05000315/LER-1978-042-03, /03X-1 on 780710:during Startup Testing,Flux Map Measurement Was Not Processed During Specified Time Limit. Though Flux Map Was Obtained,It Was Not Processed Due to Change in Manpower Requirements

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/03X-1 on 780710:during Startup Testing,Flux Map Measurement Was Not Processed During Specified Time Limit. Though Flux Map Was Obtained,It Was Not Processed Due to Change in Manpower Requirements
ML17317A886
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/16/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317A880 List:
References
LER-78-042-03X, LER-78-42-3X, NUDOCS 7901220127
Download: ML17317A886 (3)


LER-1978-042, /03X-1 on 780710:during Startup Testing,Flux Map Measurement Was Not Processed During Specified Time Limit. Though Flux Map Was Obtained,It Was Not Processed Due to Change in Manpower Requirements
Event date:
Report date:
3151978042R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION NRC F M 366 (7 77)

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9 QB 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 DURING INITIAL START UP TESTING FOLLOWING A REFUELING OUTAGE THE F

MEASUREMENT REQUIRE D BY T.S. 4.2. 2. 2 dl A WAS NOT PROCESSED WITHIN THE SPECIFIED TIME LIMIT OF 24 HOURS FOLLOWING A RTP INCREASE OF GREATER THAN 20 PER" CENT ~

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10 11 12 13 18 19 20 SEQUENTIAI.

OCCURRENCE REPORT REVISION LF R]RP EVENT YEAR REPORT NO.

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~ZQ25 Q26 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 THE REQUIRED FLUX MAP WAS OBTAINED WITHIN 24 HOURS FOLLOWING THE POWER INCREASE

HOWEVER, DUE TO MANPOWER REQUIREMENTS DURING THIS TESTING PERIOD WAS NOT PROCESS WITHIN THE TIME LIMIT TO DETERMINE THAT F (Z)

REMAINED WITHIN ITS LIMIT.

THE MAP WAS PROCESSED APPROXIMATELY 48 HOURS FOLLOWING THE POWER INCREASE WITH DISCOVERY DESCRIPTION Q32 80 80 LOCATIONOF RELEASE Q 80 44 80 7 TG/QgDI'gy 80 80 NRC USE ONLY EVO 80 0a 68 69, 616-465-5901 NAME OF PREPARER T. P.

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SATISFACTORY RESULTS.

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10 12 13 44 45 46 ACTIVITY CONTENT RE4$ ASED OF RQ.EASE AMOUN7'F ACTIVITY EZ '>>

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10 45 PERSONNEL EXPOSURES Q

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11 12 LOSS OF OR DAMAGE.TOFACILITYQ43 TYPE

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10 PUBLICITY ISSUED DESCRIPTION ~~

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SUPPLEMENT TO LER¹ 78-042/03X-1 SUPPLEMENT TO CAUSE DESCRIPTION SUBSEQUENT TO THIS EVENT NUCLEAR ENGINEERING PERSONNEL HAVE REVIEWED THE ADMINISTRATIVE REQUIREMENTS FOR THE PERFORMANCE, COMPLETION AND REVIEW OF SURVEILLANCE TESTS.

NO FURTHER ACTION IS PLANNED.