05000315/LER-1978-066-03, /03L-0 on 781229:during Routine Startup,Rod Position Indication for Rods F-4,D-6 & K-6 Exceeded 12 Step Limit of Tech Specs.Caused by Drift of Signal Conditioning Modules

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/03L-0 on 781229:during Routine Startup,Rod Position Indication for Rods F-4,D-6 & K-6 Exceeded 12 Step Limit of Tech Specs.Caused by Drift of Signal Conditioning Modules
ML17317A888
Person / Time
Site: Cook 
Issue date: 01/16/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317A880 List:
References
LER-78-066-03L, LER-78-66-3L, NUDOCS 7901220137
Download: ML17317A888 (2)


LER-1978-066, /03L-0 on 781229:during Routine Startup,Rod Position Indication for Rods F-4,D-6 & K-6 Exceeded 12 Step Limit of Tech Specs.Caused by Drift of Signal Conditioning Modules
Event date:
Report date:
3151978066R03 - NRC Website

text

NRC FORM 366 I7177)

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LICENSEE CODE 14 15 U. S. NUCLEAR REGULATORY COMMISSION LlCENSEE EVENT REPORT Q1 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 0 0

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I I PE~I 25 26 LICENSE TYPE 30 57 CAT 58 LICENSE NUMBER CON'T

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6 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 DURING A ROUTINE START-UP ROD POSITION INDICATION FOR RODS F-4 D-6 AND K-6 80 QB EXCEEDED THE TWELVE STEP LIMIT IMPOSED BY T.S. 3.1.3.2.

THE ACTION STATEMENT REQUIREMENTS WERE OBSERVED WITH INDICATION RETURNED TO NORMAL WITHIN THE

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~07 SPECIFIED TIMIE,LIMIT.

SIMILAR OCCURRENCES INCLUDE: 050-0315/76-13,44 54'315 77-27 28 33 34 0315/78-04,07,38,46,64:

050-0316/78-07,08,22,31,41,64,75 84 AND 93 ~

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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.

CODE TYPE NO.

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COMPONENT TAKEN ACTJON ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB.

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Q" 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27

~10 IN ALL CASES IT WAS DISCOVERED THAT THE SIGNAL CONDITIONING MODULES HAD DRIFTED

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EACH MODULE WAS ADJUSTED FOR THE CORRECT INDICATION FOLLOWING VERIFICATION OF THE SECONDARY COIL VOLTAGES.

AN ENGINEERING REVIEW IS IN PROGRESS TO DETERMINE THE CAUSE OF THIS RECURRING PROBLEM.

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FACILITY STATUS

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10 12 13 44 ACTIVITY CONTENT REL~SED OF RELEASE AMOUNTOF ACTIVITY Q3 Z

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10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION QSB 7 ~00 0

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8'9 11 12 13 PERSONNEL INJURIES

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NA 80 80 80 7 T Yz2D /yp 80 80 80 NRC USE ONLY ESO 2

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68 69, PHQNE'16-465-METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32

~A QRE OPERATOR",OBSERVATION 45 46 LOCATIONOF RELEASE Q NA 45

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