ML17312A554

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Insp Repts 50-528/95-25,50-529/95-25 & 50-530/95-25 on 951217-960127.Violations Noted.Major Areas Inspected:Onsite Review of Event,Operational Sv,Maint & Surveillance Observations,Onsite Engineering & Plant Support Activities
ML17312A554
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 02/22/1996
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312A552 List:
References
50-528-95-25, 50-529-95-25, 50-530-95-25, NUDOCS 9602260382
Download: ML17312A554 (62)


See also: IR 05000528/1995025

Text

ENCLOSURE

2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/95-25

50-529/95-25

50-530/95-25

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating

Station,

Units 1,

2,

and

3

Inspection At:

Haricopa County,

AZ

Inspection

Conducted:

December

17,

1995,

through January

27,

1996

Approved:

Inspectors:

K. Johnston,

Senior Resident

Inspector

D. Garcia,

Resident

Inspector

J.

Kramer,

Reside

spector

>rsc

, , ie

,

e

r

r

s

anc

Z ZZ- Q

ate

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of onsite

review of an event,

operational

safety verification, maintenance

and

surveillance

observations,

onsite engineering,

plant support activities,

inspection

followup items,

and review of licensee

event reports

(LERs).

Results

Units

1

2

and

3

Plant

0 erations

Inadequate

communications

between

the operations,

maintenance

and

engineering

organizations

resulted

in the failure to perform

a required

operability determination

(OD) evaluation for a degraded

condition of

the Train

B essential

chilled water system

(EC) chiller.

Unit 3

operators

had considered

the chiller operable for a week even

though it

was in

a degraded

condition which would have required

manual

actions to

assure

continued operability during

an event

(Section 4.2).

'7602260382

960223

PDR

ADOCK 05000528

8

PDR

l

i

~

Operations failed to critically assess

an incomplete operability

determination

evaluation

provided by the engineering

organization

regarding safety related solenoid valves.

Plant operations

approved

an

OD evaluation for several

safety-related

solenoid valves

even

though the

engineering

evaluation did not thoroughly address

the effects of

potential

heat

damage

on the Technical, Specification functions of some

of the valves

(Section

7. 1).

~

Plant operations

implemented

an informal posttrip action which had

operators

begin boration before the action

was prescribed

by operating

procedures.

This guidance

was not formally reviewed to assure

consistency

with established

operating

procedure

requirements

(Section

3. I).

~

Plant operators

failed to follow the shutdown margin procedure

requirements

to continue boration until reactor coolant

system

boron

concentration

was confirmed to meet

shutdown margin requirements.

This

was

a licensee identified noncited violation (Section 3. 1).

Operators failed to ensure that adequate

precautions

were taken prior to

attempting to return

a Unit 2 condensate

pump to service.

As

a result,

a loss of pump suction

caused

the trip of both main feedwater

pumps

and

a subsequent

reactor trip (Section

2. I).

A Unit 3 shift supervisor

demonstrated

a good questioning attitude prior

to

a moderator

temperature

coefficient

(MTC) test.

The indepth

questioning contributed to the identification of excessively

conservative

shutdown margin calculations

and

an inaccuratelj

drawn

transient

insertion limit (TIL) curve (Section 6.1).

In addition,

the

shift supe> visor responded

promptly to concerns

regarding

a deficiency

with an

EC valve which contributed to the discovery of other system

control setpoint deficiencies

(Section 4.3).

Maintenance

Maintenance

technicians

demonstrated

strong

equipment

knowledge

and

proper maintenance

procedure

usage during the performance of mainten'ance

work (Section 5).

Maintenance

personnel

only corrected

an immediate deficiency in the

level

oF refrigerant in

a Unit 3

EC chiller without documenting

the

problem,

as prescribed

by the corrective action process.

This resulted

in

a missed opportunity to assess

the potential

impact

on system

performance

and operability (Section

4. 1).

Maintenance

did not thoroughly understand

the impact that

a chiller oil

leak could have

on the system operability

and the

need for an

operability determination.

Maintenance

personnel

failed to adequately

assure

that operations

personnel

were thoroughly aware that operation of

I

1

l

an

EC chiller with a significant oil leak would require

manual

actions

and of the implications of those actions

(Section

4.2).'n

ineerin

~

Haintenance,

system

and design engineers,

responsible

for the

EC system,

demonstrated

weak communications with each other

and did not ensure that

parameters

important to the operability of the chillers were

communicated

to maintenance

technicians

and the operations staff.

For

example:

~

Following a chiller trip in which refrigerant level

was

an

apparent contributor,

engineers

did not ensure that technicians

were fully cognizant of previous refrigerant level discrepancies

(Section

4. 1).

~

Haintenance

engineers

did not involve system'r

design

engineers

in the decision to consider

a chiller operable with a significant

oil leak (Section 4.2).

~

System

and design engineers

did not ensure

maintenance

and

operations

personnel

were aware that

a water leak rate of

approximately

2 drops per second

could impact the

EC system

operability (Section 4.3).

~

Nuclear Assurance

performed

a thorough

assessment

of a Unit I

EC chiller

trip and identified that the evaluation of the trip by maintenance

and

system engineering

had not been thorough.

In addition,

Nuclear

Assurance

identified that engineering

had

been

slow to resolve design

issues

regarding

the impact of cold spray

pond temperatures

on the

operability of the chillers (Section 4. 1).

~

An engineering

team,

established

to review emergency diesel

generator

cooldown trips,

completed

an excellent investigation.

They established

that several

deficiencies contributed to the problems, initiated

appropriate corrective actions,

and developed

a presentation

for the

diesel

owners

group (Section 7.2).

Plant

Su

ort

~

Contractor personnel

displayed

poor housekeeping

practices

during the

platform construction

in the mainsteam

support structure.

Hanagement

aggressively

assured

that the contractor

understood

and

implemented

their expectations,

which resulted

in improved conditions in the area

(Section 8).

f

'

~Summar;e

Ins ection Findin s:

~0en

Items

One violation was identified (530/9525-01)

involving the failure to

identify a condition adverse

to quality (Section

F 1).

One violation was identified (530/9525-02)

involving failure to follow

the operability determination

procedure

(Section 4.2).

~

One violation was identified (528/9525-03)

involving the failure to

perform leak rate testing of the

EC system

(Section 4.3).

~

One noncited violation was identified involving failure to follow the

shut

down margin

(SDN) procedure

(Section

3. 1).

~

Inspection

Followup Item 530/9525-04

(Section 6.1)

I

Closed

Items

~

Unresolved

Item 528/9521-01

(Section

4)

~

Violation 529/9431-02

(Section 9.1)

~

Violation 529/9431-05

(Section 9.2)

~

Violation 530/9438-01

(Section 9.3)

~

LERs 528/94-05,

Revision 2; 528/94-07,

Revision

1; 528/94-09,

Revision

1; 528/94-10,

Revision

1; 529/94-04,

Revision 2; 529/94-08,

Revision

1 (Section

10)

Attachment:

1.

Persons

Contacted

and Exit Heeting

2.

List of Acronyms

DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 began

the inspection period at

100 percent

power.

On December

29,

1995,

the unit reduced

power to 40 percent for repairs to the condenser

hotwell.

On December

31, the unit returned

to 100 percent

power and remained

there throughout the inspection period.

1.2

Unit 2

Unit 2 began

the inspection

period at

100 percent

power.

On January

21,

1996,

a reactor trip occurred following an attempt to return

a condensate

pump to

service

(see Section

2. 1).

On January

23, the unit was returne'd to

100 percent

power operation

and operated

at this power for the remainder of

the inspection period.

1.3

Unit 3

Unit 3 operated

at full power for the duration of the inspection period.

2

ONSITE RESPONSE

TO EVENTS

(93702)

2. 1

Loss of Feedwater

and Reactor Tri

Unit 2

On January

21,

1996, Unit 2 tripped from 100 percent

power due to low steam

generator level.

Prior to the trip, operators

were attempting to place the

Condensate

Pump

C, which had

been out of service for several

weeks,

in

service.

In the process of aligning the

pump, air was introduced into the

suction of the operating

condensate

pumps

as

a result of a failure to have

explicit procedural

steps

to require filling and venting of the condensate

line,

The transient

caused

a lowered suction pressure

to the two running

condensate

pumps

and

a loss of suction to both of the main feedwater

pumps.

The main feedwater

pumps tripped causing

a loss of feedwater

and

a subsequent

reactor trip.

The steam generator levels continued to decrease

until

an

automatic signal

started

both auxiliary feedwater

pumps.

Posttrip plant

recovery

was normal

and the licensee classified

the event

as

an uncomplicated

reactor trip.

The inspector

responded

to the unit trip and noted that the operators

were

responding

well to the event

and all required safety

equipment

was operating

as designed.

Operators

properly controlled primary plant parameters,

recovered

steam generator

inventory,

and secured

the unloaded

operating

emergency diesel

generators

in

a timely manner.

The inspector

concluded that

the crew's

use of procedures

was strong.

I

ff

,f

l,

The inspector

noted that the licensee

investigation

olanned to evaluate

further corrective actions

including proceduralizing

the filling and venting

of the condensate

pump

and piping during plant operations.

The inspector will

evaluate

the corrective actions during

LER closure.

The inspector

observed

the reactor startup

on January

22 and noted

good

communications

and procedure

usage.

The inspector

concluded that the

operating

crew demonstrated

an overall strong performance.

3

OPERATIONAL SAFETY VERIFICATION

(71707)

3.1

SDM and Boration

On March 3,

1995,

the licensee identified

a condition where the

1 percent

SDM required in Technical Specification

3. 1. 1. 1 did not provide adequate

SDH for the limiting license basis

steam line break event in Mode

3

(LER 528/95-002).

As

a result,

the licensee

established

administrative

controls to apply the requirement of Technical Specification 3. 1. 1.2 for

Technical Specification 3. 1. 1. l.

Technical Specification 3. 1. 1.2 required

between

a

4 and 6.5 percent

SDM, dependent

on the reactor coolant

system

temperature,

and

was analyzed for the limiting license

basis

steam line break

event.

At the

end of the inspection period,

the licensee

was preparing to

submit

a licensee

amendment

to address

the adequacy of the requirements

of

TS 3.1.1.1.

The shift technical

advisors

developed

a reactivity control worksheet to

provide information to the operators

on reactivity worth and minimum boron

concentration

to satisfy the 6.5 percent

SDM requirement.

The inspector

noted

that several

crews

used

the information as part of the crew brief at the

beginning of the shift to addrc"s the

SDM requirements

should

a unit shut

down

occur.

As

a result,

the worksheet often indicated that the posttrip

SDH was

inadequate.

The amount of boric acid addition indicated

by the worksheet

was

more than what was actually required

because

the assumptions

associated

with

the worksheet

were overly conservative.

As

a result,

the worksheet often

indicated that the posttrip

SDH was inadequate.

The licensee

had issued

a night order

on December

7,

1995, discussing posttrip

SDH.

The night order explained that following a reactor trip, the operators

would need to borate to maintain

adequate

SDH.

The night order further

explained that the operators

should review the reactivity control worksheet

on

a shiftly basis

in order to have

an idea of how much borated water must

be

added following a unit trip.

3.1.1

Reactor Trip Event

Unit 2

On January

21,

1996, shortly following the unit

trip, the operators

injected

800 gallons of borated water consistent

with the

reactivity control worksheet

information.

The licensee

subsequently

obtained

a reactor coolant

sample

and performed

Procedure

72ST-9RX09,

"Shutdown

Hargin," and determined

that the boron concentration

was

16 parts

per million

f

less

than the minimum required

boron concentration

for adequate

SDM.

The

operators

injected

an additional

400 gallons of borated water to compensate

for this deficiency

and stopped

the boration.

The shift technical

advisor,

during review of the

SDM calculation, identified

that Procedure

72ST-9RX09 required continuous

boration until the

SOM was

satisfied.

The shift technical

advisor informed operations

management

present

in the control

room of the continuous

boration requirement.

Operations

management

directed the operators

to re-establish

boration until the

SOM was

verified with a reactor coolant

sample.

The operators

injected

an additional

200 gallons of borated water before the shift technical

advisor verified the

SDM acceptance

criteria were met.

3. 1.2

Licensee

Evaluation

During the posttrip evaluation,

the licensee

concluded that operators

had

a

flawed understanding

that

SDM requirements

would be met by adding the amount

of boron indicated

on the reactivity control worksheet.

The inspector

agreed

with the licensee's

conclusion.

On January

22, the licensee

issued

a night order

and held crew briefings for

the operators

to clarify management's

expectation

regarding reactivity

control.

The briefing indicated that the reactivity control worksheet

provided useful

and accurate

information but would not

be used

as direction to

start borating in order to meet

SDM requirements.

During posttrip conditions,

the emergency

operating

rocedures

would provide direction to operate

the

plant, including the verification of SOM.

In addition,

the briefing indicated

that, if a boration

was started

to meet

SDM requirements,

the boration would

continue until

SDM requirements

were verified by chemistry sample.

The inspector

noted that the licensee

issued

a revision to

Procedure

72ST-9RX09

on January

26, to clarify the contingency actions to

maintain

a continuous

boration until

SDM was satisfied.

In addition,

the

licensee

performed calculations,

which concluded for all cases

of the current

unit cycles that

a

5 percent

SDM would be established

and that the

5 percent

SOM would be suFficient to compensate

for the reactivity addition of the

limiting steam line break.

The inspector

noted that the licensee

planned to

further evaluate

SDM corrective actions

as part of the trip investigation.

The inspector

noted that the'uidance

to operators

to borate

immediately

following a reactor trip had not been

included in the emergency

operating

procedures

and

had not received

a formal review.

The inspector

concluded that

the use of this informal guidance

was not consistent with the philosophy of

the emergency

operating

procedures.

The inspector

discussed

the informal

guidance

concern with pl,ant management.

Plant

management

agreed with the

inspector's

concern

and indicated that they would evaluate to ensure that

a

guidance

developed for operators

to mitigate plant deFiciencies

is formally

reviewed.

The inspector

concluded that the licensee's

corrective actions

were

appropriate.

I(

3.1.3

Conclusions

The inspector

concluded that the licensee's

corrective actions to address

the

boration

issues

were appropriate.

Although the operating

crew failed to

follow the

SDH Procedure

72ST-9RX09 for boration requirements,

this licensee

identified and corrected violation is being treated

as

a noncited violation,

consistent

with Section VII of the

NRC Enforcement

Policy.

4

ESSENTIAL CHILLED WATER (EC)

SYSTEM

(37751,

62703,

71707,

92720,

92902)

In

NRC Inspection

Report 50-528/95-21;

50-529/95-21;

50-530/95-21,

the

inspector

opened

Unresolved

Item 528/9521-01

to perform further review of the

problems

experienced

in both the Units

1 and

3

EC systems

on November

27,

1995.

The Unit

1 Train

B chiller had tripped unexpectedly

and the Unit 3

chiller was declared

inoperable

due to oil pump cavitation

and then declared

operable after the addition of more oil.

During the inspection period,

the

inspector identified concerns

regarding

EC system sensitivity to water

inventory loss.

In addition,

the inspector considered

Unresolved

Item 528/9521-01

closed.

4.1

Refri erant Levels

The licensee initiated Condition Report/Disposition

Report

(CRDR) 1-5-0215 in

response

to the Unit

1 Train

B chiller trip that occurred

on November 27.

Prior to completing

a root cause

evaluation for the trip, the licensee

suspected

that low refrigerant level in the cooler

may have

been

a

contributing factor.

The licensee identified that the Unit

1 Train

B chiller

refrigerant level

was low in its band.

I

In 1990,

HVAC engineering

had "stablished that refrigerant levels in the

cooler should

be maintained

between

3 and

7 inches in accordance

with

Engineering

Evaluation Report

(EER) 90-EC-031.

The licensee

had translated

these

values into a weekly preventive maintenance

task.

The high and low

levels

had

been defined

as the maximum and minimum operability limits.

The

inspector

noted that, following the Unit

1 Train

B chiller trip,

HVAC

technicians

increased

the

shutdown refrigerant levels in all three units

as

necessary

to slightly greater

than

6 inches to prevent

a trip on "low

refrigerant temperature."

4. 1. 1

Control of Refrigerant

Levels

On December

20,

1995, during

a system walkdown to verify the licensee's

corrective actions,

the inspector identified that the refrigerant level in the

Unit 3 Train

B chiller was

above

7 inches.

The inspector notified the shift

supervisor,

who in turn contacted

a

HVAC technician.

The

HVAC technician

confirmed that the refrigerant level

was

7 3/8 inches,

lowered the level to

6 1/4 inches,

and documented

this activity in a weekly preventive

maintenance

work order.

The shift supervisor

concluded that the chiller had

been operable with the

reFrigerant level

ab'ove

7 inches

based

on

a discussion

with HVAC maintenance

personnel.

On January

4,

1996,

the inspector determined that

a

CRDR had not been

initiated to document

and resolve the refrigerant level discrepancy.

The

inspector obtained

the completed weekly chiller preventive maintenance

tasks

for November

and December.

The inspector

noted that

a week prior to

December

20,

1995,

the refrigerant level

was recorded

at

4 3/4 inches.

The

week Following December

20, the refrigerant level

was recorded

at

3 3/8 inches.

The inspector determined

that these

changes

in level represent

up to

25 percent of the

1 ton refrigerant

volume.

The inspector concluded that the high refrigerant level

and the abnormal

trend

represented

a condition adverse

to quality which, according to the licensee's

corrective action program,

required that

a

CRDR be initiated,

The inspector

concluded that the failure of the maintenance

technicians

to initiate a

CRDR

demonstrated

that they were not fully cognizant of refrigerant level issues,

despite

the recent trip of the Unit

1 Train

B chiller.

The inspector further

concluded that maintenance

engineering,

who had responsibility for the chiller

preventive maintenance

program

and

had

been

involved in the review of the

chiller trip, had not ensured

that the maintenance

technicians

were

sufficiently aware of previous refrigerant level discrepancies.

The failure

to identify a condition adverse

to quality is

a violation of 10 CFR Part 50,

Appendix B, Criterion XVI. (530/9525-01)

On February

1,

1996,

the licensee initiated

CRDR 9-6-0078 to address

this

issue.

HVAC 'technicians

suspected

that the level

changes

may be due to

a

leaking isolation valve between

the refrigerant storage

tanks

and the cooler

and scheduled

a work order to investigate.

4.1.2

Assessment

of the Chiller Trip Investigation

The inspector reviewed the progress

of CRDR 1-5-0215

and noted

tha~ the pace

of the investigation

had not been aggressive.

The inspector

noted that the

classification

oF the

CRDR had

been

changed

from "potentially significant" to

"adverse."

The root cause of the Unit

1 chiller trip had not been determined.

As of January

16, the critical setpoints

on the chiller had not been verified

and

assessed

by the

system engineer.

The inspector

noted that Nuclear Assurance

had

been performing

a concurrent

evaluation

and

had arrived at

a similar conclusion.

Nuclear Assurance

had

determined

that the

CRDR should

have

been classified

as "significant" based

on

the potential applicability of this problem to all essential

chillers.

On

January

19, Nuclear

Assurance initiated

CRDR 9-6-(019.

In addition,

Nuclear

Assurance

had identified that

NRC Information Notice 94-82,

"Concerns

Regarding

Essential

Chiller Reliability During Periods of Low Cooling Water

Temperature,"

concerning similar issues,

had not received

a timely or thorough

review.

l

-10-

The inspector questioned

the system engineer

about the effects of operating

essential

cooling water without operating

the chiller.

The system engineer

stated that, if the

EC temperature

is lowered due to cool weather

and it is

operated without the chiller operating,

the refrigerant

may migrate into the

condenser.

This would decrease

refrigerant level in the cooler,

thus

increasing

the risk of a trip on "low refrigerant temperature"

when the

chiller is called

upon to start.

The inspector

noted that

a modification had

been

proposed

to address

this concern.

However,

the licensee

had not

evaluated

the existing configuration nor implemented

interim actions.

The inspector

noted that Nuclear Assurance

had developed similar concerns

documented

in CRDR 9-6-f019.

Nuclear Assurance

referenced

six separate

EC chiller events

since

1994 which could

be attributed to control of

refrigerant levels.

Nuclear Assurance

had identified that modifications to

install

a three-way mixing valve to control refrigerant level

had

been

canceled

twice, once in 1988

and once in 1993.

Nuclear Assurance

also

identified that engineering

had not adequately

resolved

whether the chillers

could reliably operate with spray

pond temperatures

less

than 49'F.

In response

to these

issues,

HYAC maintenance

revised

the weekly chiller

preventive

maintenance

task to include seasonal

operating refrigerant levels

and the need to write

a

CRDR if the levels are not within its desired

range.

In addition,

the licensee

planned to enter the results of the weekly

preventive maintenance

into a data

base for trending purposes.

System

engineering

would have the responsibility for long term trends while

maintenance

engineering

would have the short term trending responsibilities.

The licensee

planned to implement this action in March of 1996:

4.2

Lubricatin

Oil Levels

On November 27,

1995, Unit 3 operators

declared

the Unit 3 Train A chiller

inoperable after

an auxiliary operator

noted that there

was

no observable oil

level in its oil reservoir.

Operators

subsequently

declared

the chiller

operable after adding

5 gallons of oil and performing the chiller surveillance

test.

The inspector

reviewed the licensee's

basis for operability

and

concluded that the procedure for operability determinations

had not been

implemented

and found that the basis for operability had not been well

established.

4 '.1

Background

The chiller compressor

and motor are refrigerant cooled

and oil lubricated.

A

motor-driven,

compressor

lubricating oil pump

and reservoir

are located in the

compressor

base.

The oil pump takes

suction

on the reservoir

and discharges

through

a filter and heat

exchanger

to the compressor

and motor.

The

lubricating oil is returned to the reservoir

by means of an oil return system.

There

are

two protective trips associated

with the lubricating oil system,

"Compressor

High Bearing Oil Temperature"

and

"Compressor

Low Oil Pressure."

I

There are

two sightglasses,

an upper

and lower bullseye,

that represent

the

maximum and minimum oil levels.

If the oil in the

eservo

~ 'ceeds

the

maximum level, the chiller can trip on high bearing oil temperature.

Additionally, the chiller can trip on low oil pressure

because

of low oil

levels

caused

by the low differential pressure

across

the compressor.

Since the chillers are closed

systems,

oil leaking from the seals

enters

the

refrigerant cycle.

The chillers were designed

to operate with some

amount of

oil in the refrigerant

and

a small oil return system

was installed to return

oil from the refrigerant.

However,

the oil return system

does not work

efficiently when the chiller is operated

under low loaded conditions.

As

a result of a chiller trip in 1987, engineering

performed

an evaluation,

documented

in EER 87-EC-019.

The licensee

had established

that the chiller

should not be operated

with the oil level

below the lower sightglass,

which

corresponds

to approximately 7.5 gallons of oil, or with a total oil volume in

excess of 25 gallons.

4.2.2

Timeline of Unit 3 Operation of the Train A Chiller

On October

29,

1995,

the Unit 3 Train A chiller was returned to service

following the replacement

of the rear motor bearing seal.

The

HVAC technician

initially charged

the chiller with 15 gallons of oil.

During the period of

November

10 through

November 20,

HVAC technicians

added

approximately

7 gallons of oil to the chiller in order to maintain acceptable oil levels in

the oil reservoir sightglass.

The chiller had

been

in service to support the

operation of safety-related

equipment during the Unit 3 refueling outage.

On November 26, operations

personnel

started

the Train A chiller in support of

testing Train

A auxiliary feedwater

pump, which had

been out of service for

approximately

60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> of a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> Technical Specification action statement.

Shortly after the chiller was started,

operators

observed

low oil levels in

the oil reservoir.

HVAC technicians

added

5 gallons of oil, bringing the

total calculated oil volume to 27 gallons, after discussing

the addition with

an

HVAC maintenance

engineer.

The

HVAC maintenance

engineer

suspected

that

an

oil leak had developed

on the rear motor bearing seal.

On November 27, at approximately 4: ll a.m., Unit 3 operations

personnel

declared

Train A chiller inoperable after

an auxiliary operator

heard

the

lubricating oil pump cavitating

and noted that the oil level

was not visible

in the reservoir.

The site shift manager,

shift supervisor,

and the

HVAC maintenance

team leader

discussed

the operability of the Train A chiller.

The licensee

added

5 additional gallons of oil to the chiller and performed

a chiller

surveillance test.

Maintenance

logs identified that this addition brought the

total oil in the chiller to approximately

32 gallons,

7 gallons

above the

limit established

by engineering

in

EER 87-EC-019.

Both the Train A chiller

and auxiliary feedwater

pump were declared

operable

at 6:55 a.m.

The chiller

was subsequently

shutdown,

placed

in standby,

and remained

operable.

On

~ I

-12-

Novemb r 28, the

HVAC maintenance

engineer initiated

CRDR 9-5-1185

and

developed

an action

pl-an to determine

why the chiller was losing oil from the

reservoir.

On December

4, operations

removed

the Train A chiller from service

and

HVAC

technicians

replaced

the rear motor seal o-ring as part of their corrective

maintenance.

The

HVAC technicians

determined that the o-ring had

been

damaged

during the previous maintenance

outage.

The oil recovered

from the chiller

was approximately

37 gallons,

5 gallons

more than

had

been

recorded

in

maintenance

logs.

Following the maintenance activity, operations

personnel

tested

the chiller for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

After the test

showed

no apparent oil leaks,

operations

personnel

declared

the chiller operable.

4.2.3

Assessment

of Interim Actions

On January

18,

1996,

the inspector

met with the

HVAC maintenance

team,

including the

HVAC maintenance

engineer,

to discuss their basis for

considering

the chiller operable

on November 27,

1995.

The

HVAC maintenance

engineer

had recognized that

32 gallons

exceeded

the established criteria and

that the majority of the oil was in the refrigerant,

The maintenance

engineer

stated

that the primary concern

was that, if the chiller operated

in

a full

load condition,

the oil return system would flood the oil reservoir.

He noted

that, without manual

action to remove the recovered oil, there would be

an

increased risk of a chiller trip on compressor

high bearing oil temperature.

The

HVAC maintenance

team stated that they had provided

21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> of onsite

coverage

from November

27 through

December

1, to be available if the Unit 3

Train A EC system

was called

upon, to prevent the chiller from tripping and

maintain chiller operability.

For the remainder of the time from December

2

through 4, the technicians

were available

by telephone

and

a team leader

was

also available

on backshift.

The inspector

subsequently

reviewed the unit and shift technical

advisor logs

and observed that the log entries did not clearly establish

that continued

operability of the chiller depended

on manual

action

by

a

HVAC maintenance

technician.

In addition,

the inspector determined that the Unit 3 operations

personnel

had not recognized

the fact that manual

action

was required

by the

HVAC technician to maintain operability.

Licensee

Procedure

40DP-90P26

provided guidelines

and instructions for

evaluating

the operability of a system

when

a degraded

or nonconforming

condition has

been identified.

Appendix C, to the procedure

provided several

actions

which must

be met before taking credit for manual action.

These

actions

were consistent with the guidance

in

NRC Generic Letter 91-18,

concerning operability and included

a

10 CFR 50.59 evaluation, written

instructions that prescribe

the manual

actions,

and ensuring that necessary

communications

are established.

Operations

did not implement the operability

determination

procedure,

nor were

any of the actions called out in Appendix

C

documented prior to declaring the Train A chiller operable.

The failure to

f

-13-

follow the prescribed operability evaluation

procedure

is

a violation.

(530/9525-02)

4.2.4

Assessment

of Technical

Basis

The inspector

inquired whether the maintenance

engineer

had evaluated

whether

the oil loss to the refrigerant could exceed

the oil returned to the

reservoir.

The maintenance

engineer

found that this was possible if the

chiller was operated

in

a low-load condition.

He stated that compensatory

actions

could have

been

taken to artificially load the chiller, increasing

the

rate of oil return.

The inspector

noted that these

compensatory

actions

were

not prescribed

in existing instructions.

The inspector further inquired whether the maintenance

engineer

had evaluated

the impact of the additional oil in the refrigerant

on the efficiency of the

chiller.

The maintenance

engineer

stated that, while he was confident that

the chiller efficiency would not have

been significantly impacted,

he did not

have specific basis for this conclusion,

The inspector

noted that this

confidence

may have

been

acceptable

for establishing

a reasonable

assurance

for operability on November

27.

However,

the inspector considered

that

a more

formal evaluation

was warranted to support continued operability.

The

inspector

also inquired whether

a trend of oil addition

had

been

made to

assess

whether the oil leak was degrading.

The maintenance

engineer

had not

evaluated

the trend.

The inspector determined

in discussions

with the

licensee

that the maintenance

engineer

had developed

the basis for chiller

operability without substantive

support

from either the system or design

engineers.

finally, the inspector questioned

whether the licensee

had developed

a

reasonable

basis for considering

the chiller operable

on November

27.

The

licensee

concurred that the operability determination

process

had not been

implemented

and the arguments

to support operability had not been well

developed.

On February

2,

1996,

the licensee

presented

a well developed

basis

for considering

the chiller operable

from November

27 through

December

4,

1995.

The inspector critically reviewed the licensee's

determination

and

found the basis

acceptable.

4.3

fC

S stem

Leaka

e

On January

19,

1996,

the inspector identified

an

EC chilled water system leak

which was in excess

of the maximum system leak rate identified in the system

design basis

manual

(DBH).

The inspector

subsequently

noted that past

system

configuration changes

had

made the system's operability sensitive

to

a loss

oF

inventory

as

small

as

15 gallons in the

1100 gallon system.

However,

the

licensee

had not initiated adequate

compensatory

actions to ensure that

operations

and maintenance

personnel

were

aware of this sensitivity.

In

addition,

the inspector identified that the licensee

had missed

subsequent

opportunities

to identify that the compensatory

actions

were not adequate

during their

DBN project

and in

a followup of a

1994 inspection

issue.

I

-14-

4.3.1

Original

EC System

Design

Two trains of

EC circulate through their respective refrigeration (chiller)

units,

through safety-related

equipment

room coolers,

and back through

an

EC

pump.

The

EC system

pumps, chiller units,

and chilled water expansion

tank

are located in the lowest level of the control buildings with room coolers

located at higher elevations.

The

EC system

was designed

as

a closed

loop

system

and its expansion

tank was provided with a pressurized

nitrogen cover.

Makeup to the expansion

tank was provided

by demineralized

water

and from the

condensate

storage

tank through the condensate

transfer

pumps.

The condensate

transfer

pumps,

normally in standby,

were designed

to start

on the

same

initiation signals

as the

EC system.

A solenoid-operated

valve, actuated

by

expansion

tank level instrumentation,

was designed

to open

on low expansion

tank level,

and close

on high and low-low expansion

tank level.

Nonsafety-related

instrumentation

was provided for local expansion

tank level

and pressure

and control

room annunciation of high and low expansion

tank

levels

and pressures.

The licensee's

Final Safety Analysis Report stated,

that

.

.

. "critical

conditions of the tank level

and pressure

are

alarmed

in the control

room for

leak detection."

The NRC's safety evaluation report stated that the

EC system

had met

10 CFR Part 50, Appendix A, General

Design Criteria

(GDC) 44,

45,

and

46 concerning

the design,

inspection,

and testing of cooling water

systems.

GDC 44 states

that "Suitable

.

.

. leakage

detection

.

.

. shall

be provided to assure that

.

.

. the system safety function can

be

accomplished

.

. ."

GDC 46 states

that

"The cooling water systems

shall

be

designed

to permit appropriate

periodic testing to assure

.

.

. the leaktight

integrity of its components

.

4.3.2

System Configuration

Chages

Two

EC system configuration changes

occurred

between

1990

and the time of the

inspection.

In 1990,

the licensee

removed the

EC expansion

tank

instrumentation,

which provided control

room annunciation of critical level

and pressure

parameters,

from service.

In addition,

in 1992, the licensee

concluded that it would no longer take credit for a safety-related

EC expansion

tank makeup

from the condensate

storage

tank.

The action to remove the control

room annunciation

from service

had

been

prompted

by licensee

concerns with the code boundary

excess

flow check valves,

which separated

the seismically qualified instrumentation

from nonseismically

qualified instrumentation.

As documented

in

EER 86-XH-046, the licensee

determined

that the excess

flow check valves could leak following a seismic

event with an adverse

impact

on the

EC system.

To resolve this concern,

the

licensee

closed valves

upstream 'of the excess

flow check valves.

As

a

compensatory

measure,

the licensee

established

an operator

round to read

levels

by opening the isolation valves every shift.

The licensee

stopped

taking credit for

EC system

makeup

from the condensate

storage

tank in

a design basis

event

when they recognized that the operability

ilr

-15-

of the

EC system would be dependent

upon the operabi>ity of the condensate

transfer

system.

The inspector determined that the licensee's

review of these configuration

changes

was not thorough.

The

EC system

has

a relatively small

expansion

tank,

making the system sensitive to small

volume changes.

With a relatively

small

system leak

and the loss of the nonsafety-related

makeup to the

expansion

tank,

the expansion

tank could drain

and introduce nitrogen into the

system at the suction of the

pump.

The inspector determined that both the

isolation of expansion

tank level instrumentation

and the changes

to the

classification of the condensate

storage

tank makeup

reduced

the ability of

operators

to detect

a leak

and reduced

the reliability of the system

makeup.

The inspector determined that the licensee's

10 CFR 50.59 evaluation,

performed in 1990 to address

removing the expansion

tank level

and pressure

annunciation

from service,

did not discuss

the

GDC 44 requirements

for cooling

system

leakage detection

and did not account for the

GDC 46 requirement for

leak rate testing.

At that time, the licensee

did not establish

a maximum

leak rate for the

EC system

and

had not established

a program for

EC system

leak rate testing.

The inspector determined that the compensatory

measures

to include

EC

expansion

tank level

and pressure

readings

on operator

rounds

were

appropriate.

However,

the inspector

noted that the operator

rounds

procedure

did not address

a need to monitor the system for leaks.

In addition,

maintenance

procedures '; re not implemented

which assured

that leakage

was

minimized.

While the safety evaluation

performed in 1990 was flawed,

the inspector

concluded that,

since

1992,

the licensee

has

improved the quality of

10 CFR 50.59 evaluations

to address

these

types of weaknesses.

However,

as

discussed

below, the licensee

subsequently

missed additional opportunities to

identify the weaknesses

with the

EC system configuration changes.

4.3.3

Licensee's

DBM and Associated

Calculations

In May 1994,

the licensee

issued

Revision

1 to the

EC system

DBM.

The

DBM identified that

GDC 44 had

been applied to the

EC system to establish

the system leak rate.

The

DBM provided

a system specific leakage

criteria of 9 gallons per day or 0 '75 gph

and referenced

EC hydraulic

Calculation

13-MC-EC-200 for the basis of this leak rate.

The

DBM also

identified that the

EC system

should

be tested

to assure

the overall

system

leakage did not exceed

design values calculated

in Calculation

13-MC-EC-200.

The licensee

did not initiate any immediate actions

to ensure that

a leak rate

of 0.375

gph would be detected

by operators

or

HVAC maintenance

personnel.

In

addition,

the action to establish

a system leak performance test

was captured

in one of the final phases

of the design basis reconstitution

program to be

implemented

by mid 1996.

l

I

l

-16-

The inspector determined that

a leak rate of 9 gallons per day represented

a flow of approximately

2 drops per second.

The inspector considered

that

a

leak rate this small would not be identified as

an operability concern

by

plant operators

and maintenance

personnel

unless specifically brought to their

attention.

The inspector determined that licensee

engineering

had not

identified this

as

a concern.

The inspector

found that,

in general,

the licensee's

plan to implement testing

in accordance

with a schedule for implementation

in mid 1996 appeared

acceptable.

However,

the inspector

was concerned that the plan did not

prioritize the implementation of tests

required to meet

a regulatory

requirement.

The inspector reviewed the portion of Calculation

13-MC-EC-200 pertaining to

the maximum allowed

EC water leak rate.

The inspector

noted that the basis

for the

maximum leakage

rate for the

EC system

was to maintain

adequate

expansion

tank pressure

for a period of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

assuming

no operator action

and the loss of nitrogen

makeup.

The inspector identified the following

two errors:

The calculation

assumed

that level in the

EC expansion

tank was at the

low-level makeup valve actuation setpoint

versus

the high level

makeup

valve-close setpoint.

Since the limiting condition of the calculation

was the lowest allowed nitrogen cover pressure,

using the low level

setpoint

provided

a nonconservatively

high starting

volume of nitrogen.

Assuming

a higher setpoint,

the calculation would have allowed

a leak

rate of only 0.25 gph.

The calculation using the low-level setpoint credited

expansion

tank

volume below the surge

1-:ne to the

EC pump suction.

Subtracting

the

unusable

volume would also

have provided

a leak rate of approximately

0.25 gph.

The licensee

revised their calculation

on January

24,

1996.

The revised

calculation identified that

a loss of volume of 15.2 gallons,

versus

the

originally calculated

27 gallons,

could impact system operability.

However,

the licensee

took credit for identifying a low-level condition within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

oF

an event versus

the

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

assumed

in Calculation

13-MC-EC-200.

This

change

increased

the maximum leak rate to 0.63 gph.

The inspector

found this

change

acceptable

based

on the operator

rounds

performed every 12-hour shift.

Following the inspection period,

the licensee

developed

and started to

implement

an

EC leak rate test.

The licensee

also initiated

a review of other

08Ms to identify if there

were similar tests

which required priority

implementation.

j

I0

-17-

4.3.4

Concerns

Identified by the Inspector in March

1994

In March 1994,

the inspector

performed

a walkdown of the

EC system

(see

NRC

Inspection

Report 50-528/94-09;

50-529/94-09;

50-530/94-09)

and observed that

the

EC expansion

tank instrumentation

had

been

removed

from service.

As

documented

in

NRC Inspection

Report 94-09,

the inspector

noted that there

was

no mention in the annunciator

response

procedures

that this instrumentation

was out of service.

The inspector also noted that this change

had not been

reflected in the Final Safety Analysis Report

(FSAR).

In response

to the concerns

discussed

in

NRC Inspection

Report 94-09,

the

licensee initiated

CRDR 9-4-0157.

As resolution for CRDR 9-4-0157,

the

licensee initiated

an evaluation of the existing

EC configuration.

Additionally, they initiated

an evaluation to determine if a modification to

the

EC expansion

tank level

and pressure

alarms

were necessary.

The licensee

also revised the annunciator

response

procedures

to note that the expansion

tank instrumentation

had

been valved out of service.

The licensee's

evaluation of the expansion

tank instrumentation

configuration

concluded that the 12-hour operator

rounds

was

an adequate

compensatory

measure.

The evaluation

recognized that the system design leak rate

was

9 gallons per

day.

However,

the evaluation

took credit for plant personnel

correcting

a

system leak without identifying how they would know the leak represented

a

problem.

The inspector considered

that the evaluation of CRDR 9-4-0157

represented

a missed opportunity to identify the lack of guidance to operators

and maintenance

personnel

on the limits to

EC system leakage.

In August

1994,

the Technical

Review Committee,

responsible

For reviewing all

plant change

requests,

approved

a modification which would provide seismically

qualified instruments for level

and pressure

alarms.

The committee determined

that the modification was justified and would eliminate

an operator action to

compensate

for the isolated,

nonseismically qualified level

and nressure

instrumentation.

The licensee

implemented

the modification in the Unit 2 Train

B

EC system.

At

the time of this inspection,

the licensee

had not implemented the modification

in the other five

EC trains.

On December

15,

1995,

the licensee's

work

schedule

indicated that the modifications would be completed

in by August

1996.

These modifications will restore

the chill water leak monitoring to

full conformance with the

FSAR system description.

The inspector

found that the modification performed

on Unit 2 Train

B was

appropriate

and that the plans for completion of the modifications were

acceptable.

l

\\

1

-18-

4.3.5

Deficiencies

Impacting

EC System Inventory

During the inspection period,

the inspector identified various deficiencies

that could have

impacted the

EC system inventory.

On January

10,

1996,

the inspector identified

a substantial

water leak

past

a thermowell

in the Unit 2 Train

B

EC chiller cooler.

The

magnitude of the leak had increased

recently

and could have developed

following the previous

12-hour auxiliary operator

round.

The inspector

notified the control

room supervisor

and corrective actions

were taken

by

HVAC maintenance

during the shift.

The inspector

noted that

no

attempt

had

been

made to quantify the leak and that operators

had not

considered

the impact on chiller operability.

The repair was documented

in the weekly preventive maintenance

task.

~

On January

10, the inspector

noted seal

leaks in both the Unit

1 Train

B

EC pump

and the Unit 3 Train

B

EC pump.

The Unit

1

pump seal

leak was

approximately

80 drops per minute

and the Unit 3

pump seal

leak was

approximately

120 drops per minute.

The inspector

noted that neither

pump

had

a work request

tag identifying the leak.

The inspector

subsequently

determined that there

was

an

open work request for the leak

on the Unit 3 Train

B

EC pump.

However,

the work request

was cancelled

on January

18 by the

EC maintenance

team leader

based

on

a walkdown he

had performed in December

1995.

~

On January

10,

1996,

the inspector

noted that, while there

was

no active

leak on the Unit

1 Train A EC pump, it did have

a work request

tag which

identified

a leak rate of "2-3 drops per second."

The .inqpector

subsequently

identified that this work request

had

been cancelled

in

August

1995.

~

On January

12,

1996,

the inspector

noted that the Unit 3 Train A

EC

expansion

tank makeup Valve EC-LV-015 had

a Work Request

Tag 900965,

which stated that valve would not make

up to the surge tank with the

valve open.

The inspector discussed

this work request with the Unit 3

shift supervisor.

On January

14, technicians

determined that

deficiencies

in the setpoints for the expansion

tank nitrogen regulator

and the expansion

tank level instrument controlling Valve EC-LV-015

contributed to prevent

makeup flow with the

makeup valve open.

In

essence,

the stackup of instrument setpoint deficiencies

had resulted

in

an expansion

tank pressure

that exceeded

the pressure

of demineralized

water makeup pressure.

The shift supervisor initiated

CRDR 3-6-0013 to

have the condition evaluated.

The inspector

noted the shift supervisor

was aggressive

in pursing

and ensuring resolution of these

concerns.

On January

16, the inspector

met with HVAC maintenance

management

and

team

members,

the

EC system engineer,

and the

EC design engineer.

The inspector

noted the findings discussed

above

and the current configuration of the

EC

system instrumentation.

The inspector

noted that the

EC design engineer

was

1

(I

I

l

-19-

not aware that

an

EC leak rate calculation existed.

Suhs

quent to the

meeting,

the inspector

reviewed the

DBH for the

E

system

and noted that it

specified

a maximum leakage criteria of 0.375 gph.

The inspector

informed the

licensee of the criteria.

On January

19, the inspector

performed

a rough calculation of the size of the

Units

1 and

3

EC pump seal

leaks.

The inspector estimated that the Unit 3

Train

8

EC

pump seal

leak exceeded

the 0.375

gph criteria.

The inspector

informed the licensee of this estimate.

The licensee

subsequently

collected

seal

leakage for an extended

period

and determined

the leak rate to be

approximately 0.42 gph.

The licensee

removed the

pump from service shortly after the leak rate

measurement

and repaired

the seal.

The licensee

also performed

a review of

the maximum leak rate criteria (see Section 4.3.3)

and revised it to the

0.63 gph.

The licensee

scheduled

a repair of the leaking Unit

1

EC pump seal

for the next Train A outage.

4.3.6

Conclusions

The inspector

concluded that the

EC system configuration

changes

had not been

appropriately

reviewed

and that the c'ompensatory

actions

had not been

adequate.

In addition, the licensee

had subsequent

opportunities to identify

that the

EC system

was sensitive to

a system leak.

In particular,

in

February

1994,

the licensee

performed

a calculation which determined that the

system

maximum leak rate

was

9 gallons per day.

In Hay 1994, the licensee

recognized

a regulatory requirement that this leak rate

be verified with

testing. 'owever,

the licensee

had not established

testing

and

had not made

operations

or maintenance

personnel

aware that

a relatively small

system leak

could exceed

design basis calculations.

The inspector

subsequently

identified

a system leak which exceeded

the design basis calculation.

The failure to perform

EC system leak rate testing

was identified as

a

violation of 10 CFR Part 50, Appendix B, "Test Control."

(528/9525-03)

The inspector considered

that the licensee

had identified this violation in

Hay 1994.

However,

the inspector considered

that the licensee

had not

corrected

the violation in a reasonable

time.

This conclusion

was

based

on

the relatively small size of the maximum leak rate of the system,

the

consequences

of a loss of

EC system

volume during

a design basis

event,

the

initial lack of recognition of the

HVAC maintenance

and engineering

team of

the potential

impact of

EC system leakage,

and the presence

during the

inspection of a leak which exceeded

this leak rate.

4.4

EC

S stem Review Conclusions

The inspector discussed

these

findings with plant management

at the exit

meeting

and in subsequent

discussions.

The licensee

recognized that the

performance

of the

HVAC team,

including maintenance,

system engineering,

and

design engineering,

had

been

weak.

In addition,

they concurred that

~

1

'

-20-

manaevent

had not been sufficiently critical in thei- evaluation of the

team's

performance

in the resolution of the

EC system issues.

The licensee initiated

an

EC system task force modeled after the successful

emergency diesel

generator

task force, discussed

in Section 7.2, to address

problems identified by the line organization,

Nuclear Assurance,

and the

inspectors.

5

MAINTENANCE OBSERVATIONS

(62703)

5. 1

Essential

Chiller Haintenance

Unit

1

On January

10,

1996,

the inspector

observed

the

HVAC technicians verify the

setpoint

and operation of the low refrigerant temperature

switch for the

Train

B chiller.

The inspector

noted that the technicians

were knowledgeable

about the mechanics of the chiller.

The technicians

performed the component

manipulations

as directed

by the maintenance

task.

The inspector

concluded

that the technicians'erformance

of the maintenance

task

was good.

5.2

Lon

Term Coolin

Instrument

Loo

Calibration - Unit 2

On January

17, the inspector

observed

the instrument

and calibration

technicians

perform

an instrument

loop calibration for the Train

B high

pressure

safety injection long term cooling flow transmitter.

The inspector

noted that the technicians

exhibited

good knowledge of the Rosemount

transmitters

and strong

knowledge of the maintenance

task

and calibration

equipment.

The inspector

concluded that the technicians'erformance

of the

maintenance

task was good.

5.3

Other Maintenance

Observations

The inspectors

observed

the following maintenance

activities

and determined

that they were performed

by knowledgeable

technicians

using appropriate

procedures:

~

Breaker

and cubicle alignment of a Class

4160 volt breaker

Unit

1

~

Inspection of Limitorque

SMC valve motor operator

Unit 2

6

SURVEILLANCE OBSERVATION

(61726)

6.1

HTC Test at Power - Unit 3

On January

13, the inspector monitored the preparations

for the

HTC

surveillance test.

The inspector

noted that the shift supervisor

questioned

what the effect of inserting the control element

assemblies

(CEAs) below

transient insertion limit (TIL) would have

on

SDH.

The TIL is the minimum CEA

height required to assure

that,

at

any power level, the minimum shutdown

margin is available,

maximum core peaking factors

are not exceeded,

and the

~

I

a

l

i

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-21-

reactivity inserted

by the postulated

ejection

oF '.he highest worth

CEA is

acceptable.

The inspector

noted that the shift supervisor's

proactive

questioning

before starting the

HTC test revealed

several

deficiencies.

6. 1. 1

SOH Verification

The shift supervisor directed the shift technical

advisor to calculate

the

SDM

with the

CEAs below the TIL.

The shift technical

advisor utilized the

operator assistance

program aid to calculate

the

SDM and initially reported

that the

SOH would be adequate.

Upon further review,

the shift technical

advisor identified that the incorrect operator

assistance

program aid was

used.

Using the correct program,

the shift technical

advisor determined that

the

SDN would be inadequate if the

CEAs were inserted

below the TIL.

The

licensee

issued

a

CROR to evaluate this error.

The inspector inquired whether the shift technical

advisor verified adequate

SDM using the operator assistance

program aid with all the

CEAs fully

withdrawn (150 inches).

The operator assistance

program aid indicated that

the

SDH was inadequate

because it was overly conservative.

The inspector

and

the shift supervisor discussed

the operator assistance

program

SDN results.

The shift supervisor

concluded,

and the inspector

agreed,

that the unit did

not have

an immediate safety concern since

adequate

SDH existed

as long as

CEAs remained

above the TIL curve.

The inspector

noted that the detailed

SOM

calculation contained significant conservatisms

to account for uncertainties

introduced

by the simplicity of the operator

assistance

program aid.

The

shift supervisor reverified with nuclear fuels management

that

SDH was

adequate.

The licensee

issued

a night order to all three units explaining that,

iF the

CEAs are

above the TIL curve,

the

SDN was assured

by the saFety analysis

calculations

performed prior to each cycle.

The licensee

issued

a

CRDR to

evaluate

the

SDN concerns.

The inspector

concluded that the licensee's

initial corrective actions

were appropriate.

6.1.2

TIL Curve

The licensee identified that the TIL curve in the Unit 3 Cycle

6 core

operating limits report was incorrectly drawn.

The TIL curve indicated that

for 100 percent

power, the TIL was at regulating group five at

120 inches.

The licensee

reviewed the core reload analysis

and noted that the correct

value for the curve was regulating group five at

108 inches

as it has

been in

the past for all three units.

On January

14, the licensee

issued

a revision

to the core operating limits report with the correct TIL curve.

In addition,

the licensee initiated

a

CRDR to evaluate

how the curve was changed

and not

identified.

The inspector

concluded that the licensee's initial corrective

actions

were appropriate.

-22-

On January

13, the licensee identified that, durirg the performance of several

procedures,

operators

missed

the opportunity to identify the incorrectly drawn

TIL curve.

Specifically, during the performances

of 40ST-9ZZ23,

"CEA Position

Data Log;" 40ST-92Z16,

"Routine Surveillance Daily Hidnight Logs;" and

40DP-90P05,

"Control

Room Data Sheet Instructions;" all of which refer to the

TILs, the operators

did not identify the discrepancy

that

some

CEA positions

were being recorded

below the incorrectly drawn TIL curve.

The operators

withdrew the regulating group fi,ve CEAs one step

and verified

all position indications

were greater

than

120 inches.

The licensee

issued

a

memo to all shift supervisors

to remind crew members

to exercise attention to

detail

when consulting reference

material utilized to satisfy surveillance

test procedures.

The licensee initiated

a

CRDR to further evaluate

the event.

Although there were

some instances

where

CEAs were inserted

below 120 inches,

the inspector

noted that

CEAs were never inserted

beyond the

108 inch limit of

the corrected

TIL curve.

However,

the operators

demonstrated

inattention to

detail

by not verifying the limits specified

in the procedures.

The inspector

concluded that the initial corrective action to withdraw the

CEAs one step to

ensure

compliance with the original TIL curve until issuance

of the revised

TIL curve was appropriately conservative.

In response

to the issues

identified during the

HTC test,

the licensee

initiated

a total of four CRDRs to evaluate

and disposition the issues.

The

inspector will review the licensee's

corrective actions during

a future

inspection

(Inspection

Followup Item 530/9525-04).

6. 1. 3

Conclusions

The inspector

concluded that the

hift supervisors

questioning attitude prior

to the performance of the

HTC test contributed to the identification of

several

issues.

These

issues

included:

(1) errors

by reactor engineering

relative to the TIL curve;

(2) missed opportunities

by the

ope} ators to

identify the errors in the TIL curve

due to inattention to detail;

and

(3) the

use of an outdated

operator assistance

program

by the shift technical

advisors.

The inspector

noted that the licensee

had demonstrated

a sufficient

level of concern for these reactivity control

issues

and that their immediate

corrective actions

were appropriate.

6.2

EC and Ventilation

S stems

Ino erable Action Surveillance

Unit

1

On January

10, the licensee

removed the Train

8

EC system

from service.

The

inspector

noted that the operators

did not place

an entry in the Technical

Specification

component condition record computer to evaluate

the opposite

train components

every

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

when

an

EC train was

removed

from service.

The

inspector

noted that this entry had

been routinely placed

in the computer in

the past to alert operators

to evaluate

the opposite train components.

The inspector discussed

this observation with the shiFt supervisor.

The shift

supervisor directed

a reactor operator to place

the entry into the computer.

I

i

I

-23-

The inspector discussed

the event with operations

management.

The operations

department

leader

noted that the procedure directs

an operator to make the

computer entry "if desired."

The operations

department

leader

issued

an

instruction

change

request

to clarify the procedure

and operations

management's

expectation

that the entry into the computer shall

be performed.

The inspector

noted that, while the initial procedure

was weak, it had not

resulted

in

a performance

problem.

The inspector

concluded that the

corrective actions

were appropriate.

7

ONSITE ENGINEERING

(37551)

7. 1

Solenoid Valve 0 erator

De raded Internal Wirin

On January

3, the inspector

noted during

a routine review of the Unit

1 logs,

that

an operability determination

had

been

performed

on December

22,

1995,

concerning

the operability of several

solenoid-operated

valves inside

containment.

On January

4,

1996,

the inspector

reviewed the operability

determination with both environmental qualifications

(Egs)

and valve services

engineers.

The inspector identified that the operability determination,

as

documented

on December

22,

1995, did not provide sufficient basis for

operability.

On January

5,

1996,

the licensee

revised

the operability

determination

and initiated investigation actions to provide additional

information.

7. l. 1

Actions Taken

h-

the Licensee Prior to January

4

On November

16,

1995, during maintenance activities

on Unit 3 pressurizer

steam

space

sample line containment isolation Valve SS-UV-205, valve services

technicians

identified that the internal wiring f.r the valve had

been

severely

heat

damaged.

The valve was

an environmentally qualified

solenoid-operated

valve.

The heat

damage

was to the lead wires spliced to the

electrical

conduit seal

assembly

(ECSA) which established

the environmentally

qualified seal for the solenoid housing.

The insulation of several

wires was

found to be cracked,

in some instances

exposing

the conductor,

and the

fiberglass

sleeving

over the wires had lost its elastomer coating.

Additionally, the

ECSA sealing material

appeared

to have melted.

On November 21, valve services

engineering initiated

a

CRDR which was

subsequently

assigned

to the

E() group.

The

CRDR was determined

to be

potentially significant

and

an evaluation

was completed

by the

Eg group

on

December

20.

Although

a history search

performed for the initial evaluation,

had not identified any similar failures, valve services

personnel

identified

a

similar failure in 1993

on Unit 2 Valve SS-UV-204 to the

Eg group

on

December

21.

This prompted the licensee

to consider

an operability

determination for the following valves:

I

Reactor coolant

sample valve for the hot leg, pressurizer

surge line,

and pressurizer

steam

space

(SS-UV-203,

-204 and -205, respectively) for

all three units.

Six steam generator

sample valves for all three units.

~

Two auxiliary pressurizer

spray Valves

CH-UV-203 and -205 in Units

2

and 3.

The Unit

1 valves were

a different model.

Plant operations

completed

an operability determination

on December

22 in

accordance

with Procedure

40DP-90P26.

The licensee

had determined that the condition represented

a significant

condition adverse

to quality and performed

a root cause

review on both the

ECSAs found on Unit 3 SS-UV-205

and Unit 2 SS-UV-204.

In addition, the

Eg

group performed

a Justification for Continued Operation

as required

by

10 CFR 50.49.

7.1.2

Assessment

of the

OD

On January

4,

1996,

the inspector questioned

the adequacy of the

OD based

on

the following observations:

~

.

The

OD identified that the degraded

fiberglass

sleeving

guarded

against

shorting

and that it was not expected

to further degrade significantly.

The inspector

found that this statement

was not well supported.

The

inspector

noted that lead wires were relatively long and would have

been

tightly packed

inside the housing.

Although the SS-UV-205,performed

adequately prior to its disassembly, it appeared

that similar

degradation

at other point". in the wiring could lead to

a fault.

In

addition,

the wiring from Unit 2 SS-UV-204

had faulted.

The

OD stated that in a review of the operating circuits,

a failure

could only either cause

a valve to close or result in a loss of position

indication.

The valves

are de-energize

to close.

The inspector

questioned

whether

a fault between

a solenoid wire and

an indication

wire could either cause

a valve to open or keep

an open valve from

closing.

The licensee

subsequently

determined that it was possible for

an open valve to remain

open

due to

a fault.

The

OD stated that the safety function of the reactor coolant

and

steam

generator

sample valves

was to close to provide containment isolation.

However,

the

OD did not address

the Technical Specification 3.3.F 1

function for these

valves to open to support postaccident

sampling.

The

OD noted that the safety function of the pressurizer

spray valves

was to open.

However, it discussed

the availability of redundant

means

called out in the emergency

operating

procedure

to perform the

same

i

0

f

-25-

Function.

The

OD did not address

the Technical Specification 3.4.3.2

requirement that both auxiliary pressurizer

spray valves

be operable.

7.1.3

Licensee Actions Taken After January

4,

1996

On January

5, the licensee

performed

more investigation

and revised the

OD.

The licensee

discussed

their conclusions

that the subject valves

remained

operable with the inspector,

Region

IV personnel,

and the

NRR project manager

during

a conference call.

The revised

OD was

based

on additional

information

and analysis

gathered

since January

4.

The inspector

concluded that this

information and analysis

provided reasonable

assurance

that the subject

valves

remained

operable.

In addition,

the licensee

identified that there

was

a timing circuit which,

following the opening of one of these

solenoid valves,

dropped

the voltage

applied to the solenoid

from the opening voltage of 125 Vdc to

a holding

voltage of 40 Vdc.

They noted that this circuit was not tested

and its

failure would not directly be observed.

They suspected

that the failure of

this timing circuit could have

caused

the

damage to Unit 3 SS-UV-205.

The licensee

subsequently

initiated testing of the circuits to the subject

valves to determine if there

were

any existing faults

and to check the

functioning of the timing circuits.

The licensee identified four timing

circuits that were not functioning properly, including the circuit for Unit 3

Valve SS-UV-205.

The licensee

also identified two other conditions which

contributed to the excess

heat to Valve SS-UV-205.

The valve operator

housing

had

been insulated,

increasing

the heat retained

in the valve operator.

In

addition,,in,.1994

a modification had

been

made to this family of valves.

The

licensee

had lowered the point where the

ECSA entered

the valve operator

housing with respect

to the valve body, increasing

the heat to which the

ECSA

was exposed.

The licensee

determined that, while none of these conditions

alone could have resulted

in the damage,

the three

combined would have.

The licensee

inspected all of the subject valves

and

removed insulation in the

instances

where it was identiFied.

The licensee

also evaluated

the as-found

conditions of all the subject valves

and concluded that they were operable.

7. 1.4

Licensee

Followup Actions

The licensee initiated

a significant condition investigation which was

underway at the

end of the inspection period.

In addition,

they planned to

perform

a lessons

learned evaluation of problems identified during their

investigation.

The inspector

discussed

some preliminary findings with the

engineering

department

leader responsible for Eg.

He noted that the following

problems

would be reviewed:

~

The

CRDR initiated for the Unit 3 SS-UV-205 deficiency was prematurely

assigned

to the

Eg group.

This assignment

presupposed

that the cause

t

was environment related.

~

I

I

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l

-26-

The history search did not reveal similar problems with ECSAs.

However,

a similar failure was identified by the valve services

group.

~

The licensee

had originally planned

to perform

a root cause

evaluation

for the

1993 failure of Unit 2 SS-UV-204.

This evaluation

had not been

performed.

~

As discussed

above,

the configuration

and environmental

conditions for

many of these

valves did not match the

Eg analysis.

7. 1.5

Operability Determinations

The inspector discussed

the findings regarding-the

OD for the

ECSAs,

as well

as the failure to document

an

OD for the Unit 3 Train A

EC chiller (see

Section 4.2), with the operations

department

leader responsible for the

OD

process.

The inspector

noted that the evaluation contained

in the

ECSA

OD

addressed

the operability of several

valves,

each with more than

one

safety-related

function.

The

OD had not been structured

such that

a reader

could easily determine

what deficient condition was being addressed

for a

given function.

The operations

department

leader concurred with the

inspector's

assessment.

In addition,

the operations

department

leader recognized

that the

ECSA

OD

contained substantially

more information than the process

intended

and did not

capture

what additional

information was needed

to further develop the

determination.

He noted that these

weaknesses

had

been previously identified

and that

he planned to address

these

issues

with further training and

a

procedure

revision planned for mid 1996.

The inspector

noted that the

problems

observed,

during this inspection period regarding

OD, concerned

the

implementation of the procedure

and not its content.

The inspector considered

that the planned actions to be appropriate if an emphasis

was placed

on the

program implementation.

7.1.6

Conclusions

In summary,

the inspector identified that operations

failed to critically

assess

an incomplete operability determination

evaluation provided

by the

engineering

organization regarding safety related

solenoid valves.

Plant

operations

approved

an

OD evaluation for several

safety-related

solenoid

valves

even though the engineering

evaluation did not thoroughly address

the

effects of potential

heat

damage

on the Technical Specification functions of

some of the valves.

The inspector

observed

that when the weakness

in the

OD

evaluation

was brought to the licensee's

attention,

they took prompt actions

to re-perform the evaluation

and provided

a thorough analysis.

Additionally,

the licensee

took prompt action to inspect for and correct deficient plant

conditions.

The inspector

noted that the licensee

had initiated

a lessons

learned evaluation of the issue

and

had identified weaknesses

in the

implementation of the corrective actions,

the

Eg,

and the

OD programs.

-27-

7.2

Emer enc

Diesel

Generator

Cooldown Tri

Evaluation

In

NRC Inspection

Report 50-528/95-21;

50-529/95-21;

50-530/95-21,

the

inspector

noted that the licensee

had established

a multi-discipline task

force to determine

the cause of several

emergency diesel

generator

cooldown

trips.

During this inspection period,

the task Force completed its

investigation.

The task force determined that minor degradation

of several

different components

in the nonsafety-related

maintenance

run protective trip

circuitry had apparently

combined to cause

the spurious trips.

They

identified that

some of the degradation

was due to aging

and that

some of the

degradation

had

been

induced

by maintenance

practices.

The task force presented

their findings to plant management

and initiated

corrective actions to address

the deficiencies identified.

They also

presented

their findings to the Cooper-Bessemer

diesel

owners group.

The inspector

noted that the evaluation

performed

by the task force was

an

exceptional

product.

The investigation to identify the deFiciencies

had

been

based

on reviews of industry experience,

equipment

performance

trending, field

observations

and troubleshooting,

interviews with operators,

and laboratory

testing.

The results

were documented

in a clear format describing

the

conditions

found, the apparent

causes

of the deficiencies,

and the corrective

actions that were initiated.

8

PLANT SUPPORT

(71750)

Hain Steam

Su

ort Structure

Platform Installation

Unit I

On December

21,

1995,

the inspector

observed

poor housekeeping

and

construction practices

during the installation

oF

a platform in the main

steam

support structure.

Specifically, the inspector

noted that welding

equipment

was left energized

during

a lunch break

and minimal barriers

were

present

to contain metal filings from drilling, grinding,

and welding.

The

inspector discussed

the observations

with the shift supervisor,

and the

director of site maintenance,

and modifications.

On January

3,

1996,

the

inspector

noted that the construction

area

housekeeping

had greatly improved.

At the exit meeting,

the inspector

presented

the concern that the maintenance

foreman

and workers

had

a low sensitivity towards

housekeeping

when working in

safety-related

spaces

in an operating unit.

The site maintenance

director

agreed with the inspector's

concerns

and indicated that the licensee's

expectations

for housekeeping

were re-enforced

to the contractors

performing

the platform installation.

In addition,

the director indicated that the

prejob briefings for the contractors

would address

what equipment could be

affected

by the work being preformed.

The licensee

informed the contractor's

management

that the licensee's

standards

for housekeeping

were not being met.

The inspector

concluded that the licensee's

response

to the issue

was

excellent.

\\

0

-28-

9

FO'LOWUP - OPERATIONS

(92901)

9. 1

Closed

Violation 529 9431-02:

Boron Concentration

Not Verified Ever

2 Hours

This violation involved the failure to determine

the reactor coolant

system

boron concentration

at the frequency specified in the core operating limits

report

when

a startup

channel

high neutron flux alarm was

removed

from

service.

The licensee

determined

that the cause of the violation was that the shift

supervisor

and control

room supervisor did not correctly determine

the

appropriate

actions for an inoperable startup

channel

and the crew did not

question

the assessment

of the required actions.

In addition, the maintenance

task

and surveillance

logs did not provide adequate

guidance for the action

required with a startup

channel

inoperable,

The licensee initiated several

corrective actions.

The licensee

added

a note

to the routine surveillance

logs to perform 4XST-XZZ24, "Startup

Channel

High

Neutron Flux Alarm Inoperable

3. 1.2.7,"

when

a startup

channel

is out of

service.

The licensee

changed

36MT-9SE07,

"Excore Startup

Channel

Calibration," to add the requirement

to perform 4XST-XZZ24 prior to removing

startup

channels

from service.

The licensee

issued

a night order to all

three units discussing

the event

and reinforcing management's

expectations

on

performance of surveillance tests.

The inspector

reviewed the procedures

previously mentioned

and noted that the

changes

were

implemented.

The inspector

concluded that the licensee

conducted

a thorough review of the issue

and performed appropriate corrective actions.

9.2

Closed

Violation 529 9431-05:

Failure to Follow CVCS Procedure

Dilution Event

This violation involved the failure to ensure

the automatic

makeup valve

closed after the desired

volume of water

had

been

added to the reactor coolant

system.

The inspector verified the corrective actions described

in the

licensee's

response letter,

dated

January

6,

1995, to be reasonable

and

complete.

The inspector

noted that

no similar problems

were identified.

In

addition,

the inspector questioned

several

licensed

operators

about the

performance of the automatic

makeup valve

and all responded

that the valve

exhibited

no deficiencies.

9.3

Closed

Violation 530 9438-01:

Incom lete Lineu

Durin

Reduced

Inventor

0 erations

This violation involved the failure to align the required reactor coolant

system

makeup

flow paths prior to entering

a reduced

inventory condition.

As

a result,

the licensee

entered

an event with high safety significance.

jl,'fl

-29-

The licensee

determined

the root cause of the event

was

a personnel

error on

the part of the control

room supervisor.

The licensee

noted that the control

room supervisor lost

command

and control of the evolution in that

he did not

direct the alignment or verify the alignment of the makeup flow paths.

The

licensee

concluded that the error by the control

room supervisor

was

an

isolated

performance error and the control

room supervisor

was returned to

onshift duties.

The licensee initiated several

dedicated

midloop crews consisting of a senior

reactor operator 'and

a reactor operator

to perform the midloop evolutions.

The crews were in addition to the normal

crew complements

The inspector

assessed

the performance of the licensee

in several

midloop

conditions.

The inspector

noted

a minor weakness

in the use of the sightglass

for level verification

(NRC Inspection

Report 50-528/95-06;

50-529/95-06;

50-530/95-06).

The inspector

noted strengths

in the performance of the most

recent

midloop evolutions

(NRC Inspection

Reports

50-528/95-10;

50-529/95-10;

50-530/95-10

and 50-528/95-21;

50-529/95-21;

50-530/95-21).

The inspector

concluded that the licensee's

performance of the midloop evolutions

have

significantly improved since the occurrence of the violation.

10

IN OFFICE REVIEM OF LERs

(90712)

The following LER revisions

were reviewed inoffice and determined

to be

acceptable.

The

LERs were issued to correct typographical

errors

and

add

component identification codes.

LER 528/94-05,

Revision 2:

Core Protection Calculator,

Delta-T Power

Fluctuations

LER 528/94-07,

Revision

1:

Surveillance

Requirement

Hissed for

Containment

Purge Isolation Valves

LER 528/94-09,

Revision

1:

Letdown Isolation Valve Leakage

Impact

On

Appendix

R Requirements

LER 528/94-10,

Revision

1:

Hisalignment of Limitorque Torque Switch

Contact

Bar Prevented

Remote Operation of HOVs

LER 529/94-04,

Revision 2:

Class

1E Batteries

in

a Degraded

Condition

LER 529/94-08,

Revision

1:

Use of Uncalibrated

Boronometer

Causes

a

TS

SR to

Be Hissed

ATTACHHENT 1

1

Persons

Contacted

1.1

Arizona Public Service

Com an

  • T. Cannon,

Department

Leader,

Nuclear Engineering

and Projects

  • R. Flood, Department

Leader,

System Engineering

  • B. Grabo,

Section

Leader,

Compliance,

Nuclear Regulatory Affairs

  • W. Hartley, Offsite Review Committee

Member

  • R. Hazelwood,

Engineer,

Nuclear Regulatory Affairs

  • M. Hypse,

Section

Leader, Electrical Maintenance

Engineering

  • A. Krainik, Department

Leader,

Nuclear Regulatory Affairs

  • J. Levine, Vice-President,

Nuclear Operations

  • R. Lucero,

Department

Leader,

Electrical Maintenance

  • D. Mauldin, Director, Maintenance
  • W. Montefour, Senior Representative,

Strategic

Communications

  • G. Overbeck,

Vice President,

Nuclear Support

  • C. Russo,

Department

Leader,

Nuclear Assurance

  • C. Seaman,

Director, Nuclear Assurance

  • W. Stewart,

Executive Vice-President,

Nuclear

1.2

NRC Personnel

  • D. Kirsch, Chief, Reactor Projects

Branch

F

  • K. Johnston,

Senior Resident

Inspector

  • D. Garcia,

Resident

Inspector

  • J. Kramer, Resident

Inspector

1.3

Others

  • F. Gowers, Site Representative,

El

Paso Electric

  • K. Slagle,

Manager,

San Onofre N<<clear Oversight

  • Denotes those

present

at the exit interview meeting held

on January

24,

1996.

The inspectors

also held discussions

with and observed

the actions of other

members of the licensee's

staff during the course of the inspection.

2

EXIT MEETING

An exit meeting

was conducted

on January

24,

1996.

During this meeting,

the

inspectors

summarized

the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

r

t[

ATTACHMENT 2

LIST OF ACRONYMS

CEA

CRDR

DBM

EC

ECSA

EER

Eg

FSAR

GDC

HVAC

LER

MTC

OD

SDM

TIL

control element

assembly

condition report/disposition

report

design basis

manual

essential

chilled water

electrical

conduit seal

assembly

engineering

evaluation report

environmental qualification

final safety analysis report

general

design criteria

heating, ventilation,

and air conditioning

licensee

event reports

moderator

temperature

coefficient

operability determination

shut

down margin

transient

insertion limit

i

'

k