ML17308A205

From kanterella
Jump to navigation Jump to search
Insp Repts 50-335/86-02 & 50-389/86-01 on 860114-0210. Deviation Noted:Fsar Design Criteria/Objectives Could Not Be Met in That Several Exterior Doors Blocked Open & Ventilation Lineup Improper
ML17308A205
Person / Time
Site: Saint Lucie  
Issue date: 02/28/1986
From: Bibb H, Crlenjak R, Elrod S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17216A453 List:
References
50-335-86-02, 50-335-86-2, 50-389-86-01, 50-389-86-1, IEIN-85-084, IEIN-85-84, NUDOCS 8603210073
Download: ML17308A205 (11)


See also: IR 05000335/1986002

Text

UNITEDSTATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.IN.

ATLANTA,GEORGIA 30323

1 p,R REOIIC

<Gi'

A

Cl

P

~O ~

++*++

Report Nos.:

50-335/86-02

and 50-389/86-01

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket NosrI

50-335

and 50-389

Facility Name:

St.

Lucie

1 and

2

License Nos.:

DPR-67

and NPF-16

Inspection

Conducted:

Januar

14

February

10,

1986

Inspectpps: &- L I

~ R.

V. Crlenjak,

Se ior Resident

Inspector

W.

C~

Qr H.

E. Bibb, Resident

Inspector

Approved by: +

LI

~ S.

A. El rod, Secti on Chi ef

Division of Reactor Projects

Da

e Signed

4

Da

e

igned-

i~3 3a

Da e

ignedd

SVMMARY

Scope:

This

inspection

entailed

160

inspector-hours

onsite

in the

areas

of

Technical

Specification

compliance,

operator

performance,

overall

plant

operations,

quality

assurance

practices,

station

and

corporate

management

practices,

corrective

and

preventive

maintenance

activities,

site

security

procedures,

radiation control activities, surveillance activities

and Inspection

and Enforcement Information Notice (IEIN) review.

Results:

One deviation

was identified (paragraph

3).

86032i0073

86030>

PDR

ADOCK 05000335

PDR

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

K. Harris, St.

Lucie Site Vice President

D. A. Sager,

Plant Manager

  • J.

H. Barrow, Operations

Superintendent

T. A. Diliard, Maintenance

Superintendent

  • L. W. Pearce,

Operations

Supervisor

R. J . Frechette,

Chemi stry Supervisor

C.

G. Leppla, Instrumentation

and Control (I&C) Supervisor

P.

L. Fincher, Training Supervisor

C. A. Pell, Technical Staff Supervisor (Acting)

E. J . Wunderlich,

Reactor

Engineering

Supervisor (Acting)

H.

F. Buchanan,

Health Physics

Supervisor

G-.-Longhouse,

Security Supervisor

J.

Barrow, Fire Prevention

Coordinator

J. Scarola,

Assistant Plant Superintendent

- Electrical

C. Wilson, Assistant Plant Superintendent

- Mechanical

N.

G.

Roos, Quality Control Supervisor

Other

licensee

employees

contacted

included

technicians,

operators,

mechanics,

security force members,

and office personnel.

  • Attended exit interview

2.

Exit Interview

The inspection

scope

and findings were

summarized

on February

7,

1986, with

those

persons

indicated in paragraph

1 above.

The licensee did not identify

as

proprietary

any

of the

materials

provided

to

or

reviewed

by

the

inspectors

during this inspection.

3.

Licensee Action on Previous Inspection

Findings

(CLOSED)

Unresol ved

Item

(UNR) 389/85-30-01

Reactor

Auxi 1 iary

Bui 1 ding

(RAB) VentilatMn

a%d Exterior Door Status.

On

November

15,

1985,

while

performing

a walkdown of the Unit 2

RAB, the inspector

noted that several

exterior doors were

open

and there existed,

through the

open

doors,

a flow

of air from inside to outside (i.e., building pressure

was positive).

The

RAB ventilation lineup is normally operated

such that air flow would be the

reverse

of that

described

above (i.e., building pressure

negative).

The

Unit 2 Final

Safety

Analysis

Report

(FSAR)

paragraphs

9.4

and

9.4.3.1

discuss

design criteria and objectives of the

RAB ventilation system.

Since

these

design criteria/objectives

could not

be

met with

RAB exterior doors

open

on

November

15,

1985,

this

UNR is closed

and is

now considered

a

deviation

from the Unit 2

FSAR,

DEV 389/86-01-01:

Improper

RAB Ventilation

and Exterior Door Status.

(CLOSED)

UNR 389/85-21-01

Anti-Reverse

Rotation

Pin Reportability.

The

anti-reverse

rotation device

(ARRD) on several

Unit 2 reactor coolant

pumps

(RCP)

were

found to

be degraded

during an inspection

by the licensee (ref.

IE Report 50-335,389/85-21).

The

licensee

determined

that this

degraded

condition

was

not reportable

because

the

AARD could still carry out its

intended function.

On December 2-6,

1985,

an inspection

was conducted

by

a

NRC RII inspector; it was concluded that this item was not reportable

under

10 CFR 50.72,

50.73,

or Part

21 (ref. IE Report

50-335,389/85-31).

This

item is considered

closed.

4.

Unresolved

Items

Unresolved

items

are matters

about which more information is required to

determine

whether

they

are

acceptable

or

may

involve

a violation

or

deviation.

A new unresolved

item is discussed

in paragraph

12.

During the

inspectson

period,

the inspectors

verified plant operations

in

compliance with selected

Technical Specification

(TS) requirements.

Typical

of these

were confirmation of compliance with the

TS for reactor

coolant

chemistry,

refueling

water

tank,

containment

pressure,

control

room

ventilation

and

AC and

DC electr ical sources.

The inspectors verified that

testing

was

performed

in

accordance

with

adequate

procedures,

test

instrumentation

was calibrated,

limiting conditions

for operation

(LCOs)

were

met,

removal

and

restoration

of

the

affected

components

were

accomplished,

test results

met requirements

and were reviewed by personnel

other

than

the individual directing the test,

and that

any deficiencies

identified

during

the

testing

were

properly

reviewed

and

resolved

by

appropriate

management

personnel.

The inspector

observed all aspects

of the following surveillance:

1-140005+ .Rev.

13

Reactor Protection

System

Periodic Logic Matrix

Test

Portions of the following surveillance

were also observed:

1-1630028,

Rev.

7 - New Fuel Handling Crane Operation

Plant Tours

The

inspectors

conducted

plant tours periodically during

the

inspection

interval

to verify that monitoring

equipment

was

recording

as required,

equipment

was

properly

tagged

operations

personnel

were

aware

of plant

conditions,

and plant houseke5ping

efforts were

adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean

areas

were being controlled in accordance

with

procedures,

excess

equipment or material

was stored properly and combustible

material

and

debri s

were

di sposed

of expeditiously.

During tours

the

inspectors

looked

for

the

existence

of

unusual

fluid leaks,

piping

vibrations,

pipe

hanger

and

seismic restraint

settings,

various

valve

and

breaker positions,

equipment

caution

and danger

tags,

component

positions,

adequacy

of fire fighting equipment,

and instrumentation calibration dates.

Some tours were conducted

on backshifts.

The

inspectors

routinely

conducted

partial

walkdowns of

Emergency

Core

Cooling

Systems

(ECCS).

Valve,

breaker/switch

lineups

and

equipment.

conditions

were

randomly verified both locally and

in the control

room.

During the inspection

period,

the inspectors

conducted

a complete

walkdown

in the accessible

areas of the Unit

1 and

2 Component Cooling Mater Systems

(CCWS)

to verify that

the

lineups

were

in

accordance

with licensee

requirements

for operability

and

equipment

material

conditions

w'ere

satisfactory.

Additionally, flowpath verifications were

performed

on the

High Pressure

Safety Injection (HPSI)

system

and

the Auxiliary Feedwater

(AFM) system.

Plant Operations

Review

The

inspectors

periodically

reviewed shift logs

and

operations

records,

including

data

sheets,

instrument

traces,

and

records

of

equipment

malfunctions.

This review included control

room logs

and auxiliary logs,

operating orders,

standing orders,

jumper logs and equipment tagout records.

The

inspectors

routinely

observed

operator

alertness

and

demeanor

during

plant tours.

During routine operations,

operator

performance

and

response

actions

were

observed

and

evaluated.

The

inspectors

conducted

random

off-hours

inspections

during

the

reporting

interval

to

assure

that

operations.

and security

remained

at

an acceptable

level.

Shift turnovers

were observed to verify that they were conducted in accordance

with approved

licensee

procedure."

The

inspectors

performed

an

in-depth

review of the

following safety-related

tagouts

(clearances):

1"1-109

1-2-2

1"2-15

2-2-13

2-1-17

18 Charging

Pump

A Boric Acid Makeup

Pump Discharge

Check Valve

MV-09-9 lA Auxiliary Feedwater to

1A Steam Generator

2A Charging

Pump

Condensate

Storage

Tank Nitrogen Seal

On February 7,

1986, with reactor

power at approximately

100 percent,

Unit

1

tripped

during

performance

of

a

monthly Reactor

Protection

System

(RPS)

logic matrix test (OP-1-1400059).

All systems

functioned

as designed.

The

test is performed to verify proper operation

of the trip circuit breakers

(TCB) which interrupt

power ty the control

element

assemblies

(CEAs)

and

thereby trip the reactor.

-Th4 trip occurred

at the

step

in the procedure

which requires

TCBs

1

and

5 to

be

in the

tripped/open

position.

While

repositioning

the logic matrix relay selector

switch prior to TCBs

1 and

5

closing,

TCBs 4 and 8 opened

unexpectedly,

resulting in a loss of power to

the

CEA bus

and

the reactor trip.

The

cause

of the trip was traced

to

a

faulty matrix relay selector

switch which caused

a matrix relay to actuate

out of sequence,

opening

TCBs 4 and 8.

Additionally, it was discovered that

one relay

(AB4) had

a test coil with

a lower resistance

than

the others.

The faulty switch

and relay

were

both replaced.

Also replaced

were

two

other matrix relay selector

switches that

showed slight indications of wear.

The plant is considering

an evaluation of the switch design

and

a possible

design

change

which would replace

the

switches with ones

of

a different

design.

The unit was returned to service the

same

day.

Technical Specification

Compliance

Ouring this reporting interval, the inspectors verified compliance with LCOs

and

the results

of selected

surveillance

tests.

These verifications "were

accomplished

by direct observation

of monitoring

instrumentation,

valve

positions,

switch positions,

and review of completed

logs

and records.

The

licensee's

compliance with

LCO action

statements

was

reviewed

on selected

occurrences

as they happened.

Maintenance

Observation

Station

maintenance

activities

on

selected

safety-related

systems

and

components

were observed/reviewed

to ascertain

that they were conducted

in

accordance

with requirements.

The following items

were

considered

during

this

review:

LCOs

were

met, activities were

accomplished

using

approved

procedures,

functional testing

and/or calibrations

were

performed prior to

returning

components

or

systems

to service,

quality control

records

were

maintained, activities were

accomplished

by qualified personnel,

parts

and

materials

used

were

properly certified,

and radiological

controls

were

implemented

as

required.

Work requests

were

reviewed

to determine

the

status

of outstanding

jobs

and to

assure

that priority was

assigned

to

safety-related

equipment.

The inspectors

observed

portions of the following

maintenance activities (Plant Work Orders):

3027 -

1C Charging

Pump

3028

Pressurizer

Code Safety Valve Nozzle

3031 -

Valve 1100E Bonnet

3034 -

1A Boric Acid Makeup

Pump Seal

1l

10.

Review of Nonroutine Events

Reported

by the Licensee

The following Licensee

Event

Reports

(LERs)

were

reviewed for potential

generic

impact,

to detect

trends,

and

to

determine

whether

corrective

actions

appeared

appropriate,

Events

which were reported

immediately were

also reviewed

as they occurred 'to determine that

TSs were being met and that

the public health

and safety

were properly considered.

The following LERs

are

considered

closed;

an in-depth

review was

performed

on the asterisked

LERs.

Unit 1

85-08

-

Tardy Surveillance

of Main

Steam

Isolation

Valves

Due to

Personnel

Error

"85-09

-

Defective Procedure

Leads to Lift Rig Failure

85-10

Control

Room Ceiling

Support

Structure

Outside Its

Design

Basis

Oue to Design Error

"85-11

-

Engineered

Safeguards

Actuations

Due to Loose

Fuse

Unit 2

"85-09

-

Manual Reactor Trip - Reactor Coolant

Pump High Vibration

Physical

Protection

12.

The inspectors

verified by observation

and interviews during the reporting

interval that

measures

taken

to assure

the

physical

protection

of the

facility

met

current

requirements.

Areas

inspected

included

the

organization

of the security force,

the establishment

and

maintenance

of

gates,

doors

and isolation

zones

in the proper conditions,

proper

access

controls

and badging,

and adherence

to procedures.

IE Information Notice (IEIN) Review

The inspectors

have continued

to review the licensee's

actions in response

to IEIN 85-84.

The licensee

has indicated,

as reported in the last monthly

resident report (ref.

IE Report

Nos. 50-335,389/85-36),

that the installed

main steam isolation valve (MSIV) air accumulators

are of sufficient volume

to ensure

MSIV closure.

The

NRC, Region II has recently questioned

licensee

practices

in performing testing of air operated/aided

automatic valves which

are required to function ("fail safe")

under

loss

of air/actuator

power

conditions.

Most air

systems

are

designed

with air accumulators

which

ensure

valve operations

when the

normal air system/supply

is lost.

the

licensee

has

performed

testing

as

required

by the

TS to

ensure

valve

"C

<s

operability.

Additional testing is performed periodically under the plant's

inservice.

testing

(IST)

program

as

required

by

10 CFR 50.55a

and

the

applicable

ASME Boiler and

Pressure

Vessel

(BPV)

Codes.

One point

in

question deals with required testing of fail safe valves.

The MSIYs may be

considered

part of this category

and

as

such

may require testing with the

instrument air supply,

as welf,as electric power,

removed.

The licensee

has

hot interpreted

the

removal. of instrument air while fail safe testing

the

MSIVs as

a requirement

due to the valves'esign

and function.

Until the

NRC

Region II IST/ASME

Code

special i sts

complete

an

inspection

of

the

current

licensee

practices

for testing fail safe valves, this item will be

tracked

as

an Unresolved

Item (335/86-02-01,

389/86-01-'02),

Removing Air

While Testing "Fail Safe" Valves.

P'