ML17311B284

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Insp Repts 50-528/95-18,50-529/95-18 & 50-530/95-18 on 950924-1104.Noncited Violations Noted.Major Areas Inspected:Onsite Response to Plant Events,Operational Safety,Maint & Surveillance Activities & LER Review
ML17311B284
Person / Time
Site: Palo Verde  
Issue date: 11/24/1995
From: Huey F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311B283 List:
References
50-528-95-18, 50-529-95-18, 50-530-95-18, NUDOCS 9512050275
Download: ML17311B284 (30)


See also: IR 05000528/1995018

Text

ENCLOSURE

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/95-18

50-529/95-18

50-530/95-18

Licenses:

Licensee:

NPF-41

NPF-51

NPF-74

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

,Facility Name:

Palo Verde Nuclear Generating Station,

Units 1, 2,

and

3

Inspection At:

Maricopa County, Arizona

I

Inspection

Conducted:

September

24 through

November 4,

1995

Inspectors:

K. Johnston,

Senior Resident

Inspector

J.

Kramer, Resident

Inspector

'. Garcia,

Resident

Inspector

D. Acker, Senior Project Engineer

Approved:

uey, Acting

C

>e

,

eactor

ProJects

anc

F

te

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of onsite

response

to plant events,

operational

safety,

maintenance

and surveillance

activities, onsite engineering,

refueling activities

and licensee

event report

review.

Results

Units

1

2

and

3

0 erations

~

A control

room supervisor

in Unit 3 reviewed the wrong section of

the steam generator

blowdown system procedure,

which led to

exceeding

licensed

thermal

power.

A non-cited violation was

identified (Section 2,1).

~

A control

room supervisor

demonstrated

excellent

command

and

control during the planned

shutdown in Unit 3 (Section 2.2).

95l2050275

951%24

PDR

ADOCK 05000528

6

PDR

'

.

An auxiliary operator in Unit 3 displayed

good attention to detail

for identifying non-seismic qualified scaffolding in safety-

related

equipment

rooms.

The use of improperly qualified

scaffolding

was identified as

a non-cited violation (Section 2.3).

A work control senior reactor operator in Unit 3 failed to

properly review

a work order clearance,

resulting in

a loss of

reactor coolant

system inventory.

A non-cited violation was

identified (Section 2.4).

Two auxiliary operators

in Unit 3 failed to properly align and

independently verify a valve required for reactor coolant

system

draindown.

A non-cited violation was identified (Section 2.5).

A reactor engineer

in Unit 3 displayed

a lack of attention to

detail resulting in

a mispositioned

fuel assembly

in the spent

fuel pool.

Also, refueling personnel

exhibited insensitivity

towards

a reactivity management

issue.

A non-cited violation was

identified (Section

6. 1).

Refueling machine

personnel

were knowledgeable

about refueling equipment

and procedures

(Section 6.2).

t

Haintenance

Surveillance

~

Electrical maintenance

personnel

responded

appropriately to

a

failure of the Unit 2, Train

B diesel

generator

(Section 3. 1).

~

Hechanical

maintenance

personnel

displayed

good judgement during

troubleshooting efforts on the Unit 2, Train A auxiliary feedwater

pump (Section 3.2).

En ineerin

and Technical

Su

ort

~

Haintenance

engineering

displayed

a questioning attitude

and good

knowledge of Technical Specifications

when evaluating

a high pressure

safety injection

pump relief valve lifting (Section

5. 1).

Summar

of Ins ection Findin s:

A non-cited violation was identified for failure to follow a steam

generator

blowdown procedure

(Section

2. 1).

A non-cited violation was identified for failure to follow a procedure

for installing seismically qualified scaffolding (Section 2.3).

A non-cited violation was identified for failure to follow a clearance

generation

procedure

(Section 2.4).

A

'l'

,

,,[

ld

'fi

l

~

A non-cited violation was identified for failure to follow a

valve'osition

verification procedure

(Section 2.5).

~

A non-cited violation was identified associated

with mispositioning of a

fuel assembly

in the spent fuel pool (Section 6. 1).

~

One licensee

event report was reviewed

and closed

(Section 7).

Attachments:

1.

Persons

Contacted

and Exit Meeting

2.

List of Acronyms

0

l

l

l

l

e

4-

1

PLANT STATUS

Units

1 and

2 operated

throughout the inspection

period at full power with no

significant events.

Unit 3 began the inspection period at

100 percent

power.

On October

14, the

unit was taken off-line in preparation for a refueling outage.

On October

18,

the unit entered

Node

6. and

began

a core offload on October 20.

The unit

ended

the inspection

period with the core offloaded to the spent fuel pool.

2

OPERATIONAL SAFETY VERIFICATION

(71707)

2. 1

Misali nment in the Steam Generator

Blowdown

S stem - Unit 3

On September

23, operators

placed

the steam generator

blowdown system in a

configuration that was not consistent

with that

assumed for the secondary

calorimetric calculation performed

by the core operating limits supervisory

system

(COLSS).

As

a result, for a period of approximately nine hours,

COLSS

underestimated

actual

power by approximately 0. 11 percent

power.

The

secondary calorimetric provided by COLSS was the primary indication of power

used

by operators

and

as

a result,

the plant

was operated slightly above

100

percent

power for approximately

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The steam generator

blowdown system

has three

modes of operation;

normal,

abnormal,

and high rate.

On September

23, chemistry personnel

requested

that

operators

return the system to normal rate from the abnormal rate.

The

control

room supervisor

had both the abnormal

blowdown flow control valve and

the isolation valves closed.

At the following shift turnover, the*night shift control

room supervisor

informed the oncoming day shift control

room supervisor that the

abnormal

blowdown isolation valves were isolated.

The day shift control

room

supervisor

determined that the isolation valves

should

have

been

open

and

directed

an auxiliary operator to reopen

the valves.

The day shift control

room supervisor

recognized that the abnormal

blowdown

lineup was not consistent

with the lineup established

for the test

used to

develop the blowdown flow constant that is entered

into the

COLSS for the

secondary calorimetric calculation.

The test

was performed with the

abnormal

blowdown isolation valves in the open position

and the flow control valves in

the closed position.

The flow control valves

are not designed to be leak

tight in the closed position,

and

an

assumed

leakage rate

was incorporated

into the blowdown constant test.

The inspector

noted that in COLSS,

the steam flow equals

feed flow minus

,blowdown flow.

With the abnormal

blowdown isolated,

actual

blowdownflow was

less

than the constant

inserted into COLSS.

Therefore,

actual

steam flow was

greater

than

COLSS calculated

steam flow.

Since

secondary

power was directly

related to steam flow, actual

power was greater

than indicated

power.

l

The licensee

subsequently

determined that licensed

thermal

power

had

been

exceeded.

The operators

reduced reactor

power from 100 percent to 98.8

percent for an hour to ensure that the

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> average

power was less

than

100

percent.

The licensee

calculated that the highest hourly power was

100. 14

percent

and the highest

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> rolling average

power was 100.07 percent.

The licensee initiated

a condition report/disposition

request

(CRDR) to

evaluate

the event.

They found that the control

room supervisor

had reviewed

the wrong section of the

blowdown system operating

procedure,

and noted that

the control

room supervisor

had performed the actions to isolate the blowdown

isolation valves without including the rest of the control

room team in the

decision.

Additionally, the licensee

found that the precaution

and

limitations steps

provided misleading

informati.on and noted other causal

factors that

may have contributed to the event.

Also, the licensee"noted

that

the change

in operating philosophy to leave the blowdown isolation valves to

the blowdown flash tank open

was communicated

to Units

1 and 2, but there

was

no documented

evidence that this change

was effectively communicated

to Unit

3.

e

The licensee

performed the following corrective actions:

~

Issued

a night order to all- three units describing the event

and the

procedure

weaknesses.

Initiated

a procedure

change to eliminate the inaccurate

precaution

and

limitation step

and subsequently

issued

a

new revision to the procedure.

Counseled

the control

room supervisor

on the event.

Issued 'a letter to the shift supervisors

and control

room supervisors

detailing operation

teamwork issues

and expectations.

Issued

an operations

news flash

on the procedure

change

process

and the

necessity of informing operators

of procedure

changes.

Planned to discuss

the event in licensed operator training.

The inspector

reviewed the

CRDR and the corrective actions.

Additionally, the

inspector

reviewed

a Licensee

Event Report (50-530/95-02).

The inspector

noted that the event

was

bounded

by the assumptions

in the Updated

Final

Safety'nalysis

Report for thermal

power of 102 percent.

This licensee

identified and corrected violation is being treated

as

a non-cited violation,

consistent

with Section VII of the

NRC Enforcement

Policy.

2.2

Plant Shutdown

Unit 3

On October

14,

1995', during

a night shift tour, the'inspector

observed

operations

personnel

commence

a planned reactor

shutdown in preparation of the

fifth refueling outage for Unit 3.

The operations staff began the decrease

in

P

,

reactor

power at approximately

10:24 p.m.

The inspector

observed

the reactor

operator manually trip the reactor at 27 percent reactor

power.

Following the reactor trip, the control

room operators

implemented

the

standard

post trip procedures.

The inspector

observed

control

room operators

respond to plant anomalies

and various alarms.

The inspector

noted

good

procedure

usage

and communications.

The inspector

concluded that the control

room supervisor'isplayed

excellent

command

and control, the operators

were

attentive

and responded

appropriately to various alarms.

2.3

Non-seismicall

uglified Scaffoldin

Installed

Unit 3

On October

16,

1995, during routine area

rounds.,

an auxiliary operator

identified non-seismic

scaffolding installed in both trains of the essential

cooling water heat

exchanger

rooms.

The auxiliary operator notified the shift

supervisor

and discussed,

the. operability concern for the essential

cooling

water heat exchanger.

The backshift scaffolding supervisor,

site shift

manager,

and the outage control

manager

were also informed of the event.

The scaffolding supervisor

determined that the scaffolding was not built to

the required seismic qualifications

and directed

a scaffolding crew to rebuild

the scaffolding in accordance

with seismic qualifications stated

in Procedure

30DP-9WP11,

Revision 5, "Scaffolding Instructions."

A previous

example of

non-seismic scaffolding installed in areas with safety-related

equipment

was

identified by the

NRC and documented

in Inspection

Report 95-12.

The licensee

initiated

an operability determination

and

a

CRDR.

Licensee

management

initiated

a stop work for all scaffolding installation, briefed the

scaffolding crews

on the event,

and performed

a walkdown of all installed

scaffolding in Unit 3.

The scaffolding

crew, installed the scaffolding

on October

14 using Procedure

30DP-9WP11,

Revision 4.

Revision

4 allowed the scaffolding crew foreman the

flexibilityto determine

whether or not scaffolding would be installed to

seismic qualifications.

The previous day, Revision

5 to the procedure

became

effective

as part of the corrective actions for the inspector's

previous

concerns.

In addition to other enhancements

to the procedure,

Revision

5 did

not allow the foreman the flexibilityto determine

whether or not scaffolding

would be installed to seismic qualifications.

The licensee

had briefed

7 of

the

9 scaffolding crews

on Revision

5 to the'procedure.

The other two crews

'ad

been

on their scheduled

days off.

The scaffolding crew in question

had

not been

aware of the

new procedure revision.

The two crews were briefed

after the scaffolding

had

been installed incorrectly.

However,

the

scaffolding crew did not question

the adequacy of the installed scaffolding.

The inspector

noted that the scaffolding crew failed to construct

the

scaffolding in accordance

with Revision

4 of the procedure.

In addition, the

scaffolding foreman responsible for the October

14 job had also

been

involved

with the previous

events

documented

in Inspection

Report 95-12.

The inspector

t

noted the inadequacy

of communications

and the improper verification of the

most current procedure revision.

P

I

0

The non-seismic

scaffolding

was identified by the auxiliary operator

when the

unit was in Node 5.

Technical Specifications

do not require the essential

cooling water heat

exchangers

to be operable

in Node 5.

However,

the

scaffolding

had

been installed

on October

14,

when the plant was in Node

4

when both trains of essential

cooling water heat

exchangers

were required to

, be operable.

Design engineering

performed

an evaluation

which determined that the as-found

conditions of the scaffolding would not have

damaged

the essential

cooling

water heat

exchangers

during

a seismic event.

Therefore,

the non-seismic

scaffolding

had

no impact

on the operability of the essential

cooling water

'eat

exchanger.

The inspector discussed

this determination with the design

engineer

and agreed with the licensee's

conclusion.

The licensee

counselled

and disciplined the foreman

who was involved in both

events

and provided additional training to the scaffolding crews.

The

licensee

issued

a night order to all op'erators

describing the event.

The

night order indicated that operations

personnel will make the decision for the

approval of non-seismic scaffolding in seismic areas.

The normal expectation

is to have seismic scaffolding always erected

around safety-related

components.

This licensee identified and corrected violation is being treated

as

a non-cited violation, consistent

with Section VII of the

NRC Enforcement

Policy.

2.4

Im ro erl

Authorized Clearance

Causes

a Loss of Reactor Coolant

S stem

Inventor

Unit 3

On October

16, three

days into the Unit 3 refueling outage,

the work control

senior reactor operator authorized

a clearance

without first ensuring that the

required plant configuration

had

been established.

Approximately

15 minutes

after the clearance

was hung,

a reactor operator identified an increasing

level in the reactor drain tank and that leakage

was

coming from the reactor

coolant

system.

The control

room staff evaluated

the activities in progress

and determined that

a recently issued

clearance

drained the reactor coolant

system through the reactor coolant

pumps.

The licensee

suspended

the

clearance,

and stopped

the loss of reactor coolant

system inventory.

The

licensee

calculated that

a

6 gpm reactor coolant

system leak occurred for

total of 51 minutes.

The licensee

determined that the work control senior reactor operator

was

busy

at the beginning of the shift and

numerous

clearances

required authorization

prior to issuance.

An outage coordinator placed

several

reactor coolant

pump

clearances

in the work control senior reactor operator's

basket for review and

authorization.

One of the clearances

required plant conditions to be at half-

pipe,

whereas

actual

plant condition was approximately

50 percent pressurizer

level.

The licensee

defined half-pipe

as

a midloop condition with the core

offloaded.

The work control senior reactor operator

performed

an abbreviated

review of, the clearances

and authorized

implementation.

The work control

senior reactor operator indicated

he recognized

the

scope of the work on the

reactor coolant

pump clearance,

but did not consider

the clearance

scope in

I

conjunction with the plant conditions present

at that time.

The licensee

reinforced the procedure

requirement of 40DP-90P29,

"Clearance

Generation,"

which requires that special

instructions

be placed

on the

clearance

cover sheet that explain the required plant conditions to hang the

clearance.

The licensee

reviewed all the clearances

and

added

special

instructions to the clearances

when necessary.

The licensee initiated

a

clearance

process

review as

a result of this

and previous clearance

problems.

In addition, the licensee

planned to ensure that sufficient additional

work

control

manpower is available'uring

periods of increased

outage activity.

The inspector

reviewed the licensee

evaluation,

discussed

the corrective

actions with operations

management,

and concluded that the corrective actions

were appropriate.

Although the licensee failed to follow the procedure for

clearance

generation,

this licensee identified and corrected violation is

being treated

as

a non-cited violation, consistent

with Section VII of the

NRC

Enforcement Policy.

2.5

m ro er Valve

ineu

Durin

Reactor Coolant

S stem Draindown

Unit 3

On October

17, operations

personnel

attempted to lower reactor coolant system

level

by performing

a draindown to the refueling water tank.

The operators

reviewed

a previously performed valve lineup and discovered that

a required

open valve,

CH-495,

was closed.

The control

room staff directed

an auxiliary

operator to reposition the valve,

and the draindown continued

as expected.

The licensee identified that

an auxiliary operator

had failed to properly

.position valve CH-495 when performing the valve lineup prior to the draindown,

and another auxiliary operator

had failed to properly perform an independent

verification that the valve was open.

During the performance of the initial

positioning

and independent verification, the 'licensee

noted that both

auxiliary operators

were in the

same

room during the valve manipulation.

The

inspector

noted that, while the licensee

procedure

does

not require phys'ical

separation

during verification activities, it recommends

physical

separation

to avoid errors.

The licensee

issued

a night order

and operations

news flash describing

the

event

and the expectations

for proper

independent

review.

The licensee

initiated

a

CRDR to evaluate

the event

and identify further corrective

actions.

The inspector concluded that the initial corrective actions

were

adequate.

The inspector will continue to monitor auxiliary operator

performance.

At the exit meeting,

the inspector

noted the weaknesses

in auxiliary operator

performance

which were identified in the previous

inspection

period

(NRC

Inspection

Report 50-528/95-16;

529/95-16;

530/95-16),

and expressed

concern

for the recent auxiliary operator

performance

problems.

Licensee

management

acknowledged

the recent operations

performance

problems,

and described

current

actions to address

human performance

errors

and weaknesses

in the

implementation of .the equipment

clearance

program.

The inspector

noted that

0

1

the licensee's

reviews in these

areas

were appropriate

and plans to assess

these

areas

in a future inspection.

This licensee

identified and corrected

violation is being treated

as

a non-cited violation, consistent

with Section

VII of the

NRC Enforcement Policy.

3

MAINTENANCE OBSERVATIONS

(62703)

3. 1

Overs

eed Tri

s on Diesel

Generator

Durin

Testin

- Unit

2

During the month of October

1995,

the Unit 2 Train

B diesel

generator

experienced

three

non-emergency trips during operability surveillance testing.

None of the involved trips would have affected the ability of the diesel

generator

to properly function during

an actual

emergency start condition.

Electrical

maintenance

engineering

provided action plans for troubleshooting

and correcting the problems.

The inspector

observed partial troubleshooting

efforts

by the electrical

maintenance

technicians.

The inspector

concluded

that the maintenance

activities were performed appropriately

and these trips

did not impact the safety function of the diesel

generator.

3.1.1

First Trip

On October 3, the diesel

generator

experienced

a trip.

The local

panel

indicated

an "overspeed trip" alarm,

but the overspeed butterfly valve did not

shut, confirming that

an actual

overspeed trip had not occurred.

During an

actual

overspeed

condition, the mechanical

overspeed

governor would trip the

butter'fly valve in the turbocharger air inlet.

Operations

personnel

notified

the electrical

maintenance

engineers

and initiated

a

CRDR.

The electrical

maintenance

technician identified

a loose wire connection

in a

junction box from one of the overspeed butterfly valve limit switches.

There

are

two limit switches

on the butterfly valve which provide overspeed trip

signals

in both the emergency

and test

mode.

The loose connection

made

up the

one out of two logic signals required for a non-emergency

mode trip.

The

licensee

tightened

the wire and initiated

a work request to inspect the

junction boxes for loose connections

on the remaining diesel

generators.

The

inspection of the other junction boxes did not identify other loose wire

connections.

After a satisfactory test run, the Train

8 diesel

generator

was

returned to operable

status.

3. 1.2

Second Trip

On October

18, the diesel

generator

experienced

another indicated

overspeed

trip during

a surveillance test.

The indications

were similar to the previous

overspeed trip that occurred

on October 3.

After extensive troubleshooting,

electrical

maintenance

engineers

identified

a problem with a fiber optic

receiver board.

The technicians

replaced

the fiber optic receiver

board

and

other circuitry boards

and relays.

The trip circuitry and power supplies

had

been

checked.

The limit switches

mounted

on the diesel

were checked for

continuity,

however the inside of the limit switches

could not

be tested

without taking them apart.

The diesel

generator

was tested

and returned to

0'

I

I

-10-

service.

The electrical

maintenance

engineer

suspected

that both trips could have

been

induced

by vibration since both trips occurred after the diesel

generator

had

been started

and loaded.

The trip circuitry remains

energized

at all times

and there were

no indications of a non-emergency trip while the diesel

was in

stand-by

mode.

The electrical

maintenance

department

leader,

site shift

manager,

and shift supervisor conferred

and decided to replace

the two

overspeed limit switches.

3.1.3

Third Trip

On October

21, after the replacement

of the limit switches,

the diesel

generator

was tested

and tripped at full load

on

" Incomplete

Sequence,"

another

non-emergency trip. If the diesel

engine

does

not attain the first

speed point before the timer times out,

an incomplete

sequence

is initiated

and the unit shuts

down.

The diesel

was quarantined

and electrical technicians

began troubleshooting.

An electrical

maintenance

technician identified another

bad fiber optic relay

board.

The inspector

questioned

the electrical

maintenance

engineer

about the

previous

board replacement

and whether or not this board should

have

been

replaced.

The engineer

stated that this board

was not related to the previous

maintenance

activities or the overspeed trips.

The electrical

maintenance

department

leader,

engineers,

technicians,

and the site shift manager

had

a

conference call with the inspectors

and regional

management

to discuss

the

plan of action.

The electrical

maintenance

engineer stated that

no other

malfunctions were identified,

and that the fiber optic board

was replaced

and

the diesel

generator

was satisfactorily retested.

Operations

returned the

Train

B diesel

generator

to service.

3. 1.4

Conclusions

A multi-discipline diesel

generator

task force team

was established

to

determine

the root cause of failure of the recent trips and to provide

an

assessment

of the trips

and control problems.

The team planned to assess

all

trips since

1993

and major events

relevant to the Train

B diesel

generator

for

common

mode failures

and adverse

trends.

The corrective actions will also

be

evaluated

by the

team for effectiveness.

The inspector

concluded that appropriate

actions

were being taken for the

recent trips to the diesel

and the initiation of the task force team

was noted

as

a good effort by management.

3.2

Auxiliar

Feedwater

Pum

Hi

h Vibrations

Unit 2

On October 23,

1995, during the performance of a surveillance test,

the Unit 2

steam driven auxiliary feedwater

pump failed to meet the acceptance

criteria

for pump bearing vibration,

and the

pump

was subsequently

declared

inoperable.

Mechanical

maintenance

engineers

were notified and

a

CRDR was initiated.

k

!

The mechanical

maintenance

engineer

developed

an action plan to determine the

cause of .the vibration.

The inspector

attended

meetings with mechanical

maintenance

engineers

and vibration experts

to discuss

possible

causes.

Oil

samples

were taken,

and the licensee

concluded that bearing

damage

was not the

cause.

Vibration analysts

determined that the vibration data

and maintenance

history indicated that

a coupling misalignment

may have

been the cause.

Mechanical

maintenance

technicians

removed the

pump half of the coupling

and

found that the coupling did not have

a proper interference fit with the shaft.

After the licensee

discussed

this problem with the vendor,

the licensee

determined that the coupling misalignment

would be

a contributor to outboard

bearing vibration.

The technicians

replaced

the

pump half of the coupling

with a new coupling that

had

been field balanced.

The licensee

performed

a postmaintenance

test

and collected vibration data.

The vibrations were below the action level range,

and engineering

recommended

that operations

perform the operability surveillance test.

The surveillance

test

was performed satisfactorily

and the

pump was returned to service.

An

additional test

was performed the next day for trending purposes

to ensure

that the

pump coupling replacement

had reduced

outboard bearing vibrations.

The inspector

observed

the vibration technician obtain data.

The vibration

data obtained

was within the acceptance

criteria.

The last surveillance test performed prior to the October

23 test

was

satisfactory,

however,

because

this

pump

showed

an increasing

trend in

vibrations, the decision

was

made

by mechanical

maintenance

engineering to

place the

pump

on increased

frequency testing until the next refueling outage.

The inspector

concluded that the actions

taken

were appropriate

and will

continue to assess

the licensee's

evaluations of pump performance.

3.3

Other Maintenance

Observations

The inspectors

observed

the following maintenance

activities

and determined

that they were performed acceptably:

~

Charging

Pump

"A" Drain Line Cleaning

Unit 3

~

Ground Fault Relay Replacement

on LPSI Injection Valve - Unit 2

4

SURVEILLANCE OBSERVATION

(61726)

The inspectors

observed

the following surveillance activities

and determined

that they were performed acceptably:

~

Reactor Protection

System Functional Matrix Testing

Unit I

Integrated

Safeguards

Testing

Unit, 3

~

Battery Charger

18 Month Load Test

Unit 3

-12-

5

ONS ITE ENGINEERING '(37551)

5.1

Hi

h Pressure

Safet

In'ection

Pum

Relief Valve Lifted Durin

Surveillance

Unit

2

On October

18, during

a surveillance test of the train

B high pressure

safety

injection pump, relief valve

PSV409 lifted.

The

name plate rating of PSV409

was

10 gpm.

The onshift crew noted that the relief fully opened

and

calculated

the leakage

at

15 gpm.

The high pressure

safety injection

pump

passed

the surveillance test

acceptance

criteria of pump response

time,

differential pressure,

pump vibration,

and miniflow flow rate.

The onshift

crew performed

an operability determination

and concluded that the

pump was

operable.

The licensee initiated

a

CROR to further evaluate

the problem.

On October 20, maintenance

engineering

received

the

CROR and questioned

the

operability of the system to meet Technical Specification Surveillance

Requirement 4.5.2.e.4,

due to the relief valve lifting early.

The

surveillance

requirement

stated,

in part, that all emergency

core cooling

system piping outside of containment

have

a total leakage

less

than

one

gpm

when pressurized

to 40 psi:

The train

B high pressure

safety injection

pump

had

a leakage of greater

than

10

gpm at

1877 psi.

The licensee

replaced

the

relief valve and initiated the evaluation of the cause of failure.

The

inspector

concluded that the maintenance

engineer

displayed

a good knowledge

of Technical Specifications

and

a strong questioning attitude.

The licensee

tested

the relief valve to determine

the actual relief setpoint.

The relief valve lifted at

a pressure

of 2053 psi, with a required setpoint of

2050 psi.

The licensee

planned to continue to evaluate

the events

and plant

conditions that caused

the initial failure mechanism of the relief valve since

the

pop test

was not conclusive.

The inspector discussed

the Octob'er

18 high pressure

safety injection pump

operability determination with the site shift manager.

The inspector

concluded that the assumption

used

by operations

personnel

that the relief

valve would be seated

at 40 psi

was appropriate.

The inspector will continue

to monitor engineering's

evaluation of the relief valve-failure

as part of

future routine inspection.

6

REFUELING ACTIVITIES

(60705

AND 60710)

6. 1

Mis ositioned

Fuel

Assembl

in

S ent Fuel

Pool - Unit 3

On October 22, the licensee

mispositioned

a fuel assembly

in the spent fuel

pool.

The licensee

moved the fuel assembly

to the correct location

upon

discovery of the error.

The inspector

noted that the cause of the event

was

that the reactor engineer,

located

in the control

room, directed

the spent

fuel handling machine operator to place the fuel assembly into the wrong

location.

The inspector

noted that the safety significance of mispositioning

,the fuel assembly

was minimal

due to the high boron concentration

of the spent

fuel pool.

)

'

-13-

The licensee

corrected

.the immediate

concern of the mispositioned

fuel

assembly,

however,

the inspector

expressed

concern that operators

continued to

move fuel for approximately

two hours before suspending

fuel movement to

evaluate

the event

and to take action to prevent reoccurrence.

In addition,

operators relied

upon verbal direction from the reactor engineer to the spent

fuel handling machine operator

on placement of the fuel assembly.

The spent

fuel handling machine operator did not have

an independent

tracking sheet to

verify proper fuel location.

The licensee

briefed involved refueling personnel

to describe

the event

and

corrective actions.

The licensee

placed

a tracking sheet

on the spent fuel

handling machine to provide

an independent verification of the fuel assembly

placement.

The licensee

issued

a night order. describing the event

and

initial corrective actions

and initiated

a

CRDR to evaluate further corrective

actions.

The inspector

concluded that after the licensee

suspended

fuel

movement,

the corrective actions

were appropriate.

At the exit meeting,

the inspector

addressed

the concern that refueling

personnel

appeared

to be insensitive to reactivity management

problems,

and

that by not having

a tracking method for the fuel assemblies

on the spent fuel

handling machine

they lacked defense

in depth.

Licensee

management

acknowledged

the inspectors

concerns.

This licensee identified and corrected

violation is being treated

as

a non-cited violation, consistent

with Section

VII of the

NRC Enforcement Policy.

The inspector

noted that operators

on the refueling machine

were knowledgeable.

about the equipment

and displayed

good verification of the required

coordinates

set in the machine to retrieve the next assembly.

The limited

senior reactor operator displayed appropriate

knowledge of the

abnormal

operating

procedure for loss of refueling pool level.

The inspector

noted

adequate

foreign material

exclusion controls'he

inspector

concluded that

the performance of refueling machine

personnel

was good.

t

6.2

Observation of Core Offload

Unit 3

On October

21, the inspector

observed

portions of core offload activities from

the control

room and the refueling machine inside containment.

The inspector

noted that in the control

room,

personnel

demonstrated

good communications

and

professionalism.*

V

i

I'

1

ATTACHMENT 1

1

PERSONS

CONTACTED

l. 1

Arizona Public Service

Com

an

  • J. Bailey, Vice President,

Nuclear Engineering

  • S. Burns,

Department

Leader,

Design Engineering

  • I. Chavez,

Section

Leader,

Instrument

and Controls Maintenance

  • P. Crawley, Director, Nuclear Fuels

Management

  • B. Dayyo, Senior Representative,

Strategic

Communications

  • R. Flood,

Department

Leader,

System Engineering

  • R. Hazelwood,

Engineer,

Nuclear Regulatory Affairs

  • H. Hodge,

Department

Leader,

Nuclear Engineering

  • W. Ide, Director, Operations
  • K. Jones,

Section

Leader,

Maintenance

Services

  • A. Krainik, Department

Leader,

Nuclear Regulatory Affairs

J.

Levine, Vice President,

Nuclear Production

  • R. Lucero,

Department

Leader,

Electrical

Maintenance

  • D. Hauldin, Director, Maintenance
  • G. Overbeck,

Vice President,

Nuclear Support

  • C. Seaman,

Director, Nuclear Assurance

  • B. Thiele, Section

Leader,

Nuclear Fuels

Hanagement

  • H. Winsor, Section

Leader,

Mechanical

Maintenance

Engineering

1.2

NRC Personnel

  • R. Huey, Chief, Region

IV Reactor Projects

Branch

F

  • D. Garcia,

Resident

Inspector

  • J. Kramer,

Resident

Inspector

1.3

Others

  • F. Gowers, Site Representative,

El

Paso Electric

  • R. Henry, Site Representative,

Salt River Project

  • Denotes those present

at the exit interview meeting held

on November 3,

1995.

The inspector also held discussions

with and observed

the actions of other

members of the licensee's

staff during the course of the inspection.

2

EXIT MEETING

An exit meeting

was conducted

on November 3,

1995.

During this meeting,

the

inspectors

summarized

the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

l

J

,I

'

-15-

ATTACHNENT 2

COLSS

=

CRDR

LIST OF ACRONYHS

core operating limits supervisory

system

condition 'report/disposition

request