ML17317A887

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LER 78-065/03L-0 on 781229:indication for Pressurizer Level Channel 2 Deviated Approx 5% from Other 2 Channels.Caused by Gas Pocket in Sensing Line
ML17317A887
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/16/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317A880 List:
References
LER-78-065-03L, LER-78-65-3L, NUDOCS 7901220132
Download: ML17317A887 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT E

CONTROL BLOCK: QI {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

~

I 6

~ol M I D C C 1 QG 0 0 0 0 0 0 0 0 0 0 0 Q34 1 1 1 1 QA IQE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 7 8 9 LICENSEE CODE CON'T 7 8 SOURCE ~LQB 60 61 0 5 0 0 0 DOCKET NUMBER 3 1 5 68 Q7 69 1 2 2 9 EVENT DATE 7 8 74 Qs 0 75 I I REPORT DATE 6 7 80 Q

EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 ON 12 29 78 THE INDICATION FOR PRESSURIZER LEVEL CHANNEL TWO WAS DISCOVERED TO HAVE A DEVIATION OF APPROXIMATELY FIVE PER CENT FROM THE OTHER TWO CHANNELS ~ THE CHANNEL TWO BISTABLES WERE PLACED INTO THE TRIP MODE PURSUANT TO T S~ ~ TABLE 3 ~ 3-3

~O4 ITEM 1D ACTION STATEMENT 14B. SIMILAR OCCURRENCES INCLUDE RO 050-315/78-10,41

~06 59 AND 050-316/78-61.

~O7

~os 80 7 8 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~IA QK 10 QE ~ZQ13 12 I

13 N S T R 0 18 QA ~TQEE 19

~ZQ1E 20 7 8 9 11 SEQUENTIAL OCCURRENCE REPORT REVISION Q11 LERIRP REFDRT ACTION FUTURE

~~

EVENT XEAR 21 22 EFFECT

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23 SHUTDOWN

~06 24 REPORT NO.

B 26

~~

27

~03 28 ATTACHMENT CODE 29 NPRDMI TYPE

~L 30 PRIME COMP.

~

31 NO.

32 0

COMPONENT TAKEN ACTION ON PLANT'ETHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~QEE~ÃQ13 ~ZQ23 ~ZQ>> O O O O ~NQ23 ~NQEA +NQEE B 0 0 0 Q23 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS A27 THE CAUSE OF THE PROBLEM WAS ATTRTBUTED TO A GAS POCKET LOCATED IN THE SENSING LINE. THE SENSING LINE WAS REFILLED TO REMOVE THE GASES AND UPON RESTORATION, CHANNEL INDICATION RETURNED TO NORMAL. A DESIGN CHANGE (RFC-12-1598) HAS BEEN ISSUED TO RECTIFY THIS PROBLEMS 4

80 7

~l~

8 9 FACILITY STATUS D QEE ~00

% POWER 0 QEG OTHER STATUS NA

~

~p METHOD OF DISCOVERY

~BQ31 CHANNEL CHECK DISCOVERY DESCRIPTION Q32 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE 7 8 9 Z Q ~ZQ34 10 11 NA 44 45 NA 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION QSB 7 8 9 o o oQ 11 12 FACILITV 7 ac lao a(3 ~ 80 80 EOEE OF OR DAMAGE TO QAE TYPE DESCRIPTION Z Q4. NA 8 9 10 80 7

P U 8 L I CITY NRC USE ONLY ISSUED DESCRIPTION KZ &NQ44 8 9 10 NA 68 69, 80 o o

2 0

T~ P ~ Bei lmBn PHDNE, 61 6 465 5901 NAME OF PREPARER

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