ML17311A879

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Notice of Deviation from Insp on 950226-0408.Deviation Noted:Failure to Follow Procedures for Testing of Standby Gas Turbine Generators as Specified in QA Plan Described in Chapter 17 of UFSAR
ML17311A879
Person / Time
Site: Palo Verde 
Issue date: 05/12/1995
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311A878 List:
References
50-528-95-06, 50-528-95-6, NUDOCS 9505190106
Download: ML17311A879 (2)


See also: IR 05000226/2004008

Text

ENCLOSURE 1,

NOTICE OF DEVIATION

Arizona

Publ i c Servi ce

Company

Palo Verde Nuclear Generating

Station

Docket:

50-528

L'icense:

NPF-41

During an

NRC inspection

conducted

on February

26 through April 8,

1995,

a

deviation of your Updated Final Safety Analysis Report was identified.

In

accordance

with the "General

Statement of Policy and Procedure for NRC

Enforcement Actions,"

10 CFR Part 2, Appendix C, the deviation is listed

below:

The Palo Verde Updated Final Safety Analysis Report,

Section

17.2F.6,

provides guality Assurance

commitments for station blackout coping

equipment.

Section 17.2F.6.3.2.3,

"Instructions,

Procedures,

and

Drawings," states,

in part, that ".

.

. tests

.

.

. for compliance with

10

CFR 50.63 shall

be prescribed

by documented

instructions,

procedures,

and drawings

and shall

be accomplished

in accordance

with these

documents."

In partial

implementation of these

commitments,

Procedure

70TP-2GT02,

Revision 0,

"GTG Parallel

Operation With Nonclass

1E Loads," provided

instructions for the testing of the gas turbine generators

(GTGs).

Step 8. 1. 11. 1 states,

in part, to complete Section 6.4 of

Procedure

550P-OGTOl,

"Gas Turbine Generator

1 Operating Instructions,"

prior to paralleling

GTG ¹I to offsite power.

Procedure

550P-OGTOl,

Section 6.4,

Step 6.4.3. 1, specifies that the operator

ensure that the

GTG

1 speed control isoch/droop

switch is in the droop position.

Contrary to the above,

on March 9,

1995, prior to paralleling

GTG

1 to

offsite power,

a nonlicensed

operator did not accomplish testing of

station blackout coping equipment

(the

GTGs) in accordance

with test

instructions in that

he did not ensure that the

GTG

1 speed control

isoch/droop

switch was in the droop position.

The switch remained

in

the isoch position

and

as

a result

GTG

1 tripped when it was paralleled

to offsite power.

Please

provide to the U.S. Nuclear Regulatory

Commission,

ATTN:

Document

Control

Desk,

Washington,

D.C. 20555, with a copy to the Regional

Administrator,

Region

IV, 611

Ryan Plaza Drive, Suite 400, Arlington, Texas

76011,

and

a copy to the

NRC Resident

Inspector at the facility that is the

subject of this Notice, in writing within 30 days of the date of this Notice,

(1) the reason(s)

for the deviation, or if contested,

the basis for disputing

the deviation,

(2) the corrective steps that have

been taken

and the results

achieved,

(3) the corrective steps that will be taken to avoid further

deviations,

and (4) the date

when full compliance will be achieved.

Where

good cause is shown, consideration will be given to extending the response

t

time.

Dated at Arlington, Texas,

this 12th day of Hay 1995

'PSOSf90106

950512

PDR

ADQCK 05000528

6

PDR