05000315/LER-1979-027-03, /03L-0 on 790416:during Refueling W/Emergency Diesel Generator AB inoperable,600 Volt Bus 11D Made Inoperable by Removal of Normal Feed Breaker T1112 for Cleaning.Caused by Personnel Error.Operators Reinstructed

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/03L-0 on 790416:during Refueling W/Emergency Diesel Generator AB inoperable,600 Volt Bus 11D Made Inoperable by Removal of Normal Feed Breaker T1112 for Cleaning.Caused by Personnel Error.Operators Reinstructed
ML17317B186
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 05/09/1979
From: Lease R
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B184 List:
References
LER-79-027-03L, LER-79-27-3L, NUDOCS 7905150438
Download: ML17317B186 (2)


LER-1979-027, /03L-0 on 790416:during Refueling W/Emergency Diesel Generator AB inoperable,600 Volt Bus 11D Made Inoperable by Removal of Normal Feed Breaker T1112 for Cleaning.Caused by Personnel Error.Operators Reinstructed
Event date:
Report date:
3151979027R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION ICENSEE EVfNT REPORT QI (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 6 0 Q'4

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~os 600 VOLT BUS 11D WAS ALSO MADE INOPERABLE BY REMOVAL Of NORMAL FEED BREAKER TllD2 FOR CLEANING AND INSPECTION.

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TOTAL TIME INOPERABLE IIAS 1

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