ML17317B500

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IE Insp Repts 50-315/79-10 & 50-316/79-07 on 790521-24. Noncompliance Noted:Failure to Develop Repair Procedures Prior to Beginning of Work
ML17317B500
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 06/28/1979
From: Danielson D, Key W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17317B498 List:
References
50-315-79-10, 50-316-79-07, 50-316-79-7, NUDOCS 7908290529
Download: ML17317B500 (5)


See also: IR 05000315/1979010

Text

U.S.

NUCLEAR REGULATORY COMMISSION

OFFICE

OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-315/79-10;

50-316/79-07

Docket No. 50-315;

50-316

License

No. DPR-58;

DPR-74

Iicensee:

American Electric Power Service

Corporation

Indiana

and Michigan Power

Company

2 Broadway

New York, NY

10004

Facility Name:

D.

C.

Cook Nuclear Power Plant, Units

1 and

2

Inspection At:

D.

C.

Cook Site,

Bridgman, Michigan

Inspection

Conducted:

May 21-24,

1979

Inspector:

W. J.

Key

Approved By:

D.

. Danielson,

Chief

Engineering Support Section

Ins ection Summar

Ins ection on

Ma

21-24

1979

(Re ort No. 50-315/79-10

50-316/79-07)

piping.

Observation of feedwater pipe crack repair activities.

The

inspection involved

a total of 28 inspector-hours

on site by one

NRC

inspector.

Results:

Of the two areas

inspected,

no apparent

items of noncompliance

or deviations

were identified in one area;

one apparent

item of noncom-

pliance

was identified in one area (infraction - failure to .develop

repair procedures prior to starting work - Paragraph

1).

DETAILS

Persons

Contacted

Indiana

and Michi an Power

Com an

(IBM)

+D. Shaller, Plant Manager

  • B. Svensson,

Assistant Plant Manager

  • J. Stietzel, Quality Assurance

Supervisor

G. Montenegro, Quality Control Supervisor

H. Bolinger, Assistant ISI Coordinator

American Electric Power Service

Cor oration

(AEP)

J. Jensen,

NSSS Engineer

D. Patience,

Metallurgist

Michi an De artment of Labor

A. Kozlowski, Boiler Division Supervisor

  • Denotes those present at the exit interview.

Functional or Pro

ram Areas Ins ected

1.

Feedwater

S stem Pi in

Cracks - Units

1 and

2

Due to unidentified nonradioactive

leakage of about

3

GPM into the

containment building, Unit 2 was shut

down on May 19,

1979.

The

licensee's

inspection revealed

through wall cracking in the 16" 90

elbow on feedwater

system loops

1 and 4.

The cracking is circumferential

and up stream of the weld joining the elbow to the steam generator

nozzle.

On May 21,

1979, the inspector arrived on site to examine the cracking

and to review the licensee's

repair activities.

The inspector

observed

excavation of the defective areas in process;

excavation

had started

on May 20,

1979.

A review of the licensee's

activities

to date indicated that the extent

and cause of cracking had not been

determined

and procedures

to adequately

control the repair activities

had not been established

as required by Technical Specification 6.8.1

and

ASME Section XI.

This is an item of noncompliance identified

in Appendix A.

(316/79-07-01)

The licensee

stopped excavation of the defective areas

and developed

special procedures

for the repair activities.

- 2-

Additional excavation of the defective areas failed to clear the

defects.

The licensee

then performed radiographic

examination of

the Unit 2 loops

1 and

4 affected

areas

and revealed

more extensive

cracking.

The affected areas

of loops

2 and

3 were radiographed.

The licensee

then radiographically

examined the

same

area

on three

loops of Unit 1 and revealed

cracking as in Unit 2.

Due to water

in loop 4, this area

could not be examined by the end of this inspection.

The inspector

reviewed the radiographs,

confirming that all were

cracked.

Limited ultrasonic examination

was performed by Southwest

Research

Institute

(SWRI) with confirmed reflectors

from the cracked

area of

the elbow.

A boat sample

was

removed from Unit 1, loop 3, for

analysis, half was sent to Chicago Service Laboratory and half was

sent to Westinghouse.

Other samples

were taken from Unit 1, loop 2,

Unit 2, loops 1, 2, 3,

and 4.

The

NRC was supplied with a ring

sample

from Unit 2, loop 2, for independent

analysis.

Except

as noted,

no items of noncompliance

or deviations

were identified.

2.

Review of As Build Documentation

The inspector

reviewed the original installation documentation of

fit-up and welding of the elbow to steam generator

nozzles.

Documentation indicates that installation was in accordance

with

procedures,

and the radiographic film of welds

shows

them to meet

code acceptance

requirements.

3.

Review of Re air Procedures

The inspector

reviewed the following procedures

that are to be used

for feedwater piping repair activities.

a.

Procedure

No.

12 MHP-SP-001, Revision 0, dated

May 28,

1979,

titled "Special Procedure for Steam Generator

Feedwater Inlet

Nozzle Elbow Repair."

This procedure will be revised

as needed

when more analysis information is generated.

b.

Instruction No. PMI-1010, Revision 3, dated August 30,

1976,

titled "Organization and Responsibilities

of AEPSC and

IBM

Power Companies."

c.

Welding Procedure

No. 23.88,

23 '8a,

and 1.3e.

No items of noncompliance

or deviations

were identified.

a

4.

Exit Interview

The inspector

met with licensee

representatives

(denoted in the

Persons

Contacted

paragraph)

at the conclusion of the inspection

on

May 24,

1979.

The inspector

summarized

the scope

and findings of

the inspection,

and discussed,

in detail, the item of noncompliance

identified in Appendix A of this report.

4

1 ~

a