ML17306A275

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Insp Repts 50-528/91-35,50-529/91-35 & 50-530/91-35 on 910908-1012.Violations Noted.Major Areas Inspected:Previous Items,Review of Plant Activities,Engineered Safety Feature Sys Walkdowns,Surveillance Testing & Plant Maint
ML17306A275
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 11/08/1991
From: Koltay P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17306A273 List:
References
50-528-91-35, 50-529-91-35, 50-530-91-35, NUDOCS 9111260173
Download: ML17306A275 (51)


See also: IR 05000528/1991035

Text

Re ort Nos.

Docket Nos.

License

Nos.

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

50-528/91-35,

50-529/91-35,

and 50-530/91-35

50-528,

50-529,

and 50-530

NPF-41,

NPF-51,

and NPF-74

Licensee

Facilit

Name

Arizona Public Service

Company

P.

0.

Box 53999, Station

9012

Phoenix,

AZ 85072-3999

d

t

d

d

d

t

d

tt

d dt tt

Units 1, 2,

and

3

Ins ection Conducted

September

8 through October 12,

1991

A

roved

B

o tay,

ie

Reactor Projects

Section II

pg

c(

a e'gne

Ins ectors

D.

Coe,

F. Ringwald,

J.

Sloan,

M. Young,

M. Ang,

Senior

Resident

Inspector

Resident

Inspector

Resident

Inspector

Resident

Inspector

Project Inspector,

Region

V

Ins ection

Summar

Ins ection

on

Se tember

8 throu

h October

12

1991

(Re ort Numbers

an

Areas Ins ected

Routine, onsite,

regular

and backshift inspection

by

our res)

en

inspectors,

and

one inspector

from the Region

V staff.

Areas

inspected

included:

previously identified items; review of plant activities;

engineered

safety feature

system walkdowns - Units 1, 2,

and 3; surveillance

testing - Units 1, 2,

and 3; plant maintenance

- Units 1, 2,

and 3; reactor

trip and main steam isolation system

(MSIS) actuation - Unit 1; preparations

for refueling - Unit 2; unescorted visitor - Unit 2; scaffolding deficiencies

- Unit 2; worker responsibility - Unit 2; main steam safety valve

(MSSV)

setpoint testing - Unit 2; undersized

welds - Unit 2; equipment qualification

audit review - Units 1, 2,

and 3; employee

concerns

program activities-

Units 1, 2,

and 3; review of employee qualifications - Units 1, 2,

and

3 and

review of licensee

event reports - Units 1, 2,

and 3.

During this inspection the following Inspection

Procedures

were utilized:

35502,

35702,

41500,

60705,

61726,

62703,, 71707,

71710,

92700,

92701,

92702,

and 93702,

9lli2hOi73 9iii08

PDR

ADQCK 05000528

G

PDR

)

I

!

-2-

Results

Of the

16 areas

inspected,

one non-cited

and

one cited violation

were ~Bentified.

The cited violation pertained to the loss of control

over

an escorted visitor in Unit 2 (paragraph

9),

and the non-cited violation

pertained to deficient surveillance test procedures

used in Units', 2,

and

3

(paragraph

4).,

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters

None

Summar

of Violations

Summar

of Deviations

0 en Items

Summar

Stren ths Noted

1

Non-Cited Violation - Units 1, 2,

and

3

1

Cited Violation - Unit 2

None

ll items closed,

8 items left open,

and

3 new items opened.

The licensee's

self assessment

program identified several

weaknesses

in their

environment qualifications

(Eg) program through the use of a gA audit.

Also,

a

QC person with welding experience identified an inadequate

existing weld on

a charging

pump line during observation of unrelated

maintenance.

Meaknesses

Noted

The quality of engineering

work was found weak in two areas.

First was the

recent incorporation of surveillance test criteria, which were slightly

non-conservative

with respect to Technical Specifications.

Second,

a scaffold

was found contacting

a safety-related

cable tray support without an engineering

analysis that approved the configuration.

i

DETAILS

Persons

Contacted

The below listed technical

and supervisory personnel

were

among those

contacted:

Arizona Public Service

(APS)

~R.

Adney,

J.

N. Bailey,

"D. Blackson,

  • T. Bradish,

R.

Cherba,

~A. Fakhar,

"R. Flood,

J.

Fogarty,

  • D. Fuller,

"R. Fullmer,

D.

Gouge,

"S. Guthrie,

  • M. Ide,

J.

Levine,

~D. Mauldin,

  • J. Minnicks,

G. Overbeck,

~L. Perea,

~R.

Rouse,

  • R. Prabhakar,

C.

Russo,

R. Schaller,

T. Schriver,

J. Scott,

J. Scott,

  • R. Stevens,
  • J. Thompson,

Plant Manager,

Unit 3

Vice Pres ident,

Nuc 1 ear

Sa fety

8 Licens i ng

(NS8 L)

Manager,

Central

Maintenance

Manager,

Compliance

Manager, Quality Systems

Supervisor,

Site Nuclear Engineering

8 Construction

Plant Manager,

Unit 2

Manager,

Mork Control Unit 2

Manager,

Chemistry Unit 1

Manager, Quality Audits and Monitoring

Manager,

Plant Support

and (Chairman Plant

Review Bd.)

Dep. Director, Nuclear Safety

Plant Manager,

Unit 1

Vice President,

Nuclear

Power Production

Manager, Site Maintenance

Manager,

Maintenance

Unit 3

Site Director, Technical

Support

(STS)

Technical Asst., Technical

Support

Supervisor,

Compliance

Manager, Quality Engineering

Manager, Quality Control

(QA/QC)

Manager, Assistant Plant Unit 1

Manager, Assistant Plant Unit 2

Manager, Assistant Plant Unit 3

General

Manager,

Chemistry

Director, Licensing

8 Compliance

Tech. Asst., Plant Standards

The inspectors

also talked with other licensee

and contractor personnel

during the course of the inspection.

"Personnel

in attendance

at the Exit meeting held with the

NRC Resident

Inspectors

on October 17,

1991.

In addition,

M. Ang, Region

V NRC Inspector,

met with licensee

representatives

on October ll, 1991, for an exit briefing.

The results

of his inspection

are included in this report.

I

0

2.

Prey ious 1

Identi fied Items - Units

1

2

and

3 (92701

and 92702)

Unit 1

(0 en) Enforcement

Item (528/90-20-02):

"Post-Accident

Sam lin

s

em

ver- ressunza

>on

-

ni

2.

This event involved the overpressurization

of the

PASS system

due

to miscommunication

leading to a valve misalignment.

All immediate

corrective actions

were complete.

This item has

been left open to

evaluate

the completion of the commitment in the response

to the

notice of violation to evaluate "...the adequacy of administrative

controls for formal communications for non-operations

department

personnel

manipulating plant equipment at the

PVNGS."

The

licensee

s initial evaluation included the Chemistry Department.

The inspector

questioned

whether this evaluation should

be expanded

to other non-operations

department

personnel.

This question

resulted in a subsequent

evaluation which identified additional

non-operations

groups which manipulate plant equipment

and required

the revision of applicable procedures

to more f'ormally control

communications

during these activities.

Subsequent

to this

additional evaluation,

the inspector identified that Component

and

Specialty Engineering personnel

who perform local leak rate testing

on electrical penetrations

and other non-fluid components

also

manipulate plant components

outside the boundary of a clearance.

The inspector then questioned

whether all non-operations

groups

which manipulate plant components

have

been identified.

The

licensee

is considering this question.

This item will remain

open

pending the completion of this evaluation.

(Closed)

Followu

Item (528/90-20-04):

"Inadvertent

Shutdown

oo

1n

ass

-

nl

This item involved bypass

flow through valves SI-HV-690/691,

resulting from a design wherein the motor operator

may not always

drive the disc into its seat.

A limit switch indicates

the valve

is closed in the control

room when the disc reaches

five percent

open.

Thus, the operator

may release

the

hand switch prior to the

valve becoming fully shut.

Should this occur,

a portion of the

shutdown cooling flow to the reactor

vessel

would be bypassed

back

to the

pump suction without any indication of this in the control

room.

As an interim measure,

the licensee

revised procedures

4XOP-XSIOl,

"Shutdown Cooling Initiation," to require operators to manually

shut these

valves to ensure

they are fully closed.

However, in

Inspection

Report 528/91-01,

the inspector identified a discrepancy

between the interim fix and a recommendation in the Engineering

Evaluation Request,

90-SI-093, for abandonment

of manual

operation

of these

valves

due to the indeterminate

torque applied which could

result in overthrust or underthrust.

Since then, the licensee

has modified their revision to procedures

4XOP-XSI01 to require operators

after receiving

a closed

indication, to hold the hand swstch for five seconds

in the

"JOG

J

1

(

i ~

(

CLOSE" position to ensure that the valve is fully seated.

(Correspondingly,

the licensee

has initiated

a Motor Operated

Valve

Operating Guideline to preclude

problems associated

with overthrust

and underthrust resulting from manual

operation of valves.)

The

inspector

concluded that the interim measure

is consistent with the

recommendation

in the

EER for abandonment

of manual

operation of

val ves SI-HV-690/691.

Further,

as long-term corrective action, the licensee

is pursuing

action via PCR-90-SI-13-051

which recommends

modification of the

control logic of the valve design

such that the limit switch (which

provides indication) and the torque switch (which disengages

the

motor operator)

perform in parallel

when the valve is

a maximum of

one percent

open (instead of current five percent).

This

modification is scheduled

to be implemented durinq the fourth

refueling outage for all three units.

This item ss closed.

(0 en) Followu

Item (528/91-15-01):

"Limitor ue Grease

Ins ection

e uac

-

n>

This event involved identified deficiencies in the licensee's

Limitorque grease

inspection

program.

The inspector

reviewed

completed Incident Investigation Report (IIR) 9-1-0064 (formerly

3-3-91-018).

The IIR had

a list of conclusions

but no action plan

to implement these

conclusions.

The licensee

indicated that each

conclusion will be addressed

by specific actions

and

a Commitment

Action Tracking System

(CATS) item will be generated for each item.

The inspector

noted that

a general

CATS item exists,

but specific

CATS items for each conclusion

have not yet been created.

The

licensee

stated that these

CATS items are being created.

The

inspector

concluded that while this IIR appears

to adequately

address

grease

requirements

from a lubrication standpoint,

grease

requirements

from an Equipment Qualification (EQ) standpoint still

appear to be unclear.

This item will remain

open pending

resolution of this

EQ aspect.

(Closed) Violation (528/91-26-03):

"Failure to Pro erl

Perform

a

urvei

ance

es

-

n>

This item addresses

corrective actions resulting from the failure

to properly perform

a verification step for the Core Protection

Calculator

(CPC) addressable

constants

changed

during Surveillance

Test (ST) 77ST-lSB08,

"CPC Channel

"B" Functional Test."

The

licensee

determined that the event

was caused

by inattention to

detail

by the test performer and

a reactor operator.

In addition

to the administration of discipline in accordance

with the

licensee

s Positive Discipline Program,

changes

were

made to this

procedure

and to two other procedures

to require independent

verification of the proper

changes.

Additionally, a change to the

CPC Addressable

Constants

Log form was initiated to improve it from

a human factors standpoint to more clearly indicate the correct

value to be set in the

CPC.

II

I

0

The inspector

concluded that the licensee's

corrective actions

and

actions to prevent recurrence

were adequate.

This item is closed.

Unit 3

(0 en) Enforcement

Item (530/91-01-01):

"Diesel Generator

ns

ec ion

urve>

ances

o

er orme

urban

u

own

nest

This item identified that the licensee

had not adhered to the

TS

Surveillance

Requirement

(SR) 4. 8. l.l. 2. d. 1 which required

Emergency Diesel Generator

(EDG) inspections

to be performed with

the unit shutdown.

Licensee

LER 1-91-002 reported

occasions

when

these

inspections

were performed with the unit at power.

The

licensee's

response

to the Notice of Violation included identifying

other Technical Specification

SRs which are required to be

performed only when the unit is shutdown

and initiating procedure

changes

to add precautions

in the appropriate

surveillance tests.

The inspector also reviewed the licensee's

Incident Investigation

Report (IIR) 3-1-91-017A on this issue.

Based

on this review, the

inspector

concluded that the corrective actions

noted

above

were

appropriate.

The inspector

noted that the IIR also addressed

the

question of what vendor

recommended

inspections

were required

pursuant to

SR 4. 8. 1. l. 2. d, 1.

The IIR concluded that

APS had

previously excluded

from the Surveillance Test (ST) program several

items from the vendor

annual

inspection list, choosing

instead to

use the corrective

and preventive maintenance

programs to

accomplish

these

items.

One of these

items

was for checking the "operation

and calibration

of all [EDGj control

and safety

shutdown devices."

The IIR noted

that, of the three safety

shutdown trip devices active during the

emergency

run mode of operation,

two of them were Preventive

Maintenance

(PM) tasks with frequency of 1R (refueling), allowed to

extend

up to three years.

One of the IIR conclusions

was to reduce

this interval to 18 months in accordance

with the vendor's

recommendations.

Due to the safety significance of the proper

calibration of these

devices,

the inspector

reviewed the

PM history

for several

of them and determined that one device,

a Unit 1

generator differential relay,

had not been calibrated in over

two years,

and currently did not have

an evaluation

signed

by the

Plant Manager allowing extension of the

PM interval,

as is required

by the licensee's

PM program.

Based

on this observation

the

licensee initiated Condition Report/Disposition

Request

(CRDR)

9-1-0200 to assess

the cause of this condition.

This open item

will remain

open until the licensee

completes their eva'iuation.

The inspector further noted that the IIR acknowledged that there

was

no documented

basis for excluding certain vendor required

inspections

from the

ST program.

The inspector

encouraged

the

licensee to reconsider

the technical

and safety significance basis

I'

for treating certain vendor requirements

as

PMs rather than

STs.

The licensee

indicated that the

CRDR would re-examine this basis.

(0 en) Followu

Item (530/91-19-03):

"Mestin house

ARD Rela

al ure

-

ns

This item involved the failure of a Westinghouse

ARD 660-UR relay,

the associated

10 CFR Part 21 report,

and other failures.

The

licensee

has not completed

Engineering Evaluation

Requests

(EERs)

91-ZA-016 or 01-ZA-033, which include the root cause

of failure

evaluation for these

relays.

This item will remain

open

until the inspector

can review these

EERs.

(Closed)

Followu

Item (530/91-26-01):

"Overvolta

e of the A-C

o)nc>

ence

a rex

ower

u

nl

This item involved an overvoltage condition of the A-C coincidence

matrix power supply PS-12 during testing.

Troubleshooting

was

inconclusive

and the power supply

has performed properly since this

event.

The licensee

has

issued

a work order to replace this power

supply during the next outage.

The inspector

concluded that this

is prudent.

This item is closed.

Units 1

2

and

3

(Closed)

Followu

Item (528/90-42-03):

"Startu

Transformer

oa

1n

-

n>

s

an

This item involves verifying the implementation of changes

to

procedure

4XOP-XNAOl, "13.8

KV Electrical

System (NA)," which were

made

as

a result of an

NRC Electrical Distribution Safety

Functional

Inspection

(EDSFI) observation that the startup

transformers

could be inadvertently overloaded.

This condition

could result from two units sharing the

same startup transformer

secondary windings,

and could

come without warning if an automatic

bus transfer occurs.

The

EDSFI (Inspection

Report 528/90-42,

Paragraph

2.4) considered that the licensee's

proposed

method of

limitinq loads

was acceptable.

This method includes blocking the

automatic transfer for the non-Class

lE loads of the unit whose

loads would have

been

connected

to their alternate

startup

transformer,

and monitoring loads

on the startup transformer

when

it is loaded

by more than

one unit.

The inspector

reviewed the changes

to the procedure.

The changes

appeared

to address

the monitoring, blocking,

and loading

requirements

and methods in detail,

and adequately

implemented the

methodology previously found acceptable

by the EDSFI.

The changes

were implemented

on December

14,

1990.

The inspector also

confirmed during a startup transformer

NAN-X02 outage that the

automatic transfer

was blocked

as required,

and that the Unit 3

Shift Supervisor

was aware of the loading requirements.

Based

on

this review, this item is closed.

(Closed) Violation (528/90-42-06):

"Failure to Per form Maintenance

n

ae

eae

anes

-

n>

s

an

This violation resulted

from failure to implement written

procedures

for the performance

of vendor

recommended

Preventive

Maintenance

(PM) on class

1E load centers

D25,

D26,

D27,

and

D28.

The licensee

scheduled

the

PM to be accomplished

every third

refueling outage.

The vendor recommendation

was for annual

performance.

The

PM tasks

had been prepared

but were not approved

or implemented at the time since the

PMs were not due.

The licensee initially revised the scheduled

PM frequency to once

per refueling.

Additionally, these

and other

PM tasks

were already

being reviewed

as part of a major

PM task force project,

scheduled

for completion

by December

31,

1991.

Further adjustments

to the

PM

scope

and frequency for these

components

resulted

from these task

force recommendations.

The annual

PM addressed

in the violation

had been reassigned

a frequency of once

per three refuelings,

and

the twelve week

PM mentioned in Inspection

Report 528/90-42

(Paragraph

4.3) has

been

enhanced

to include thermography

and

has

been

reassigned

a frequency of once per refueling.

These

changes

were justified on the basis of the maintenance

history, the

controlled environment in which these

panels

are located,

the

operational risk of maintenance

on these

panels while the unit is

on line,

and the scope of other

PMs associated

with these

panels.

The inspector

concluded that the licensee's

corrective actions

appear

adequate.

This item is closed.

(Closed)

Unresolved

Item (528/90-46-01):

"Essential Chiller

e ri eran

eve

era i

s

)ms

s

-

ns

s

an

92701)

This item involves the licensee's

efforts to determine

the

refrigerant level range in which the essential

chillers are

operable.

Currently no such

range

has

been determined.

In June,

1991,

the chiller vendor responded

to the licensee's

request for

information but declined to specify

a refrigerant level range,

other than the design

optimum levels, in which the chiller would be

capable of supplying cooling demands

from none to the full design

load.

The vendor dsd present technical

considerations

affected

by

operation at high and low refrigerant levels.

The licensee's

weekly Preventive

Maintenance

(PM) task

(No. 039874)

to monitor operating parameters

under established

standard

conditions

does specify

a required

range (specific to each chiller,

but based

on the

same refrigerant charge),

and instructs the worker

to notify the shift supervisor,

the

HVAC foreman,

and the

responsible

Systems

Engineer

(SE) of all readings

outside the

required

range.

However, the chi llers have not been declared

inoperable

on the basis of readings

outside the required

range.

The

SE does

not evaluate

these

readings

to determine operability,

since there is no technical

basis for the evaluation.

The inspector

reviewed the

PM data

sheets

and found three

occasions,

one in each unit, in which the refrigerant levels

required adjustment to be restored to the required

band since this

Unresolved

Item was identified in November 1990.

These

are

documented

in Work Orders

(WOs) 455240 (Unit 1

December

18, 1990),

WO 462238 (Unit 2 - February 1, 1991),

and

WO 491622 (Unit 3-

May 9, 1991).

A review of the associated

Unit Logs indicates that

the Essential

Chilled Water loops were not declared

inoperable

on

any of these

occasions,

though because

Unit 3 was not in Modes

1

though

4 at the time, operability was not required.

The

EC system is required to be operable to support the operability

of other important safety equipment,

including the auxiliary

feedwater

system

and the Emergency

Core Cooling Systems.

It did

not appear that this issue

was being aggressively

addressed,

as

no

action

had been taken since the licensee

received the vendor's

reply in June,

1991.

This was discussed

with licensee

management,

who committed to regard the required

range specified in the

PM task

as the operable

band,

though at a later time the band

may be

enlarged if justified.

The licensee

committed to revise the

PM

task to clarify this position, to ensure that the Shift Supervisor

was notified as

soon

as

a reading outside the band is identified,

and to document in the

PM work order the as-found readings

and any

corrective action taken.

Based

on these

licensee

commitments, this

item is closed.

(0 en) Followu

Item (528/91-04-02):

"Undervolta

e Rela

Testin "-

nl

s

an

This item involved evaluation of the method

used to test the timing

of Agastat relays in the undervoltage

and low voltage monitoring

circuitry for the 4160 volt Class

1E buses

PBA-S03 and

PBB-S04.

The licensee

had committed to revise the previous test method

because it allowed repetitive testing of the relays,

which in

effect preconditioned

them, potentially giving false assurance

of

their ability to perform their required safety function.

The inspector

reviewed the revised procedure,

32ST-9Z103,

"Surveillance Test Procedures

for the Class

4160

Bus Undervoltage

Protective Relays."

The Surveillance

Test (ST) method

was

changed

such that the relays were evaluated

against the acceptance

criteria

on the first actuation,

and repeated

tests

were not allowed.

The

inspector

concluded that this aspect of the test

was adequate.

During a review of the undervoltage

and low voltage acceptance

criteria, which had been

changed during the procedure

revision, the

inspector

determined that both the

new and the old acceptance

criteria were slightly non-conservative

with respect to the

Technical Specifications

(TS) surveillance

requirements.

The

licensee

confirmed this and initiated Condition Report/Disposition

Request

(CRDR) 9-1-0144 to evaluate this condition.

The licensee

confirmed that the relay setpoints actually set or verified during

the most recent

ST performances

are

above the minimum values

specified in the TS.

The licensee

determined that the relays were

l

l

(

I

never non-conservatively

set.

The acceptance

criteria and

requirements

are

summarized

as follows:

TS

Table 3.3-4

32ST-9ZZ03*

Rev.

4

32ST-9ZZ03*

Rev.

5

Loss of Voltage:

> or = 3250

> or = 92.85

> or = 92.8

(3249.75

on bus)

(3248 on bus)

Degraded

Voltage:

83.7 - 106.9

(2929.5-

3741.5)

2930 - 3744

83.7 - 106.97

(2929.5-

3743. 95)

The procedure

gives the acceptance

criteria in voltage

on the

secondary

side of a 4200: 120 volt potential transformer.

Bus

voltages,

shown in parentheses,

are not provided in the

procedure.

The inspector

noted that errors in the acceptance

criteria were not

identified during review and approval of the revisions to the

surveillance

procedure.

The procedure

was reviewed

by the

Procedure

Review Group and was approved

by the Manager,

Plant

Standards.

The critical technical

review of procedures

affecting

safety is essential

to safe operation of the plant,

and the

inspector considers this error serious

because

the process failed

to prevent the erroneous

procedure

from being implemented.

In this

case

the error was not large in magnitude

and actual

setpoints

are

satisfactory,

so the safety significance is minimal.

However, this

indicates

a weakness

in the quality of engineering

support.

The failure to accurately translate

TS surveillance

requirements

into ST procedures

appears

to be in violation of NRC requirements.

The violation is not being cited because

the criteria specified in

Section V.A. of the Enforcement Policy were satisfied

(NCV

528/91-35-01).

The inspector

noted that

PCN 2 to Revision

5 of the

ST corrected

the

Loss of Voltage limit, but not the Degraded Voltage limits.

In response

to thss observation,

the licensee

submitted Instruction

Change

Request

24260 to change

the Degraded Voltage range to 85.0-

106. 9 volts (2975 - 3741. 5 volts), consistent with the

TS.

The ST, apparently consistent with the

TS

allows the Degraded

Voltage setpoint

(70 percent - 90 percent] to be set wel'I below the

Loss of Voltage setpoint

(78 percent).

This does not appear

consistent with the Updated Final Safety Analysis Report

(UFSAR) or

the Safety Evaluation Report

(SER), which both specify

a 90 percent

Degraded Voltage setpoint.

The licensee

is evaluating appropriate

changes

to the TS,

and is currently setting the Degraded

Voltage

relays

near the upper

end of the allowed range.

The inspector

encouraged

the licensee to continue that practice until the

licensee

resolves

the licensing basis for this setpoint.

This item

will remain

open pending completion of the licensee's

evaluation,

being documented

in

CRDR 9-1-0144.

5.

(0 en) Violation (528/91-04-04):

"Control of Motor 0 crated Valve

esl

n

n orma

1on

-

ns

s

an

This violation resulted

from the failure to maintain. design

documents

updated.

The licensee's

corrective

actions

included

deleting the Motor Operated

Valve

(MOV) torque switch settings

(thrust limits) from the design output documents.

This design

information is now being controlled by use of Engineering

Evaluation

Requests

(EERs) instead of the design drawing.

This

appears

to represent

less rigorous control than that required for

design information,

and was questioned

by the inspector.

Corrective Action Report

(CAR) 91-0021

was issued to address

this

programmatic conflict.

The initial response

by Engineering

was

found unacceptable

the equality Assurance

organization.

The revised

response

from Engineerinq,

which was overdue,

was not yet available

for review.

This item will remain

open pending review of the

completed

and accepted

response

to

CAR 91-0021.

(Closed)

NRC Information Notice (IN-91-13): "Inade uate Testin

of

mer enc

iese

enera

ors

s

-

nl

s

This item involved the adequacy of

EDG test conditions with regard

to worst-case

loads

and ambient temperatures

during testing,

and

appropriate

load shedding considerations.

The licensee

evaluated

this in Corrective Action Tracking System

(CATS) Item 051261,

and

concluded that

EDG testing for Units 1, 2,

and

3 is adequate

with

regards to worst-case

emergency

loads

and conditions.

The

NRC EDSFI Report dated

December

1990 addressed

similar concerns

for adequate

margin for maximum loads during accident conditions.

In response

to these

concerns,

the licensee

revised the

EDG loading

calculation (Revision 6, dated April 18, 1991) to include power

factors

and loads

under worst-case

conditions.

The resultant

values for maximum loads

and limiting power factors are

bounded

by

Surveillance Test Procedure

73ST-XDG01/02 (Integrated

Safeguards

Testing).

With outside

ambient temperatures

exceeding

113 degrees

F within

the last year (outside that assumed for the site in the

UFSAR), the

licensee initiated Engineering Evaluation

Request

(EER) 90-HC-017

to evaluate

the validity of the ambient temperatures

assumed

in the

EDG design.

The licensee

concluded that the standing calculations

are valid provided temperatures

greater

than

113 degrees

F do not

ersist for a period of time exceeding

0.5 percent of the year.

inally, load shedding is tested per 73ST-XDG01/02 and verified

through

a sequence

of events

recorder.

The licensee

has

concluded

that this test procedure

provides the operators with sufficient

information to allow them to load the

EDGs to simulate worst-case

conditions.

This item is closed.

One non-cited violation of NRC requirements

was identified

(Paragraph 2.c.4.).

10

3.

Review of Plant Activities (71707

and 93702)

Unit 1

b.

Unit 1 entered

the reporting period operating at 100 percent

power.

On September

14,

1991,

a Part-Length Control Element Assembly

(PLCEA) slipped partially into the core, forcing a power reduction.

During the power reduction,

the

No.

1 steam generator

feedwater

economizer valve failed open,

causing the steam generator

level to

increase until the reactor tripped and

a main steam isolation

actuation

occurred

(see

Paragraph

7).

The unit cooled

down to Mode

5 on September

17,

1991.

The economizer

valve positioner

was

replaced

and the cause of the slipped

CEA was corrected.

Other

maintenance

needs

included replacing the "dogbone seal"

between the

main turbine and the "C" condenser,

replacing the gaskets

on two

pressurizer

safety valves,

and repackinq other valves which were

contributing to an elevated

gaseous activity in the containment

building.

Following this maintenance,

the plant was heated

up,

reaching

Mode 4 on September

21 and

Mode

3 on September

22,

1991.

The reactor

was brought to criticality at 2:33 a.m.

on September

24,

and

Mode 1 was entered at 7:09 a.m.

The generator

was

synchronized to the grid at ll:07 a.m.

on September

24, 1991,

and

a

slow power ascension

was conducted.

The power ascension

was

interrupted at 65 percent

power to allow xenon to stabilize while

monitoring dose equivalent iodine.

Power was increased

to

100 percent

on September

28.

On October 7, 1991,

power was reduced

to about

68 percent to allow for inspection

and repair of the "A"

main feedwater

pump low pressure

steam inlet check valve.

The unit

was returned to 100 percent

power on October 8, 1991,

where it

remained until the end of the reporting period.

Unit 2

C.

Unit 2 operated at essentially

100 percent

power throughout this

reporting period.

Significant scheduled activities included main

steam safety valve setpoint testing

and fuel receipt for the

upcoming refueling outage.

Pressurizer

code safety relief valve

RCN-PSV-200 continued to exhibit apparent

seat

leakage, within the

technical specification limits.

Based

on Operations

and

Engineering Departments'valuations,

coordinated

compensatory

actions limited the rise in tail pipe and reactor drain tank

temperatures.

The plant experienced

sticking of No.

2 steam

generator

economizer

feed regulating valve,

SGN-FV-1122;

on

requiring prompt operator

manual action to control

steam generator

level.

Maintenance

was able to make temporary repairs

and the

valve was returned to service.

Unit 3

Unit 3 remained at essentially

100 percent

power throughout this

reporting period.

j

11

d.

Plant Tours

The following plant areas

at Units 1, 2,

and

3 were toured by the

inspectors

during the inspection:

Auxiliary Building

Control

Complex Building

Diesel

Generator

Building

Fuel Building

Main Steam Support Structure

Radwaste

Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The

2.

3.

4

5.

following areas

were observed

during the tours:

0 eratin

Lo s and Records - Records

were reviewed against

ec naca

peel

)ca lons and administrative control procedure

requirements.

Monitorin

Instrumentation - Process

instruments

were observed

or corre at>on

etween

c annels

and for conformance with

Technical Specifications

requirements.

Shift Staffin

- Control

room and shift staffing were observed

or con ormance with 10 CFR Part 50.54.(k), Technical

Specifications,

and administrative procedures.

E ui ment Lineu

s - Various valves

and electrical

breakers

were ven ie

o be in the position or condition requi red by

Technical Specifications

and administrative

procedures

for the

applicable plant mode.

E ui ment Ta

in

- Selected

equipment, for which tagging

reques

s

a

een initiated,

was observed to verify that tags

were in place

and the equipment

was in the condition

specified.

General

Plant

E ui ment Conditions - Plant equipment

was

o serve

or )n >ca sons

o

sys

em leakage,

improper

lubrication,

or other conditions that could prevent the

systems

from fulfillingtheir functional requirements.

The inspector

noted two occasions

in which the turbine

outboard bearing oil level in the Unit 3 turbine driven

Auxiliary Feedwater

(AFM) pump was about 1/8 inch above the

upper mark in the sight glass.

This is the fourth time in one

year that

a high level indication was observed

by the

NRC,

indicating that the licensee

has not yet identified the root

cause of this condition.

In each

case,

the licensee

restored

the level to within the band.

The licensee

has previously

determined that oil level discrepancies

such

as these

would

not affect the operability of the pumps.

The inspector

encouraged

the licensee to give more attention to this issue.

12

The inspector

noted that the general

conditions in the Unit 2

AFW pump rooms, including the pumps,

though acceptable,

reflect

a lower level of maintenance

attention than the

conditions in Units 1 and 3.

The inspector

noted rust

on the

pump pedestals

and indications of small active oil leaks.

A

pool of oil had accumulated

on the pedestal

of the turbine

driven pump.

The inspector

concluded that these deficiencies

did not appear to affect operability of the

pumps.

The

licensee

responded that the

pumps

and pedestals

were scheduled

for refurbishment during the coming Unit 2 refueling outage.

7.

Fire Protection - Fire fighting equipment

and controls were

f

ithT hi

1Sp i(i ti

d

admi nistrati ve procedures.

8.

Plant Chemistr

- Chemical analysis results

were reviewed for

con ormance

ws

h Technical Specifications

and administrative

control procedures.

9.

~Secor'it

Activities observed for conformance with regulatory

requirements,

the site security plan,

and administrative

procedures

included vehicle and personnel

access,

and

protected

and vital area integrity.

10.

Plant Housekee

in

- Plant conditions

and material/equipment

s orage

were

o served to determine

the general

state of

cleanliness

and housekeeping.

11.

Radiation Protection Controls - Areas observed

included

con ro

po)n

opera )on, records of licensee

surveys within

the Radiological Controlled Areas

(RCA), posting of radiation

and high radiation areas,

compliance with Radiation

Exposure

Permits

(REP), proper wearing of personnel

monitoring devices,

and personnel

frisking practices.

No violations of NRC requirements

or deviations

were identified.

4.

En ineered Safet

Feature

(ESF)

S stem Walkdowns - Unit 2 (71710)

An inspection of the Unit 2

Low Pressure

Safety Injection (LPSI) system

was performed to verify system lineup, configuration and equipment

condition on a sampling basis.

A representative

sample of LPSI

equipment

and piping were inspected

in the Auxiliary Building, the pipe

chase,

the refueling water tank

(RWT) area

and in the control

room.

The following conditions

were noted.

i

13

Valve Handwheel

"OPEN" Direction Arrows

The. handwheels

for manual

operation of the following motor operated

valves

had

"OPEN" direction arrows po'inting both in the clockwise

and counterclockwise directions

marked

on their handwheels:

2 CHA-HV 531,

2 CHB-HV 530,

and

2 SIB-HY 0307

In addition, the handwheel for the

LPSI pump discharge train "A"

manual isolation valve had

an

"OPEN" direction arrow pointing in

the clockwise direction which would be the shut direction for

normal opening valves.

The

"OPEN" direc'tion marking was

on the

bottom of the handwheel

indicating that the handwheel

may have

been

installed upside

down.

The inspector

looked at the stem position

and local valve position indication and noted that the valve

appeared

to be in the required

open position.

The inspector

informed the control

room Shift Supervisor of the

above

noted conditions

and stated that the valves should

be

confirmed to be in their required positions.

The inspector also

informed the Systems

Engineering Supervisor

and Compliance of the

observed conditions,

Systems

Engineering initiated Condition

Report/Disposition

Request

2-1-0130 to identify and correct the

noted condition.

The inspector also noted that

a similar condition

had

been previously noted,

and was discussed,

during the

December

1,

1989 Unit 3 Pre-restart

management

meeting

(NRC Meeting Report

89-55,

paragraph

3).

Pending further inspection of licensee

corrective actions,

the cond)tion was identified as Inspector

Follow-up Item 529/91-35-02.

Subsequently,

the licensee verified

that the subject valves were in their requbed positions.

Pi

e

Su

ort Observation

The inspector

noted that

a snubber type pipe support

2 SI 120

HOOG,

supporting the

LPSI pump miniflow recirculation line, was installed

approximately

5 feet from a pipe restraint that appeared

to

restrict pipe movement in the direction that the snubber

would

normally allow pipe movement for thermal

expansion of the piping.

The inspector

questioned

the installation

and discussed

the design

with Nuclear Engineerinq personnel.

The design personnel

confirmed

the inspectors

observation that the installat)on

was unusual

but

showed the inspector that the piping analysis

had considered

the

unusual installation

and determined it to be acceptable.

The

inspector

had

no further questions

regarding the observed condition.

Pi in

Confi uration

During the walkdown of the

LPSI pump supply piping, the inspector

noted that the piping was routed from the

RWT in the yard area,

through the pipe chase,

to the

LPSI pumps in the Auxiliary

Building and to containment penetrations,

but observed

no

intermediate piping anchors that would allow an analytical

subdivision of the piping analysis.

The inspector inquired

how

14

the varying seismic

response

spectra for the various locations

~ noted were taken into consideration

in the piping analysis.

The

licensee

stated that the subject pipi,ng had essentially

been

analyzed in two parts;

one stress

problem analyzed

the piping from

the

RWT to portions of the piping in the Auxiliary building and

a

second

analyzed the remainder of the piping utilizing a. structural

overlap modeling technique.

NUREG/CR-1980 provided

an

NRC approved

method for dynamic analysis of piping using

a structural

overlap

method that had been

benchmarked

and determined to have

conservatively

accounted

for or minimized the interaction

between

the subdivided parts of the stress

problem.

The inspector

requested

the licensee to inform the inspector, if the

NUREG was

not used,

what methodology

was

used for the overlap modeling

performed

and the basis for the acceptability of the modeling.

UFSAR section 3.9. 1.2. 1 indicates that

non-NSSS piping was analyzed

using

a finite element analysis

computer program,

ME 101, that

typically performs analysis

anchor to anchor.

The noted

UFSAR

section did not describe

an overlap modeling method for use with ME

101.

Nuclear Engineering piping analysis

personnel

stated that

they would determine

the methodology

used for the overlap modeling

for the subject piping analysis

and would determine

the basis for

acceptability of that methodology.

Pending the licensee's

evaluation of the noted condition and further

NRC inspection of the

licensee

s evaluation,

the condition was identified as Unresolved

Item 529/91-35-03.

No violations of NRC requirements

or deviations

were identified.

5.

Surveillance Testin

- Units 1

2

and

3 (61726)

a.

b.

Selected

surveillance tests

required to be performed

by the

Technical Specifications

(TS) were reviewed

on a sampling basis to

verify that:

1) the surveillance tests

were correctly included

on

the facility schedule;

2)

a technically adequate

procedure

existed

for performance of the surveillance tests;

3) the surveillance

tests

had been performed at the frequency specified in the TS;

and

4) test results satisfied

acceptance

criteria or were properly

dispositioned.

Specifically, portions of the following surveillances

were observed

by the inspectors

during this inspection period:

Unit 1

~roce

ure

Oescri tion

36ST-9SA01

ESFAS Train "A" Subgroup

Relay Monthly Functional

Test

Unit 2

~roce

ure

36ST-2SE06

40ST-9HF01

Descri tion

Log Power Functional Test

Engineered

Safety Feature

Pump

Room Air Exhaust

15

40ST-9HF02

Fuel Building Essential

Ventilation System

Operabi l ity Test 4. 9. 12. a

Unit 3

~roce

ure

Descri tion

36ST-3SE06

40ST-9HP02

43ST-3DG01

73ST-9CL06

Log Power Functional

Test

Containment

Hydrogen Analyzer Functional Test

Diesel Generator

A" Test 4.8. 1. 1.2.A

Containment Ventilation Purge Isolation Valves (42

inches)

Penetration

56

The inspector

observed

the performance of the Local

Leak Rate Test

(LLRT) on the Unit 3, 42-inch "containment purge valve CP-UV-2A.

The valve failed the test.

The inspector

noted that the valve

had

not been manipulated

since the previous

LLRT, which was successful.

Because this involves

a potential

degradation

of containment

integrity, the inspector will review the root cause of failure

evaluation being documented

in Condition Report/Disposition

Request

(CRDR) 3-1-0141 (Followup Item 530/91-35-04).

The inspector

noted minor discrepancies

during the performance of

36ST-3SE06,

"Log Power Functional Test."

These did not appear to

affect the validity of the surveillance test results.

The

discrepancies

were discussed

with appropriate

management

personnel.

The inspector

noted that the lead test performer

(ETP) did not meet

the minimum qualifications for this test although

a second test

performer did meet them.

I8C supervision

s expectation

in this

case

was that the

LTP be qualified but the licensee's

program only

requires

one of the test performers to be qualified.

Involved

personnel,

including the foreman,

were counseled.

The inspector

concluded that the licensee's

corrective actions

were adequate.

No violations of NRC requirements

or deviations

were identified.

6.

Plant Maintenance - Units 1

2

and

3 (62703)

a.

b.

During the inspection period,

the inspector

observed

and reviewed

selected

documentation

associated

with the maintenance

and problem

investigation activities listed below to verify compliance with

regulatory requirements,

compliance with administrative

and

ma)ntenance

procedures,

required equality Assurance/equality

Control

involvement, proper

use of safety taqs,

proper equipment alignment

and

use of jumpers,

personnel

qualif)cations,

and proper retesting.

The inspector verified that reportability for these activities was

correct.

Specifically, the inspector witnessed portions of the following

maintenance activities:

16

II it 2 ~ti t.i

o "8" Feed

Pump Oil Seal

Rework

o Instrument Air equality Preventive

Maintenance

o Troubleshoot/Repair

RU 142,

24 Volt Power

Supply

o Rack out "8" High Pressure

Safety Injection

Pump Breaker

o Troubleshoot/Repair

CEDMCS

o Replace

Gaskets

on Pressurizer

PSVs

o "B'eater

Drain

Pump Seal

Repair

Following the observation of work on the Unit 1 pressurizer

safety

valves

by the Central

Maintenance

Department

on September

19, 1991,

the inspector verified the calibration of the tool used.

The tool,

a 100 to 500 foot-pound torque wrench,

was within the correct

calibration band;

however, it was not pre-functionally tested

as

required

by the recently implemented functional test program.

The inspector

noted that the licensee

had initiated a functional

test program that was aggressively

implemented at all three units

by their respective

Mechanical

Maintenance

Departments.

The

inspector also noted that the implementation of the functional test

program varied considerably

between the Central

Maintenance

Departments.

The work observed

on the Unit 1 pressurizer

safety

valves

had

no plans in place for implementation of the functional

test program at the time of the inspection.

Subsequent

discussions

were held with Site Maintenance

Management

to discuss

management

intent for the uniform implementation of the

functional test program.

Management

stated that the intent was

that this program

be consistently

implemented

among all departments

to the extent possible considering the availability of test

apparatus,

time,

and technicians

trained to use the apparatus.

Management

stated that the program

was being implemented

on a

staggered

basis - applying to the individual Units first, then to

central

maintenance.

The licensee

independently initiated this

functional test program which goes

above

and beyond the

requirements

for torque wrench calibration.

The inspector

concluded that such

a program is conducive to safety

and good

maintenance

practices

and when fully implemented will enhance

the

licensee's

maintenance

program.

2 it 2 ~ti ti

o 2EPKAH15

AC Input Breaker Appendix

R Test 32MT-9ZZ74

o Installation of Conduit Support in "A" DC Equipment

Room per

DCP

2-XJ-HJ-056

o Fuel Receipt Inspection

78MT-9FH01

During the performance

of 32MT-9ZZ74, "Molded Case Breaker Test,"

on the Swing "A-C" Battery Charger

2-E-PKA-HF-15, the inspector

noted tie wraps missing from one phase of the

AC input leads to the

adjacent Train "A" battery charger

2-E-PKA-HF-11, compared to the

other two phases,

and compared to all three

phases

on

2-E-PKA-HF-15.

This resulted in one plastic spacer

being

potentially loose inside

a safety grade battery charger.

The

0

l

17

inspector

concluded that in some

cases

unrestrained

material

can

cause

degradation

of safety related

equipment.

At the exit the

licensee

acknowledged

the inspector's

comments

and the inspector

encouraged

the licensee to increase sensitivity in this area.

Unit 3 Descri tion

o Fire Barrier Malkdowns

o Adjust CPA-UV-2A Stop Nuts

o Repack

3FPN-VM-78

o Functionally Test Containment

Spray

Pump "A"

o Troubleshoot

Load Limit Potentiometer

on Main Turbine

o Troubleshoot

"B" Core Protection Calculator

o

PPS "B" Power Supply Replacement

Preparations

No violations of NRC requirements

or deviations

were identified.

Reactor Tri

and Main Steam Isolation

S stem

(MSIS) Actuation - Unit 1

an

A reactor trip and

MSIS occurred in Unit 1 on September

14,

1991, at

5:22 p.m.

(MST), after the

No.

1 Steam Generator

(SG) feedwater

economizer

control valve failed full open during a downpower transient.

The

reactor

was at 53K power at the time of the trip, which was caused

by

high level in the

No.

1 SG.

During the event, all safety equipment

actuated

as designed,

with the exception of the

No.

2

SG downcomer

blowdown valve, which failed to close.

However, this valve,

SGA-UV-227,

was previously

known to be faulty and was already isolated

sn accordance

with Technical Specification requirements.

The unit was stabilized in

Mode 3.

The downpower in progress

at the time of the event

was initiated because

a Part-Length Control

Element Assembly

(PLCEA) had slipped approximately

50 inches during routine

CEA surveillance testing at 3:Ol p.m.

The

licensee

was reducing power to less than

50 percent to satisfy

PLCEA

insertion limits requirements,

because

operators

were unable to restore

the slipped

PLCEA to within the group deviation limits.

A failed timer

circuit card in the Control

Element Drive Mechanism

(CEDM) Control

System

was found to have

caused

the slippage.

The inspector

noted that,

as allowed by procedure,

the

PLCEAs had not been tested with the other

CEAs earlier that week during the performance of a surveillance test

which monitors the

CEDM coils, since the

PLCEAs had been

moved during

the previous

week.

The licensee

is considering

a program enhancement

requiring coil traces of all

CEAs prior to performing

CEA operability

checks.

Condition Report/Disposition

Request

(CRDR) 1-1-0073

was initiated to

investigate this trip event,

including the Root Cause of Failure

(RCF)

of the economizer valve failure and the slipped

PLCEA.

A Notification of Unusual

Event

(NUE) was conservatively

declared

during

the event

and was terminated after verification that primary and

secondary

chemi stry parameters

were within expected

ranges.

18

Following the trip, the licensee

elected to cool

down to Mode

5 to

perform unrelated

maintenance.

Mode

5 was reached

on September

17,

1991.

Following completion of this maintenance,

the plant was heated

up, achieving

Mode

3 on September

22.

The reactor

was brought to

criticality at 2:33 a.m.

on September

24.

Mode 1 was entered at 7:09

a. m.

and the generator

was synchronized to the grid at 11: 07 a.m.

on

September

24,

1991

'uring

the power ascension,

Reactor Coolant System

(RCS)

Dose Equivalent

Iodine (DEI) was closely monitored because

an increasing trend prior to

the trip indicated increased

fuel defects.

An existing Justification

for Continued Operation

(JCO) requires

equi librium DEI to be less than

0.2 uCi/ml, and the value prior to the Unit 1 trip was

0. 17 uCi/ml.

The

licensee

implemented

an action plan addressing this issue,

including

taking actions to increase

the availability of all three charging

pumps

to maximize purification flow, putting

a freshly mixed resin

bed in the

delithiating ion exchanger,

and frequently sampling the

RCS for DEI

determination.

The power ascension

was interrupted at 65 percent

power

to allow xenon to stabilize near its equilibrium value to allow a better

determination of DEI.

Based

on the licensee's

analyses,

DEI did not

appear to be approaching

the

JCO limit in the short term, though it

might become limiting before the end of the current cycle.

Because

of the previous trend in DEI, the licensee

submitted

a revised

JCO to

NRR for review and approval to increase

the equilibrium DEI

limit to 0.4 uCi/ml.

This revision was approved

on October 9, 1991.

No violations of NRC requirements

or deviations

were identified.

Pre arations for Refuelin

- Unit 2 (60705)

The inspector attended

several

meetings,

reviewed work order status,

conducted plant tours,

reviewed the outage

schedule,

interviewed several

members of the plant and support staffs,

and reviewed several

procedures

to assess

the preparations

for the Unit 2 refueling outage

scheduled to

begin

on October 17,

1991.

The inspector

reviewed the plans for steam

generator

eddy current testing includinq plans for using the movable

rotating pancake

probe.

The )nspector )dentified an example of poor

visitor escort control discussed

in Paragraph

9 of this report which

appeared

to be related to the hiring of a contractor in preparation for

the outage.

The inspector

also identified weaknesses

in the scaffolding

program discussed

in Paragraph

10.

With the exception of these

deficiencies,

the inspector

concluded that in the areas

reviewed,

the

refueling preparations

appeared

appropriate.

No violations of NRC requirements

or deviations

were identified.

Unescorted Visitor - Unit 2 (71707)

At about 2:00 p.m.

on October 7, 1991, the inspector

observed

the

designated

escort of a visitor leave the visitor unattended

in the "D"

Vital

DC Equipment

Room of the Unit 2 Control Building.

The visitor had

not been granted

unescorted

access

to this vital area.

This is an

apparent violation of NRC requirements

(Violation 529/91-35-05).

19

A similar event occurred

on June

12,

1990,

as

documented

in

Inspection

Report 528/90-29,

and resulted

in a Notice of Violation.

This report also

documented

another

example of poor visitor control

by

the assigned

escort.

The escort

program

was revised

as

a result of the

Notice of Violation issued with report 528/90-29.

Inspection

Report

528/91-04 also referred to poor control of visitors by escorts.

The

inspector

noted that the event

on October

7, 1991 and the examples cited

in Inspection

Report 528/91-04 occurred after the escort program

was

revised.

The inspector also noted that the examples cited in Inspection

Report 528/91-04 occurred at the beginning of the last outage at the

Palo Verde Nuclear Generating Station.

The inspector

concluded that

these

examples

represent

a deficiency in escort visitor control.

Based

on the continuing observations

of escort deficiencies,

the inspector

considers this to be

a program weakness.

At the exit the inspector

emphasized

the importance of maintaining

good visitor escort control,

particularly as the Unit 2 outage is about to begin.

One violation of NRC requirements

was identified.

Scaffoldin

Deficiencies - Unit 2 (71707)

On October

7, 1991, the inspector

noted that scaffolding in the Train

"B" Engineered

Safety Features

(ESF) switchgear

room did not meet the

clearance

requirements

of the licensee's

scaffolding program in that

portions of the scaffold were in contact with a safety related

cable

tray,

and certain portions of the scaffold should

have

been in

contact with and braced against the wall, but were not.

Engineering

Evaluation

Request

(EER) 91-ZJ-024,

which evaluated this scaffold, did

not specify minimum clearance

between the scaffold and safety related

equipment,

and required the scaffold to be braced against the wall at

six points.

As a result of the inspector's

questions

the scaffolding was modified to

create

some clearance

from the cable tray.

The inspector

subsequently

noted that the modified scaffolding still was not braced against,

nor in

contact with the wall.

During subsequent

interviews with licensee

Component

and Specialty Engineerinq personnel,

the inspector

determined

that the scaffolding program contains

two potential

weaknesses.

Procedure

30DP-9WPll, "Scaffolding Instructions," requires

the system

engineer to sign the scaffold tag to verify that the scaffold meets

Seismic Category

IX requirements

when scaffolding is erected in

accordance

w)th an

EER, but does not specify

a maximum length of time

that scaffoldinq can

be in place prior to this signature

by the system

engineer.

The inspector concluded that it is possible for scaffolding

which does

not meet Seismic Category

IX requirements

to be present for

an unspecified

length of time before this condition is identified by the

system engineer.

The inspector also determined that the calculations

used to evaluate

the potential

impact of scaffolding on safety related

plant components

do not include the

mass of material that may be placed

on the scaffolding.

The inspector

concluded that the potential exists

for scaffolding in use in the plant, with the load that could reasonably

be placed

on the scaffolding, to exceed

the Seismic Category

IX

requirements

because

the calculations

consider

the scaffolding unloaded.

20

The licensee

committed to perform

a calculation

by November 4,

1991

on

the seismic qualification of the scaffolding in the "B" train

ESF

switchgear

room, which did not meet the cl,earance

requirements

of the

licensee's

scaffolding program.

The licensee

has initiated

CRDR

2-1-0131 to address

the inspector's

questions.

The inspector will

review the licensee's

response

to these

programmatic

weaknesses,

the

final

CRDR disposition,

and this calculation

when it is complete

(Unresolved

Item 529/91-35-04)

Worker Res onsibilit

- Unit 2 (71707)

On September

26, 1991, the inspector

noted that the Plant Computer

(PC)

page display

PC-3 for main feedwater

pump performance

indicated

approximately

1095 thousand

pounds

mass

per

hour (klbm/hr) steam flow to

the "A" main feed

pump turbine while the "B" main feed

pump turbine

indicated approximately

625 klbm/hr.

The inspector questioned

the

difference

between

the two pumps

and was told by an operator that the

"B" pump steam flow parameter

was not working, and that it always read

about

625,

The inspector

noted that

a Work Request

(WR) or Control

Room

Deficiency Log (CRDL) entry had not been

made.

An operator stated that

the plant computer

was for information only, and the standard practice

was to not make

CRDL entries for

PC page display deficiencies.

Condition Report/Disposition

Request

(CRDR) 2-1-0112

was written as

a

result of the inspector's

questions.

The inspector

concluded that an

operator's

knowing about

a problem with a control

room display and not

initiating corrective action represented

a weakness

in the overall

corrective action program,

in that corrective action cannot occur if

problems

are not documented

when they are identified.

The licensee

acknowledged

the inspector's

comments.

No violations of NRC requirements

or deviations

were identified.

Main Steam Safet

Valve (MSSV) Set oint Testin

- Unit 2 (71707)

On October 9, 1991, during

MSSV setpoint testing the inspector

asked

a

Control

Room operator to test the communication

system required

by

Section 6.4 of surveillance test procedure

73ST-9ZZ18,

"Main Steam

PSV

[Pressure

Safety Valve] Set Pressure Verification."

The control

operator

was unable to establish

communication utilizing the radio

designated

at the pre-job briefing for this purpose.

A few minutes later the inspector

observed

the engineer

responsible

for

communication with the control

room fail to respond to a plant page

until that individual

s supervisor

prompted

a response.

The inspector

encouraged

licensee

management

to ensure that when communication devices

are issued that personnel

are able to utilize them for plant operations

and testing.

The licensee

acknowledged

the inspector's

comments

and

affirmed management's

expectation for communications to be effective,

No violations of NRC requirements

or deviations

were identified.

t

21

Undersized

Welds - Unit 2 (71707)

During performance

of an unrelated

inspection in the Unit 2 "B" charging

pump room,

a quality control inspector

noted that two welds

on

a drain

line at the

pump discharge

were slightly undersized.

Material

Non-Conformance

Report

(MNCR) 91-CH-2024

was initiated and the welds

were replaced.

The inspector

concluded that this was

a good example of

the benefits of looking beyond the focus of specific tasks to identify

and correct other

deficiencies'o

violations of NRC requirements

or deviations

were identified.

E ui ment

uglification Audit Review - Units

1

2

and

3 (35502

and

The inspector

reviewed the licensee's

self initiated Equipment

qualification (Eg) assessment

(Final Report August 1991)

and discussed

the report

s findings with the licensee.

The report identified several

major weaknesses

in the licensee's

Eg program,

and concluded that "the

existing program will not effectively ensure

continued qualification of

Palo Verde Nuclear Generating Station

(PVNGS)

Eg equipment,

as required

by 10 CFR 50.49."

The immediate impact on the facility was assessed

to

be minimal because "relatively few Eg components

have reached their

required Eg-related

maintenance

interval. 'ad the

Eg program not been

similarly assessed

until 1993 or beyond,

the licensee

concluded that

many more in-plant deficiencies

would have

been identified.,

However,

the small

number of field deficiencies actually identified in this

assessment

were manageable

without impacting plant operations

due to

operability issues.

One significant finding of the assessment

was the lack of a complete

high energy line break analysis for the auxiliary building.

A

Justification for Continued Operation

(JCO)

was developed,

concluding

that power operation

was acceptable

while the analysis

and resultant

corrective actions

were completed.

The assessment

resulted in the issuance

of nine Corrective Action

Reports

(CARs), eight equality Deficiency Reports

(gDRs), five Material

Nonconformance

Reports

(MNCRs), and two Warehouse

Deficiency Notices

(WDNs).

'Several

immediate or short term corrective actions

were

recommended

and management

responses

to these

are being tracked via the

Corrective Action Tracking System

(CATS).

Included in the

recommendations

are plant walkdowns, worker training, backlog reduction,

reevaluation of Preventive

Maintenance

(PM) due dates,

a review of the

thermal

and radiation analyses

associated

with limited life components

to verify their qualified lives and replacement

schedules,

and several

procedure

revisions.

The assessment

was performed at the request of the Vice President-

Engineering

and Construction.

As potential

problem areas

were

identified, the schedule

was extended

twice to allow a more thorough

review.

l~~

22

The inspector

concluded that the licensee

had effectively used the

Quality Assurance

(QA) resources

to identify significant problems in the

EQ program,

and that the

QA organization

was successful

in evaluating

the potential significance of several

minor observations

and in

convincing management

of the

need for major programmatic

changes

and

extensive corrective

actions.

Additionally, the

QA response

to an

engineering

recommendation

to perform this

EQ assessment

was

an

indication of effective functioning of the

QA program.

No violations of NRC requirements

or deviations

were identified.

Review of Em lo ee Concerns

Pro

ram Activities - Units 1

2

and

3

The inspector

reviewed

13 Employee

Concerns

Program

(ECP) files

initiated in 1991 to determine if the identified concerns

were being

evaluated

and dispositioned

in a manner conducive to enhancing

nuclear

safety.

The inspector

found that all of the

ECP files reviewed appeared

to be complete

and thorough.

The technical

issues

were identified and

addressed

with appropriate corrective actions initiated.

Those files

dealing with administrative issues,

such

as fitness for duty

evaluations,

also indicated corrective actions

where appropriate.

One file indicated that

a person

was only looking for the

NRC's phone

number,

but that the

ECP person receiving the call was able to persuade

the caller to convey his concern to the

ECP.

The

ECP file. indicated

that the concern

was dealt with in a manner which satisfied the caller.

The inspector also found the

ECP evaluation to be complete

and thorough.

Another file involved a complaint of employment discrimination

(demotion) for having brought previous

concerns to the

ECP.

The

complaint was referred to appropriate on-site

management for review and

resolution.

Even though management

conducted this review of its own

performance

regarding the handling of the case,

the review appeared

to

be objective

and provided clear evidence

supporting the demotion of the

individual.

The inspector

concluded that these

ECP files were evaluated

by the

licensee

in a manner conducive to identifying and correcting problems.

No violations of NRC requirements

or deviations

were identified.

Review of

Em lo ee

ualifications - Units 1

2

and

3 (41500)

The inspector

reviewed the qualifications of twenty, randomly-selected

supervisory

and non-supervisory

employees

in the Unit 2 Maintenance

and

Central

Maintenance

Departments.

The educational

and training

backgrounds

and experience

of those

reviewed were evaluated in

accordance

with ANSI Standard

3. 1-1978, to assure that the minimum

supervisory or non-supervisory

requirements,

as applicable,

had been

met.

Based

on the review, all employees

were found to meet or exceed

these

requirements.

No violations of NRC requirements

or deviations

were identified.

Review of Licensee

Event

Re orts - Units 1

2

and

3 (92700)

The following LERs were reviewed

by the Resident Inspectors.

23

a.

Unit 2

(Closed)

LER 529/87-04-Ll:

"Reactor Tri

While Performin

roun

so

a ion

ue

o

na

e

ua

e

n orma ion

-

ni

2.

This item was initially reviewed in Inspection

Report

529/87-28.

The supplement

was issued to address

specific

corrective actions which have

been identified and

implemented

since the initial report.

The inspector evaluated

these

actions

and concluded that they appear appropriate.

This item

is closed.

(Closed)

LER 529/91-01-LO:

"Containment

Pur

e Isolation

c ua ion

s

em

on ro

oom

ssen ia

i

ra ion

c ua ion

s

em

ni

c ua ion

ue

o

ersonne

rror"

This event

was discussed

in Inspection

Report 529/91-19 in

Paragraph

118.

The

LER does

not suggest

any additional

issues.

This item is closed.

(Closed)

LER 529/91-02-LO: "Dail

Reactor Coolant

Pum

i ra ion

a

a

n ineerin

va ua ion

isse

-

ni

(92700)

This item involved the fai lure of the Shift Technical

Advisor

(STA) to perform the daily engineering

review of Reactor

Coolant

Pump

(RCP) vibration data

on June

18,

1991 as required

by item IV.A.2 of the Unit 2 Confirmatory Order Modifying the

Facility Operating

License

NPF-51 date

November

19,

1987.

This is

a repeat of a similar event reported in

LER 528/89-01.

This failure was discovered

on June

19,

1991.

The June

18,

1991 data were reviewed

and found to meet the acceptance

criteria.

The licensee

concluded that this was

a coqnitive

personnel

error.

The licensee

s investigation identified that

the individual responsible for the omission initialed the

STA

turnover check sheet for this item as required

by step 3.5. 1

of 72AC-9ZZ01, Shift Technical Advisor Shift Conduct,

but did

so prior to performing the evaluation

and then subsequently

failed to perform it.

A similar event,

documented

in

Inspection

Report 528/529/530/89-43,

resulted in a Notice

of Violation for an Operator initialing completion of a step

which had not been completed.

The corrective action for the

present

event included disciplining the individual and

discussing

the event with all STAs.

In addition, although not

documented

in the

LER, the licensee

is adding this activity to

the technical specification tracking reminder computer in the

control

room which alarms to remind operators

to perform

various required activities.

At the exit meeting,

the

inspector confirmed that the licensee

management

expectation

is for items to be complete before being checked or initialed

on checklists.

This item is closed.

l

i',

24

b.

Units

2 and

3

l..

(0 en)

LER 529/90-04-LO/Ll Pressurizer

Code Safet

Relief

ave

e-o)ns

u

o

oerance-

nl

an

ae

ave

e

owns

u

o

oerance

- Unit3

These

LERs reported

as-found Pressurizer

Code Safety Valves

(PSVs)

and Hain Steam

Code Safety Valves

(HSSVs) outside the

tolerance permitted by Technical Specifications

(TS) (plus or

minus

one percent).

As-found HSSV setpoints

ranged

from 2.8

percent

low to 1.7 percent high.

PSVs were

up to 3.6 percent

high.

The licensee attributed these results to setpoint

drift, a performance limitation of these

valves.

TS change

requests

have

been submitted to relax these tolerances

up to

three percent.

Evaluations

have

been performed which suggest

that postulated

accidents with these

as-found setpoints

would

not have resulted in reactor coolant system pressure

rising

above the

TS safety limit.

The inspector raised

several

questions

regarding these

evaluations.

The licensee

is

obtaining additional information to answer the inspector's

questions.

These

items will remain

open pending the

completion of the inspector's

review.

c.

Unit 3

l.

(Closed)

LER 530/91-07-LO:

"Reactor

Shutdown

Re uired

b

ec

n>ca

ecl

1ca ion

-

nl

)s repor

escr)

es

e

uqus

,

, shutdown of Unit 3

required

by Technical Specification 3.8.3. 1 due to a failed

Class

1E inverter.

This event is described

in NRC Inspection

Report 530/91-29,

Paragraph

17.

This item is closed

on the

basis of the prior rev>ew.

No violations of NRC requirements

or deviations

were identified.

1 ~ .

~Eit

N ti

Exit meetings

were held on October ll

licensee

management,

during which the

this report were generally discussed.

proprietary any materials provided to

during the inspection.

and 17,

1991 with

observations

and conclusions

in

The licensee

did not identify as

or reviewed by the inspectors

1

i