides

and industry codes or standards

and in conformance with

Technical Specifications.

The following items were considered

during this review:

The

limitipg conditions for operation

were met while components

or

systems

were

removed

from service;

approvals

were obtained

prior to initiating the work; activities were accomplished

using approved procedures

and were inspected

as applicable;

functional testing and/or calibrations

were performed prior to

returning components

or systems

to service; quality control

records

were maintained; activities were accomplished

by qualified

personnel;

parts

and materials

used were properly'certified;

radiological controls were implemented;

and, fire prevention

controls were implemented.

The following maintenance activities were observed/reviewed:

Unit

1

Unit

1

J.O.

63382

BIT valve replacement

J.O.

63529

West containment

spray

pump weld

repair

"2-

Unit

1

Unit

1

Unit

1

J.O.

55989

J.O.

63544

J.O.

63366

Unit

1

Unit

1

Unit

1

J.O.

59088

J.O.

63554

J.O.

12037

Unit

1

Unit

1

Unit

1

Unit

1

Unit

1

Unit 2

J.O.

12023

J.O.

63393

J.O.

55205

J.O.

63328

J.O.

57377

J.O.

25179

Unit 2

Unit 2

J.O.

24096

J.O.

20665

Unit

1

J.O.

63795

IAB emergency diesel timing check

West MiR pump cleaning

East centrifugal charging

pump seal

rebuilding

West motor driven auxiliary feed

pump

valve repair

Incore flux mapping system drive motor

repair

Containment pressure

indicator repair

Wind speed

and direction recorder

repair

1-CD emergency diesel valve repair

PORV motor repair

RCP seal repair

No.

3 accumulator valve repair

MCC breaker

replacement

Pressurizer

level control circuit

repair

Comparator

and rate circuit repair

Modification of ice condensor

door

frames

The inspector noted several

instances

where Forms

No.

PMI

2290-1

and No. 2290-3 were not fully completed'he

licensee's

management

agreed to take, action to improve performance in this

area.

During a tour it was noted the Unit

1 pressurizer

power operated

relief valve, NRV-151, was closed.

The PORV's had recently

undergone

tests

by the operations

department

to determine

which

valves

were leaking.

A job order had not yet been issued for

this valve.

The licensee

agreed

to insure

a job order was

issued for this valve.

No items of noncompliance

were identified.

b.

Preventive

Maintenance

The preventive maintenance

system

was reviewed to determine if

it was current for safety related

components.

The inspector

observed that attachment

30 of the preventive

maintenance

system,

Plant Winterizing, had not been

completed

in October

as required by the system.

The licensee

stated that

much of the work has been completed

and stated that the remainder

would be completed in a timely manner.

The preventive maintenance

system at present

does not have

a

central status

system,

and many procedures

have

hand written

changes

and additions.

The system is in the process of being

reorganized with a new control system.

The licensee

has

begun

- 3-

a typing and the review/approval

process

to allow the

new

system to be implemented in a timely manner.

No items of noncompliance

were identified.

c.

Facility Procedures

The facility maintenance

procedures

listed below were reviewed

to verify that they were adequate

and consistent with Technical

Specifications.

1.

Maintenance

Procedures

12

MHP

5021.002.003

12

MHP

5021.003.001

12

MHP

5021.009.001

12

MHP

5021.032.001L

MHP

5021.032.001K

2.

Preventive

Maintenance

Procedures

Attachment

10

Attachment

26

No items of noncompliance

were identified.

3.

Surveillance

a.

Procedures

The inspector

reviewed several surveillance tests

selected

from

the Technical Specifications to ensure that the tests

were

covered

by properly approved procedures;

that these

procedures

contained

adequate

preparation

or prerequisites,

included

acceptance

criteria,

and provided for system restoration following

testing.

The following procedures

examined:

OHP.4030.STP.004

OHP.4030.STP.005

OHP.4030.STP.030

THP.4030

~ THP.352

OHP.4030.STP.007

THP.4030.STP.205

THP.4030.STP.216

OHP.4030.STP.013

OHP.4030.STP.020

Athough acceptance

criteria were specified in a section of each

procedure,

there

were

some instances

in which acceptance

criteria

sections

could have been

more complete.

An example is the

15

minute minimum pump run time required by the monthly surveillance

on the Unit

1 centrifugal charging

pumps

as specified in Technical Specification 4.1.2.3.c.

Acceptance criteria for pump run

4

times are not listed in the surveillance

procedure,

although

start

and stop time are recorded.

Other Unit

1 pumps require

the

15 minute minimum run during the monthly surveillances.

No items of noncompliance

were identified.

b.

Completed Surveillances

Completed surveillances

were reviewed for Unit

1 to verify that

surveillances

were performed within the required periodicity

and that the results

were within the Technical Specifications.

A check for completeness

of surveillance

records

was also

made.

Unit

1 Technical Specification 4.1.2.3.c

requires that the

centrifugal charging

pumps

(CCP) be run for a minimum of 15

minutes during the monthly surveillance.

Contrary to the above requirement,

the Unit

1 West

CCP was run for

only five minutes during the monthly surveillance

OHP.4030.STP.004

conducted

on June

16,

1980.

Inclusion of the

15 minute acceptance

criteria in this and

other test procedures,

as discussed

in Paragraph

A (Procedures)

above,

would have possibly prevented this noncompliance.

The

inspector

emphasized

the value of a review of all test procedures

for which this criterion is applicable.

This is an item of noncompliance identified in Appendix A

(50-315/80-20"01).

Records of completed surveillance tests

are required to be

maintained by Technical Specification 6.10.l.d.

The licensee

was unable to produce for review the following of completed

Unit

1 surveillances.

Surveillance Test

Sheet

No.

Date(s)

~Con onent

OHP.4030.STP.030

OHP.4030.STP.030

OHP.4030.STP.030

OHP.4030.STP.030

OHP.4030.STP.030

OHP.4030.STP.013

OHP.4030.STP.020

OHP.4030 'TP.020

OHP.4030.STP.004/005

6.7

6.7

6.5

6.5

6.5

6.1

6.2

6.2

All

January

1-24,

1980

June

1,

1980

June 3,4,5,15,

1980

May 2,

1980

April 14,29,30,

1980

January

31,

1980

February,

1980

May,

1980

July,

1980

N/A

N/A

N/A

N/A

N/A

No.

1 H2 Recombiner

East Train

West Train

Both Pumps

The licensee

has

agreed to locate these

records.

This is con-

sidered

an unresolved

item pending the licensee locating these

records

(50-315/80-20-01).

- 5-

c

~

ISI Operatility Testing Program - Pumps

The inspector

reviewed the licensee's

pump testing program to

verify compliance with the requirements

of 10 CFR 50.55a(g).

Pump test records

revealed that tests

had been

conducted

on all

applicable

pumps at the required frequencies

with properly

approved procedures.

Test methods

were found to be satisfactory.

The licensee

has not established

reference

values for pump

inlet pressure

as required by ASME Section XI Article IWP-3110.

Reference

values provide

a basis for establishing

acceptable

instrument accuracy

not, only to comply with the

ASME Section XI

requirements,

but to provide confidence in test data

used to

measure

pump performance

and establish

pump operability.

This is an item of noncompliance identified in Appendix A (50-315/80-20-02)

and (50-316/80-16-01).

d.

ISI Operability Testing Program - Valves

The inspector

reviewed the licensee's

valve testing program to

verify compliance with the requirements

of 10 CFR 50.55a(g).

Examination of the licensee's

approved ISI valve test program,

status

summaries

and several test procedures

revealed that the

licensee

has performed tests at the required frequencies

against

appropriate

acceptance

criteria.

The licensee is currently in

the process of revising the test program.

The revised program's

requirements will be reflected in the program status

summary

which, according to the licensee, will be updated biweekly.

No items of noncompliance

were identified.

4.

Licensee

Event

Re ort Followu

a

~

(Closed) Unit

1 I.icensee

Event Report

(LER) 80-15/03L-0 dated

July 29,

1980 was reviewed.

This report stated that while in

Mode

6 the train "B" centrifugal charging

pump failed,

due to a

broken shaft, while the train "A" diesel

was out of service.

Core alterations

were halted

and the train "A" diesel

was

placed in service.

The train "B" charging

pump was subsequently

repaired using

a "new" design shaft.

The failed shaft problem

has

been

a recurring problem with the "old" design shaft.

All

pumps

now in operation are using the "new" design shaft.

No

further problems are anticipated.

This item is considered

closed.

No items of noncompliance

were identified.

b.

(Closed) Unit 2 Licensee

Event Report

(LER) 80-26/03L-0 were re-

viewed.

Two check valves

(R-156 and R-157) were recently determined

by the licensee

to be containment isolation valves.

This LER was

submitted to satisfy reporting requirements

concerning previous

-6-

events involving the valves.

The valves were not included in

the type

C leak test prior to November

1978.

Check valve R156

had been installed backward.

On November

18,

1978,

check valve

R156 was

removed

and reinstalled correctly.

Both valves success-

fully passed

the type

C leak test

and were included in the

applicable surveillance test procedure.

The inspector verified

implementation of these corrective actions.

This item is

considered

closed.

No items of noncompliance

were identified.

C.

(Closed

) Unit

1 Licensee

Event Report

(LER) 80-25/03L-0 was

reviewed.

On September

29,

1980,

a glycol isolation valve was

determined

inoperable

upon failure to fully close during containment

isolation valve testing.

The valve was exercised until it

functioned correctly.

Corrective action by the licensee

consisted

of increasing surveillance test frequency

from quarterly to

monthly.

The inspector learned that the valve failed the first

monthly surveillance

performed

on November

13,

1980.

The

licensee

was informed that increased

surveillance testing

as

a

proposed corrective action in the forthcoming LER would be

considered

inadequate

and that cause identification and

a

timely fix should be addressed.

No items of noncompliance

were identified.

d.

(Open) Unit 2 Licensee

Event Report

(LER) 80-32/03L-0 was

reviewed.

This IER stated that on September

4,

1980 during

a

surveillance test to return the East

RHR pump to service after

maintenance

the

pump was unstable

and declared

inoperable.

This was stated

to be the first event of this type.

The licensee

stated that the test procedure

did not provide for removing all

air in the system during filland vent and that the procedure

was

changed to correct this.

The inspector

reviewed the following

records

associated

with the event:

(1)

Unit 2 Control Room Iog July 1,

1980 to September

4,

1980

(2)

Clearance

Permit I.og July 20 to September

4,

1980

(3)

Monthly Opera)jng Reports for September,

August and

July,

1980.

(4)

Condition Report - C/R No. 2-8-80-237

(5)

Condition Report - C/R No. 2-9-80-254

(6)

Job Order Number 00354

(7)

Job Order Number 24250

(8)

1-0HP.4030.STP.005

Revision

8 dated April 2,

1980 with

ten temporary sheets

(9)

2-0HP.4030.STP.005

Revision

3 dated

June

19,

1979 with

17 temporary sheets

1/

I.etters

D. V. Shaller to Director,

OMI and

PC

USNRC dated October

14,

September

12,

and August 6,

1980.

" 7-

(10) 2-0HP.4021.008.001

Filling and Venting of Emergency

Core Cooling System Revision

1 dated April 18,

1978

(ll) SOE Log July 23 to September

4,

1980

(12) Operations

Department

DIR dated October

20 transmitting

completed

STP's to vault.

The report was found to be incorrect

and inaccurate in the

areas

as listed below:

(a)

The surveillance test

was conducted

as

a routine monthly

test

(2-0HP.4030.STP.005),

not a test performed to return

the East

RHR pump to service.

Clearance

Permit logs and

the logs

show that the last time the system

had been

removed

from service

was July 23,

1980 at

1855 hours0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br /> for work on

IRV-310.

The system

was logged

as being returned to service

on July 24,

1980.

(b)

The problem had been observed

on August 4,

1980 while

performing routine surveillance test 2-0HP.4030.STP.005.

Log entries

on August 4,

1980

show the

pump was started

at 0359 hours0.00416 days <br />0.0997 hours <br />5.935847e-4 weeks <br />1.365995e-4 months <br />

and stopped at 0401 hours0.00464 days <br />0.111 hours <br />6.630291e-4 weeks <br />1.525805e-4 months <br />

due to poor suction

pressure.

At 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> the

pump was started after venting.

At 0428 it was stopped

again because

of poor suction.

At

0540 the

pump was again started after venting. It was run

until 0643 hours0.00744 days <br />0.179 hours <br />0.00106 weeks <br />2.446615e-4 months <br />.

A condition report (2-8-80-237)

was

initiated.

The licensee classified the event

as not re-

quiring a LER.

The originator of the condition report con-

ducted the investigation.

The investigation

was essentially

a rehash of the event with the following statement, "I do

not have

any explanation for the air in the system."

PSNRC

review accepted this.

This condition report appears

to have

received

a superficial investigation

and review.

A review

of the operating

and maintenance

history would have revealed

that the maintenance

on July 23,

1980 had been the source of

the air.

The decision that the event

was not reportable at

that time was very questionable

and in retrospect

represents

noncompliance with Technical Specification 6.9.1.8 reporting

requirements.

(c)

Records

show that the last maintenance

performed

on

the East

RHR train prior to the event

was July 23,

1980.

Valves IRV-310 and

RH 128E had packing leaks

repaired

(Job Orders

00354 and 24250).

The East

RHR

train was

removed

from service

on July 23,

1980 at

1855 hours0.0215 days <br />0.515 hours <br />0.00307 weeks <br />7.058275e-4 months <br />

and returned to service

on 1035 hours0.012 days <br />0.288 hours <br />0.00171 weeks <br />3.938175e-4 months <br />

on

July 24,

1980.

The logs do not show that the East

RHR pump was operated

to verify operability nor could

-8-

a completed surveillance test be found that indicated

the train was tested.

The Clearance

Permit 22056

under which the repairs

had been

made

has

been destroyed

(allowable under the licensee's

administrative procedure).

Discussions with the personnel

who developed

the

clearance

indicate that the East

RHR pump was not

tagged out, only the heat

exchanger

and associated

valves.

It is not clear at this time if the heat

exchanger

was drained to facilitate the repairs or if

the fluid drained out of the heat exchanger

during

the repairs.

In any case it does not appear that any

operability test of the

pump was conducted following

the return to service.

The licensee

has

a procedure

for filling and venting, 2-0HP.4021.008.001.

No

completed sign off for this procedure

could be found.

A review of the procedure indicates't

would have

been usable for filling and venting with changes

to

the initial conditions.

It is not clear that changes

to the surveillance pro-

cedure

2-0HP.4030STP.005 will prevent the event from

happening

again

as the procedure

was not used to

return the system to operation.

The real problem

appears

to be lack of an effective policy on the

return to service of safety related

equipment that

include an evaluation of the method of removal from

service,

maintenance

performed,

procedures

used

and

what procedures

are to be used during the return to

service

and that, equipment

be test operated.

The air introduced into the East

RHR train degraded

the performance

'f

that train such that it could not be relied upon to fulfillthe

LCO with respect

to a large break loss of coolant accident

and

insure continued operation of the East

RHR pump during small break

loss of coolant accident.

In the case of the large

LOCA the air induced into the

RHR pump

suction by the miniflow line from the heat exchanger outlet would

produce

a reduction in head

developed

by the pump,

as observed

by

the licensee

on August 4 and September

4,

1980.

This would delay

injection by this

RHR pump as reactor coolant system pressure

would

need to decay further than that assumed in the accident analysis

before injection occurred.

Also the entrained air in the injection

water would reduce the injection flow rate until flushed into the

Reactor Coolant System.

In case of a small break

LOCA the

RHR pump would be required to

operate for a period of time on miniflow,

This is the

same

mode of

operation that the pump is tested

under during the monthly surveillance

test.

During the August and September tests

the operators

intervened

and stopped

the pump when the pressures

and currents

were erratic,

indicating cavitation and abnormal

pump performance.

Given these

indications they would have probably also stopped

the pump in the

event of a

LOCA to prevent

damage

to the pump.

Hence, it would have

been unavailable until the operator

had time to investigate

the cause

of the erratic performance.

The following caution notes

from the

RHR

pump technical

manual are quoted to show the manufactures

concern

regarding operation of the

pump with air in the system.

CAUTION

"BEFORE STARTING OR WHILE OPERATING THE PUMP THE CASING AND SUCTION

LINE MUST BE COMPLETELY FILLED WITH THE LIQUID BEING PUMPED.

THE

ROTATING PARTS

DEPEND

ON THIS LIQUID FOR LUBRICATION AND THE PUMP

MAY SEIZE IF OPERATED WITHOUT LIQUID.

THE CASING AND SUCTION LINE

MUST BE FILLED WITH LIQUID DURING STARTING, OPERATION AND SHUTDOWN

PERIODS."

CAUTION

"1.

NEVER OPERATE THE RESIDUAL HEAT REMOVAL PUMPS

WITHOUT PUMP/SYSTEMS

BEING COMPELTELY PRIMED.

2

.

~

~

~

~

~

~

~ J

~

3.

~

~

~

~

~

~

4.

WHEN OPERATING FOR

SOME TIME AT REDUCED CAPACITY) MUCH OF THE

PUMP

HORSEPOWER WILL GO INTO THE LIQUID IN THE FORM OF HEAT.

A BY-PASS MUST BE PROVIDED UNDER THESE CONDITIONS TO PREVENT THE

LIQUID FROM BECOMING HOT ENOUGH IN THE PUMP TO VAPORIZE.

FOR

CONTINUOUS PUMP OPERATION,

THE MINIMUMFLOW FOR SAFE

OPERATION OF THIS PUMP IS 500 GPM."

The function of the East

RHR train could have been significantly degraded

during this time period

as described

above but it still may have provided

a portion of its design capability for accident mitigation.

The Technical

Specification Limiting Conditions for Operations implicitly require the

equipment

be at full capacity

and reliability.

This was not the case

with the East

RHR train between July 23,

1980

and September

4,

1980.

On January

13,

1981

a meeting

was held in the Region III office to discuss

this event with the licensee.

Attending for the licensee

were:

J. Dolan, Vice Chairman Engineer

R. Hunter, Executive Vice President for Construction

and Nuclear Engineering

B. Svensson,

Assistant Plant Manager

R. Keith, Operations

Superintendent

A. Grimes, Chief Mechanical Engineer

S. Milioti, Assistant Division Head Nuclear Engineering

Region III personnel

attending were:

J. Keppler, Regional Director

R. Heishman,

Chief, Reactor Operations

and Nuclear Support Branch

A. Davis, Deputy Director

10-

C. Norelius, Regional Enforcement Coordinator

D. Boyd, Section Chief, Projects

Section

4

K. Baker, Section Chief, Nuclear Support Section

2

E. Swanson,

Senior Resident

Inspector

The licensee outlined the results of his review.

The licensee believes

that the quarterly portion of the surveillance test introduces

the air

into the systems.

The licensee is investigating this and other possible

causes.

The licensee

stated

the problem had occured

again during the

January

4,

1981 test.

The licensee

stated that the test frequency

would be increased

to weekly until the source of the air was identified.

In addition he would analyze

the effects of the air on system performance

during large

and small loss of coolant accidents.

This matter is considered

unresolved

pending completion of the licensee's

review and subsequent

review of these results

by Region III.

5.

Tours

The inspectors

toured various portions of the facility to observe

activities in progress.

The inspector noted that fire doors

on the north end of the Auxiliary

feed water pump area

were wired and blocked open.

These

doors are

U.L. three hour rated doors.

This is considered

an unresolved

item

pending review of the licensee's fire hazard analysis

and NRR's

SER.

(50-315/80-20-02)

(50-316/80-16-01)

6.

Unresolved

Items

Unresolved

items are matters

about which more information is required

in order to ascertain

whether they are addeptable

items,

items of

noncompliance

or deviations.

Unresolved

items during this inspection

are discussed

in Paragraphs

3,

4 and 5.

7.

Exit Interview

The inspectors

met with licensee

representatives

(denoted in Para-

graph

1) at the conclusion of the inspection

on November 21,

1980.

The inspectors

summarized

the purpose,

scope

and findings of the

inspection.

- 11 "

I

I